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Sample records for kori nuclear unit-1

  1. Development of the MARS input model for Kori nuclear units 1 transient analyzer

    International Nuclear Information System (INIS)

    Hwang, M.; Kim, K. D.; Lee, S. W.; Lee, Y. J.; Lee, W. J.; Chung, B. D.; Jeong, J. J.

    2004-11-01

    KAERI has been developing the 'NSSS transient analyzer' based on best-estimate codes for Kori Nuclear Units 1 plants. The MARS and RETRAN codes have been used as the best-estimate codes for the NSSS transient analyzer. Among these codes, the MARS code is adopted for realistic analysis of small- and large-break loss-of-coolant accidents, of which break size is greater than 2 inch diameter. So it is necessary to develop the MARS input model for Kori Nuclear Units 1 plants. This report includes the input model (hydrodynamic component and heat structure models) requirements and the calculation note for the MARS input data generation for Kori Nuclear Units 1 plant analyzer (see the Appendix). In order to confirm the validity of the input data, we performed the calculations for a steady state at 100 % power operation condition and a double-ended cold leg break LOCA. The results of the steady-state calculation agree well with the design data. The results of the LOCA calculation seem to be reasonable and consistent with those of other best-estimate calculations. Therefore, the MARS input data can be used as a base input deck for the MARS transient analyzer for Kori Nuclear Units 1

  2. Nuclear design report for Kori nuclear power plant unit 1, cycle 13

    Energy Technology Data Exchange (ETDEWEB)

    Zee, Sung Kyun; Moon, Bok Ja; Cho, Byeong Ho; Jung, Yil Sup [Korea Atomic Energy Research Institute, Taejon (Korea, Republic of)

    1993-04-01

    This report presents nuclear design calculations for cycle 13 of Kori unit 1. Information is given on fuel loading, power density distributions, reactivity coefficients, control rod worths and operational limits. In addition, the report contains all necessary data for the startup tests including predicted values for the comparison with the measured data. The reload consists of 44 KOFA`s enriched by nominally 3.70 w/o U{sub 235}. Among the KOFA`s, 16 fuel assemblies contain gadolinia rods. The fuel assemblies in the core are arranged in a low leakage loading pattern. The cycle length of cycle 13 amounts to 355 EFPD corresponding to a cycle burnup of 13240 MWD/MTU. (Author) 8 refs., 55 figs., 16 tabs.

  3. Functional Analysis of Kori Unit 1

    International Nuclear Information System (INIS)

    Choi, Seong Soo; Han, Jeong Hyun; Heo, Tae Young

    2009-07-01

    Function Analysis of Kori Unit 1 has been performed as a part of independent human factors review tasks for control room renovation of the plant. The top level goal defined for the scope of function analysis is 'Generate Electricity'. Through this function analysis of Kori Unit 1, the detailed sub-functions extracted from the existing design documents and procedures, functional relationships among the high level functions, functional classification of each hierarchical level, and tree diagrams of the hierarchical function structures of the plant were developed and identified as the result of the project. In addition, we investigated and compiled the specifications of MMIS devices used in Ulchin Nuclear Power Plant Unit 5,6 in accordance with the request from KAERI. The results of those researches will be used as basis data for independent review of the control room MMIS design of the Kori Unit 1

  4. Nuclear design report for Kori nuclear power plant unit 1, cycle 14

    Energy Technology Data Exchange (ETDEWEB)

    Park, Chan Oh; Kim, Joo Young; Park, Sang Yoon; Song, Jae Woong; Lee, Chong Chul; Baik, Joo Hyun [Korea Atomic Energy Research Institute, Taejon (Korea, Republic of)

    1994-06-01

    This report presents nuclear design calculations for cycle 14 of Kori unit 1. Information is given on fuel loading, power density distributions, reactivity coefficients, control rod worths and operational limits. In addition, the report contains all necessary data for the startup tests including predicted values for the comparison with the measured data. The reload consists of 44 KOFA`s enriched by nominally 3.70 w/o U{sub 235}. Among the KOFA`s, 16 fuel assemblies contain gadolinia rods. The fuel assemblies in the core are arranged in a low leakage loading pattern. The cycle length of cycle 14 amounts to 366 EFPD corresponding to a cycle burnup of 13680 MWD/MTU. (Author) 8 refs., 55 figs., 16 tabs. nozzle by vortex formation during mid-loop operation condition are experimentally investigated. The critical submergence is determined for various types of suction nozzle, and the measurements of velocity distribution are performed in the flow fields near the t-shaped suction nozzle. (Author) 11 refs., 41 figs., 13 tabs.

  5. The trip status and the reduction countermeasure in Kori nuclear power plant unit 1 and 2

    International Nuclear Information System (INIS)

    Kim, Jung-Soo

    1991-01-01

    Nuclear power account for 36% of Korea's total electric capacity and provided over 50% of the net electric power supply by June 1991. These plants supply US with the cheapest and most stable electric supply available. However each units capacity is very large and a plant trip due to failure of a component or a human error has a great influence on the nations electric power supply and drastically decreases the reserve margin. This report will analyze the trip causes and measure the trip frequency from the first commercial operation of Kori unit 1 and 2 to the end of June 1991, reflect to the plant operation, management and facility modification, etc. This will minimize the number of trips or urgent power reductions and thus contribute to an increase in plant capacity factor and safety, and stabilize the electric power demand and supply. The safety and the economy of nuclear power plant have to be secured and raised respectably by increasing the capacity factor. Since the prevention of trips plays an important role in the plant safety and economy, we have to do our best to prevent the unexpected trip

  6. Development and application of the lancing system of delta-60 steam generator-Kori nuclear power plant unit 1

    International Nuclear Information System (INIS)

    Jeong, W. T.; Han, D. Y.; Ahn, N. S.; Jo, B. H.; Hong, Y. W.

    2001-01-01

    A lancing system for removing the deposits on the tube sheet of a nuclear steam generator using high pressure water was developed and applied to Kori Nuclear Power Plant( NPP) Unit 1. As the place where the lancing system is to be installed is relatively high radioactive area, every part consisting the equipment is carefully selected to be radiation resistant. The lancing robot was designed to be water proof to aviod possible malfunction of the lancing robot because of high pressure water. To minimize radiation exposure to operators, the system was designed considering easy installation and maintenance in mind. Water ejection nozzle are designed to have high strength with special material and heat treatment so as to lessen abrasion caused by high pressure ejection. The lancing system showed good performance during the on-site lancing using the system for Delta-60 steam generator of Kori NPP No. 1 in October 2000

  7. Neutron spectrum measurement inside containment vessel at Kori nuclear power plant unit 1

    Energy Technology Data Exchange (ETDEWEB)

    Han, J. M.; Kim, T. W.; Kim, K. D.; Youn, C. H. [Nuclear Environment Technology Institute, Taejon (Korea, Republic of)

    2003-10-01

    There would be a case for the radiation worker have to work inside of the containment vessel to inspect or repair reactor facilities. In this case, the information about distribution of neutron field is needed to estimate neutron exposure dose of worker. Neutron spectra were measured by BMS(Bonner Multisphere Spectrometer) at 4 points of 6 ft and 20 ft, 2 points of 44 ft, 5 points of 70 ft in containment vessel of Kori unit 1. From the calculation, the following results were obtained. Neutron fluxes of 6 ft were between 2.623 x 10{sup 2} and 2.746 x 10{sup 4} neutron/cm{sup 2}{center_dot}sec, average neutron energies were between 9.209 x 10{sup -6} and 3.377 x 10{sup -2} MeV, equivalent doses of neutron were between 0.025 and 2.675 mSv/hr. Neutron fluxes of 20 ft were between 1.771 x 10{sup 1} and 1.682 x 10{sup 3} neutron/cm{sup 2}{center_dot}sec, average neutron energies were between 6.084 x 10{sup -6} and 2.988 x 10{sup -1} MeV, equivalent doses of neutron were between 0.004 and 0.228 mSv/hr. Neutron fluxes of 44 ft were between 3.367 x 10{sup 2} and 3.483 x 10{sup 2} neutron / cm{sup 2}{center_dot}sec, average neutron energies were between 3.962 x 10{sup -2} and 7.360 x 10{sup -2} MeV, equivalent doses of neutron were between 0.069 and 0.089 mSv/hr. Neutron fluxes of 70 ft were between 4.553 x 10{sup 3} and 1.407 x 10{sup 4} neutron/cm{sup 2}{center_dot}sec, average neutron energies were between 3.668 x 10{sup -4} and 6.764 x 10{sup -2} MeV, equivalent doses of neutron were between 0.449 and 2.660 mSv/hr.

  8. Reload safety evaluation report for Kori nuclear power unit 1, cycle 14

    International Nuclear Information System (INIS)

    Kim, Joo Young; Kim, Oh Hwan; Nam, Kee Il; Kim, Du Ill; Ban, Chang Hwan; Choi, Dong Uk

    1994-05-01

    This report presents the reload safety evaluation for Kori-1, Cycle 14 and demonstrate that the reactor core being entirely composed of KOFA as described in the report will not adversely affect the safety of the public and the plant. All of the accidents comprising the licensing bases which could potentially be affected by the fuel reload have been reviewed for the Cycle 14 core design described herein. (Author) 1 refs., 9 figs., 5 tabs

  9. Reload safety evaluation report for Kori nuclear power plant unit 1, cycle 13

    International Nuclear Information System (INIS)

    Park, Chan Oh; Moon, Bok Ja; Cho, Byeong Ho; Nam, Kee Il; Kim, Oh Hwan; Chang, Doo Soo; Yoon, Han Young; Kim, Du Ill; Ban, Chang Hwan; Choi, Dong Uk

    1993-03-01

    This report presents the reload safety evaluation for Kori-1, Cycle 13 and demonstrates that the reactor core being composed of various fuel assembly types applied in this evaluation will not adversely affect the safety of the public and the plant. All of the accidents comprising the licensing bases which could potentially be affected by the reload fuel assemblies have been reviewed for the Cycle 13 core and results are described in this report. (Author)

  10. Spent fuel pool cooling system upgrade for Kori Unit 1

    International Nuclear Information System (INIS)

    Sun Park, Jong; In Shin, Kyung

    2014-01-01

    Following Fukushima nuclear power plant accident, the needs for reliable performance of its own safety functions of Spent Fuel Pool Cooling System (SFPCS) has risen significantly to maintain the plant in a safe condition. Regulatory Guide 1.13 of United States Nuclear Regulatory Commission (USNRC) requires the SFPCS shall be designed safety related as Quality Group C and Seismic Category 1. However, the existing Spent Fuel Pool (SFP) of KORI Unit 1 was not designed as a safety system. In order to comply with the above licensing requirement for the extended operational life of KORI Unit 1, it has been decided to add a safety related Seismic Category 1 Makeup System to KORI Unit 1 and the existing SFPCS to be modified in dedicated channels with safety related equipment to enhance system's reliability as a means of providing diversity. This paper focuses on describing the relevant design requirements, applications, and supplemental facilities to the SFPCS of KORI Unit 1. (authors)

  11. Preparation status for continuous operation of Kori unit 1 NPP in Korea

    International Nuclear Information System (INIS)

    Choi, C.H. . E-mail : chechee@khnp.co.kr

    2005-01-01

    Kori unit 1 Nuclear Power Plant is the first commercial operation plant in Korea. In Korea, the life extension of NPP beyond design lifetime reached practically application stage. Preparations status for continuous operation of Kori unit 1, Many researches have demonstrated that life extension beyond design lifetime is possible in terms of technology. This paper is to introduce and to share the continuous operation preparations status and schedule for Kori unit 1 License Renewal Process an additional every 10 years beyond the design life 30 years term. (author)

  12. Experience of Ko-Ri Unit 1 water chemistry

    International Nuclear Information System (INIS)

    Tae Il Lee

    1983-01-01

    The main focus is placed on operational experience in secondary system water chemistry (especially the steam generator) of the Ko-Ri nuclear power plant Unit 1, Republic of Korea, but primary side chemistry is also discussed. The major concern of secondary water chemistry in a PWR is that the condition of the steam generator be well maintained. Full flow deep bed condensate polishers have recently been installed and operation started in July 1982. Boric acid treatment of the steam generator was stopped and only the all volatile treatment method was used thereafter. A review of steam generator integrity, the chemistry control programme, secondary water quality, etc. is considered to be of great value regarding the operation of Unit 1 and future units now under startup testing or construction in the Republic of Korea. (author)

  13. Main Control Room Upgrade for Kori Unit 1 in Korea

    International Nuclear Information System (INIS)

    Ha, Jae Taeg; Choi, Moon Jae

    2014-01-01

    Kori Unit 1 is a 30 years old nuclear power plant and its MCR and MCB was upgraded based on the latest Human Factors Engineering (HFE) principles. The objectives of applying the Human Factors Engineering (HFE) principles are to minimize the human errors and to enhance the safe operation of the plant. In order to systematically incorporate the HFE design principles into the Human System Interface (HSI) design, HFE Program Plan (HFEPP) for Kori Unit 1 was developed and the plan provided an overview of the HSI design process along with detailed methods and results. The upgrade includes addition of Bypassed and Inoperable Status Indication System (BISI) and the replacement of the conventional MMI devices such as hardwired hand switches, recorders and indicators with new advanced control and display devices using VDUs (Video Display Units). The VDUs significantly improve the effectiveness and efficiency of the monitoring function. Plant Monitoring System (PMS) and Plant Annunciator System (PAS) were upgraded also by replacing the outdated systems with advanced digital systems with future expansion capability. In addition, the MCR related equipment and/or facilities were replaced or improved. Some of these include the enhancement of MCR interior designs for better working environment, dimmable ceiling lighting, aesthetically pleasing decor of ceiling, wall and floor as well as ergonomically improved operator consoles

  14. Main Control Room Upgrade for Kori Unit 1 in Korea

    Energy Technology Data Exchange (ETDEWEB)

    Ha, Jae Taeg; Choi, Moon Jae [KEPCO, Daejeon (Korea, Republic of)

    2014-08-15

    Kori Unit 1 is a 30 years old nuclear power plant and its MCR and MCB was upgraded based on the latest Human Factors Engineering (HFE) principles. The objectives of applying the Human Factors Engineering (HFE) principles are to minimize the human errors and to enhance the safe operation of the plant. In order to systematically incorporate the HFE design principles into the Human System Interface (HSI) design, HFE Program Plan (HFEPP) for Kori Unit 1 was developed and the plan provided an overview of the HSI design process along with detailed methods and results. The upgrade includes addition of Bypassed and Inoperable Status Indication System (BISI) and the replacement of the conventional MMI devices such as hardwired hand switches, recorders and indicators with new advanced control and display devices using VDUs (Video Display Units). The VDUs significantly improve the effectiveness and efficiency of the monitoring function. Plant Monitoring System (PMS) and Plant Annunciator System (PAS) were upgraded also by replacing the outdated systems with advanced digital systems with future expansion capability. In addition, the MCR related equipment and/or facilities were replaced or improved. Some of these include the enhancement of MCR interior designs for better working environment, dimmable ceiling lighting, aesthetically pleasing decor of ceiling, wall and floor as well as ergonomically improved operator consoles.

  15. Plant specific PTS analysis of Kori Unit 1

    Energy Technology Data Exchange (ETDEWEB)

    Sung-Yull, Hong; Changheui, Jang; Ill-Seok, Jeong [Korea Eletric Power Research Inst., Daejon (Korea, Republic of); Tae-Eun, Jin [Korea Power Engineering Company, Yonging (Korea, Republic of)

    1997-09-01

    Currently, a nuclear PLIM (Plant Lifetime Management) program is underway in Korea to extend the operation life of Kori-1 which was originally licensed for 30 years. For the life extension of nuclear power plants, the residual lives of major components should be evaluated for the extended operation period. According to the residual life evaluation of reactor pressure vessel, which was classified as one of the major components crucial to life extension, it was found by screening analysis that reference PTS temperature would exceed screening criteria before the target extended operation years. In order to deal with this problem, a plant-specific PTS analysis for Kori-1 RPV has been initiated. In this paper, the relationship between PTS analysis and Kori-1 PLIM program is briefly described. The plant-specific PTS analysis covers system transient analysis, downcomer mixing analysis, and probabilistic fracture mechanics analysis to check the integrity or RPV during various PTS transients. The step-by-step procedure of the analysis will be described in detail. Finally, various issues regarding RPV materials and its integrity will be briefly mentioned, and their implications on Kori-1 PTS analysis will be discussed. Despite of the screening analysis result concern, it is now expected that Kori-1 PTS issues can be handled through the plant-specific PTS analysis. (author). 14 refs, 4 figs, 2 tabs.

  16. Life extension program of KORI Unit 1 NPP in Korea

    International Nuclear Information System (INIS)

    Hong, Sun-Yull

    1998-01-01

    The two phases of Life extension program for KORI Unit 1 NPP are presented. Phase I is completed. It was concluded that life extension is a feasible option in technical and economic aspects. Detailed analysis of RPV is underway, plan for Phase II is finished. It deals with screening and sorting of all relevant SSCs, detailed life evaluation of SSCs, ageing management program and documentation for license renewal application

  17. Design Modification of Kori Unit 1 for the Equipment Qualification

    International Nuclear Information System (INIS)

    Park, J. W.; Kim, M. Y.; Han, K. T.; Park, J. D.

    2007-01-01

    There has not been a strict regulatory requirements for the Equipment Qualification(EQ) in 1970's when Kori Unit 1 had begun the construction and the commercial operation. The Korean regulatory body requested the EQ on the various safety-related components, as a result of Periodic Safety Review. However, the EQ itself is impossible in some areas, due to the high pressure/temperature and flooding environment conditions from the pipe breaks. Design modification is being considered in the Auxiliary Building, the Intermediate Building, the Component Cooling Water Heat Exchanger Building and the Turbine Building, in order to mitigate the environmental conditions for the EQ

  18. Determination of optimum pressurizer level for kori unit 1

    Energy Technology Data Exchange (ETDEWEB)

    Song, Dong Soo; Lee, Chang Sup; Lee Jae Yong; Kim, Yo Han; Lee, Dong Hyuk [Korea Electric Power Research Institute, Taejon (Korea, Republic of)

    1997-12-31

    To determine the optimum pressurizer water level during normal operation for Kori unit 1, performance and safety analysis are performed. The methodology is developed by evaluating {sup d}ecrease in secondary heat removal{sup e}vents such as Loss of Normal Feedwater accident. To demonstrate optimum pressurizer level setpoint, RETRAN-03 code is used for performance analysis. Analysis results of RETRAN following reactor trip are compared with the actual plant data to justify RETRAN code modelling. The results of performance and safety analyses show that the newly established level setpoints not only improve the performance of pressurizer during transient including reactor trip but also meet the design bases of the pressurizer volume and pressure. 6 refs., 5 figs. (Author)

  19. Determination of optimum pressurizer level for kori unit 1

    Energy Technology Data Exchange (ETDEWEB)

    Song, Dong Soo; Lee, Chang Sup; Yong, Lee Jae; Kim, Yo Han; Lee, Dong Hyuk [Korea Electric Power Research Institute, Taejon (Korea, Republic of)

    1998-12-31

    To determine the optimum pressurizer water level during normal operation for Kori unit 1, performance and safety analysis are performed. The methodology is developed by evaluating {sup d}ecrease in secondary heat removal{sup e}vents such as Loss of Normal Feedwater accident. To demonstrate optimum pressurizer level setpoint, RETRAN-03 code is used for performance analysis. Analysis results of RETRAN following reactor trip are compared with the actual plant data to justify RETRAN code modelling. The results of performance and safety analyses show that the newly established level setpoints not only improve the performance of pressurizer during transient including reactor trip but also meet the design bases of the pressurizer volume and pressure. 6 refs., 5 figs. (Author)

  20. Analysis of the necessity for inserting new surveillance capsule into the Kori Unit 1 RPV to monitor material fracture toughness

    International Nuclear Information System (INIS)

    Song, Taek Ho

    2007-01-01

    In association with monitoring of reactor pressure vessel (RPV) fracture toughness, surveillance capsule test specimens have been used to monitor the material property of nuclear reactor vessel. As far as Kori Unit 1 is concerned, 6 capsules were put into the vessel before commercial operation of the plant. Up to now, all the six capsules have been withdrawn to test and monitor the fracture toughness of RPV material. The last capsule has been withdrawn on June this year, and the Kori unit 1 has been shut downed since July 2007 and will be shut downed until December this year for about 6 months, preparing the life extension of the plant to operate the plant 10 more years. With the situation that all the surveillance capsules have been withdrawn, public ask the following question, 'To extend the life of Kori Unit 1 more than 10 years, is it necessary to insert new surveillance capsules into the Kori Unit 1 to monitor RPV material fracture toughness?' In connection with this issue, planning project have been carried out since spring this year. In this paper, it is described that inserting new surveillance capsule into the Kori Unit 1 RPV has some meaning in some public acceptance point of view and is not necessary in material engineering point of view

  1. Economic evaluation of Kori and Wolsong Unit 1 plant life extension

    International Nuclear Information System (INIS)

    Song, T. H.; Jeong, I. S.

    2002-01-01

    24 years have been passed since Kori Unit 1 began its commercial operation, and 19 years have been passed since Wolsong Unit 1 began its commercial operation. As the end point of design life become closer, plant life extension and periodic safety assessment is paid more and more attention to by the utility company. In this paper, the methodologies and results of plant lifetime management economic evaluations of both units have been presented in comparison with Korean standard nuclear power plant 10, 20 and 30 year life extension cases respectively. In addition to that, sensitivity analysis and break even point analysis results are presented with the variables of capacity factor, operation and maintenance cost, and discount rate

  2. Evaluation on radioactive waste disposal amount of Kori Unit 1 reactor vessel considering cutting and packaging methods

    International Nuclear Information System (INIS)

    Choi, Yu Jong; Lee, Seong Cheol; Kim, Chang Lak

    2016-01-01

    Decommissioning of nuclear power plants has become a big issue in South Korea as some of the nuclear power plants in operation including Kori unit 1 and Wolsung unit 1 are getting old. Recently, Wolsung unit 1 received permission to continue operation while Kori unit 1 will shut down permanently in June 2017. With the consideration of segmentation method and disposal containers, this paper evaluated final disposal amount of radioactive waste generated from decommissioning of the reactor pressure vessel in Kori unit 1 which will be decommissioned as the first in South Korea. The evaluation results indicated that the final disposal amount from the top and bottom heads of the reactor pressure vessel with hemisphere shape decreased as they were cut in smaller more effectively than the cylindrical part of the reactor pressure vessel. It was also investigated that 200 L and 320 L radioactive waste disposal containers used in Kyung-Ju disposal facility had low payload efficiency because of loading weight limitation

  3. Evaluation of SPACE code for simulation of inadvertent opening of spray valve in Shin Kori unit 1

    International Nuclear Information System (INIS)

    Kim, Seyun; Youn, Bumsoo

    2013-01-01

    SPACE code is expected to be applied to the safety analysis for LOCA (Loss of Coolant Accident) and Non-LOCA scenarios. SPACE code solves two-fluid, three-field governing equations and programmed with C++ computer language using object-oriented concepts. To evaluate the analysis capability for the transient phenomena in the actual nuclear power plant, an inadvertent opening of spray valve in startup test phase of Shin Kori unit 1 was simulated with SPACE code. To evaluate the analysis capability for the transient phenomena in the actual nuclear power plant, an inadvertent opening of spray valve in startup test phase of Shin Kori unit 1 was simulated with SPACE code

  4. Development of a GUI based RETRAN running environment for Kori NPP units 1 and 2

    Energy Technology Data Exchange (ETDEWEB)

    Kim, Kyung Doo

    2000-09-01

    RETRAN was developed by EPRI and introduced for domestic use. RETRAN, which is a best-estimate system code approved by USNRC and used by most utilities in US, can be used in various plant support activities such as licensing calculations for plant design changes, EOP validation, and training. RETRAN, however, has been limited to only a few groups of specialists because of the difficulty involved in its usage. The aim of this project is to develop a graphic user interface (GUI) based code running environment for RETRAN named PRE (RETRAN Running Environment) in order to assist ordinary users in their input preparation, code execution, and output interpretation. TRIP and CONTROL BLOCK and VOLUME/JUNCTION input cards from base input are designed to be able to modify the existing input cards and add a new input cards through dialog boxes for users who have not much expertise in use of RETRAN. The RRE is designed to provide the calculated results though on-line X-Y graphs, plant mimics, indicators, nodalization window for easy interpretation of its output. It also provides the replay function using pre-calculated results saved in files. The RRE was developed for Kori NPP units 1 and 2 using Delphi 4.0 and Visual Fortran 6.0 and it runs on personal computers to increase the accessibility. The RRE developed in this study for Kori units 1 and 2 can be used in various plant support activities which require thermal-hydraulic analysis of the NSSS (Nuclear Steam Supply System) such as licensing calculations for plant design change, validation of EOP improvement, and operator training. The RRE developed can be expanded its application to other nuclear plants with low expense.

  5. Development of a GUI based RETRAN running environment for Kori NPP units 1 and 2

    International Nuclear Information System (INIS)

    Kim, Kyung Doo

    2000-09-01

    RETRAN was developed by EPRI and introduced for domestic use. RETRAN, which is a best-estimate system code approved by USNRC and used by most utilities in US, can be used in various plant support activities such as licensing calculations for plant design changes, EOP validation, and training. RETRAN, however, has been limited to only a few groups of specialists because of the difficulty involved in its usage. The aim of this project is to develop a graphic user interface (GUI) based code running environment for RETRAN named PRE (RETRAN Running Environment) in order to assist ordinary users in their input preparation, code execution, and output interpretation. TRIP and CONTROL BLOCK and VOLUME/JUNCTION input cards from base input are designed to be able to modify the existing input cards and add a new input cards through dialog boxes for users who have not much expertise in use of RETRAN. The RRE is designed to provide the calculated results though on-line X-Y graphs, plant mimics, indicators, nodalization window for easy interpretation of its output. It also provides the replay function using pre-calculated results saved in files. The RRE was developed for Kori NPP units 1 and 2 using Delphi 4.0 and Visual Fortran 6.0 and it runs on personal computers to increase the accessibility. The RRE developed in this study for Kori units 1 and 2 can be used in various plant support activities which require thermal-hydraulic analysis of the NSSS (Nuclear Steam Supply System) such as licensing calculations for plant design change, validation of EOP improvement, and operator training. The RRE developed can be expanded its application to other nuclear plants with low expense

  6. Development of Neutronics Model for ShinKori Unit 1 Simulator

    Energy Technology Data Exchange (ETDEWEB)

    Hong, JinHyuk; Lee, MyeongSoo; Lee, SeungHo; Suh, JungKwan; Hwang, DoHyun [KEPRI, Daejeon (Korea, Republic of)

    2008-05-15

    ShinKori-Unit 1 and 2 is being built in the Kori site which will be operated at 2815 MWt of thermal core power. The purpose of this paper is to report on the performance of the developed neutronics model of ShinKori Unit 1 and 2. Also this report includes the convenient tool (XS2R5) for processing the large quantity of information received from the DIT/ROCS model and generating cross-sections. The neutronics model is based on the NESTLE code inserted to RELAP5/MOD3 thermal-hydraulics analysis code which was funded as FY-93 LDRD Project 7201 and is running on the commercial simulator environment tool (the 3KeyMaster{sup TM} of the WSC). As some examples for the verification of the developed neutronics model, some figures are provided. The output of the developed neutronics model is in accord with the Preliminary Safety Analysis Report (PSAR) of the reference plant.

  7. The 5th surveillance testing for Kori unit 1 reactor vessel materials

    Energy Technology Data Exchange (ETDEWEB)

    Chang, Kee Ok; Kim, Byoung Chul; Lee, Sam Lai; Choi, Kwun Jae; Gong, Un Sik; Chang, Jong Hwa; Joo, Yong Sun; Ahn, Sang Bok; Hong, Joon Hwa [Korea Atomic Energy Research Institute, Taejeon (Korea)

    2000-08-01

    Surveillance testing for reactor vessel materials is performed in order to evaluate the irradiation embrittlement due to neutrons during operation and set the condition of safe operation of nuclear reactor. The 5th surveillance testing was performed primarily by Korea Atomic Energy Research Institute and Westinhouse corporation partially involved in testing and calculation data evaluation in order to obtain reliable test result. Fast neutron fluences for capsule V, T, S, R and P were 5.087E+18, 1.115E+19, 1.228E+19, 2.988E+19, and 3.938E+19n/cm2, respectively. The bias factor, the ratio of calculation/measurement, was 0.940 for the 1st through 5th testing and the calculational uncertainty, 7% satisfied the requirement of USNRC Reg.Guide DG-1053, 20%. The best estimated neutron fluence for reactor vessel inside surface was 1.9846E+19n/cm{sup 2} based on the end of 17th fuel cycle and it was predicted that the fluences of vessel inside surface at 24, 32, 40 and 48EFPY would reach 3.0593E+19, 4.0695E+19, 5.0797E+19 and 6.0900E+19n/cm{sup 2} based on the current calculation. PTS analysis for Kori unit 1 showed that 27.93EFPY was the threshold value for 300 deg F requirement. 71 refs., 33 figs., 52 tabs. (Author)

  8. Dose mapping in working space of KORI unit 1 using MCNPX code

    Energy Technology Data Exchange (ETDEWEB)

    Lee, C. W.; Shin, C. H.; Kim, J. G. [Hanyang University, Seoul (Korea, Republic of); Kim, S. Y. [Innovative Techonology Center for Radiation Safety, Seoul (Korea, Republic of)

    2004-07-01

    Radiation field analysis in nuclear power plant mainly depends on actual measurements. In this study, the analysis using computational calculation is performed to overcome the limits of measurement and provide the initial information for unfolding. The radiation field mapping is performed, which makes it possible to analyze the trends of the radiation filed for whole space. By using MCNPX code, containment building inside is modeled for KORI unit 1 cycle 21 under operation. Applying the neutron spectrum from the operating reactor as a radiation source, the ambient doses are calculated in the whole space, containment building inside, for neutron and photon fields. Dose mapping is performed for three spaces, 6{approx}20, 20{approx}44, 44{approx}70 ft from bottom of the containment building. The radiation distribution in dose maps shows the effects from structures and materials of components. With this dose maps, radiation field analysis contained the region near the detect position. The analysis and prediction are possible for radiation field from other radiation source or operating cycle.

  9. Assessment of Coping Capability of KORI Unit 1 under Extended Loss AC Power and Loss of Ultimate Heat Sink Initiated by Beyond Design Natural Disaster

    Energy Technology Data Exchange (ETDEWEB)

    Kim, Chang Hyun; Ha, Sang Jun [KHNP CRI, Daejeon (Korea, Republic of); Han, Kee Soo [Nuclear Engineering Service and Solution (NESS) Co. Ltd., Deajeon (Korea, Republic of); Park, Chan Eok [KEPCO Engineering and Constructd., Deajeon (Korea, Republic of)

    2016-10-15

    In Korea, the government and industry performed comprehensive safety inspection on all domestic nuclear power plants against beyond design basis external events and fifty action items have been issued. In addition to post- Fukushima action items, the stress tests for all domestic nuclear power plants are on the way to enhance the safety of domestic nuclear power plants through finding the vulnerabilities in intentional stress conditions initiated by beyond design natural disaster. This paper presents assessment results of coping capability of KORI Unit 1 under the simultaneous Extended Loss of AC Power (ELAP) and Loss of Ultimate Heat Sink (LUHS) which is a representative plant condition initiated by beyond design natural disaster. The assessment of the coping capability of KORI Unit 1 has been performed under simultaneous the extended loss of AC power and loss of ultimate heat sink initiated by beyond design natural disaster. It is concluded that KORI Unit 1 has the capability, in the event of loss of safety functions by beyond design natural disaster, to sufficiently cool down the reactor core without fuel damage, to keep pressure boundaries of the reactor coolant system in transient condition and to control containment and temperature to maintain the integrity of the containment buildings.

  10. Assessment of Coping Capability of KORI Unit 1 under Extended Loss AC Power and Loss of Ultimate Heat Sink Initiated by Beyond Design Natural Disaster

    International Nuclear Information System (INIS)

    Kim, Chang Hyun; Ha, Sang Jun; Han, Kee Soo; Park, Chan Eok

    2016-01-01

    In Korea, the government and industry performed comprehensive safety inspection on all domestic nuclear power plants against beyond design basis external events and fifty action items have been issued. In addition to post- Fukushima action items, the stress tests for all domestic nuclear power plants are on the way to enhance the safety of domestic nuclear power plants through finding the vulnerabilities in intentional stress conditions initiated by beyond design natural disaster. This paper presents assessment results of coping capability of KORI Unit 1 under the simultaneous Extended Loss of AC Power (ELAP) and Loss of Ultimate Heat Sink (LUHS) which is a representative plant condition initiated by beyond design natural disaster. The assessment of the coping capability of KORI Unit 1 has been performed under simultaneous the extended loss of AC power and loss of ultimate heat sink initiated by beyond design natural disaster. It is concluded that KORI Unit 1 has the capability, in the event of loss of safety functions by beyond design natural disaster, to sufficiently cool down the reactor core without fuel damage, to keep pressure boundaries of the reactor coolant system in transient condition and to control containment and temperature to maintain the integrity of the containment buildings

  11. Multi-dimensional analysis of the ECC behavior in the UPI plant Kori Unit 1

    International Nuclear Information System (INIS)

    Bae, Sungwon; Chung, Bub-Dong; Bang, Young Seok

    2008-01-01

    A multi-dimensional transient analysis during the LBLOCA of the Kori Unit 1 has been performed by using the MARS code. Based on 1-D nodalization of the Kori Unit 1, the reactor vessel nodalizations have been replaced by the multi-dimensional component. The multi-dimensional component for the reactor vessel is designed as 5 radial, 8 peripheral, and 21 vertical grids. It is assumed that the fuel assemblies are homogeneously distributed in inner 3 radial grids. The outer 1 radial grid region is modeled as the core bypass. The outer-model 1 radial grid is used for the downcomer region. The corresponding heat structures and fuels are modified to fit for the multi-dimensional reactor vessel model. The form drag coefficients for the upper plenum and the core have been designated as 0.6 and 9.39, respectively. The form drag coefficients for the radial and peripheral directions are assigned to the same on the assumption of homogeneous distribution of the flow obstacles. After obtaining the 102% power steady operation condition, cold leg LOCA simulation is performed during 400 second period. The multi-dimensional steady run results show no severe differences compared to the traditional 1-D nodalization results. After the ECC injection starts, a liquid pool is maintained at the upper plenum because the ECCS water can not overcome the upward gas flow that comes from the reactor core through the upper tie plate. The depth of ECCS water pool is predicted as about 20% of the total height from the upper tie plate and the center line of the hot leg pipe. At the vicinity region of the active ECCS show higher depth of liquid pool. The accumulated water flow rate passing the upper tie plate is calculated by the transient result. Much downward water flow is obtained at the outer-most region of upper plenum space. The downward flow dominant region is about 32.3% of the total upper tie plate area. The accumulated ECCS bypass ratio is predicted as 27.64% at 300 second. It is calculated

  12. Review of the research proposal for the steam generator retired from Kori unit 1

    Energy Technology Data Exchange (ETDEWEB)

    Kim, Joung Soo; Han, Joung Ho; Kim, Hong Pyo; Lim, Yun Soo; Lee, Deok Hyun; Hwang, Seong Sik; Hur, Do Haeng [Korea Atomic Energy Research Institute, Taejeon (Korea)

    2002-03-01

    The tubes of the steam generator retired form Kori unit 1 have many different kinds of failures, such as denting pitting, wastage, ODSCC, PWSCC.Korea Electric Power Research Institute (KEPRI) submitted a research proposal for the steam generator to the Korea Institute S and T Evaluation and Planning (KSITEP). The KISTEP requested Korea Atomic Energy Research Institute to review the proposal by organizing a committee which should be composed of the specialists of the related domestic research institutes. Opinions of the committee on the objectives, research fields, economic benefit and validity in the research proposal were reviewed and suggested optimal research fields to be fulfilled successfully for the retired steam generator. Also, the rolls for the participants in the research works were allocated, which is critical in order to do the project effectively. 6 figs., 5 tabs. (Author)

  13. Thermal recovery characteristics of Kori-unit 1 linde 80 weld

    International Nuclear Information System (INIS)

    Chi, S. H.; Hong, J. H.; Kuk, I. H.; Kim, I. S.

    1997-01-01

    The recovery activation energy, the order of reaction and the characteristic recovery rate constant were determined by isochronal (573K -823K) and isothermal (723K - 775K) annealing experiments on specimens made from a broken half of a Kori-Unit 1 surveillance weld specimen (fluence: 1.21 x 10 23 n/m 2 , E (1MeV, Cu: 0.29 wt%) to investigate the recovery characteristics of a high copper weld of neutron-irradiated reactor pressure vessel (RPV). Vickers microhardness tests were conducted to trace the recovery behavior after heat treatments. The results were analyzed in terms of recovery stages, behavior of responsible defects and recovery kinetics. It was shown that recovery occurred through two annealing stages (stage I: 673K - 753K, stage II: 753K - 823K) with recovery activation energies of 2.68 eV and 2.83 eV for stage I and II, respectively. The isothermal hardness recovery at 723 K and 775 K coincided with the ratio of the characteristic rate constant for each recovery stage. The order of reaction was 2 for both recovery stages. The recovery activation energies of present specimens are approximately equal to that of copper diffusion in α-iron in the presence of vacancies, suggesting that recovery may occur through the diffusion of copper atoms. The present results strongly support the copper precipitate coarsening model. (author)

  14. Continuous operation of NPP Kori Unit 1 - Fireproof paint for cables

    International Nuclear Information System (INIS)

    Wendt, Dipl-Ing. Ruediger; Kim, Duill; Sik, Cho Hong

    2008-01-01

    Fireproof cable coating materials have been used in European NPP, especially in Germany, Russia, Ukraine, Czech Republic, Lithuania, Switzerland. Wide experiences were made during operation while applying these systems. In NPP Kori, Unit 1, a fire proof cable coating project was realised for the first time in a NPP of KHNP. The scope of services of the cable trays to coat amounts to 15,587m 2 . In different fire compartments and rooms the cables should be coated partially respectively completely with the fire proof cable coating system. The extent of cable surfaces to coat was stipulated by KHNP on the basis of an analysis made by KHNP. The project was tendered on the basis of a technical specification of KHNP. The specification is mainly predicted on Korean and US standards. The most important criteria for the fire proof cable coating is resumed as follows: The fireproof cable coating has to assure the fire protection of the cables for a period defined and for operational conditions defined in such a manner that the general conditions for the operation of the cable installation will not be affected

  15. Assessment on the Reactor Containment Cooling Capability of Kori Unit 1 Under LOCA Conditions with Loss of Offsite Power

    International Nuclear Information System (INIS)

    Lee, Jin Yong; Park, Jong Woon; Kim, Hyeong Taek

    2006-01-01

    The fan cooler system is designed to remove heat from containment under postulated accident conditions. During a postulated LOCA concurrent with a Loss of Offsite Power (LOOP), the Component Cooling Water (CCW) pumps that supply cooling water to the fan cooler and the fan that supplies containment air to the fan cooler will temporarily lose power. Then, the high temperature steam in the containment atmosphere will pass over the fan cooler tubing without forced cooling water flow. In that case, boiling may occur in the fan cooler tubes causing steam bubbles to form and pass into the attached CCW piping creating steam voids. Prior to the CCW pumps restart, the presence of steam and subcooled water can induce the potential for water hammer. As the CCW pumps restart, the accumulated steam condenses and the pumped water can produce a water hammer when the void closes. The hydrodynamic loads caused by such a water hammer event could challenge the integrity and the function of the fan cooler and associated CCW system. With respect to this phenomena, the United States Nuclear Regulatory Commission (USNRC) issued the Generic Letter (GL) 96-06, which requests an assessment of the possibility of boiling and water hammer in the cooling water system. The objectives of this study are to develop a analysis method for predicting the thermal hydraulic status of containment fan cooler and then to assess the containment fan cooler of Kori Unit 1 using the developed model under a LOCA with LOOP

  16. Lifetime management research trend of Kori-1 nuclear power plant

    International Nuclear Information System (INIS)

    Kim, J. S.; Jeong, I. S.; Hong, S. Y.

    1998-01-01

    KEPRI launched the Nuclear Power Plant Lifetime Management Study(II) for the management of the latter half life of Kori-1. Main goal of LCM-IV study is the detail evaluation of main equipment life and establishment of aging management based on LCM-IV result. The result of LCM-IV on the kori-1 confirmed the technical and economical feasibility of life extension beyond the design life. Owing to absence of The regulatory policy for the life extension in korea, LCM-IV will focus on the minimum study which is essential for the actual lifetime management for the old nuclear power plant. License renewal study is expected after the establishment of Regulatory policy about the life extension of nuclear power plant. LCM trend in korea and abroad, result of technical and economical feasibility study and summary of LCM-IV is described on this paper

  17. Postirradiation examination of Kori-1 nuclear power plant fuels

    International Nuclear Information System (INIS)

    Ro, S.G.; Kim, E.K.; Lee, K.S.; Min, D.K.

    1994-01-01

    Full size fuels discharged from Kori-1 PWR nuclear power plant have been subjected to postirradiation examination. The fuels under investigation were irradiated for one- to four-reactor cycles. Nondestructive examination and dismantling of the fuel assemblies have been conducted in the pool of the postirradiation examination facility (PIEF) of Korea Atomic Energy Research Institue. Subsequently nondestructive and destructive examinations of fuel rods have been performed in the hot cells of the PIEF. An evaluation of fuel burnup behaviors was based on the postirradiation examination data and the nominal design values. The results did not show any evidence of abnormalities in the fuel integrity. (orig.)

  18. Postirradiation examination of Kori-1 nuclear power plant fuels

    Science.gov (United States)

    Seung-Gy, Ro; Eun-Ka, Kim; Key-Soon, Lee; Duck-Kee, Min

    1994-05-01

    Full size fuels discharged from Kori-1 PWR nuclear power plant have been subjected to postirradiation examination. The fuels under investigation were irradiated for one- to four-reactor cycles. Nondestructive examination and dismantling of the fuel assemblies have been conducted in the pool of the postirradiation examination facility (PIEF) of Korea Atomic Energy Research Institute. Subsequently nondestructive and destructive examinations of fuel rods have been performed in the hot cells of the PIEF. An evaluation of fuel burnup behaviors was based on the postirradiation examination data and the nominal design values. The results did not show any evidence of abnormalities in the fuel integrity.

  19. Reload safety evaluation report for kori nuclear power plant unit 2 cycle 9

    International Nuclear Information System (INIS)

    Cho, Beom Jin; Kim, Si Yong; Kim, Oh Hwan; Nam, Kee Il; Um, Gil Sup; Ban, Chang Hwan; Choi, Dong Uk; Yoon, Kyung Ho

    1992-04-01

    The Kori Nuclear Power Plant Unit 2 (Kori-2) is anticipated to be refuelled with 16x16 Korean Fuel Assemblies (KOFA), which are based on the KAERI design starting from Cycle 8. This report presents a reload safety evaluation for Kori-2, Cycle 9 and demonstrates that the reactor core being composed of various fuel assembly types as described below will not adversely affect the safety of the public and the plant. The evaluation of Kori-2, Cycle 9 was accomplished utilizing the methodology described in 'Reload Transition Safety Report for KORI 2' (Ref. /1-1/). The reload core for Kori-2, Cycle 9 is entirely comprised of 16x16 KOFA. In the Kori-2 licensing documentation to KEPCO the reference safety evaluation was provided for the operation of a reactor core fully loaded with KOFA as well as associated proposed changes to the Kori-2 Technical Specifications. The reload for Kori-2, Cycle 9 also introduces UO 2 /Gd 2 O 3 containing fuel rods. The use of fuel rods with Gd 2 O 3 poisoning of the fuel has been approved as a part of the above mentioned licensing documentation. All of the accidents comprising the licensing bases which could potentially be affected by the fuel reload have been reviewed for the Cycle 9 core design described herein. (Author)

  20. Marine ecosystem analysis for Kori nuclear power plant

    International Nuclear Information System (INIS)

    Lee, C.H.; Kim, Y.H.; Cho, T.S.

    1980-01-01

    The effect of both radioactive and thermal effluents discharged from the plant on aquatic ecosystem is one of the primary concerns in evaluating the environmental impact due to the operation of the nuclear power plant. Biological alteration of aquatic ecosystems may be resulted from radioactive effluents, thermal pollution and chemical releases. There is also another possible synergistic effect, that is, the combination of the above stresses, which may cause an impact severer than that of the sum of the individual impact. This report deals with species diversity and seasonal variations of those numbers of phytoplankton, marine algae and microorganisms, and distribution of radioactivity of marine organisms, as well as those data pertaining to sea water analysis. The present survey is designed to provide a partial baseline information for environmental impact assessment of Kori nuclear plant unit no. 1. (author)

  1. Marine-ecosystem analysis for the Kori nuclear power plant

    International Nuclear Information System (INIS)

    Lee, J.H.; Kim, Y.H.

    1979-01-01

    The effects of radioactive effluents and warm water discharged from the plant on aquatic ecosystem is one of the primary considerations in evaluating the impact due to the operation of the nuclear power plant. Biological alteration of aquatic ecosystems may be resulted from radioactive effluents, thermal pollution and chemical releases; there is also the possible synergistic effect, that is, the combination of the above stresses, which may cause an effect greater than that of the sum of the individual effects. This report deals with species diversity and seasonal vegetation of phytoplankton, marine algae and microorganisms, radioactive contamination of marine organisms, and lateral distribution of sea water temperature from discharge point. The present investigation is designed to provide a partial baseline information for environmental safety against Kori nuclear power plant. (author)

  2. Measurement of gamma ray flux within the containment building at the first unit of Kori nuclear power station

    Energy Technology Data Exchange (ETDEWEB)

    Kim, T. W.; Kim, K. D.; Yoon, C. H.; Han, J. M.; Hu, Y. H. [Korea Hydraulic and Nuclear Power Company, Taejon (Korea, Republic of)

    2004-07-01

    To evaluate gamma ray dose response of GM counter being used for monitoring of gamma ray field in nuclear power plants, gamma ray energy spectra and fluxes were obtained for three positions at the unit 1 of the Kori nuclear power station. By applying the response values of Eberline's E112B survey meter to the results, the doses represented on the survey meter were overestimated from 1.31 to 1.37 times when compared to the real doses for these three positions.

  3. Relative power density distribution calculations of the Kori unit 1 pressurized water reactor with full-scope explicit modeling of monte carlo simulation

    International Nuclear Information System (INIS)

    Kim, J. O.; Kim, J. K.

    1997-01-01

    Relative power density distributions of the Kori unit 1 pressurized water reactor calculated by Monte Carlo modeling with the MCNP code. The Kori unit 1 core is modeled on a three-dimensional representation of the one-eighth of the reactor in-vessel component with reflective boundaries at 0 and 45 degrees. The axial core model is based on half core symmetry and is divided into four axial segments. Fission reaction density in each rod is calculated by following 100 cycles with 5,000 test neutrons in each cycle after starting with a localized neutron source and ten noncontributing settle cycles. Relative assembly power distributions are calculated from fission reaction densities of rods in assembly. After 100 cycle calculations, the system coverages to a κ value of 1.00039 ≥ 0.00084. Relative assembly power distribution is nearly the same with that of the Kori unit 1 FSAR. Applicability of the full-scope Monte Carlo simulation in the power distribution calculation is examined by the relative root mean square error of 2.159%. (author)

  4. Development of Level-2 PSA Technology: A Development of the Database of the Parametric Source Term for Kori Unit 1 Using the MAAP4 Code

    Energy Technology Data Exchange (ETDEWEB)

    Kang, Chang Soon; Mun, Ju Hyun; Yun, Jeong Ick; Cho, Young Hoo; Kim, Chong Uk [Seoul National University, Seoul (Korea, Republic of)

    1997-07-15

    To quantify the severe accident source term of the parametric model method, the uncertainty of the parameters should be analyzed. Generally, to analyze the uncertainties, the cumulative distribution functions(CDF`S) of the parameters are derived. This report introduces a method of derivation of the CDF`s of the basic parameters, FCOR, FVES and FDCH. The calculation tool of the source term is the MAAP version 4.0. In the MAAP code, there are model parameters to consider an uncertain physical and/or chemical phenomenon. In general, the parameters have not a point value but a range. In this paper, considering this point, the input values of model parameters influencing each parameter are sampled using LHS. Then, the calculation results are shown in the cumulative distribution form. For a case study, the CDF`s of FCOR, FVES and FDCH of KORI unit 1 are derived. The target scenarios for the calculation are the ones whose initial events are large LOCA, small LOCA and transient, respectively. It is found that the distributions of this study are consistent to those of NUREG-1150 and are proven to be adequate in assessing the uncertainties in the severe accident source term of KORI Unit 1. 15 refs., 27 tabs., 4 figs. (author)

  5. An advanced NSSS integrity monitoring system for Shin-Kori nuclear units 3 and 4

    International Nuclear Information System (INIS)

    Oh, Y. G.; Kim, H. B.; Galin, S. R.; Kim, S. H.; Lee, S. J.

    2009-01-01

    The advanced design features of NSSS (Nuclear Steam Supply System) Integrity Monitoring System for Shin-Kori Nuclear Units 3 and 4 are summarized herein. During the overall system design and detailed component design processes, many design improvements have been made for the system. The major design changes are: 1) the application of a common software platform for all subsystems, 2) the implementation of remote access, control and monitoring capabilities, and 3) the equipment redesign and rearrangement that has simplified the system architecture. Changes give an effect on cabinet size, number of cables, cyber-security, graphic user interfaces, and interfaces with other monitoring systems. The system installation and operation for Shin-Kori Nuclear Units 3 and 4 will be more convenient than those for previous Korean nuclear units in view of its remote control capability, automated test functions, improved user interface functions, and much less cabling. (authors)

  6. An Advanced NSSS Integrity Monitoring System for Shin-Kori Nuclear Units 3 and 4

    Science.gov (United States)

    Oh, Yang Gyun; Galin, Scott R.; Lee, Sang Jeong

    2010-12-01

    The advanced design features of NSSS (Nuclear Steam Supply System) Integrity Monitoring System for Shin-Kori Nuclear Units 3 and 4 are summarized herein. During the overall system design and detailed component design processes, many design improvements have been made for the system. The major design changes are: 1) the application of a common software platform for all subsystems, 2) the implementation of remote access, control and monitoring capabilities, and 3) the equipment redesign and rearrangement that has simplified the system architecture. Changes give an effect on cabinet size, number of cables, cyber-security, graphic user interfaces, and interfaces with other monitoring systems. The system installation and operation for Shin-Kori Nuclear Units 3 and 4 will be more convenient than those for previous Korean nuclear units in view of its remote control capability, automated test functions, improved user interface functions, and much less cabling.

  7. The experiences to improve plant performance and reliability of Ko-Ri nuclear power plants

    Energy Technology Data Exchange (ETDEWEB)

    Kang, Ho Weon [Korea Electric Power Corp. Ko-Ri nuclear power division, Ko-Ri (Korea, Republic of)

    1998-07-01

    This paper provides a discussion of the lessons learned from operational experience and the future plans to improve performance of the Ko-Ri plant. To operate nuclear power plants safely with good performance is the only way to mitigate the negative image of nuclear power generation to the public and to enhance the economical benefit compared to other electrical generation method. Therefore, in a continuous effort to overcome a negative challenge from outside, we have driven an aggressive 'OCTF' campaign as part of safety. As a result of our efforts, the following remarkable achievements have been accomplished. (1) 3 times of OCTF during recent three years (2) Selected twice as a top notch power plant on the list of NEI magazine in terms of plant capacity factor (3) No scram recorded in 1997 for all 4 units at Ko-Ri site. Ko-Ri is now undergoing the large scale plant betterment projects for retaking-off our operating performance to the level of new challenge target. Such improvement of critical components in the reactor coolant system and turbine system greatly contribute to increase the safety and reliability of the plant and to shortening of the planned outage period as well as to reduction of radiation exposure and radwaste. (Cho, G. S.). 5 tabs., 10 figs.

  8. The experiences to improve plant performance and reliability of Ko-Ri nuclear power plants

    International Nuclear Information System (INIS)

    Kang, Ho Weon

    1998-01-01

    This paper provides a discussion of the lessons learned from operational experience and the future plans to improve performance of the Ko-Ri plant. To operate nuclear power plants safely with good performance is the only way to mitigate the negative image of nuclear power generation to the public and to enhance the economical benefit compared to other electrical generation method. Therefore, in a continuous effort to overcome a negative challenge from outside, we have driven an aggressive 'OCTF' campaign as part of safety. As a result of our efforts, the following remarkable achievements have been accomplished. (1) 3 times of OCTF during recent three years (2) Selected twice as a top notch power plant on the list of NEI magazine in terms of plant capacity factor (3) No scram recorded in 1997 for all 4 units at Ko-Ri site. Ko-Ri is now undergoing the large scale plant betterment projects for retaking-off our operating performance to the level of new challenge target. Such improvement of critical components in the reactor coolant system and turbine system greatly contribute to increase the safety and reliability of the plant and to shortening of the planned outage period as well as to reduction of radiation exposure and radwaste. (Cho, G. S.). 5 tabs., 10 figs

  9. Nuclear design report for Kori nuclear power plant unit 4 cycle 8

    Energy Technology Data Exchange (ETDEWEB)

    Zee, Sung Kyoon; Jung, Yil Sub; Kim, Si Yung [Korea Atomic Energy Research Institute, Taejon (Korea, Republic of)

    1993-07-01

    This report presents nuclear design calculations for cycle 8 of Kori unit 4. Information is given on fuel loading, power density distributions, reactivity coefficients, control rod worths and operational limits. In addition, the report contains all necessary data for the startup tests including predicted values for the comparison with the measured data. The reload consists of 76 KOFA`s enriched by nominally 3.70 w/o U{sub 235}. Among the KOFA`s 48 fuel assemblies contain gadolinia rods. The fuel assemblies in the core are arranged in a low leakage loading pattern. The cycle length of cycle 8 amounts to 421 EFPD corresponding to a cycle burnup of 16950 MWD/MTU. (Author) 8 refs., 55 figs., 17 tabs.

  10. Nuclear design report for Yonggwang nuclear power plant unit 1, cycle 8

    International Nuclear Information System (INIS)

    Cho, Young Chul; Kim, Jae Hak; Park, Sang Yoon; Zee, Sung Kyun; Lee, Sang Keun; Ahn, Dawk Hwan

    1993-10-01

    This report presents nuclear design calculations for cycle 8 of Kori unit 1. Information is given on fuel loading, power density distributions, reactivity coefficients, control rod worths and operational limits. In addition, the report contains all necessary data for the startup tests including predicted values for the comparison with the measured data. The reload consists of 76 KOFA's enriched by nominally 3.70 w/o U 235 . Among the KOFA's, 56 fuel assemblies contain gadolinia rods. The fuel assemblies in the core are arranged in a low leakage loading pattern. The cycle length of cycle 8 amounts to 447 EFPD corresponding to a cycle burnup of 18020 MWD/MTU. (Author) 8 refs., 39 figs., 17 tabs

  11. Nuclear design report for Yonggwang nuclear power plant unit 1, cycle 8

    Energy Technology Data Exchange (ETDEWEB)

    Cho, Young Chul; Kim, Jae Hak; Park, Sang Yoon; Zee, Sung Kyun; Lee, Sang Keun; Ahn, Dawk Hwan [Korea Atomic Energy Research Institute, Taejon (Korea, Republic of)

    1993-10-01

    This report presents nuclear design calculations for cycle 8 of Kori unit 1. Information is given on fuel loading, power density distributions, reactivity coefficients, control rod worths and operational limits. In addition, the report contains all necessary data for the startup tests including predicted values for the comparison with the measured data. The reload consists of 76 KOFA`s enriched by nominally 3.70 w/o U{sub 235}. Among the KOFA`s, 56 fuel assemblies contain gadolinia rods. The fuel assemblies in the core are arranged in a low leakage loading pattern. The cycle length of cycle 8 amounts to 447 EFPD corresponding to a cycle burnup of 18020 MWD/MTU. (Author) 8 refs., 39 figs., 17 tabs.

  12. Numerical Simulation of Groundwater Flow at Kori Nuclear Power Plant Site

    International Nuclear Information System (INIS)

    Sohn, Wook; Sohn, Soon Whan; Chon, Chul Min; Kim, Kue Youn

    2010-01-01

    Recently, the understanding of hydrogeological characteristics of nuclear power sites is getting more importance with increasing public concerns over the environment since such understanding is essential for an environmentally friendly operation of plants. For such understanding, the prediction of groundwater flow pattern onsite plays the most critical role since it is the most dynamic of the factors to be considered. In this study, the groundwater flow at the Kori Plant 1 site has been simulated numerically with aim of providing fundamental information needed for improving the understanding of the hydrogeological characteristics of the site

  13. IAEA Completes Expert Mission to Kori 1 Nuclear Power Plant in the Republic of Korea

    International Nuclear Information System (INIS)

    2012-01-01

    Full text: An international team of nuclear safety experts led by the International Atomic Energy Agency (IAEA) has completed a review of safety practices at the Kori 1 Nuclear Power Plant (NPP) near Busan in the Republic of Korea. The IAEA assembled the team at the request of Korea Hydro and Nuclear Power Co., Ltd. (KHNP) following a station blackout event on 9 February 2012. The team - comprised of experts from Belgium, France, Sweden, United Kingdom and the IAEA - conducted its mission from 4 to 11 June 2012 under the leadership of the IAEA's Division of Nuclear Installation Safety. The expert mission applied the methodology of the IAEA's Operational Safety Review (OSART) missions and covered the areas of Management, Organization and Administration; Operations; Maintenance and Operating Experience. The conclusions of the review are based on the IAEA's Safety Standards, which are developed by the Agency to help nations improve their nuclear safety practices, which are the responsibility of every nation that undertakes nuclear-related activities. Throughout the review, the exchange of information between the experts and plant personnel was very open, professional and productive. Prior to the mission, Korea's Nuclear Safety and Security Commission completed an interim investigation, and it continues to perform additional investigations and technical reviews. The Commission identified corrective actions for the plant concerning reinforcing safety culture, emergency diesel generator reliability, configuration control and risk management during refueling outage, test and maintenance procedures and emergency action level declaration. The expert mission confirmed that some corrective actions have already been completed and others are in progress. The expert mission found the management and staff of Kori 1 NPP to be committed and working hard to complete all improvements. The root cause analysis of the event at Kori 1 NPP is still in progress and is expected to lead to

  14. Estimation of residual stress distribution for pressurizer nozzle of Kori nuclear power plant considering safe end

    Energy Technology Data Exchange (ETDEWEB)

    Song, Tae Kwang; Bae, Hong Yeol; Chun, Yun Bae; Oh, Chang Young; Kim, Yun Jae [Korea University, Seoul (Korea, Republic of); Lee, Kyoung Soo; Park, Chi Yong [Korea Electric Power Research Institute, Daejeon (Korea, Republic of)

    2008-08-15

    In nuclear power plants, ferritic low alloy steel nozzle was connected with austenitic stainless steel piping system through alloy 82/182 butt weld. Accurate estimation of residual stress for weldment is important in the sense that alloy 82/182 is susceptible to stress corrosion cracking. There are many results which predict residual stress distribution for alloy 82/182 weld between nozzle and pipe. However, nozzle and piping system usually connected through safe end which has short length. In this paper, residual stress distribution for pressurizer nozzle of Kori nuclear power plant was predicted using FE analysis, which considered safe end. As a result, existing residual stress profile was redistributed and residual stress of inner surface was decreased specially. It means that safe end should be considered to reduce conservatism when estimating the piping system.

  15. Thermal Analysis for Environmental Qualification of Kori Nuclear power plant unit 3 and 4

    International Nuclear Information System (INIS)

    Seo, Kwi Hyun; Byun, Choong Sup; Song, Dong Soo

    2006-01-01

    This paper shows the temperature profiles of safety related electrical equipment exposed to MSLB inside containment. It must be demonstrated that the LOCA qualification conditions exceed or are equivalent to the maximum calculated MSLB conditions. COPATTA as Bechtel's vendor code is used for the containment pressure and temperature prediction in power uprating project for Kori 3,4 and Yonggwang 1,2 nuclear power plants(NPPs). However, CONTEMPT-LT/028 is used for calculating the containment pressure and temperatures in equipment qualification project for the same NPPs. Power uprating code that is, COPATTA benchmarking study performed in six equipment at saturation temperature and surface temperature. Specially, thermal analysis carefully investigate that view point environmental qualification and NUREG- 0588 be mentioned in regard to safety-related heat sink it boundary condition or geometry information

  16. Thermal Analysis for Environmental Qualification of Kori Nuclear power plant unit 3 and 4

    Energy Technology Data Exchange (ETDEWEB)

    Seo, Kwi Hyun [ENERGEO Inc., Sungnam (Korea, Republic of); Byun, Choong Sup; Song, Dong Soo [KEPRI, Taejon (Korea, Republic of)

    2006-07-01

    This paper shows the temperature profiles of safety related electrical equipment exposed to MSLB inside containment. It must be demonstrated that the LOCA qualification conditions exceed or are equivalent to the maximum calculated MSLB conditions. COPATTA as Bechtel's vendor code is used for the containment pressure and temperature prediction in power uprating project for Kori 3,4 and Yonggwang 1,2 nuclear power plants(NPPs). However, CONTEMPT-LT/028 is used for calculating the containment pressure and temperatures in equipment qualification project for the same NPPs. Power uprating code that is, COPATTA benchmarking study performed in six equipment at saturation temperature and surface temperature. Specially, thermal analysis carefully investigate that view point environmental qualification and NUREG- 0588 be mentioned in regard to safety-related heat sink it boundary condition or geometry information.

  17. Science, society, and America's nuclear waste: Unit 1, Nuclear waste

    International Nuclear Information System (INIS)

    1992-01-01

    This is unit 1 in a four-unit secondary curriculum. It is intended to provide information about scientific and societal issues related to the management of spent nuclear fuel from generation of electricity at nuclear powerplants and high-level radioactive waste from US national defense activities. The curriculum, supporting classroom activities, and teaching materials present a brief discussion of energy and electricity generation, including that produced at nuclear powerplants; information on sources, amounts, location, and characteristics of spent nuclear fuel and high-level radioactive waste; sources, types and effects of radiation; US policy for managing and disposing of spent nuclear fuel and high-level radioactive waste and what other countries are doing; and the components of the nuclear waste management system

  18. Effects of environmental radiation of Kori nuclear power plant on the human population

    International Nuclear Information System (INIS)

    Kim, Y.J.

    1979-01-01

    In order to clarify and protect the effects of environmental radiation according to the operation of Kori nuclear power plant on human population, the base line survey for the human monitoring, the fauna of land nocturnal insects, and the karyotypes of amphibian species which have been living around the power plant site were carried out. ''Kilchunri'' population which took for the human monitoring lie within a 2km distance from power plant site. Human monitoring, house and food characteristics, individual experience of X-ray exposures, human chromosome analysis and fauna of nocturnal land insects were surveyed and expressed in numerical tables. Chromosome number obtained from the amphibia which were collected around the power plant area was as follows; Kaloula borealis 2N=30, Rana amurensis 2N=26, Rana dybouskii 2N=24, Rana rugosa 2N=26, Rana migromaculata 2N=26, Rana plancyi 2N=26, Bombina orientalis 2N=24, Hyla arborea 2N=24, Bufo stejnegeri 2N=22, and Bufo bufo 2N=22. (author)

  19. Final report on effects of environmental radiation of Kori nuclear power plant on human population

    International Nuclear Information System (INIS)

    Kim, Y.J.; Kim, J.B.; Chung, K.H.; Lee, K.S.; Kim, S.R.; Yang, S.Y.

    1980-01-01

    In order to clarify and protect the effects of environmental radiation according to the operation of Kori nuclear power plant on the human population, the base line survey for the human monitoring, human life habits, expected individual exposure dose, frequencies of chromosomal aberration, gene frequencies and karyotypes in amphibia, fauna, and radiation sensitivities in microorganisms which have been living around the power plant site were carried out. Kilchonri population which took for the human monitoring lie within a 2 km distance from the power plant site. Human monitoring, house and food characteristics, individual experience of x-ray exposures, human chromosome analysis and fauna were surveyed and expressed in numerical tables. Chromosome number obtained from the amphibia which were collected around the power plant area was as follows: Kaloula borealis 2N=30, Rana amurensis 2N=26, Rana dybouskii 2N=24, Rana rugosa 2N=26, Rana nigromaculata 2N=26, Rana plancyi 2N=26, Bombina orientalis 2N=24, Hyla arborea 2N=24, Bufo stejnegeri 2N=22, Bufo bufo 2N=22. (author)

  20. Effect of preemptive weld overlay sequence on residual stress distribution for dissimilar metal weld of Kori nuclear power plant pressurizer

    Energy Technology Data Exchange (ETDEWEB)

    Bae, Hong Yeol; Song, Tae Kwang; Chun, Yun Bae; Oh, Chang Young; Kim, Yun Jae [Korea Univ., Seoul (Korea, Republic of); Lee, Kyoung Soo; Park, Chi Yong [Korea Electric Power Research Institute, Daejeon (Korea, Republic of)

    2008-07-01

    Weld overlay is one of the residual stress mitigation method which arrest crack. An overlay weld sued in this manner is termed a Preemptive Weld OverLay(PWOL). PWOL was good for distribution of residual stress of Dissimilar Metal Weld(DMW) by previous research. Because range of overlay welding is wide relatively, residual stress distribution on PWR is affected by welding sequence. In order to examine the effect of welding sequence, PWOL was applied to a specific DMW of KORI nuclear power plant by finite element analysis method. As a result, the welding direction that from nozzle to pipe is better good for residual stress distribution on PWR.

  1. Effect of preemptive weld overlay sequence on residual stress distribution for dissimilar metal weld of Kori nuclear power plant pressurizer

    International Nuclear Information System (INIS)

    Bae, Hong Yeol; Song, Tae Kwang; Chun, Yun Bae; Oh, Chang Young; Kim, Yun Jae; Lee, Kyoung Soo; Park, Chi Yong

    2008-01-01

    Weld overlay is one of the residual stress mitigation method which arrest crack. An overlay weld sued in this manner is termed a Preemptive Weld OverLay(PWOL). PWOL was good for distribution of residual stress of Dissimilar Metal Weld(DMW) by previous research. Because range of overlay welding is wide relatively, residual stress distribution on PWR is affected by welding sequence. In order to examine the effect of welding sequence, PWOL was applied to a specific DMW of KORI nuclear power plant by finite element analysis method. As a result, the welding direction that from nozzle to pipe is better good for residual stress distribution on PWR

  2. System and Software Design for the Plant Protection System for Shin-Hanul Nuclear Power Plant Units 1 and 2

    International Nuclear Information System (INIS)

    Hwang, In Seok; Kim, Young Geul; Choi, Woong Seock; Sohn, Se Do

    2015-01-01

    The Reactor Protection System(RPS) protects the core fuel design limits and reactor coolant system pressure boundary for Anticipated Operational Occurrences (AOOs), and provides assistance in mitigating the consequences of Postulated Accidents (PAs). The ESFAS sends the initiation signals to Engineered Safety Feature - Component Control System (ESF-CCS) to mitigate consequences of design basis events. The Common Q platform Programmable Logic Controller (PLC) was used for Shin-Wolsung Nuclear Power Plant Units 1 and 2 and Shin-Kori Nuclear Power Plant Units 1, 2, 3 and 4 since Digital Plant Protection System (DPPS) based on Common Q PLC was applied for Ulchin Nuclear Power Plant Units 5 and 6. The PPS for Shin-Hanul Nuclear Power Plant Units 1 and 2 (SHN 1 and 2) was developed using POSAFE-Q PLC for the first time for the PPS. The SHN1 and 2 PPS was delivered to the sites after completion of Man Machine Interface System Integrated System Test (MMIS-IST). The SHN1 and 2 PPS was developed to have the redundancy in each channel and to use the benefits of POSAFE-Q PLC, such as diagnostic and data communication. The PPS application software was developed using ISODE to minimize development time and human errors, and to improve software quality, productivity, and reusability

  3. System and Software Design for the Plant Protection System for Shin-Hanul Nuclear Power Plant Units 1 and 2

    Energy Technology Data Exchange (ETDEWEB)

    Hwang, In Seok; Kim, Young Geul; Choi, Woong Seock; Sohn, Se Do [KEPCO EnC, Daejeon (Korea, Republic of)

    2015-10-15

    The Reactor Protection System(RPS) protects the core fuel design limits and reactor coolant system pressure boundary for Anticipated Operational Occurrences (AOOs), and provides assistance in mitigating the consequences of Postulated Accidents (PAs). The ESFAS sends the initiation signals to Engineered Safety Feature - Component Control System (ESF-CCS) to mitigate consequences of design basis events. The Common Q platform Programmable Logic Controller (PLC) was used for Shin-Wolsung Nuclear Power Plant Units 1 and 2 and Shin-Kori Nuclear Power Plant Units 1, 2, 3 and 4 since Digital Plant Protection System (DPPS) based on Common Q PLC was applied for Ulchin Nuclear Power Plant Units 5 and 6. The PPS for Shin-Hanul Nuclear Power Plant Units 1 and 2 (SHN 1 and 2) was developed using POSAFE-Q PLC for the first time for the PPS. The SHN1 and 2 PPS was delivered to the sites after completion of Man Machine Interface System Integrated System Test (MMIS-IST). The SHN1 and 2 PPS was developed to have the redundancy in each channel and to use the benefits of POSAFE-Q PLC, such as diagnostic and data communication. The PPS application software was developed using ISODE to minimize development time and human errors, and to improve software quality, productivity, and reusability.

  4. Reload safety evaluation report for kori nuclear power plant unit 4, cycle 8

    International Nuclear Information System (INIS)

    Park, Chan Oh; Jung, Yil Sup; Kim, Si Yong; Kim, Ki Hang; Kwon, Hyuk Sung; Oh, Dong Seok; Kim, Du Ill; Ban, Chang Hwan; Choi, Dong Uk

    1993-06-01

    This report presents the reload safety evaluation for Kori-4, Cycle 8 and demonstrate that the reactor core being entirely composed of KOFA as described in the report will not adversely affect the safety of the public and the plant. All of the accidents comprising the licening bases which could potentially be affected by the fuel reload have been reviewed for the Cycle 8 core design described herein. (Author)

  5. FIND: Douglas Point Nuclear Generating Station, Units 1 and 2

    International Nuclear Information System (INIS)

    Moore, M.M.

    1975-12-01

    This index is presented as a guide to microfiche items 1 through 136 in Docket 50448, which was assigned to Potomac Electric Power Company's Application for Licenses to construct and operate Douglas Point Nuclear Generating Station, Units 1 and 2. Information received from August, 1973 through July, 1975 is included

  6. Evaluation of Perry Nuclear Power Plant Unit 1 technical specifications

    International Nuclear Information System (INIS)

    Baxter, D.E.; Bruske, S.J.

    1985-11-01

    This document was prepared for the Nuclear Regulatory Commission (NRC) to assist them in determining whether the Perry Nuclear Power Plant Unit 1 Technical Specifications (T/S), which govern plant systems configurations and operations, are in conformance with the requirements of the Final Safety Analysis Report (FSAR) as amended, and the requirements of the Safety Evaluation Report (SER) as supplemented. A comparative audit of the FSAR as amended, and the SER as supplemented was performed with the Perry T/S. Several discrepancies were identified and subsequently resolved through telephone conversations with the staff reviewer and the utility representative. Pending completion of the resolutions noted in Parts 3 and 4 of this report, the Perry Nuclear Power Plant Unit 1 T/S, to the extent reviewed, are in conformance with the FSAR and SER

  7. Evaluation of Watts Bar Nuclear Plant Unit 1 Technical Specifications

    International Nuclear Information System (INIS)

    Baxter, D.E.; Bruske, S.J.

    1985-08-01

    This document was prepared for the Nuclear Regulatory Commission (NRC) to assist them in determining whether the Watts Bar Nuclear Plant Unit 1 Technical Specifications (T/S), which govern plant systems configurations and operations, are in conformance with the assumption of the Final Safety Analysis Report (FSAR) as amended, and the requirements of the Safety Evaluation Report (SER) as supplemented. A comparative audit of the FSAR as amended, and the SER as supplemented was performed with the Watts Bar T/S. Several discrepancies were identified and subsequently resolved through discussions with the cognizant NRC reviewer, NRC staff reviewers and/or utility representatives. The Watts Bar Nuclear Plant Unit 1 T/S, to the extent reviewed, are in conformance with the FSAR and SER

  8. Evaluation of Shoreham Nuclear Power Station, Unit 1 technical specifications

    International Nuclear Information System (INIS)

    Baxter, D.E.; Bruske, S.J.

    1985-08-01

    This document was prepared for the Nuclear Regulatory Commission (NRC) to assist them in determining whether the Shoreham Nuclear Power Station Unit 1 Technical Specifications (T/S), which govern plant systems configurations and operations, are in conformance with the assumptions of the Final Safety Analysis Report (FSAR) as amended, and the requirements of the Safety Evaluation Report (SER) as supplemented. A comparative audit of the FSAR as amended, and the SER as supplemented was performed with the Shoreham T/S. Several discrepancies were identified and subsequently resolved through discussions with the cognizant NRC reviewer, NRC staff reviewers and/or utility representatives. The Shoreham Nuclear Power Station Unit 1 T/S, to the extent reviewed, are in conformance with the FSAR and SER

  9. Containment Response Analysis for Equipment Qualification of Kori Nuclear Power Plant Unit 3 and 4

    Energy Technology Data Exchange (ETDEWEB)

    Byun, Choong Sup; Song, Dong Soo; Hwang, Yong Jun [Korea Electric Power Research Institute, Taejon (Korea, Republic of); Seo, Kwi Hyun; Song, Wan Jung [ENERGEO Inc., Sungnam (Korea, Republic of)

    2006-07-01

    Equipment that is used to perform a necessary safety function must be capable of maintaining functional operability under all service condition postulated to occur during the installed life for the time it is required. The pressure and temperature analyses for loss of coolant accident and main steam line break accident provide the bounding test envelope inside containment for the operability evaluation of safety equipment in harsh environmental. This paper describes the results of the containment pressure and temperature analysis for the equipment qualification (EQ) envelopes of Kori unit 3 and 4.

  10. Development of the Kori 1 simulator for the MCR modernization

    Energy Technology Data Exchange (ETDEWEB)

    Lee, Myeong Soo; Hong, Jin Hyuk [KHNP Central Research Institute, Daejeon (Korea, Republic of)

    2012-10-15

    Kori Unit 1 is the first commercial nuclear power reactor, pressurized water reactor that came into commercial service in April 1978 and is licensed for continued operation till 2017. The Main Control Board (MCB) was designed and was not applied the Human Factor Engineering (HFE) program during the construction phase but was performed the D CRDR (Detailed Control Room Design Review) as a post-TMI action. So Korea Hydro Nuclear Power, Ltd. (KHNP) has selected the hybrid type MCR by considering the existing equipment conditions and the operability of the plant as follows. .. Operator console upgrade, .. Plant Computer System (PCS) upgrade, .. PAS (Plant alarm System) upgrade, .. Remote Shutdown Panel (RSP) upgrade, .. Electrical control panel upgrade, and .. Interior improvement including lighting system. KINS will conduct the safety review of the new control room in Kori 1 as the same review level of construction permit (CP), operating license (OL) process. KHNP Central research Institute (CRI) developed a Kori 1 Full Scope Simulator (FSS) to have HFE Verification and Validation Test and operator training for the new modernized I and C of the MCR. This paper describes the several features and the results of the Kori 1 FSS. The NSSS thermal hydraulics model for the Kori 1 Simulator was developed by using the RELAP5 RT code, the real time version of RELAP5 developed by Idaho National Laboratory(INL). It could be configured from RELAP5/MOD3.2 by choosing the correct set of conditional coding and the base RELAP5 nodalization was shown in Figure 2. The NESTLE is a true two energy group neutronics code that computes the neutron flux and power for each node at every time step.

  11. Planning for decommissioning of Ignalina Nuclear Power Plant Unit-1

    International Nuclear Information System (INIS)

    Poskas, P.; Poskas, R.; Zujus, R.

    2002-01-01

    In accordance to Ignalina NPP Unit 1 Closure Law, the Government of Lithuania approved the Ignalina NPP Unit 1 Decommissioning Program until 2005. For enforcement of this program, the plan of measures for implementation of the program was prepared and approved by the Minister of Economy. The plan consists of two parts, namely technical- environmental and social-economic. Technical-environmental measures are mostly oriented to the safe management of spent nuclear fuel and operational radioactive waste stored at the plant and preparation of licensing documents for Unit 1 decommissioning. Social-economic measures are oriented to mitigate the negative social and economic impact on Lithuania, inhabitants of the region, and, particularly, on the staff of Ignalina NPP by means of creating favorable conditions for a balanced social and economic development of the region. In this paper analysis of planned radioactive waste management technologies, licensing documents for decommissioning, other technical-environmental and also social-economic measures is presented. Specific conditions in Lithuania important for defining the decommissioning strategy are highlighted. (author)

  12. ATWS analysis for Browns Ferry Nuclear Plant Unit 1

    International Nuclear Information System (INIS)

    Dallman, R.J.; Jouse, W.C.

    1985-01-01

    Analyses of postulated Anticipated Transients Without Scram (ATWS) were performed at the Idaho National Engineering Laboratory (INEL). The Browns Ferry Nuclear Plant Unit 1 (BFNP1) was selected as the subject of this work because of the cooperation of the Tennessee Valley Authority (TVA). The work is part of the Severe Accident Sequence Analysis (SASA) Program of the US Nuclear Regulatory Commission (NRC). A Main Steamline Isolation Valve (MSIV) closure served as the transient initiator for these analyses, which proceeded a complete failure to scram. Results from the analyses indicate that operator mitigative actions are required to prevent overpressurization of the primary containment. Uncertainties remain concerning the effectiveness of key mitigative actions. The effectiveness of level control as a power reduction procedure is limited. Power level resulting from level control only reduce the Pressure Suppression Pool (PSP) heatup rate from 6 to 4 0 F/min

  13. Sludge Removal and Retrieval of Foreign Object in SG of Kori Nuclear Power Plant, Unit 4

    International Nuclear Information System (INIS)

    Jeong, Wootae; Kim, Sangtae; Kim, Youngkug; Kang, Seokchul

    2014-01-01

    Sludge deposit was removed and foreign objects were inspected and retrieved on secondary side tube sheet of the SG during January 23 and February 22, April 15 and 27 in 2013. FOLAS-I lancing system, video probe and retrieval tools were used for lancing and foreign object removal respectively. Operators of the lancing system participated in mock-up training before doing the service to minimize operation time and radiation dose. Foreign objects were searched on top of 7 th TSP (tube support plate), on annulus and in tube bundle. Four objects were found and removed on annulus and in tube bundle. During the 21 st OH of Kori NPP unit 4, we removed 345.9 kilo gram of sludge and four foreign objects from three steam generators. Foreign objects which were removed from inside of SG showed us that relatively large object such as the hooked bolt might exists in steam generators. We can conclude that identifying and removing foreign object is very important to avoid possible tube failure. Removing circular metal of 152.4 gram also was successfully removed

  14. 75 FR 36700 - Exelon Generation Company, LLC; Three Mile Island Nuclear Station, Unit 1; Environmental...

    Science.gov (United States)

    2010-06-28

    ...; Three Mile Island Nuclear Station, Unit 1; Environmental Assessment and Finding of No Significant Impact... Company, LLC (the licensee), for operation of Three Mile Island Nuclear Station, Unit 1 (TMI-1), located... Three Mile Island Nuclear Station, Units 1 and 2, NUREG-0552, dated December 1972, and Generic...

  15. Millstone Unit 1 plant vulnerabilities during postulated severe nuclear accidents

    International Nuclear Information System (INIS)

    Khalil, Y.F.

    1993-01-01

    Generic Letter 88-20, Supplement No. 1 (Ref. 1), issued by the Nuclear Regulatory Commission (NRC) requested all licensees holding operating licenses and construction permits for nuclear power reactor facilities to perform Individual Plant Examinations (IPE) of their plant(s) for severe accident vulnerabilities and to submit the results to the Commission. This paper summarizes the major Front-End (Level-1 PRA) and Back-End (Level-2 PRA) insights gained from the Millstone Unit 1 (MP-1) IPE study. No major plant vulnerabilities have been identified from a Front-End perspective. The Back-End analysis, however, has identified two potential containment vulnerabilities during postulated events that progress beyond the Design Basis Accidents (DBAs), namely, (1) MP-1 is dominated by early source term releases that would occur within a six-hour time frame from time of accident initiation, or reactor trip, and (2) MP-1 containment is somewhat vulnerable to leak-type failure through the drywell head. As a result of the second finding, a recommendation currently under evaluation, has been made to increase the drywell head bolt's preload from 54 Kips to resist the containment design pressure value (62 psig)

  16. Fan Cooler Operation in Kori 1 for Mitigating Severe Accident

    International Nuclear Information System (INIS)

    Suh, Nam Duk; Park, Jae Hong

    2005-01-01

    The Korea Ministry of Science and Technology (MOST) issued the 'Policy on Severe Accident of Nuclear Power Plants' in August 2001. According to the policy it was required for the licensee to develop a plant specific severe accident management guideline (SAMG) and to implement it. Thus the utility has made an implementation plan to develop SAMGs for operating plants. The SAMG for Kori unit 1 was submitted to the government on January 2004. Since then, the government trusted KINS to review the submitted SAMG in view of its feasibility and effectiveness. The first principle of the developed SAMG is to use only the available facilities as it is without introducing any system change. Because Kori-1 has no mitigative facility against combustible gases during severe accident, it relies heavily both on spray and on fan cooler systems to control the containment condition. Thus one of the issues raised during the review is to know whether the fan coolers which are designed for DBA LOCA can be effective in mitigating the severe accident conditions. This paper presents an analysis result of fan cooler operation in controlling the containment condition during severe accident of Kori 1

  17. Design and implementation of an advanced protection system for the Shin-Kori 3 and 4 nuclear power plant

    International Nuclear Information System (INIS)

    Kim, Yonghak; Choi, Woongseock; Kwon, Jongsoo; Wilkosz, Stephen J.; Ridolfo, Charles F.; Yanosy, Paul L.

    2008-01-01

    The Nuclear Power Industry is currently embracing modern digital technology for upgrades to existing Instrumentation and Control (I and C) infrastructures as well as for incorporation into the next generation of new plants which will be coming 'on-line' during the next decade. This technology is being fully exploited for the next generation of advanced plant protection systems which will be initially deployed on the Shin-Kori 3 and 4 Nuclear Power Plant in the Republic of Korea. The system design for this plant protection system is being performed by the Korea Power Engineering Company (KOPEC) and builds upon the past generation of digital safety systems which were initially implemented at Ulchin 5 and 6. The advanced protection system is an evolution of this existing design and includes a number of improved operating attributes including: · Integration of Reactor Protection, Engineered Safety Features Actuation, and Qualified Indication and Alarm functions which were previously implemented by separate systems in the past. · Use of a 'soft control' interface which provides convenient accessibility to the safety systems from 'operator workstations' · Implementation of a Large Display Panel (LDP) which provides a consistent and constant representation of the overall plant state and of the plant safety status. The equipment for the advanced plant protection system is being provided by Westinghouse Electric Company (WEC) and utilizes the Westinghouse 'Common Q' Standardized qualified platform (where 'Q' denotes 'qualified'). The 'Common Q' platform is comprised of commercially dedicated Programmable Logic Controllers (PLC's), color-graphic Flat Panel Displays (FPD's) with integral touch screens, and high speed data communication links. It is a mature product that is in wide use for a number of safety-related applications. Among its key attributes are: · High overall system availability, which is achieved via use of a multiple channel configuration that is tolerant

  18. Optimal replacement and inspection periods of safety and control boards in Wolsung nuclear power plant unit 1

    International Nuclear Information System (INIS)

    Mok, Jin Il

    1993-02-01

    In nuclear power plants, the safety and control systems are important for operating and maintaining safety of nuclear power plants. Due to the failure of the instrument and control devices of nuclear power plants caused by aging, nuclear power plants occasionally trip. Since the start of first commercial operation of Kori nuclear power plant (NPP) unit 1, the trips caused by instrument and control systems account for 28% of total trips of NPPs in Korea. Even a single trip of a nuclear power plant causes an extravagant economical loss and deteriorates public acceptance of nuclear power plants. Therefore, the replacement of the instrument and control devices with proper consideration of the aging effect is necessary in order to prevent the inadvertent trip. In this work we investigated the optimal replacement periods of the digital control computer's (DCC) and the programmable digital comparator's (PDC) electronic circuit boards of Wolsung nuclear power plant Unit 1. We first derived mathematical models which calculate optimal replacement periods for electronic circuit boards of digital control computer (DCC) and for those of the programmable digital comparator (PDC) in Wolsung NPP unit 1. And we analytically obtained the optimal replacement periods of electronic circuit boards by using these models. We compared these periods with the replacement periods currently used at Wolsung NPP Unit. The periods used at Wolsung is not based on mathematical analysis, but on empirical knowledge. As a consequence, the optimal replacement periods analytically obtained for the electronic circuit boards of DCC and those used in the field shown small difference : the optimal replacement periods analytically obtained for the electronic circuit boards of PDC are shorter than those used in the field in general. The engineered safeguards of Wolsung nuclear power plant unit 1 contains redundant systems of 2-out-of-3 logic which are not operating under normal conditions but they are called

  19. 78 FR 77726 - Exelon Generation Company, LLC Three Mile Island Nuclear Station, Unit 1

    Science.gov (United States)

    2013-12-24

    ... Three Mile Island Nuclear Station, Unit 1 AGENCY: Nuclear Regulatory Commission. ACTION: Exemption... License No. DPR-50, which authorizes operation of the Three Mile Island Nuclear Station, Unit 1 (TMI-1... Facility Operating License No. DPR-50, which authorizes operation of the Three Mile Island Nuclear Station...

  20. Science, Society, and America's Nuclear Waste: Nuclear Waste, Unit 1. Teacher Guide. Second Edition.

    Science.gov (United States)

    Department of Energy, Washington, DC. Office of Civilian Radioactive Waste Management, Washington, DC.

    This guide is Unit 1 of the four-part series Science, Society, and America's Nuclear Waste produced by the U.S. Department of Energy's Office of Civilian Radioactive Waste Management. The goal of this unit is to help students establish the relevance of the topic of nuclear waste to their everyday lives and activities. Particular attention is…

  1. Accident analysis of Fukushima Daiichi Nuclear Power Station unit 1

    International Nuclear Information System (INIS)

    Kobayashi, Masahide; Narabayashi, Tadashi; Tsuji, Masashi; Chiba, Go; Nagata, Yasunori; Shimoe, Tomohiro

    2015-01-01

    As a result of the Great East Japan Earthquake that occurred on 11 March 2011, all AC and DC power at the Fukushima Daiichi NPP units 1 to 3 were lost soon after the tsunami. The core cooling function was lost, and the cores of units 1 to 3 were damaged. The purpose of this work is to clarify the progress of the accident in unit 1, which was damaged the earliest among the 3 units. Therefore, an original severe accident analysis code was developed, and the progress of the accident was evaluated from the analysis results and the actual data. As a result, the leakage path from a pressure vessel was clarified, and some lessons and knowledge were gained. (author)

  2. Development of software for the microsimulator for the KO-RI nuclear power plant unit 2

    International Nuclear Information System (INIS)

    Seok, H.; No, H.C.; Cho, S.J.; Park, S.D.; Jun, H.Y.; Lee, Y.K.

    1994-01-01

    A workstation-based real-time simulator for two-loop pressurized water reactor plants is developed for classroom training in support of a full-scale simulator, on-site transient analysis, and engineering studies. The present simulator consists of three functional modules: plant module, graphic module, and man-machine interaction module. The plant module includes models for the core kinetics, reactor coolant system, steam generator, main steam line, balance of plant, and control and protection system. Each of the models is optimized to obtain the capability of real-time simulation. The graphic module is designed to provide the user with more information at a glance by dynamically displaying schematic diagrams of the systems, symbols indicating the operating status of each component, trend curves, and the main control room. As tools for the man-machine interface, the man-machine interaction model uses a color cathode ray tube monitor, a standard keyboard, and the mouse. The interactive communication module receives parameters from the user via the keyboard and mouse, and transfers them to the plant module so as to enable the user to perform his specific actions. This module provides the user with various initiating events (malfunctions and manual controls) through SYSTEM, CONTROL ROOM, and ACCIDENTS menus, and thus a wide range of nuclear steam supply system transients can be easily simulated. The FISA-2/WS is verified through comparisons with analytical solutions, separated tests and integral tests, and predictions by RETRAN-2 and RELAP5/MOD3

  3. 76 FR 40754 - Duke Energy Carolinas, LLC Catawba Nuclear Station, Units 1 and 2; McGuire Nuclear Station, Units...

    Science.gov (United States)

    2011-07-11

    ... NUCLEAR REGULATORY COMMISSION [NRC-2011-0100; Docket Nos. 50-413 and 50-414; Docket Nos. 50-369 and 50-370; Docket Nos. 50-269, 50-270, And 50-287] Duke Energy Carolinas, LLC Catawba Nuclear Station, Units 1 and 2; McGuire Nuclear Station, Units 1 and 2; Oconee Nuclear Station, Units 1, 2, and 3; Notice...

  4. 76 FR 24538 - Duke Energy Carolinas, LLC; Catawba Nuclear Station, Units 1 and 2; McGuire Nuclear Station...

    Science.gov (United States)

    2011-05-02

    ... NUCLEAR REGULATORY COMMISSION [Docket Nos. 50-413 and 50-414; NRC-2011-0100; Docket Nos. 50-369 and 50-370; Docket Nos. 50-269, 50-270, and 50-287] Duke Energy Carolinas, LLC; Catawba Nuclear Station, Units 1 and 2; McGuire Nuclear Station, Units 1 and 2; Oconee Nuclear Station, Units 1, 2, and 3...

  5. Subsidence analysis Forsmark nuclear power plant - unit 1

    International Nuclear Information System (INIS)

    Bono, Nancy; Fredriksson, Anders; Maersk Hansen, Lars

    2010-12-01

    On behalf of SKB, Golder Associates Ltd carried out a risk analysis of subsidence during Forsmark nuclear power plant in the construction of the final repository for spent nuclear fuel near and below existing reactors. Specifically, the effect of horizontal cracks have been studied

  6. Development of a Real-Time Thermal Performance Diagnostic Monitoring system Using Self-Organizing Neural Network for Kori-2 Nuclear Power Unit

    International Nuclear Information System (INIS)

    Kang, Hyun Gook; Seong, Poong Hyun

    1996-01-01

    In this work, a PC-based thermal performance monitoring system is developed for the nuclear power plants. the system performs real-time thermal performance monitoring and diagnosis during plant operation. Specifically, a prototype for the Kori-2 nuclear power unit is developed and examined is very difficult because the system structure is highly complex and the components are very much inter-related. In this study, some major diagnostic performance parameters are selected in order to represent the thermal cycle effectively and to reduce the computing time. The Fuzzy ARTMAP, a self-organizing neural network, is used to recognize the characteristic pattern change of the performance parameters in abnormal situation. By examination, the algorithm is shown to be ale to detect abnormality and to identify the fault component or the change of system operation condition successfully. For the convenience of operators, a graphical user interface is also constructed in this work. 5 figs., 3 tabs., 11 refs. (Author)

  7. Development of the Real-time Core and Thermal-Hydraulic Models for Kori-1 Simulator

    Energy Technology Data Exchange (ETDEWEB)

    Hong, Jin Hyuk; Lee, Myeong Soo; Hwang, Do Hyun; Byon, Soo Jin [KEPRI, Daejeon (Korea, Republic of)

    2010-10-15

    The operation of the Kori-Unit 1 (1723.5MWt) is expanded to additional 10 years with upgrades of the Main Control Room (MCR). Therefore, the revision of the procedures, performance tests and works related with the exchange of the Main Control Board (MCB) are currently carried out. And as a part of it, the fullscope simulator for the Kori-1 is being developed for the purpose of the pre-operation and emergence response capability for the operators. The purpose of this paper is to report on the performance of the developed neutronics and thermal-hydraulic (TH) models of Kori Unit 1 simulator. The neutronics model is based on the NESTLE code and TH model based on the RELAP5/MOD3 thermal-hydraulics analysis code which was funded as FY-93 LDRD Project 7201 and is running on the commercial simulator environment tool (the 3KeyMaster{sup TM} of the WSC). As some examples for the verification of the developed neutronics and TH models, some figures are provided. The outputs of the developed neutronics and TH models are in accord with the Nuclear Design Report (NDR) and Final Safety Analysis Report (FSAR) of the reference plant

  8. Nuclear safety inspection in treatment process for SG heat exchange tubes deficiency of unit 1, TNPS

    International Nuclear Information System (INIS)

    Zhang Chunming; Song Chenxiu; Zhao Pengyu; Hou Wei

    2006-01-01

    This paper describes treatment process for SG heat exchange tubes deficiency of Unit 1, TNPS, nuclear safety inspection of Northern Regional Office during treatment process for deficiency and further inspection after deficiency had been treated. (authors)

  9. 75 FR 8757 - Nebraska Public Power District, Cooper Nuclear Station, Unit 1; Notice of Availability of the...

    Science.gov (United States)

    2010-02-25

    ..., Cooper Nuclear Station, Unit 1; Notice of Availability of the Draft Supplement 41 to the Generic... Renewal of Cooper Nuclear Station, Unit 1 Notice is hereby given that the U.S. Nuclear Regulatory... operating license DPR-46 for an additional 20 years of operation for Cooper Nuclear Station, Unit 1 (CNS-1...

  10. Interim reliability evaluation program: analysis of the Arkansas Nuclear One. Unit 1 Nuclear Power Plant

    International Nuclear Information System (INIS)

    Kolb, G.J.; Kunsman, D.M.; Bell, B.J.

    1982-06-01

    This report represents the results of the analysis of Arkansas Nuclear One (ANO) Unit 1 nuclear power plant which was performed as part of the Interim Reliability Evaluation Program (IREP). The IREP has several objectives, two of which are achieved by the analysis presented in this report. These objectives are: (1) the identification, in a preliminary way, of those accident sequences which are expected to dominate the public health and safety risks; and (2) the development of state-of-the-art plant system models which can be used as a foundation for subsequent, more intensive applications of probabilistic risk assessment. The primary methodological tools used in the analysis were event trees and fault trees. These tools were used to study core melt accidents initiated by loss of coolant accidents (LOCAs) of six different break size ranges and eight different types of transients

  11. 75 FR 18572 - Supplemental Environmental Impact Statement for Sequoyah Nuclear Plant Units 1 and 2 License...

    Science.gov (United States)

    2010-04-12

    ... TENNESSEE VALLEY AUTHORITY Supplemental Environmental Impact Statement for Sequoyah Nuclear Plant... National Environmental Policy Act. TVA will prepare a supplemental environmental impact statement (SEIS) to update information in the 1974 Final Environmental Statement for Sequoyah Nuclear Plant Units 1 and 2...

  12. Nuclear design report for Ulchin nuclear power plant unit 1, cycle 7

    Energy Technology Data Exchange (ETDEWEB)

    Kim, Yong Rae; Park, Yong soo [Korea Atomic Energy Research Institute, Taejon (Korea, Republic of)

    1995-04-01

    This report presents nuclear design calculations for Cycle 7 of Ulchin Unit 1. Information is given on fuel loading, power density distributions, reactivity coefficients, control rod worths and operational limits. In addition, the report contains all necessary data for the startup tests including predicted values for the comparison with the measured data. The reload consists of 56 KOFA`s enriched by nominally 4.00 w/o U{sub 235}. Among the KOFA`s 36 fuel assemblies contain gadolinia rods. The fuel assemblies in the core are arranged in a low leakage loading pattern. The cycle length of Cycle 7 amounts to 355 EFPD corresponding to a cycle burnup of 14280 MWD/MTU. (Author) 8 refs., 55 figs., 21 tabs.

  13. Nuclear design report for Yonggwang nuclear power plant unit 1 cycle 9

    Energy Technology Data Exchange (ETDEWEB)

    Cho, Young chul; Kim, Jae Hak; Song, Jae Woong [Korea Atomic Energy Research Institute, Taejon (Korea, Republic of)

    1995-03-01

    This report presents nuclear design calculations for Cycle 6 of Yonggwng Unit 1. Information is given on fuel loading, power density distributions, reactivity coefficients, control rod worths and operational limits. In addition, the report contains all necessary data for the startup tests including predicted values for the comparison with the measured data. The reload consists of 76 KOFA`s enriched by nominally 4.00 w/o U{sub 235}. Among the KOFA`s, 60 fuel assemblies contain gadolinia rods. The fuel assemblies in the core are arranged in a low leakage loading pattern. The cycle length of Cycle 9 amounts to 434 EFPD corresponding to a cycle burnup of 17470 MWD/MTU. (Author) 8 refs., 55 figs., 19 tabs.

  14. Nuclear design report for Ulchin nuclear power plant unit 1, cycle 6

    Energy Technology Data Exchange (ETDEWEB)

    Zee, Sung Kyun; Kim, Yong Rae; Park, Yong Soo; Cho, Byeong Ho; Lee, Sang Keun; Ahn, Dawk Hwan [Korea Atomic Energy Research Institute, Taejon (Korea, Republic of)

    1993-12-01

    This report presents nuclear design calculations for cycle 6 of Ulchin unit 1. Information is given on fuel loading, power density distributions, reactivity coefficients, control rod worths and operational limits. In addition, the report contains all necessary data for the startup tests including predicted values for the comparison with the measured data. The reload consists of 64 KOFA`s enriched by nominally 3.70 w/o U{sub 235}. Among the KOFA`s, 32 fuel assemblies contain gadolinia rods. The fuel assemblies in the core are arranged in a low leakage loading pattern. The cycle length of cycle 6 amounts to 369 EFPD corresponding to a cycle burnup of 14850 MWD/MTU. (Author) 8 refs., 55 figs., 17 tabs.

  15. 76 FR 19148 - PSEG Nuclear, LLC, Hope Creek Generating Station and Salem Nuclear Generating Station, Units 1...

    Science.gov (United States)

    2011-04-06

    ... NUCLEAR REGULATORY COMMISSION [Docket Nos. 50-272, 50-311, 50-354; NRC-2009-0390 and NRC-2009-0391] PSEG Nuclear, LLC, Hope Creek Generating Station and Salem Nuclear Generating Station, Units 1 and 2..., DPR-70, and DPR-75 for an additional 20 years of operation for the Hope Creek Generating Station (HCGS...

  16. Summary revaluation of energetic start-up of the unit 1 of nuclear power plant Mochovce

    International Nuclear Information System (INIS)

    Sarvaic, I.; Miskolci, M.

    1998-01-01

    The document contents stage revaluation of energetic start-up of the unit 1 of nuclear power plant Mochovce. Test results of the stage of energetic start-up are summarized in the document, valuation of important systems and block devices as well as fulfilling the operation limits and conditions has been performed. On that base conclusions and recommendations for start-up the unit 2 and for commercial operation of the unit 1 are elaborated. The valuation has been elaborated by a scientific management for start-up nuclear power plant Mochovce of nuclear safety of nuclear power facilities. Scientific management for start-up of nuclear power plant Mochovce performed continuous valuation of individual power levels after ending of each individual level and it gave its valuation to energy power level with recommendations and conditions for further start-up process and operation. Scientific management finished its activity at the unit 1 of nuclear power plant Mochovce according to a statute of scientific management for start-up after successful completion of conclusive block run. Scientific management group was founded in February 1998 at nuclear power plant Mochovce. Its members are experts from Slovak, Czech, Russian and French organizations which are participating in power plant completion. Members are listed in a supplement No. 2

  17. Station black out of Fukushima Daiichi Nuclear Power Station Unit 1 was not caused by tsunamis

    International Nuclear Information System (INIS)

    Ito, Yoshinori

    2013-01-01

    Station black out (SBO) of Fukushima Daiichi Nuclear Power Station Unit 1 would be concluded to be caused before 15:37 on March 11, 2011 because losses of emergency ac power A system was in 15:36 and ac losses of B system in 15:37 according to the data published by Tokyo Electric Power Co. (TEPCO) in May 10, 2013. Tsunami attacked the site of Fukushima Daiichi Nuclear Power Station passed through the position of wave amplitude meter installed at 1.5 km off the coast after 15:35 and it was also recognized tsunami arrived at the coast of Unit 4 sea side area around in 15:37 judging from a series of photographs taken from the south side of the site and general knowledge of wave propagation. From a series of photographs and witness testimony, tsunami didn't attack Fukushima Daiichi Nuclear Power Station uniformly and tsunami's arrival time at the site of Unit 1 would be far later than arrival time at the coast of Unit 4 sea side area, which suggested it would be around in 15:39. TEPCO insisted tsunami passed through 1.5 km off the coast around in 15:33 and clock of wave amplitude meter was incorrect, which might be wrong. Thus SBO of Fukushima Daiichi Nuclear Power Station Unit 1 occurred before tsunami's arrival at the site of Unit 1 and was not caused by tsunami. (T. Tanaka)

  18. Evaluation on Cooling Performance of Containment Fan Cooler during Design Basis Accident with Loss of Offsite Power for Kori 3 and 4 Nuclear Power Plant

    Energy Technology Data Exchange (ETDEWEB)

    Lee, Sung Bok; Lee, Sang Won [Korea Hydro and Nuclear Power Co., Ltd., Daejeon (Korea, Republic of); Park, Young Chan [Atomic Creative Technology Co., LTD., Daejeon (Korea, Republic of)

    2007-10-15

    The purpose of this study is to evaluate cooling performance of containment fan cooler units and to review a technical background related to Generic Letter 96-06. In case that design basis accident (DBA) and loss of offsite power (LOOP) occurs, component cooling water (CCW) pumps cannot provide the cooling water source to fan cooler units while fan coolers coast down. Fan cooler units and CCW pumps are restarted by emergency diesel generator (EDG) operation and it takes about 30 seconds. In this scenario, before the EDG restarts and CCW flowrate is restored, heated air in the containment passes through coil of fan cooler units without cooling water source. In this situation, the boiling of water in the fan cooler units may occur. Restarting of CCW pumps may bring about condensation by injected cooling water and water hammer may occur. This thermal-hydraulic effect is sensitive to system configuration, i.e system pressure, containment pressure/temperature, EDG restarting time, etc. In this study, the evaluation of containment fan cooler units was performed for Kori 3 and 4 nuclear power plant.

  19. Pressurized thermal shock evaluation of the Calvert Cliffs Unit 1 Nuclear Power Plant

    Energy Technology Data Exchange (ETDEWEB)

    Abbott, L [ed.

    1985-09-01

    An evaluation of the risk to the Calvert Cliffs Unit 1 nuclear power plant due to pressurized thermal shock (PTS) has been completed by Oak Ridge National Laboratory (ORNL) with the assistance of several other organizations. This evaluation was part of a Nuclear Regulatory Commission program designed to study the PTS risk to three nuclear plants, the other two plants being Oconee Unit 1 and H.B. Robinson Unit 2. The specific objectives of the program were to (1) provide a best estimate of the frequency of a through-the-wall crack in the pressure vessel at each of the three plants, together with the uncertainty in the estimated frequency and its sensitivity to the variables used in the evaluation; (2) determine the dominant overcooling sequences contributing to the estimated frequency and the associated failures in the plant systems or in operator actions; and (3) evaluate the effectiveness of potential corrective measures.

  20. Pressurized thermal shock evaluation of the Calvert Cliffs Unit 1 Nuclear Power Plant

    International Nuclear Information System (INIS)

    Abbott, L.

    1985-09-01

    An evaluation of the risk to the Calvert Cliffs Unit 1 nuclear power plant due to pressurized thermal shock (PTS) has been completed by Oak Ridge National Laboratory (ORNL) with the assistance of several other organizations. This evaluation was part of a Nuclear Regulatory Commission program designed to study the PTS risk to three nuclear plants, the other two plants being Oconee Unit 1 and H.B. Robinson Unit 2. The specific objectives of the program were to (1) provide a best estimate of the frequency of a through-the-wall crack in the pressure vessel at each of the three plants, together with the uncertainty in the estimated frequency and its sensitivity to the variables used in the evaluation; (2) determine the dominant overcooling sequences contributing to the estimated frequency and the associated failures in the plant systems or in operator actions; and (3) evaluate the effectiveness of potential corrective measures

  1. 76 FR 72007 - ZionSolutions, LLC; Zion Nuclear Power Station, Units 1 and 2; Exemption From Certain Security...

    Science.gov (United States)

    2011-11-21

    ... NUCLEAR REGULATORY COMMISSION [Docket Nos. 50-295 and 50-304; NRC-2011-0244] ZionSolutions, LLC; Zion Nuclear Power Station, Units 1 and 2; Exemption From Certain Security Requirements 1.0 Background Zion Nuclear Power Station (ZNPS or Zion), Unit 1, is a Westinghouse 3250 MWt Pressurized Water Reactor...

  2. 76 FR 24064 - Arizona Public Service Company, Palo Verde Nuclear Generating Station, Units 1, 2, and 3, Notice...

    Science.gov (United States)

    2011-04-29

    ... Service Company, Palo Verde Nuclear Generating Station, Units 1, 2, and 3, Notice of Issuance of Renewed... Company (licensee), the operator of the Palo Verde Nuclear Generating Station, Units 1, 2, and 3 (PVNGS... Plants: Supplement 43, Regarding Palo Verde Nuclear Generating Station,'' issued January 2011, discusses...

  3. 75 FR 43572 - Duke Energy Carolinas, LLC, McGuire Nuclear Station, Units 1 and 2; Environmental Assessment and...

    Science.gov (United States)

    2010-07-26

    ... NUCLEAR REGULATORY COMMISSION [Docket Nos. 50-369 and 50-370; NRC-2010-0259] Duke Energy Carolinas, LLC, McGuire Nuclear Station, Units 1 and 2; Environmental Assessment and Finding of No Significant... Energy Carolinas, LLC (the licensee), for operation of the McGuire Nuclear Station, Units 1 and 2...

  4. 75 FR 43571 - Duke Energy Carolinas, LLC; Catawba Nuclear Station, Units 1 and 2; Environmental Assessment And...

    Science.gov (United States)

    2010-07-26

    ... NUCLEAR REGULATORY COMMISSION [Docket Nos. 50-413 and 50-414; NRC-2010-0260] Duke Energy Carolinas, LLC; Catawba Nuclear Station, Units 1 and 2; Environmental Assessment And Finding of No Significant... Energy Carolinas, LLC (the licensee), for operation of the Catawba Nuclear Station, Units 1 and 2...

  5. Analysis of internal events for the Unit 1 of the Laguna Verde Nuclear Power Station. Appendixes

    International Nuclear Information System (INIS)

    Huerta B, A.; Lopez M, R.

    1995-01-01

    This volume contains the appendices for the accident sequences analysis for those internally initiated events for Laguna Verde Unit 1, Nuclear Power Plant. The appendix A presents the comments raised by the Sandia National Laboratories technical staff as a result of the review of the Internal Event Analysis for Laguna Verde Unit 1 Nuclear Power Plant. This review was performed during a joint Sandia/CNSNS multi-day meeting by the end 1992. Also included is a brief evaluation on the applicability of these comments to the present study. The appendix B presents the fault tree models printed for each of the systems included and.analyzed in the Internal Event Analysis for LVNPP. The appendice C presents the outputs of the TEMAC code, used for the cuantification of the dominant accident sequences as well as for the final core damage evaluation. (Author)

  6. Analysis of internal events for the Unit 1 of the Laguna Verde Nuclear Power Station. Appendixes

    International Nuclear Information System (INIS)

    Huerta B, A.; Lopez M, R.

    1995-01-01

    This volume contains the appendices for the accident sequences analysis for those internally initiated events for Laguna Verde Unit 1, Nuclear Power Plant. The appendix A presents the comments raised by the Sandia National Laboratories technical staff as a result of the review of the Internal Event Analysis for Laguna Verde Unit 1 Nuclear Power Plant. This review was performed during a joint Sandia/CNSNS multi-day meeting by the end 1992. Also included is a brief evaluation on the applicability of these comments to the present study. The appendix B presents the fault tree models printed for each of the systems included and analyzed in the Internal Event Analysis for LVNPP. The appendice C presents the outputs of the TEMAC code, used for the cuantification of the dominant accident sequences as well as for the final core damage evaluation. (Author)

  7. The software testing of PPS for shin Ulchin nuclear power plant units 1 and 2

    International Nuclear Information System (INIS)

    Kang, Dong Pa; Park, Cheol Lak; Cho, Chang Hui; Sohn, Se Do; Baek, Seung Min

    2012-01-01

    The testing of software (S/W) is the process of analyzing a software item to detect the differences between existing and required conditions to evaluate the features of the software items. This paper introduces the S/W testing of Plant Protection System (PPS), as a safety system which actuate Reactor Trip (RT) and Engineered Safety Features (ESF) for Shin Ulchin Nuclear Power Plant Units 1 and 2 (SUN 1 and 2)

  8. 75 FR 8149 - Arizona Public Service Company, et al. Palo Verde Nuclear Generating Station, Units 1, 2, and 3...

    Science.gov (United States)

    2010-02-23

    ...] Arizona Public Service Company, et al. Palo Verde Nuclear Generating Station, Units 1, 2, and 3... NPF-74, issued to the Arizona Public Service Company (APS, or the licensee), for operation of the Palo Verde Nuclear Generating Station (PVNGS, the facility), Units 1, 2, and 3, respectively, located in...

  9. Upgrade of Control and Protection System of the Ignalina Nuclear Power Plant Units 1 and 2

    International Nuclear Information System (INIS)

    Wright, Ronald E.; Fletcher, Norman; Sidnev, Victor E.; Bickel, John H.; Vianello, Aldo; Pearsall, Raymond D.

    2003-01-01

    The Ignalina nuclear power plant (NPP) Units 1 and 2 are Soviet-designed, RBMK (Reaktor Bolshoi Moschnosti Kipyashchiy), channelized, large power-type reactors. The original-design electrical capacity for each unit was 1500 MW. Unit 1 began operating in 1983, and Unit 2 was started up in 1987. In 1994, the government of Lithuania agreed to accept grant support for the Ignalina NPP Safety Improvement Program with funding supplied by the Nuclear Safety Account of the European Bank for Reconstruction and Development (EBRD). As conditions for receiving this funding, the Ignalina NPP agreed to prepare a comprehensive safety analysis report that would undergo independent peer review after it was issued. The EBRD Safety Panel oversaw preparation and review of the report. In 1996, the safety analysis report for Unit 1 was completed and delivered to the EBRD. Part of the analyses covered anticipated transients without scram (ATWS). The analysis showed that some ATWS scenarios could lead to unacceptable consequences in <1 min. The EBRD Safety Panel recommended to the government of Lithuania that the Ignalina NPP develop and implement a program of compensatory measures for the control and protection system before the unit would be allowed to return to operation following its 1998 maintenance outage. A compensatory control and protection system that would mitigate the unacceptable consequences was designed, procured, manufactured, tested, and installed. The project was funded by U.S. Department of Energy

  10. The estimated evacuation time for the emergency planning zone of the Kori nuclear site, with a focus on the precautionary action zone

    Energy Technology Data Exchange (ETDEWEB)

    Lee, Jang Hee; Jeong, Jae Jun [School of Mechanical Engineering, Pusan National University, Busan (Korea, Republic of); Shin, Won Ki; Song, Eun Young; Cho, Cheol Woo [Div. of Nuclear Safety, Busan Metropolitan City, Busan (Korea, Republic of)

    2016-09-15

    The emergency planning zone (EPZ) of the city of Busan is divided into the precautionary actions zone (PAZ) and the urgent protective action planning zone; which have a 5-km radius and a 20-km to 21-km radius from the nuclear power plant site, respectively. In this study, we assumed that a severe accident occurred at Shin-Kori nuclear unit 3 and evaluated the dispersion speed of radiological material at each distance at various wind speeds, and estimated the effective dose equivalent and the evacuation time of PAZ residents with the goal of supporting off-site emergency action planning for the nuclear site. The total effective dose equivalent, which shows the effect of released radioactive materials on the residents, was evaluated using the RASCAL 4.2 program. In addition, a survey of 1,036 residents was performed using a standardized questionnaire, and the resident evacuation time according to road and distance was analyzed using the VISSIM 6.0 program. According to the results obtained using the VISSIM and RASCAL programs, it would take approximately 80 to 252.2 minutes for permanent residents to move out of the PAZ boundary, 40 to 197.2 minutes for students, 60 to 232.2 minutes for the infirm, such as elderly people and those in a nursing home or hospital, and 30 to 182.2 minutes for those temporarily within the area. Consequently, in the event of any delay in the evacuation, it is estimated that the residents would be exposed to up to 10 mSv·h-1 of radiation at the Exclusion Area Boundaries (EAB) boundary and 4-6 mSv·h-1 at the PAZ boundary. It was shown that the evacuation time for the residents is adequate in light of the time lapse from the initial moment of a severe accident to the radiation release. However, in order to minimize the evacuation time, it is necessary to maintain a system of close collaboration to avoid traffic congestion and spontaneous evacuation attempts.

  11. The estimated evacuation time for the emergency planning zone of the Kori nuclear site, with a focus on the precautionary action zone

    International Nuclear Information System (INIS)

    Lee, Jang Hee; Jeong, Jae Jun; Shin, Won Ki; Song, Eun Young; Cho, Cheol Woo

    2016-01-01

    The emergency planning zone (EPZ) of the city of Busan is divided into the precautionary actions zone (PAZ) and the urgent protective action planning zone; which have a 5-km radius and a 20-km to 21-km radius from the nuclear power plant site, respectively. In this study, we assumed that a severe accident occurred at Shin-Kori nuclear unit 3 and evaluated the dispersion speed of radiological material at each distance at various wind speeds, and estimated the effective dose equivalent and the evacuation time of PAZ residents with the goal of supporting off-site emergency action planning for the nuclear site. The total effective dose equivalent, which shows the effect of released radioactive materials on the residents, was evaluated using the RASCAL 4.2 program. In addition, a survey of 1,036 residents was performed using a standardized questionnaire, and the resident evacuation time according to road and distance was analyzed using the VISSIM 6.0 program. According to the results obtained using the VISSIM and RASCAL programs, it would take approximately 80 to 252.2 minutes for permanent residents to move out of the PAZ boundary, 40 to 197.2 minutes for students, 60 to 232.2 minutes for the infirm, such as elderly people and those in a nursing home or hospital, and 30 to 182.2 minutes for those temporarily within the area. Consequently, in the event of any delay in the evacuation, it is estimated that the residents would be exposed to up to 10 mSv·h-1 of radiation at the Exclusion Area Boundaries (EAB) boundary and 4-6 mSv·h-1 at the PAZ boundary. It was shown that the evacuation time for the residents is adequate in light of the time lapse from the initial moment of a severe accident to the radiation release. However, in order to minimize the evacuation time, it is necessary to maintain a system of close collaboration to avoid traffic congestion and spontaneous evacuation attempts

  12. Start up and commercial operation of Laguna Verde nuclear power plant. Unit 1

    International Nuclear Information System (INIS)

    Torres Ramirez, J.F.

    1991-01-01

    Prior to start up of Laguna Verde nuclear power plant preoperational tests and start tests were performed and they are described in its more eminent aspects. In relation to commercial operation of nuclear station a series of indicator were set to which allow the measurement of performance in unit 1, in areas of plant efficiency and personal safety. Antecedents. Laguna Verde station is located in Alto Lucero municipality in Veracruz state, 70 kilometers north-northeast from port of Veracruz and a 290 kilometers east-northeast from Mexico city. The station consist of two units manufactured by General Electric, with a nuclear system of vapor supply also called boiling water (BWR/5), and with a system turbine-generator manufactured by Mitsubishi. Each unit has a nominal power of 1931 MWt and a level design power of 675 Mwe and a net power of 654 Electric Megawatts

  13. 76 FR 30204 - Exelon Nuclear, Dresden Nuclear Power Station, Unit 1; Exemption From Certain Security Requirements

    Science.gov (United States)

    2011-05-24

    ... contained in the Responsibility Matrix of the safeguards contingency plan.'' Part 73 of Title 10 of the Code... organization, which will have as its objective to provide high assurance that activities involving special... structures) for DNPS Unit 1 is in a form that does not pose a risk of removal (i.e., an intact reactor...

  14. 76 FR 79228 - Combined Licenses at William States Lee III Nuclear Station Site, Units 1 and 2; Duke Energy...

    Science.gov (United States)

    2011-12-21

    ... NUCLEAR REGULATORY COMMISSION [Docket Nos. 52-018 and 52-019; NRC-2008-0170] Combined Licenses at William States Lee III Nuclear Station Site, Units 1 and 2; Duke Energy Carolinas, LLC AGENCY: Nuclear.... SUMMARY: Notice is hereby given that the U.S. Nuclear Regulatory Commission (NRC) and the U.S. Army Corps...

  15. Internal event analysis of Laguna Verde Unit 1 Nuclear Power Plant. System Analysis

    International Nuclear Information System (INIS)

    Huerta B, A.; Aguilar T, O.; Nunez C, A.; Lopez M, R.

    1993-01-01

    The Level 1 results of Laguna Verde Nuclear Power Plant PRA are presented in the I nternal Event Analysis of Laguna Verde Unit 1 Nuclear Power Plant , CNSNS-TR-004, in five volumes. The reports are organized as follows: CNSNS-TR-004 Volume 1: Introduction and Methodology. CNSNS-TR-004 Volume 2: Initiating Event and Accident Sequences. CNSNS-TR-004 Volume 3: System Analysis. CNSNS-TR-004 Volume 4: Accident Sequence Quantification and Results. CNSNS-TR-004 Volume 5: Appendices A, B and C. This volume presents the results of the system analysis for the Laguna Verde Unit 1 Nuclear Power Plant. The system analysis involved the development of logical models for all the systems included in the accident sequence event tree headings, and for all the support systems required to operate the front line systems. For the Internal Event analysis for Laguna Verde, 16 front line systems and 5 support systems were included. Detailed fault trees were developed for most of the important systems. Simplified fault trees focusing on major faults were constructed for those systems that can be adequately represent,ed using this kind of modeling. For those systems where fault tree models were not constructed, actual data were used to represent the dominant failures of the systems. The main failures included in the fault trees are hardware failures, test and maintenance unavailabilities, common cause failures, and human errors. The SETS and TEMAC codes were used to perform the qualitative and quantitative fault tree analyses. (Author)

  16. Decommissioning of units 1 - 4 at Kozloduy nuclear power plant in Bulgaria

    International Nuclear Information System (INIS)

    Dishkova, Denitsa

    2014-01-01

    Nuclear safety and security are absolute priorities for the European Union countries and this applies not only to nuclear power plants in operation but also to decommissioning. In terms of my technical background and my working experience in the field of licensing and environmental impact assessment during the decommissioning of Units 1 to 4 at Kozloduy Nuclear Power Plant (KNPP) in Bulgaria, I decided to present the strategy for decommissioning of Units 1 to 4 at KNPP which was selected and followed to achieve safe and effective decommissioning process. The selected strategy in each case must meet the legislative framework, to ensure safe management of spent fuel and radioactive waste, to provide adequate funding and to lead to positive socio-economic impact. The activities during the decommissioning generate large volume of waste. In order to minimize their costs and environmental impact it should be given a serious consideration to the choice, the development and the implementation of the most adequate process for treatment and the most appropriate measurement techniques. The licensing process of the decommissioning activities is extremely important and need to cope with all safety concerns and ensure optimal waste management. (authors)

  17. Acoustic emission monitoring of preservice testing at Watts Bar Unit 1 Nuclear Reactor

    International Nuclear Information System (INIS)

    Hutton, P.H.; Pappas, R.A.; Friesel, M.A.

    1985-02-01

    Acoustic emission (AE) monitoring of selected pressure boundary areas at TVA's Watts Bar, Unit 1 Nuclear Plant in the US during hot functional preservice testing is described. Background, methodology, and results are included. The work discussed here is a major milestone in a program supported by the US NRC to develop and demonstrate application of AE monitoring for continuous surveillance of reactor pressure boundaries to detect and evaluate growing flaws. The subject work demonstrated that anticipated problem areas can be overcome. Work is continuing to AE monitoring during reactor operation. 3 refs., 6 figs

  18. Probabilistic fire risk assessment for Koeberg Nuclear Power Station Unit 1

    International Nuclear Information System (INIS)

    Grobbelaar, J.F.; Foster, N.A.S.; Luesse, L.J.

    1995-01-01

    A probabilistic fire risk assessment was done for Koeberg Nuclear Power Station Unit 1. Areas where fires are likely to start were identified. Equipment important to safety, as well as their power and/or control cable routes were identified in each fire confinement sector. Fire confinement sectors where internal initiating events could be caused by fire were identified. Detection failure and suppression failure fault trees and event trees were constructed. The core damage frequency associated with each fire confinement sector was calculated, and important fire confinement sectors were identified. (author)

  19. Summary of plant life management evaluation for Onagawa Nuclear Power Station Unit-1

    International Nuclear Information System (INIS)

    Nodate, Kazumi

    2014-01-01

    The Onagawa Nuclear Power Station Unit-1 (Onagawa NPS-1) began commercial operation on June 1, 1984, and has reached 30-year from starting of operation on June of 2014. To that end, we implemented the Plant Life Management (PLM) evaluation for Onagawa NPS-1 as our first experience. We decided on a Long-term Maintenance Management Policy from result of the evaluation, and then applied the Safety-Regulations change approval application on November 6, 2013 and its correcting application on April 16, 2014. Our application was approved on May 21, 2014 through investigation by the Nuclear Regulatory Agency. Also at implementation of the PLM evaluation, we considered effects of the Great East Japan Earthquake that occurred on March 11, 2011 against ageing phenomena. In this paper, we introduce summary of PLM evaluation for Onagawa NPS-1 and the evaluation that considered effects of the Great East Japan Earthquake. (author)

  20. Second periodic safety review of Angra Nuclear Power Station, unit 1

    Energy Technology Data Exchange (ETDEWEB)

    Martins, Carlos F.O.; Crepaldi, Roberto; Freire, Enio M., E-mail: ottoncf@tecnatom.com.br, E-mail: emfreire46@gmail.com, E-mail: robcrepaldi@hotmail.com [Tecnatom do Brasil Engenharia e Servicos Ltda, Rio de Janeiro, RJ (Brazil); Campello, Sergio A., E-mail: sacampe@eletronuclear.gov.br [Eletrobras Termonuclear S.A. (ELETRONUCLEAR), Rio de Janeiro, RJ (Brazil)

    2015-07-01

    This paper describes the second Periodic Safety Review (PSR2-A1) of Angra Nuclear Power Station, Unit 1, prepared by Eletrobras Eletronuclear S.A. and Tecnatom do Brasil Engenharia e Servicos Ltda., during Jul.2013-Aug.2014, covering the period of 2004-2013. The site, in Angra dos Reis-RJ, Brazil, comprises: Unit 1, (640 MWe, Westinghouse PWR, operating), Unit 2 (1300 MWe, KWU/Areva, operating) and Unit 3 (1405 MWe, KWU/Areva, construction). The PSR2-A1 attends the Standards 1.26-Safety in Operation of Nuclear Power Plants, Brazilian Nuclear Regulatory Commission (CNEN), and IAEA.SSG.25-Periodic Safety Review of Nuclear Power Plants. Within 18 months after each 10 years operation, the operating organization shall perform a plant safety review, to investigate the evolution consequences of safety code and standards, regarding: Plant design; structure, systems and components behavior; equipment qualification; plant ageing management; deterministic and probabilistic safety analysis; risk analysis; safety performance; operating experience; organization and administration; procedures; human factors; emergency planning; radiation protection and environmental radiological impacts. The Review included 6 Areas and 14 Safety Parameters, covered by 33 Evaluations.After document evaluations and discussions with plant staff, it was generated one General and 33 Specific Guide Procedures, 33 Specific and one Final Report, including: Description, Strengths, Deficiencies, Areas for Improvement and Conclusions. An Action Plan was prepared by Electronuclear for the recommendations. It was concluded that the Unit was operated within safety standards and will attend its designed operational lifetime, including possible life extensions. The Final Report was submitted to CNEN, as one requisite for renewal of the Unit Permanent Operation License. (author)

  1. Second periodic safety review of Angra Nuclear Power Station, unit 1

    International Nuclear Information System (INIS)

    Martins, Carlos F.O.; Crepaldi, Roberto; Freire, Enio M.; Campello, Sergio A.

    2015-01-01

    This paper describes the second Periodic Safety Review (PSR2-A1) of Angra Nuclear Power Station, Unit 1, prepared by Eletrobras Eletronuclear S.A. and Tecnatom do Brasil Engenharia e Servicos Ltda., during Jul.2013-Aug.2014, covering the period of 2004-2013. The site, in Angra dos Reis-RJ, Brazil, comprises: Unit 1, (640 MWe, Westinghouse PWR, operating), Unit 2 (1300 MWe, KWU/Areva, operating) and Unit 3 (1405 MWe, KWU/Areva, construction). The PSR2-A1 attends the Standards 1.26-Safety in Operation of Nuclear Power Plants, Brazilian Nuclear Regulatory Commission (CNEN), and IAEA.SSG.25-Periodic Safety Review of Nuclear Power Plants. Within 18 months after each 10 years operation, the operating organization shall perform a plant safety review, to investigate the evolution consequences of safety code and standards, regarding: Plant design; structure, systems and components behavior; equipment qualification; plant ageing management; deterministic and probabilistic safety analysis; risk analysis; safety performance; operating experience; organization and administration; procedures; human factors; emergency planning; radiation protection and environmental radiological impacts. The Review included 6 Areas and 14 Safety Parameters, covered by 33 Evaluations.After document evaluations and discussions with plant staff, it was generated one General and 33 Specific Guide Procedures, 33 Specific and one Final Report, including: Description, Strengths, Deficiencies, Areas for Improvement and Conclusions. An Action Plan was prepared by Electronuclear for the recommendations. It was concluded that the Unit was operated within safety standards and will attend its designed operational lifetime, including possible life extensions. The Final Report was submitted to CNEN, as one requisite for renewal of the Unit Permanent Operation License. (author)

  2. 75 FR 15745 - Arizona Public Service Company, et al. Palo Verde Nuclear Generating Station, Units 1, 2, and 3...

    Science.gov (United States)

    2010-03-30

    ...] Arizona Public Service Company, et al. Palo Verde Nuclear Generating Station, Units 1, 2, and 3; Exemption 1.0 Background The Arizona Public Service Company (APS, the licensee) is the holder of Facility... Generating Station (PVNGS), Units 1, 2, and 3, respectively. The licenses provide, among other things, that...

  3. Analysis of effects on plant performance by major measuring points in the secondary systems of Kori nuclear power plant units 3 and 4

    International Nuclear Information System (INIS)

    Lee, Jung Woon; Park, Jae Chang; Lee, Jung Woon; Kim, Jung Taek; Chang, Soon Heung; Lee, Gwang Gu; Heo, Gyun Young; Lee, Sung Jin; Han, Kyu Hyun; Shin, Byung Soo

    2003-06-01

    In this study, correlation analysis was achieved for the major sensor position and the behavior of secondary system in Kori NPP unit 3, 4. Using the data from simulation model, the correlation between sensor position and electrical output, the correlation between sensor position and heat rate, and the correlation between different sensor positions were analyzed. On the basis of study results, a performance evaluation model was proposed, which can carry out secondary system performance diagnosis

  4. 75 FR 14206 - FPL Energy Point Beach, LLC; Point Beach Nuclear Plant, Units 1 and 2; Environmental Assessment...

    Science.gov (United States)

    2010-03-24

    ... NUCLEAR REGULATORY COMMISSION [Docket Nos. 50-266 And 50-301; NRC-2010-0123 FPL Energy Point Beach, LLC; Point Beach Nuclear Plant, Units 1 and 2; Environmental Assessment and Finding of No Significant Impact The U.S. Nuclear Regulatory Commission (NRC) is considering issuance of an Exemption, pursuant to...

  5. 78 FR 77508 - Duke Energy Carolinas, LLC; William States Lee III Nuclear Station, Units 1 and 2; Combined...

    Science.gov (United States)

    2013-12-23

    ... NUCLEAR REGULATORY COMMISSION [Docket Nos. 52-018 and 52-019; NRC-2008-0170] Duke Energy Carolinas, LLC; William States Lee III Nuclear Station, Units 1 and 2; Combined Licenses Application Review AGENCY: Nuclear Regulatory Commission. ACTION: Final environmental impact statement; availability...

  6. 78 FR 40200 - Duke Energy Carolinas, LLC, Oconee Nuclear Station Units 1, 2, and 3; Independent Spent Fuel...

    Science.gov (United States)

    2013-07-03

    ... NUCLEAR REGULATORY COMMISSION [Docket Nos. 72-1004, 72-40, 50-269, 50-270, and 50-287; NRC-2013-0135] Duke Energy Carolinas, LLC, Oconee Nuclear Station Units 1, 2, and 3; Independent Spent Fuel Storage Installation; Environmental Assessment and Finding of No Significant Impact AGENCY: Nuclear...

  7. 78 FR 45575 - Duke Energy Carolinas, LLC; Oconee Nuclear Station Units 1, 2, and 3; Independent Spent Fuel...

    Science.gov (United States)

    2013-07-29

    ... NUCLEAR REGULATORY COMMISSION [Docket Nos.: 72-1004, 72-40, 50-269, 50-270, 50-287; and NRC-2013- 0135] Duke Energy Carolinas, LLC; Oconee Nuclear Station Units 1, 2, and 3; Independent Spent Fuel Storage Installation AGENCY: Nuclear Regulatory Commission. ACTION: Exemption; issuance. SUMMARY: The NRC...

  8. 75 FR 16201 - FPL Energy Point Beach, LLC; Point Beach Nuclear Plant, Units 1 and 2; Exemption

    Science.gov (United States)

    2010-03-31

    ... NUCLEAR REGULATORY COMMISSION [Docket Nos. 50-266 and 50-301; NRC-2010-0123] FPL Energy Point Beach, LLC; Point Beach Nuclear Plant, Units 1 and 2; Exemption 1.0 Background FPL Energy Point Beach.... Borchardt (NRC) to M. S. Fertel (Nuclear Energy Institute) dated June 4, 2009. The licensee's request for an...

  9. 75 FR 75704 - Pacific Gas and Electric Company (Diablo Canyon Nuclear Power Plant, Units 1 And 2); Notice of...

    Science.gov (United States)

    2010-12-06

    ... NUCLEAR REGULATORY COMMISSION [Docket Nos. 50-275-LR; 50-323-LR] Pacific Gas and Electric Company (Diablo Canyon Nuclear Power Plant, Units 1 And 2); Notice of Appointment of Adjudicatory Employee... Seismologist, Office of Nuclear Material Safety and Safeguards, has been appointed as a Commission adjudicatory...

  10. 78 FR 14361 - In the Matter of Luminant Generation Company LLC, Comanche Peak Nuclear Power Plant, Units 1 and...

    Science.gov (United States)

    2013-03-05

    ... NUCLEAR REGULATORY COMMISSION [NRC-2012-0310; Docket Nos. 50-445 and 50-446; License Nos. NPF-87 and NPF-89] In the Matter of Luminant Generation Company LLC, Comanche Peak Nuclear Power Plant, Units... Nuclear Power Plant, Units 1 and 2 (CPNPP), and its Independent Spent Fuel Storage Installation Facility...

  11. Structural design of the turbine building of Angra Nuclear Power Station, Unit 1

    International Nuclear Information System (INIS)

    Varella, L.N.; Reis, F.J.C.; Jurkiewicz, W.J.

    1978-01-01

    The Turbine Building of the Angra Nuclear Power Plant, Unit 1, and particularly its structure and structural design are described. The Turbine Building, as far as its structure is concerned, deviates from the standard structure of any turbine building due to the fact that huge ducts are provided in the foundation mat as to accomodate the circulating water system. This aspect and the fact that the building is founded upon a very deep strata of compacted and controlled fill, makes out of the building structure 'a concrete ship floating in the sea of sand', and by the same reason presents by itself an interesting structure, worth to be known to all engineers involved in design of power plants. This pape, suplemented by a few slides shown during presentation of the paper at the conference, covers the subject mainly from the designers' point of view. (Author)

  12. Analysis of core melt accident in Fukushima Daiichi-Unit 1 nuclear reactor

    International Nuclear Information System (INIS)

    Tanabe, Fumiya

    2011-01-01

    In order to obtain a profound understanding of the serious situation in Unit 1 and Unit 2/3 reactors of Fukushima Daiichi Nuclear Power Station (hereafter abbreviated as 1F1 and 1F2/3, respectively), which was directly caused by tsunami due to a huge earthquake on 11 March 2011, analyses of severe core damage are performed. In the present report, the analysis method and 1F1 analysis are described. The analysis is essentially based on the total energy balance in the core. In the analysis, the total energy vs. temperature curve is developed for each reactor, which is based on the estimated core materials inventory and material property data. Temperature and melt fraction are estimated by comparing the total energy curve with the total stored energy in the core material. The heat source is the decay heat of fission products and actinides together with reaction heat from the zirconium steam reaction. (author)

  13. Results of the 5th regular inspection of Unit 1 in the Hamaoka Nuclear Power Station

    International Nuclear Information System (INIS)

    1983-01-01

    The 5th regular inspection of Unit 1 in the Hamaoka Nuclear Power Station was carried out from March 27 to July 27, 1982. Inspection was made on the reactor proper, reactor cooling system, instrumentation/control system, radiation control facility, etc. By the examinations of external appearance, leakage, performance, etc., no abnormality was observed. In the regular inspection, personnel exposure dose was all below the permissible level. The works done during the inspection were the following: the replacement of control rod drives, the replacement of core support-plate plugs, the repair of steam piping, steam extraction pipes and feed water heaters, the repair of a waste-liquid concentrator, the installation of barriers and leak detectors, the installation of drain sump monitors in a containment vessel, the replacement of concentrated liquid waste pumps, the employment of type B fuel. (Mori, K.)

  14. Safety evaluation report related to the operation of Watts Bar Nuclear Plant, Units 1 and 2

    International Nuclear Information System (INIS)

    1995-09-01

    This report supplements the Safety Evaluation Report (SER), NUREG-0847 (June 1982), Supplement No. 1 (September 1982), Supplement No. 2 (January 1984), Supplement No. 3 (January 1985). Supplement No. 4 (March 1985), Supplement No. 5 (November 1990), Supplement No. 6 (April 1991), Supplement No. 7 (September 1991), Supplement No. 8 (January 1992). Supplement No. 9 (June 1992), Supplement No. 10 (October 1992), Supplement No. 11 (April 1993), Supplement No. 12 (October 1993). Supplement No. 13 (April 1994), Supplement No. 14 (December 1994), and Supplement No. 15 (June 1995) issued by the Office of Nuclear Reactor Regulation of the U.S. Nuclear Regulatory Commission with respect to the application filed by the Tennessee Valley Authority, as applicant and owner, for licenses to operate the Watts Bar Nuclear Plant, Units 1 and 2 (Docket Nos, 50-390 and 50-391). The facility is located in Rhea County, Tennessee, near the Watts Bar Dam on the Tennessee River. This supplement provides recent information regarding resolution of some of the outstanding and confirmatory items, and proposed license conditions identified in the SER

  15. Data book of examination of the ruptured pipe at the Hamaoka Nuclear Power Station Unit-1

    International Nuclear Information System (INIS)

    2002-03-01

    In order to investigate root cause of the pipe rupture, which took place at the Hamaoka Nuclear Power Station Unit-1 of Chubu Electric Power Company on November 7, 2001, a task force was established within the Nuclear and Industrial Safety Agency (NISA) and initiated a detailed investigation of the ruptured pipe. The Japan Atomic Energy Research Institute (JAERI) was asked from the Ministry of Education, Culture, Sports, Science and Technology (MEXT) in response to the request from NISA to cooperate as an independent neutral organization with NISA and perform an examination of the ruptured pipe independently from Chubu Electric Power Company. JAERI accepted the request by considering the fact that JAERI is an integrated research institution for nuclear research and development, a prime research institution for nuclear safety research, a research institution with experience of root-cause investigation of various nuclear incidents and accidents of domestic as well as overseas, and a research institution provided with advanced examination facilities necessary for examination of the ruptured pipe. The JAERI examination group was formed at the Tokai Research Establishment and conducted detailed and thorough examination of the pieces taken from the ruptured pipe primarily in the Reactor Fuel Examination Facility (RFEF) with the use of tools such as scanning electron microscopes and other equipments. Purpose of examination was to provide technical information in order to identify causes of the pipe rupture through examination of the pieces taken from the ruptured region of the pipe. The result of the present examination has already been reported to NISA and has also been published as the JAERI-Tech report No.2001-94. This report is a data book containing the detailed data obtained by the present examination. (author)

  16. Report of examination of the ruptured pipe at the Hamaoka Nuclear Power Station Unit-1

    International Nuclear Information System (INIS)

    2001-12-01

    In order to investigate root cause of the pipe rupture, which took place at the Hamaoka Nuclear Power Station Unit-1 of Chubu Electric Power Company on November 7, 2001, a task force was established within the Nuclear and Industrial Safety Agency (NISA) and initiated a detailed investigation of the ruptured pipe. The Japan Atomic Energy Research Institute (JAERI) was asked from the Ministry of Education, Culture, Sports, Science and Technology (MEXT) in response to the request from NISA to cooperate as an independent neutral organization with NISA and perform an examination of the ruptured pipe independently from Chubu Electric Power Company. JAERI accepted the request by considering the fact that JAERI is an integrated research institution for nuclear research and development, a prime research institution for nuclear safety research, a research institution with experience of root-cause investigation of various nuclear incidents and accidents of domestic as well as overseas, and a research institution provided with advanced examination facilities necessary for examination of the ruptured pipe. The JAERI examination group was formed at the Tokai Research Establishment and conducted detailed and thorough examination of the pieces taken from the ruptured pipe primarily in the Reactor Fuel Examination Facility (RFEF) with the use of tools such as scanning electron microscopes and other equipments. Purpose of examination was to provide technical information in order to identify causes of the pipe rupture through examination of the pieces taken from the ruptured region of the pipe. The following findings and conclusion were made as the result of the present examination. (1) Wall thickness of the pipe was significantly reduced in the ruptured region. (2) Dimple pattern resulting from ductile fracture by shearing was observed in the fracture surfaces of nearly all of the pieces and no indication of fatigue crack growth was found. (3) Microstructure showed a typical carbon

  17. Final environmental statement for Shoreham Nuclear Power Station, Unit 1: (Docket No. 50-322)

    International Nuclear Information System (INIS)

    1977-10-01

    The proposed action is the issuance of an Operating License to the Long Island Lighting Company (LILCO) for the startup and operation of the Shoreham Nuclear Power Station, Unit 1 (the plant) located on the north shore of Long Island, the State of New York, County of Suffolk, in the town of Brookhaven. The Shoreham station will employ a boiling-water reactor (BWR), which will operate at a thermal output of 2436 MW leading to a gross output of 846 MWe and a net output of about 820 MWe. The unit will be cooled by once-through flow of water from the Long Island Sound. One nuclear unit with a net capacity of 820 MWe will be added to the generating resources of the Long Island Lighting Company. This will have a favorable effect on reserve margins and provide a cost savings of approximately $62.1 million (1980 dollars) in production costs in 1980 if the unit comes on line as scheduled; additional cost savings will be realized in subsequent years. Approximately 100 acres (40 hectares) of the 500-acre (202-hectare) site of rural (mostly wooded) land owned by the applicant have been cleared. Most of this will be unavailable for other uses during at least the 40-year life of the plant. No offsite acreage has been or will be cleared. Land in the vicinity of the site has undergone some residential development that is typical for all of this area of Long Island. The operation of Shoreham Unit 1 will have insignificant impacts on this and other types of land uses in the vicinity of the site. 33 figs., 56 tabs

  18. 75 FR 13606 - Arizona Public Service Company, Palo Verde Nuclear Generating Station, Units 1, 2, and 3...

    Science.gov (United States)

    2010-03-22

    ... NUCLEAR REGULATORY COMMISSION [Docket Nos. STN 50-528, STN 50-529, and STN 50-530; NRC-2010-0114] Arizona Public Service Company, Palo Verde Nuclear Generating Station, Units 1, 2, and 3; Environmental...-74, issued to Arizona Public Service Company (APS, the licensee), for operation of the Palo Verde...

  19. Internal event analysis for Laguna Verde Unit 1 Nuclear Power Plant. Accident sequence quantification and results

    International Nuclear Information System (INIS)

    Huerta B, A.; Aguilar T, O.; Nunez C, A.; Lopez M, R.

    1994-01-01

    The Level 1 results of Laguna Verde Nuclear Power Plant PRA are presented in the I nternal Event Analysis for Laguna Verde Unit 1 Nuclear Power Plant, CNSNS-TR 004, in five volumes. The reports are organized as follows: CNSNS-TR 004 Volume 1: Introduction and Methodology. CNSNS-TR4 Volume 2: Initiating Event and Accident Sequences. CNSNS-TR 004 Volume 3: System Analysis. CNSNS-TR 004 Volume 4: Accident Sequence Quantification and Results. CNSNS-TR 005 Volume 5: Appendices A, B and C. This volume presents the development of the dependent failure analysis, the treatment of the support system dependencies, the identification of the shared-components dependencies, and the treatment of the common cause failure. It is also presented the identification of the main human actions considered along with the possible recovery actions included. The development of the data base and the assumptions and limitations in the data base are also described in this volume. The accident sequences quantification process and the resolution of the core vulnerable sequences are presented. In this volume, the source and treatment of uncertainties associated with failure rates, component unavailabilities, initiating event frequencies, and human error probabilities are also presented. Finally, the main results and conclusions for the Internal Event Analysis for Laguna Verde Nuclear Power Plant are presented. The total core damage frequency calculated is 9.03x 10-5 per year for internal events. The most dominant accident sequences found are the transients involving the loss of offsite power, the station blackout accidents, and the anticipated transients without SCRAM (ATWS). (Author)

  20. The application of FIMS to the Korean nuclear power plants

    International Nuclear Information System (INIS)

    Lee, Seung-Tae; Choi, Dae-Sik; Yang, Choong-Yeol

    2010-01-01

    The smart transmitters have been installed at selected systems of Ulchin Nuclear Units 5 and 6, and diagnosis and calibration for the smart transmitters have been carried out using the mobile calibration tools. In Shin-Kori Nuclear Units 1 and 2 and Shin-Wolsong Nuclear Units 1 and 2, which are under design and construction, the smart transmitters are installed in the places where total integrated radiation dose is below 10 Gy. FIMS (Field Instrument Management System) is applied to Shin-Kori Nuclear Units 1 and 2 and Shin-Wolsong Nuclear Units 1 and 2 to monitor and calibrate the smart transmitters remotely. FIMS is a centralized management system to allow the users to monitor the operating status, to perform the instrument diagnosis, and to carry out the calibration of locally mounted transmitters remotely during the commissioning and normal operation. (authors)

  1. Results of the 4th regular inspection in Unit 1 of the Mihama Nuclear Power Station

    International Nuclear Information System (INIS)

    1981-01-01

    The 4th regular inspection of Unit 1 in the Mihama Nuclear Power Station was made from July, 1975, to December, 1980, on its reactor and associated facilities. The respective stages of inspection during the years are described. The inspection by external appearance examination, disassembling leakage inspection and performance tests indicated crackings in piping for fuel-replacement water tank, the container penetration of recirculation pipe for residual-heat removal, and main steam-relief valve, and leakage in one fuel assembly. Radiation exposure of the personnel during the inspection was less than the permissible dose. Radiation exposure data for the personnel are given in tables. The improvements and repairs done accordingly were as follows: reapir of the piping for a fuel-replacement tank and recirculation piping for residual-heat removal, replacement of the main steam-relief valve, plugging of heating tubes for the steam-generator, replacement of pins and covers for control-rod guide pipes, improvement of safety protection system and installation of rare gas monitor. (J.P.N.)

  2. An integrated approach for investigation of failed nuclear fuel used at NPP Cernavoda Unit 1

    International Nuclear Information System (INIS)

    Tuturici, I.L.; Parvan, M.; Popov, M.; Dobrin, R.; Staicu, C.

    1996-01-01

    At NPP Cernavoda-Unit 1 the fuel surveillance and the defect detection system in operation are based on monitoring the coolant activity concentration and on measuring the flux of delayed neutrons emitted by some short-lived fission products. In order to identify the failed fuel underwater non-destructive examination has to be performed. The major interest for the availability of underwater examination consists in the necessity of a speedy acquisition of the data on failed fuel in operation and of appropriate follow-up actions to be taken. Often the identification operation will be followed by more detailed examinations on selected fuel rods in the hot cells of the Post-irradiation Examination Laboratory of the Institute for Nuclear Research at Pitesti. Transfer of selected fuel rods will be done by the use of a type B(U) road transportation cask. Such an integrated approach will help to keep the level of activity concentration of the primary circuit well below the authorized limits. (author). 2 figs., 1 tab., 2 refs

  3. Report on the Fourth Reactor Refueling. Laguna Verde Nuclear Central. Unit 1. April-May 1995

    International Nuclear Information System (INIS)

    Mendoza L, A.; Flores C, E.; Lopez G, C.P.F.

    1995-01-01

    The fourth refueling of the Unit 1 of Laguna Verde Nuclear Central was executed in the period of April 17 to May 31 of 1995 with the participation of a task group of 358 persons, included technicians and radiation protection officials and auxiliaries.The radiation monitoring and radiological surveillance to the workers was present length ways the refueling process and always attached to the ALARA criteria. The check points for radiation levels were set at: primary container or dry well, reloading floor, decontamination room (level 10.5), turbine building and radioactive waste building. To take advantage of the refueling process, rooms 203 and 213 of the turbine buildings were subject to inspection and maintenance work in valves, heaters and drains of heaters. Management aspects as personnel selection and training, costs, and countable are also presented in this report. Owing to the high cost of man-hour of the members of the ININ staff, its participation in the refueling process was in smaller number than years before. (Author)

  4. Ring thermal shield piping modification at Pickering Nuclear Generating Station 'A' Unit 1

    International Nuclear Information System (INIS)

    Brown, R.; Cobanoglu, M.M.

    1995-01-01

    Each of the four Pickering Nuclear Generating Station A (PNGSA) CANDU units was constructed with its reactor and dump tank surrounded by a concrete Calandria Vault (CV). The Ring Thermal Shield (RTS) system at PNGSA units is a water cooled structure with internal cooling channels with the purpose of attenuating excessive heat flux from the calandria shell to the end shield rings and adjoining concrete (Figure 1). In newer CANDU units the reactor calandria vessel is surrounded by a large water filled shield tank which eliminates the requirement for the RTS system. The RTS structures are situated in the space between the calandria and the vault walls. Each RTS is assembled from eight flat sided carbon steel segments, tilted towards the calandria and supported from the end shield rings. Cooling water to the RTS is supplied by carbon steel cooling pipes with a portion of the pipe run embedded in the vault walls. Flow through each RTS is divided into two independent circuits, having an inlet and an outlet cooling line. There are four locations of RTS inlet and outlet cooling lines. The inlet lines are located at the bottom and the outlet lines at the top of the RTS. The 'L' shaped section of RTS inlet and outlet cooling lines, from the RTS waterbox to the start of embedded portion at the concrete wall, had become defective due to corrosion induced by excessive Moisture levels in the calandria vaults. An on-line leak sealing capability was developed and placed in service in all four PNGSA units. However, a leak found during the 1994 Unit 1 outage was too large,to seal with the current capability, forcing Ontario Hydro (OH) to develop a method to replace the corroded pipes. The repair project was subject to some lofty performance targets. All tools had to be able to withstand dose rates of up to 3000 Rem/hour. These tools, along with procedures and personnel had to successfully repair the RTS system within 6 months otherwise a costly outage extension would result. This

  5. Kozloduy nuclear power plant. Units 1-4. Status of safety improvements. Rev. 2

    International Nuclear Information System (INIS)

    1999-01-01

    operation of the units. The plant current safety level analysis has been performed using IAEA analytical methodology according to 50-SG-O12 standard 'Periodic safety review of operational nuclear power plants'. The approach and criteria for acceptable safety level definition, developed by IAEA and presented in INSAG-8 ' was used for analysis performance. Based on this analysis a set of activities was developed, to ensures further plant operation with the necessary safety level. The measures were combined in a program called Complex program for modernization of units 1-4. The implementation of the program is foreseen for a period of four next fuel cycles and started at the beginning of 1998. In respond to the requirements for the content of this paper a detailed description of the current status of resolving of the safety issues, classified by IAEA in TECDOC 640 is presented. The whole process of safety evaluation, short and long term safety improvements presents in a systematical manner the efforts of the Government of Bulgaria, NEK Ltd and KNPP to operate these units with due respect of their nuclear safety responsibility according to Nuclear Safety Convention signed at Vienna in 1994 and ratified by Bulgarian Parliament in 1995

  6. Features of Computerized Procedure System of Shin-Kori unit 5 and 6

    International Nuclear Information System (INIS)

    Seong, Nokyu; Jung, Yeonsub; Sung, Chanho

    2016-01-01

    The Computerized Procedure System (CPS) is one of the Man Machine Interface (MMI) resources of Main Control Room (MCR) of the Advanced Power Reactor 1400 (APR1400). The CPS has been continuously improved since it was installed in Shin-Kori unit 3 and 4. The Korea Hydro Nuclear Power Central Research Institute (KHNP CRI) has found the points of improvement of CPS through CPS centered Human Factors Engineering Verification and Validation (HFE V and V) and Operating Experience Review (OER) of reference power plant. This paper shows the main features of CPS of Shin-Kori 5 and 6 unit. This paper shows the main features of CPS of Shin-Kori 5 and 6. These are some of improvements of CPS. This prototype of CPS currently is implementing in CRI. The respective function can be more detailed after testing the prototype. These features will be applied to Shin-Kori 5 and 6 CPS after HFE V and V

  7. Features of Computerized Procedure System of Shin-Kori unit 5 and 6

    Energy Technology Data Exchange (ETDEWEB)

    Seong, Nokyu; Jung, Yeonsub; Sung, Chanho [KHNP CRI, Daejeon (Korea, Republic of)

    2016-10-15

    The Computerized Procedure System (CPS) is one of the Man Machine Interface (MMI) resources of Main Control Room (MCR) of the Advanced Power Reactor 1400 (APR1400). The CPS has been continuously improved since it was installed in Shin-Kori unit 3 and 4. The Korea Hydro Nuclear Power Central Research Institute (KHNP CRI) has found the points of improvement of CPS through CPS centered Human Factors Engineering Verification and Validation (HFE V and V) and Operating Experience Review (OER) of reference power plant. This paper shows the main features of CPS of Shin-Kori 5 and 6 unit. This paper shows the main features of CPS of Shin-Kori 5 and 6. These are some of improvements of CPS. This prototype of CPS currently is implementing in CRI. The respective function can be more detailed after testing the prototype. These features will be applied to Shin-Kori 5 and 6 CPS after HFE V and V.

  8. Analysis of internal events for the Unit 1 of the Laguna Verde nuclear power station

    International Nuclear Information System (INIS)

    Huerta B, A.; Aguilar T, O.; Nunez C, A.; Lopez M, R.

    1993-01-01

    This volume presents the results of the starter event analysis and the event tree analysis for the Unit 1 of the Laguna Verde nuclear power station. The starter event analysis includes the identification of all those internal events which cause a disturbance to the normal operation of the power station and require mitigation. Those called external events stay beyond the reach of this study. For the analysis of the Laguna Verde power station eight transient categories were identified, three categories of loss of coolant accidents (LOCA) inside the container, a LOCA out of the primary container, as well as the vessel break. The event trees analysis involves the development of the possible accident sequences for each category of starter events. Events trees by systems for the different types of LOCA and for all the transients were constructed. It was constructed the event tree for the total loss of alternating current, which represents an extension of the event tree for the loss of external power transient. Also the event tree by systems for the anticipated transients without scram was developed (ATWS). The events trees for the accident sequences includes the sequences evaluation with vulnerable nucleus, that is to say those sequences in which it is had an adequate cooling of nucleus but the remoting systems of residual heat had failed. In order to model adequately the previous, headings were added to the event tree for developing the sequences until the point where be solved the nucleus state. This process includes: the determination of the failure pressure of the primary container, the evaluation of the environment generated in the reactor building as result of the container failure or cracked of itself, the determination of the localization of the components in the reactor building and the construction of boolean expressions to estimate the failure of the subordinated components to an severe environment. (Author)

  9. Draft environmental impact statement. River Bend Nuclear Power Station, Unit 1

    International Nuclear Information System (INIS)

    Anon.

    1980-01-01

    Federal financing of an undivided ownership interest of River Bend Nuclear Power Station Unit 1 on a 3293-acre site near St. Francisville, Louisiana is proposed in a supplement to the final environmental impact statement of September 1974. The facility would consist of a boiling-water reactor that would produce a maximum of 2894 megawatts (MW) of electrical power. A design level of 3015 MW of electric power could be realized at some time in the future. Exhaust steam would be cooled by mechanical cooling towers using makeup water obtained from and discharged to the Mississippi River. Power generated by the unit would be transmitted via three lines totaling 140 circuit miles traversing portions of the parishes of West Feliciana, East Feliciana, East Baton Rouge, West Baton Rouge, Pointe Coupee, and Iberville. The unit would help the applicant meet the power needs of rural electric consumers in the region, and the applicant would contribute significanlty to area tax base and employment rolls during the life of the unit. Construction related activities would disturb 700 forested acres on the site and 1156 acres along the transmission routes. Of the 60 cubic feet per second (cfs) taken from the river, 48 cfs would evaporate during the cooling process and 12 cfs would return to the river with dissolved solids concentrations increased by 500%. The terrace aquifer would be dewatered for 16 months in order to lower the water table at the building site, and Grants Bayou would be transformed from a lentic to a lotic habitat during this period. Fogging and icing due to evaporation and drift from the cooling towers would increase slightly. During the construction period, farming, hunting, and fishing on the site would be suspended, and the social infractructure would be stressed due to the influx of a maximum of 2200 workers

  10. The experience in the Cernavoda Unit 1 operation - a stimulating argument for future nuclear power development in Romania

    International Nuclear Information System (INIS)

    Rotaru, I.; Bucur, I.; Galeriu, A.C.; Budan, O.

    1999-01-01

    The Romanian nuclear program has been developed based on the option for CANDU type reactors. At the beginning, this program was unrealistically conceived and its management was inappropriate. The program was reconsidered in 1990 and the management policy and organization structure were also adapted accordingly. The paper presents, in the first part, the actual organization structure, adapted for the execution of the current and future activities, related to the nuclear power program. The performance achieved by Cernavoda Unit 1 constitutes the main part of the paper. The performances described demonstrate that the Cernavoda Unit 1 is a success and the Romania's electricity needs are satisfied in a proportion of about 12% by the nuclear power. The paper also presents a general view on Cernavoda Unit 2 perspectives. The essential conclusion of the paper is that the continuation of the nuclear program appears to be a logical option, generally accepted in Romania, limited only by financial restraints. (author)

  11. 75 FR 44292 - Northern States Power Company; Prairie Island Nuclear Generating Plant, Units 1 and 2; Notice of...

    Science.gov (United States)

    2010-07-28

    ... and DPR-60] Northern States Power Company; Prairie Island Nuclear Generating Plant, Units 1 and 2... assessment, and behavioral observation) of the unescorted access authorization program when making the... under consideration to determine whether it met the criteria established in NRC Management Directive (MD...

  12. 78 FR 29158 - In the Matter of Zion Solutions, LLC; Zion Nuclear Power Station, Units 1 and 2; Order Approving...

    Science.gov (United States)

    2013-05-17

    ... and DPR-48] In the Matter of Zion Solutions, LLC; Zion Nuclear Power Station, Units 1 and 2; Order... formed for the purpose of acquiring ES, Inc. and is held by certain investment fund entities organized by... Environmental Management Programs, in writing, of such receipt no later than one (1) business day prior to the...

  13. Law on the Decommissioning of unit 1 at the state enterprise of the Republic of Lithuania Ignalina Nuclear Power Plant

    International Nuclear Information System (INIS)

    2000-01-01

    This law regulates the legal principles for the decommissioning of unit 1 at the Ignalina Nuclear Power Plant. The main deadlines for the government in the preparation for the decommissioning are set in the law. All preparatory works should be finished before the year 2005

  14. Common cause failure analysis of the rodded scram system of the Arkansas Nuclear One-Unit 1 Plant

    International Nuclear Information System (INIS)

    Montague, D.F.; Campbell, D.J.; Flanagan, G.F.

    1986-10-01

    This study demonstrates the use of a formal method for common cause failure analysis in a reliability analysis of the Arkansas Nuclear One - Unit 1 rodded scram system. The scram system failure of interest is loss of capability of the system to shut the reactor down when required. The results of this analysis support the ATWS program sponsored by the US Nuclear Regulatory Commission. The methods used in this analysis support the NRC's Risk Methods Integration and Evaluation Program (RMIEP)

  15. Kozloduy nuclear power plant. Units 1-4. Status of safety assessment activities. Rev. 2

    International Nuclear Information System (INIS)

    1999-01-01

    This paper presents the results of the status of safety assessment activities carried out by the Kozloduy Nuclear Power Plant (KNPP) in order to evaluate the current status of the safety of its reactor units 1-4. The steam supply system of this units is based of the reactor WWER-440/ B-230, which is a PWR of Russian design developed according to the safety standards in force in USSR in late 60-s. Now a days 10 reactor units of this type are in operation in four NPPs. Despite of efforts of the different plants to implement safety improvements measures during first 10-15 years of operation of this type of reactor its major safety problems were not eliminated and were a subject of international concern. The systematic evaluation of the deficiencies of the original design of this type of reactors have been initiated by IAEA in the beginning of 1990 and brought to developing a comprehensive list of safety problems which required urgent implementation of safety measures in all plants. To solve this problems in 1991 KNPP initiated implementation of so called 'short term' safety improvement program, developed with the help of WANO under agreement with Bulgarian Nuclear Safety Authority (BNSA) and consortium RISKAUDIT. The program was based on a stage approach and was foreseen to be implemented by tree stages in very tight time schedule in order to achieve significant and rapid improvements of the level of safety in operation of the units. The Short Tenn Program was implemented between the years 1991 and 1997 thanks of the strong safety commitment of NEK and KNPP staff and the broad international cooperation and financial support. Important part of resources were supplied under PHARE program of CEC, EBRD grant agreement and EDF support. The plant current safety level analysis has been performed using IAEA analytical methodology according to 50-SG-O12 standard 'Periodic safety review of operational nuclear power plants'. The approach and criteria for acceptable safety level

  16. A study on the optimal replacement periods of digital control computer's components of Wolsung nuclear power plant unit 1

    International Nuclear Information System (INIS)

    Mok, Jin Il; Seong, Poong Hyun

    1993-01-01

    Due to the failure of the instrument and control devices of nuclear power plants caused by aging, nuclear power plants occasionally trip. Even a trip of a single nuclear power plant (NPP) causes an extravagant economical loss and deteriorates public acceptance of nuclear power plants. Therefore, the replacement of the instrument and control devices with proper consideration of the aging effect is necessary in order to prevent the inadvertent trip. In this paper we investigated the optimal replacement periods of the control computer's components of Wolsung nuclear power plant Unit 1. We first derived mathematical models of optimal replacement periods to the digital control computer's components of Wolsung NPP Unit 1 and calculated the optimal replacement periods analytically. We compared the periods with the replacement periods currently used at Wolsung NPP Unit 1. The periods used at Wolsung is not based on mathematical analysis, but on empirical knowledge. As a consequence, the optimal replacement periods analytically obtained and those used in the field show a little difference. (Author)

  17. Calvert Cliffs Nuclear Power Plant, Units 1 and 2. Annual operating report: January--December 1976

    International Nuclear Information System (INIS)

    1977-01-01

    Unit 1 successfully completed its first core cycle with unit availability of 95.2 percent. Saltwater leakage into the condenser continues to be a problem. Unit 2 achieved initial criticality November 30 and was initially paralleled to the Baltimore system on December 7. Information is presented concerning operations, specifications, maintenance, shutdowns and power reduction, and personnel exposures

  18. Oconee Nuclear Station, Units 1, 2, and 3. Semiannual operating report, January--June 1975

    International Nuclear Information System (INIS)

    1975-01-01

    Information is presented concerning operations, performance characteristics, changes, tests, inspections, containment leak tests, maintenance, primary coolant chemistry, station staff changes, reservoir investigations, plume mapping, and operational environmental radioactivity monitoring data for oconee Units 1, 2, and 3. The non-radiological environmental surveillance program is also described. (FS)

  19. Preparation for decommissioning of the Kozloduy Nuclear Power Plant units 1 and 2

    International Nuclear Information System (INIS)

    Delcheva, T.; Ribarski, V.; Demireva, E.

    2006-01-01

    The first decommissioning strategy of units 1 and 2 of Kozloduy NPP (KNPP) stipulated 3 phases: a 5 year phase including the post operation activities and preparation of the safe enclosure (SE); a 35 years SE period, followed by deferred dismantling. 'Updated Decommissioning Strategy for Units 1-4 of Kozloduy NPP' was issued in June 2006. The Updated Strategy is based on the so called 'Continuous Dismantling' Concept. The updated Strategy starts preparatory work earlier and then moves into dismantling work without a significant gap. The aim is to achieve a more optimal distribution of the dismantling activities along the time, saving jobs and the existing knowledge of the plant personnel during the decommissioning, and ensuring smooth and more effective use of financial and human resources and of the available infrastructure for waste treatment. This paper gives general information about the updated strategy and activities required for its implementation. (author)

  20. Dresden Nuclear Power Station, Units 1, 2, and 3. Annual operating report: January thru December 1976

    International Nuclear Information System (INIS)

    1977-01-01

    Net electrical energy generated by Unit 1 was 953,015.5 MWH with the generator on line 7,399.37 hrs. Unit 2 generated 4,371,553.689 MWH with the generator on line 6,664.58 hrs while Unit 3 generated 4,034,251 MWH with the generator on line 7,234.86 hrs. Information is presented concerning operations, maintenance, and shutdowns

  1. Technical evaluation of RETS-required reports for Browns Ferry Nuclear Power Station, Units 1, 2, and 3, for 1983

    International Nuclear Information System (INIS)

    Young, T.E.; Magleby, E.H.

    1985-01-01

    A review was performed of reports required by federal regulations and the plant-specific radiological effluent technical specifications (RETS) for operations conducted at Tennessee Valley Authority's Browns Ferry Nuclear Station, Units 1, 2, and 3, during 1983. The two periodic reports reviewed were (a) the Effluents and Waste Disposal Semiannual Report, First Half 1983 and (b) the Effluents and Waste Disposal Semiannual Report, Second Half 1983. The principal review guidelines were the plant's specific RETs and NRC guidance given in NUREG-0133, ''Preparation of Radiological Effluent Technical Specifications for Nuclear Power Plants.'' The Licensee's submitted reports were found to be reasonably complete and consistent with the review guidelines

  2. Technical evaluation of RETS-required reports for Rancho Seco Nuclear Generating Station, Unit 1 for 1983

    International Nuclear Information System (INIS)

    Magleby, E.H.; Young, T.E.

    1985-01-01

    A review of the reports required by Federal regulations and the plant-specific Radiological Effluent Technical Specifications (RETS) for operations conducted during 1983 was performed. The periodic reports reviewed for the Rancho Seco Nuclear Generating Station, Unit 1 were the Semiannual Effluent Release Report, January 1, 1983 to June 30, 1983 and the Radiation Exposure, Environmental Protection, Effluent and Waste Disposal Report. The principal review guidelines were the plant's specific RETS which were based on NRC guidance given in NUREG-0133, ''Preparation of Radiological Effluent Technical Specifications for Nuclear Power Plants.'' The Licensee's submitted reports were found to be reasonably complete and consistent with the review guidelines

  3. Structural review of the Palisades Nuclear Power Plant Unit 1 containment structure under combined loads for the Systematic Evaluation Program

    International Nuclear Information System (INIS)

    Liaw, C.Y.; Debeling, A.; Tsai, N.C.

    1981-12-01

    A structural reassessment of the containment structure of the Palisades Nuclear Power Plant Unit 1 was performed for the Nuclear Regulatory Commission as part of the Systematic Evaluation Program. Conclusions about the ability of the containment structure to withstand the Abnormal/Extreme Environment are presented. The reassessment focused mainly on the overall structural integrity of the containment building for the Abnormal/Extreme Environment. In this case, the Abnormal Environmental condition is caused by the worst case of either a Loss-of-Coolant Accident or a main steam line break. The Extreme Environmental condition is the Safe Shutdown Earthquake

  4. Assessment of environmental public exposure from a hypothetical nuclear accident for Unit-1 Bushehr nuclear power plant

    Energy Technology Data Exchange (ETDEWEB)

    Sohrabi, M.; Ghasemi, M.; Amrollahi, R.; Khamooshi, C.; Parsouzi, Z. [Amirkabir University of Technology, Health Physics and Dosimetry Research Laboratory, Department of Physics, Tehran (Iran, Islamic Republic of)

    2013-05-15

    Unit-1 of the Bushehr nuclear power plant (BNPP-1) is a VVER-type reactor with 1,000-MWe power constructed near Bushehr city at the coast of the Persian Gulf, Iran. The reactor has been recently operational to near its full power. The radiological impact of nuclear power plant (NPP) accidents is of public concern, and the assessment of radiological consequences of any hypothetical nuclear accident on public exposure is vital. The hypothetical accident scenario considered in this paper is a design-basis accident, that is, a primary coolant leakage to the secondary circuit. This scenario was selected in order to compare and verify the results obtained in the present paper with those reported in the Final Safety Analysis Report (FSAR 2007) of the BNPP-1 and to develop a well-proven methodology that can be used to study other and more severe hypothetical accident scenarios for this reactor. In the present study, the version 2.01 of the PC COSYMA code was applied. In the early phase of the accidental releases, effective doses (from external and internal exposures) as well as individual and collective doses (due to the late phase of accidental releases) were evaluated. The surrounding area of the BNPP-1 within a radius of 80 km was subdivided into seven concentric rings and 16 sectors, and distribution of population and agricultural products was calculated for this grid. The results show that during the first year following the modeled hypothetical accident, the effective doses do not exceed the limit of 5 mSv, for the considered distances from the BNPP-1. The results obtained in this study are in good agreement with those in the FSAR-2007 report. The agreement obtained is in light of many inherent uncertainties and variables existing in the two modeling procedures applied and proves that the methodology applied here can also be used to model other severe hypothetical accident scenarios of the BNPP-1 such as a small and large break in the reactor coolant system as well

  5. Browns Ferry Nuclear Power Station, Units 1, 2, and 3. Semiannual report, January--June 1975

    International Nuclear Information System (INIS)

    1975-01-01

    Browns Ferry units 1 and 2 operated at maximum power from January 1 to March 22 except as limited by thermal margins, fuel preconditioning, optimum power shape, maintenance, and Unit 2 start-up tests. On March 22 a cable tray fire started causing spurious starting of equipment due to faulted control cables. The reactors were manually scrammed and placed in cold shutdown for fire investigation, clean up, and fuel removal. Information is also presented concerning maintenance, radiochemistry, occupational radiation exposure, release of radioactive materials, and non-radiological environmental monitoring

  6. Subsidence analysis Forsmark nuclear power plant - unit 1; Saettningsanalys Forsmarks kaernkraftverk - aggregat 1

    Energy Technology Data Exchange (ETDEWEB)

    Bono, Nancy; Fredriksson, Anders; Maersk Hansen, Lars (Golder Associates AB (Sweden))

    2010-12-15

    On behalf of SKB, Golder Associates Ltd carried out a risk analysis of subsidence during Forsmark nuclear power plant in the construction of the final repository for spent nuclear fuel near and below existing reactors. Specifically, the effect of horizontal cracks have been studied.

  7. System Definition Document: Reactor Data Necessary for Modeling Plutonium Disposition in Catawba Nuclear Station Units 1 and 2

    International Nuclear Information System (INIS)

    Ellis, R.J.

    2000-01-01

    The US Department of Energy (USDOE) has contracted with Duke Engineering and Services, Cogema, Inc., and Stone and Webster (DCS) to provide mixed-oxide (MOX) fuel fabrication and reactor irradiation services in support of USDOE's mission to dispose of surplus weapons-grade plutonium. The nuclear station units currently identified as mission reactors for this project are Catawba Units 1 and 2 and McGuire Units 1 and 2. This report is specific to Catawba Nuclear Station Units 1 and 2, but the details and materials for the McGuire reactors are very similar. The purpose of this document is to present a complete set of data about the reactor materials and components to be used in modeling the Catawba reactors to predict reactor physics parameters for the Catawba site. Except where noted, Duke Power Company or DCS documents are the sources of these data. These data are being used with the ORNL computer code models of the DCS Catawba (and McGuire) pressurized-water reactors

  8. Critical evaluation of the nonradiological environmental technical specifications. Volume 4. San Onofre Nuclear Generating Station, Unit 1

    Energy Technology Data Exchange (ETDEWEB)

    Adams, S.M.; Cunningham, P.A.; Gray, D.D.; Kumar, K.D.

    1976-08-10

    A comprehensive study of the data collected as part of the environmental Technical Specifications program for Unit 1 of the San Onofre Nuclear Generating Station (SONGS 1) was conducted for the Office of Nuclear Regulatory Research of the U.S. Nuclear Regulatory Commission. The program included an analysis of the hydrothermal and ecological monitoring data collected during 1975. The hydrothermal analysis includes a discussion of models used in plume predictions prior to plant operation and an evaluation of the present hydrothermal monitoring program. The ecological evaluation was directed toward reviewing the strengths and weaknesses of the various sampling programs designed to monitor the planktonic, benthic, and nektonic communities inhabiting the inshore coastal area in the vicinity of San Onofre.

  9. Critical evaluation of the nonradiological environmental technical specifications. Volume 4. San Onofre Nuclear Generating Station, Unit 1

    International Nuclear Information System (INIS)

    Adams, S.M.; Cunningham, P.A.; Gray, D.D.; Kumar, K.D.

    1976-01-01

    A comprehensive study of the data collected as part of the environmental Technical Specifications program for Unit 1 of the San Onofre Nuclear Generating Station (SONGS 1) was conducted for the Office of Nuclear Regulatory Research of the U.S. Nuclear Regulatory Commission. The program included an analysis of the hydrothermal and ecological monitoring data collected during 1975. The hydrothermal analysis includes a discussion of models used in plume predictions prior to plant operation and an evaluation of the present hydrothermal monitoring program. The ecological evaluation was directed toward reviewing the strengths and weaknesses of the various sampling programs designed to monitor the planktonic, benthic, and nektonic communities inhabiting the inshore coastal area in the vicinity of San Onofre

  10. Water Hammer Analysis using RELAP5/MOD 3.3 for Yonggwang Nuclear Power Unit 1 and 2 Blowdown System

    International Nuclear Information System (INIS)

    Lee, Sang Il; Kim, Hea Zoo; Chu, Jung Ho; Ahn, Se Hong; Jung, Chang Ho

    2010-01-01

    Water hammer can be defined as a rapid pressure step occurring in the liquid in a closed pipe caused by a sudden change in the liquid velocity. This pressure acts for a period which is twice the transit time of sonic wave in the pipe. Generally, water hammer can occur in any thermal-hydraulic systems like nuclear power plant and is extremely dangerous for nuclear power plant piping system since, if the pressure induced exceeds the pressure range of the pipe given by the manufacturer, it can lead to the failure of the piping system integrity. For Yonggwang nuclear power unit 1 and 2, water hammer occurred repeatedly on the outlet piping of regenerative heat exchanger of steam generator blowdown system. Thus, design modification was performed to prevent the water hammer and the analysis of effect on water hammer before and after design modification was performed to verify the validity of the design modification

  11. Actinides inventory of the nuclear power plant of Laguna Verde Unit 1

    International Nuclear Information System (INIS)

    Martinez C, E.; Ramirez S, J. R.; Alonso V, G.

    2013-10-01

    At the present time 435 nuclear power reactors exist for the electricity generation operating in the world and 63 in construction. Mexico has two reactors type BWR in the nuclear power plant of Laguna Verde. The nuclear fuel that is used in the nuclear reactors is retired of the reactor core when the energy that this contained has been extracted. This used fuel is known as spent nuclear fuel, the problem with this fuel is that was irradiated inside the reactor and continuous emitting a high radiation, as well as a significant heat quantity when being extracted, for what is necessary to maintain it in cooling and with some shielding to be protected of the radiation that emits. This objective is achieved confining the fuel in the spent nuclear fuel pool, where it is cooled and the same pool provides the necessary shielding to maintain the surroundings in safety radiation levels for the personnel that work in the power plant. An inconvenience of the pools is its limited storage capacity and that after certain time is necessary to remove the fuel, according to the established regulation to continue operating. To correct this inconvenience, two alternatives of spent fuel disposition exist, 1) the final disposition in deep geologic repositories and 2) the reprocessing and recycled of spent fuel. Each alternative presents its particularities and specific problems; however taking many years to be able to implement anyone of them. To carry out the second option, is indispensable to estimate the total mass of actinides generated in the spent nuclear fuel, that which represents to develop a methodology for it, this action is the main purpose of the present work. Inside our calculation method was necessary to appeal to diverse computation tools as the codes Origin-S and Keno V.a. Later on the obtained were compared with a problem type Benchmark, being obtained a smaller absolute error to 1.0%. (Author)

  12. Safety Evaluation Report related to the operation of Diablo Canyon Nuclear Power Plant, Units 1 and 2 (Docket Nos. 50-275 and 50-323)

    International Nuclear Information System (INIS)

    1984-07-01

    Supplement 27 to the Safety Evaluation Report for Pacific Gas and Electric Company's application for a license to operate Diablo Canyon Nuclear Power Plant, Unit 1 (Docket No. 50-275), has been prepared by the Office of Nuclear Reactor Regulation of the US Nuclear Regulatory Commission. This supplement addresses the revisions to the license conditions and to the Technical Specifications as they relate to Amendment 10 to Diablo Canyon, Unit 1 Facility Operating License, DPR-76

  13. Quality assurance evolution at Laguna Verde Nuclear Power Plant Unit 1 and 2, regulatory aspects

    International Nuclear Information System (INIS)

    Leon Martinez, Cenobia

    1996-01-01

    Quality Assurance (QA) in Mexico started with the construction of the Laguna Verde Nuclear Power Plant. The Nuclear Regulatory Body, based in the adopted regulation, required the use of Quality Assurance in the design, construction and operation of the Plant. This paper describes the evolution of QA from its beginnings, through its developing phase up to this time, and shows the role of the Regulatory Body, which has participated actively in the implantation of QA in a properly manner, enforcing the utility in avoiding deviations and non-compliancies with the established regulation. (author)

  14. Severe Accident Sequence Analysis Program: Anticipated transient without scram simulations for Browns Ferry Nuclear Plant Unit 1

    International Nuclear Information System (INIS)

    Dallman, R.J.; Gottula, R.C.; Holcomb, E.E.; Jouse, W.C.; Wagoner, S.R.; Wheatley, P.D.

    1987-05-01

    An analysis of five anticipated transients without scram (ATWS) was conducted at the Idaho National Engineering Laboratory (INEL). The five detailed deterministic simulations of postulated ATWS sequences were initiated from a main steamline isolation valve (MSIV) closure. The subject of the analysis was the Browns Ferry Nuclear Plant Unit 1, a boiling water reactor (BWR) of the BWR/4 product line with a Mark I containment. The simulations yielded insights to the possible consequences resulting from a MSIV closure ATWS. An evaluation of the effects of plant safety systems and operator actions on accident progression and mitigation is presented

  15. Management of main generator condition during long term plant shut down at Higashidori Nuclear Power Station Unit 1

    International Nuclear Information System (INIS)

    Kato, Seiji

    2014-01-01

    Higashidori Nuclear Power Station Unit 1 shut down on February 6, 2011 to start 4th refuel outage. On March 11, 2011, we keep going refuel outage on this moment a large earthquake occurred and tsunami was generated following it which called 'Great East Japan Earthquake'. Refuel outage takes 3 ∼ 5 months normally but Higashidori NPS still keeping shut down over 3 years due to some issues. In this paper, we introduce about management of Main generator condition during long term plant shut down situation in addition to normal plant shut down situation to keep well. (author)

  16. 77 FR 13156 - Carolina Power & Light Company; Shearon Harris Nuclear Power Plant, Unit 1; Exemption

    Science.gov (United States)

    2012-03-05

    ... generation, and cladding oxidation from the metal/water reaction shall be calculated using the Baker-Just... boiling or pressurized light-water nuclear power reactor fueled with uranium oxide pellets within... spring 2012. The AREVA fuel design consists of low enriched uranium oxide fuel within M5 \\TM\\ zirconium...

  17. 76 FR 55422 - Indiana Michigan Power Company; Donald C. Cook Nuclear Plant, Unit 1; Exemption

    Science.gov (United States)

    2011-09-07

    ... CFR 50.46, ``Acceptance criteria for emergency core cooling systems for light-water nuclear power... contain acceptance criteria for the emergency core cooling system (ECCS) for reactors fueled with zircaloy... CFR Part 50 (1) when the exemptions are authorized by law, will not present an undue risk to public...

  18. Nuclear power plant life time improvement and management program in Korea

    International Nuclear Information System (INIS)

    Sung Yull Hong; Ill Seok Jeong; Taek Ho Song

    1995-01-01

    Korea Electric Power Research Institute (KEPRI) of Korea Electric Power Corporation (KEPCO) has performed a lifetime management of nuclear power plant program (LMNPP), ''Nuclear Power Plant Lifetime Management (PLIM) (I)'', since November 1993, which is a feasibility study of the Kori Unit 1 lifetime management including aging evaluation of the thirteen major components. The results of the PLIM(I) will provide information which is necessary for decision making of the Kori Unit 1 lifetime improvement. A plan of the work scope and schedule for the next phase, PLIM(II), will also be provided by this project. This paper introduced KEPRI's basic strategy of LMNPP, PLIM organization, current status, some interim results of the PLIM(I), and other related programs in Korea. So far, we have done field data survey, systems/structures screening, components prioritization, lifetime evaluation methodology study, and fracture mechanics tests of the Kori Unit 1 reactor pressure vessel surveillance coupons. Currently life assessment of the major components and PLIM economic evaluation of Kori Unit 1 are under way. (author)

  19. Experience and development of on-line BWR surveillance system at Onagawa nuclear power station unit-1

    International Nuclear Information System (INIS)

    Kishi, A.; Chiba, K.; Kato, K.; Ebata, S.; Ando, Y.; Sakamoto, H.

    1986-01-01

    ONAGAWA nuclear power station Unit-1 (Tohoku Electric Power Co.) is a BWR-4 nuclear power station of 524 MW electric power which started commercial operation in June 1984. To attain high reliability and applicability for ONAGAWA-1, Tohoku Electric Power Co. and Toshiba started a Research and Development project on plant surveillance and diagnosis from April 1982. Main purposes of this project are to: (1) Develop an on-line surveillance system and acquire its operating experience at a commercial BWR, (2) Assist in plant operation and maintenance by data acquisition and analysis, (3) Develop a new technique for plant surveillance and diagnosis. An outline of the project, operating experience gained from the on-line surveillance system and an introduction to new diagnosis techniques are reported in this paper. (author)

  20. Integrated Plant Safety Assessment: Systematic Evaluation Program. Millstone Nuclear Power Station, Unit 1, Northeast Nuclear Energy Company, Docket No. 50-245. Final report

    International Nuclear Information System (INIS)

    1983-02-01

    This report documents the review of the Millstone Nuclear Power Station, Unit 1, operated by Northeast Nuclear Energy Company (located in Waterford, Connecticut). Millstone Nuclear Power Station, Unit 1, is one of ten plants reviewed under Phase II of this program. This report indicates how 137 topics selected for review under Phase I of the program were addressed. Equipment and procedural changes have been identified as a result of the review. It is expected that this report will be one of the bases in considering the issuance of a full-term operating license in place of the existing provisional operating license. This report also addresses the comments and recommendations made by the Advisory Committee on Reactor Safeguards in connection with its review of the Draft Report, issued in November 1982

  1. Occupational exposure analysis at the unit 1 of Almirante Alvaro Alberto nuclear power plant

    International Nuclear Information System (INIS)

    Moraes, A.

    1985-01-01

    In order to obtain a complete knowledge of occupational conditions in a PWR nuclear power station, the individual and collective dose distributions are being analysed during the Angra I (Rio de Janeiro - Brazil) station activities. Work conditions with identification of critical areas and groups as well as classification of tasks related to reactor maintenance and startup periods are also studied. This paper analyses radiological data measured at different power levels of the reactor and during maintenance and repair services as well as the refueling operation. (author)

  2. Damage of the Unit 1 reactor building overhead bridge crane at Onagawa Nuclear Power Station caused by the Great East Japan Earthquake and its repair works

    International Nuclear Information System (INIS)

    Sugamata, Norihiko

    2014-01-01

    The driving shaft bearings of the Unit 1 overhead bridge crane were damaged by the Great East Japan Earthquake at Onagawa Nuclear Power Station. The situation, investigation and repair works of the bearing failure are introduced in this paper. (author)

  3. Technical specifications for Grand Gulf Nuclear Station, Unit 1 (Docket No. 50-416). Appendix A to License No. NPF-13

    International Nuclear Information System (INIS)

    1984-08-01

    The Grand Gulf Nuclear Station, Unit 1 Technical Specifications were prepared by the US Nuclear Regulatory Commission to set forth the limits, operating conditions and other requirements applicable to a nuclear facility as set forth in Section 50.36 of 10 CFR part 50 for the protection of the health and safety of the public

  4. Long-term measurement with calorimetric probes at unit 1 of V-1 nuclear power plant

    International Nuclear Information System (INIS)

    Erben, O.; Szasz, Z.; Jirousek, V.; Teren, S.

    1989-01-01

    Two calorimetric probes were tested at the first unit of the Bohunice V-1 nuclear power plant in long-term operation, i.e., during one whole reactor duty time. Each probe consisted of five fission calorimeters and one compensation calorimeter with a tungsten body. The actual calorimeters were provided with jacketed thermocouples 0.5 mm indiameter and 19 m in length. A detailed description is presented of the measuring chains and measurement techniques. Also described is the method of the disposal of the irradiated probes. The method is presented of the evaluation of measured data and the results are discussed of the analysis of these data. The measurements, including measurements during reactor shut-down and the results of the analysis of the measured data proved good viability and stability of the used calorimetres. The method of measuring the thermocouple signals is simple and the in-service evaluation of required data is quick. In order to increase measurement efficiency it would be appropriate to complete the measuring chain and to automate it. Reliability is a affected merely by protecting the thermocouples against mechanical damage during measurement probe handling and on the reactor. (Z.M.). 5 figs., 5 tabs., 5 refs

  5. Lessons learned from the seismic reevaluation of San Onofre Nuclear Generating Station, Unit 1

    International Nuclear Information System (INIS)

    Russell, M.J.; Shieh, L.C.; Tsai, N.C.; Cheng, T.M.

    1987-01-01

    A seismic reevaluation program was conducted for the San Onofre Nuclear Generating Station, Unit No. 1 (SONGS 1). SEP was created by the NRC to provide (1) an assessment of the significance of differences between current technical positions on safety issues and those that existed when a particular plant was licensed, (2) a basis for deciding on how these differences should be resolved in an integrated plant review, and (3) a documented evaluation of plant safety. The Systematic Evaluation Program (SEP) seismic review for SONGS 1 was exacerbated by the results of an evaluation of an existing capable fault near the site during the design review for Units 2 and 3, which resulted in a design ground acceleration of 0.67g. Southern California Edison Company (SCE), the licensee for SONGS 1, realized that a uniform application of existing seismic criteria and methods would not be feasible for the upgrading of SONGS 1 to such a high seismic requirement. Instead, SCE elected to supplement existing seismic criteria and analysis methods by developing criteria and methods closer to the state of the art in seismic evaluation techniques

  6. Auxiliary feedwater system risk-based inspection guide for the Beaver Valley, Units 1 and 2 nuclear power plants

    International Nuclear Information System (INIS)

    Lloyd, R.C.; Vehec, T.A.; Moffitt, N.E.; Gore, B.F.; Vo, T.V.; Rossbach, L.W.; Sena, P.P. III

    1993-02-01

    In a study sponsored by the US Nuclear Regulatory Commission (NRC), Pacific Northwest Laboratory has developed and applied a methodology for deriving plant-specific risk-based inspection guidance for the auxiliary feedwater (AFW) system at pressurized water reactors that have not undergone probabilistic risk assessment (PRA). This methodology uses existing PRA results and plant operating experience information. Existing PRA-based inspection guidance information recently developed for the NRC for various plants was used to identify generic component failure modes. This information was then combined with plant-specific and industry-wide component information and failure data to identify failure modes and failure mechanisms for the AFW system at the selected plants. Beaver Valley Units 1 and 2 were selected as two of a series of plants for study. The product of this effort is a prioritized listing of AFW failures which have occurred at the plant and at other PWRs. This listing is intended for use by NRC inspectors in the preparation of inspection plans addressing AFW risk-important components at Beaver Valley Units 1 and 2

  7. A study on determination methods of fueling machine heavy water supply setpressure for Wolsong nuclear power plant unit 1

    International Nuclear Information System (INIS)

    Kim, J. M.; Jeong, B. Y.; Baek, S. J.; Noh, T. S.; Kim, Y. H.; Park, W. K.

    2001-01-01

    The present Wolsong 1 Fuel Handling (F/H)D 2 O Supply Pressure Control System, based on an analog cascaded Proportional-Integral-Differential (PID) control, is less accurate and requires more labor for test and maintenance in comparison with up-to-data digital controllers. Furthermore, F/H operator and technical staff have recently encountered difficulties in operation and maintenance because of frequent occurrences of system instability and failure, and obsolescence of hardware. However the analysis and design review of F/H D 2 O Supply Pressure Control System have not been performed appropriately. Therefore, the design review of F/H D 2 O Supply Pressure Control System has been thoroughly reviewed and analyzed. Based on the analysis results, the optimum pressure setpoints and its determination methods have been proposed for Wolsong Nuclear Power Plant Unit 1

  8. Seismic structural fragility investigation for the San Onofre Nuclear Generating Station, Unit 1 (Project I); SONGS-1 AFWS Project

    International Nuclear Information System (INIS)

    Wesley, D.A.; Hashimoto, P.S.

    1982-04-01

    An evaluation of the seismic capacities of several of the San Onofre Nuclear Generating Station, Unit 1 (SONGS-1) structures was conducted to determine input to the overall probabilistic methodology developed by Lawrence Livermore National Laboratory. Seismic structural fragilities to be used as input consist of median seismic capacities and their variabilities due to randomness and uncertainty. Potential failure modes were identified for each of the SONGS-1 structures included in this study by establishing the seismic load-paths and comparing expected load distributions to available capacities for the elements of each load-path. Particular attention was given to possible weak links and details. The more likely failure modes were screened for more detailed investigation

  9. 77 FR 47121 - Calvert Cliffs Nuclear Power Plant, LLC; Calvert Cliffs Nuclear Power Plant, Units 1 and 2...

    Science.gov (United States)

    2012-08-07

    ... for Nuclear Power Plant Personnel,'' endorses the Nuclear Energy Institute (NEI) report NEI 06-11...(c)(25). Pursuant to 10 CFR 51.22(b), no environmental impact statement or environmental assessment... hereafter in effect. The facility consists of two pressurized-water reactors (PWRs) located in Calvert...

  10. Safety evaluation report related to the operation of Diablo Canyon Nuclear Power Plant, Units 1 and 2 (Docket Nos. 50-275 and 50-323)

    International Nuclear Information System (INIS)

    1983-12-01

    Supplement 20 to the Safety Evaluation Report for Pacific Gas and Electric Company's application for licenses to operate Diablo Canyon Nuclear Power Plant, Unit 1 and Unit 2 (Docket Nos. 50-275 and 50-323), has been prepared by the Office of Nuclear Reactor Regulation of the US Nuclear Regulatory Commission. This supplement reports on the verification effort for Diablo Canyon Unit 1 that was performed between November 1981 and the present in response to Commission Order CLI-81-30 and an NRC letter of November 19, 1981 to the licensee. Specifically, Supplement 20 addresses those issues and other matters identified in Supplements 18 and 19 that must be resolved prior to Unit 1 achieving criticality and operating at power levels up to 5% of rated full power. This SER Supplement applies only to Diablo Canyon Unit 1

  11. Analogue to digital upgrade project-boiler feedwater control system for Bruce Power nuclear units 1 & 2

    International Nuclear Information System (INIS)

    Long, R.

    2012-01-01

    Bruce Power Nuclear Generating Station A, “Bruce A” is in the final stages of its Restart Project. This capital project will see a large scale rehabilitation of Units 1 and 2 resulting in addition of 1500MW of safe, reliable, clean electricity to the Ontario grid. Restart Project Scope 375, Boiler Feedwater Controls Upgrade was sanctioned to replace obsolete analog devices with a modern digital control system. This project replaced the existing Foxboro H Line analog controls which comprised of 81 individual control modules and support instrumentation. The replacement system was a Triconex Triple Modular Redundant PLC which interfaces with two redundant touch screen monitors. The upgraded digital system incorporates the following controls: 1. Boiler Level Control Loops 2. Dearator Level Control Loops 3. Dearator Pressure Control Loops 4. Boiler Feedwater Recirculation Flow Control Loops A number of technical challenges were addressed when installing a new digital system within the existing plant configuration. Interfaces to new, old and refurbished field devices must be understood as well as implications of connecting to the plant’s Digital Control Computers (DCC’s) and newly installed Steam Generators. The overall project involved many stakeholders to address various requirements from conceptual / design stage through procurement, construction, commissioning and return to service. In addition, the project highlighted the unique requirements found in Nuclear Industry with respect to Human Factors and Software Quality Assurance. (author)

  12. MSR redesign and reconstruction at Indiana Michigan Power Company's Donald C. Cook Nuclear Power Plant, Unit 1

    International Nuclear Information System (INIS)

    Yarden, A.L.; Tam, C.W.; Benes, J.D.; Arnold, W.E.

    1993-01-01

    When Indiana Michigan Power Company's (I and M) 1089- MWe, PWR, Donald C. Cook Nuclear Plant, Unit 1, (Cook 1) in Bridgeman, Michigan went into commercial operation in late 1975, its turbine generator included two Moisture Separator Reheater (MSR) vessels. Each of these original MSRs contained, in addition to the moisture separation section, a single stage 2-pass reheater consisting of 5/8 inch O.D., finned CuNi tubes with main heating steam as an energy source. The enormous size of the tube bank, with a vertical orientation of its tubes' U-bends, led the designer to choose two separate headers for the inlet side and outlet side of the tube bank. Over the years, these 2-pass reheaters had deteriorated mechanically such that maintenance costs had increased considerably. Also, the MSR performance in terms of MWe gain, had fallen off as a result of a gradual reduction of both superheat and moisture separation efficiency. In 1990, these MSRs were totally reconstructed with inherently different 4-pass reheaters and upgraded moisture separation systems. The performance and other direct parameters of these newly retrofitted and improved MSRs have exceeded original design specifications, and their operational stability has improved markedly. This MSR reconstruction at Cook 1 is the first of its kind to include a 4-pass reheater in association with a nuclear turbine generator of this design. This paper highlights the problems and solutions associated respectively with the original reheaters in the Cook 1 MSRs and their recent redesign, reconstruction, and performance

  13. Safety Evaluation Report related to the operation of Grand Gulf Nuclear Station, Units 1 and 2 (Docket Nos. 50-416 and 50-417). Supplement 6

    International Nuclear Information System (INIS)

    1984-08-01

    Supplement 6 to the Safety Evaluation Report for Mississippi Power and Light Company et al. joint application for licenses to operate the Grand Gulf Nuclear Station, Units 1 and 2, located on the east bank of the Mississippi River near Port Gibson in Claiborne County, Mississippi, has been prepared by the Office of Nuclear Reactor Regulation of the US Nuclear Regulatory Commission. This supplement reports the NRC staff's evaluation of open items from previous supplements and Technical Specification changes required before authorizing operation of Unit 1 above 5% of rated power

  14. Safety Evaluation Report related to the operation of Grand Gulf Nuclear Station, Units 1 and 2 (Docket Nos. 50-416 and 50-417). Supplement No. 5

    International Nuclear Information System (INIS)

    1984-08-01

    Supplement 5 to the Safety Evaluation Report for Mississippi Power and Light Company, et al., joint application for licenses to operate the Grand Gulf Nuclear Station, Units 1 and 2, located on the east bank of the Mississippi River near Port Gibson in Claiborne County, Mississippi, has been prepared by the Office of Nuclear Reactor Regulation of the US Nuclear Regulatory Commission. This supplement reports the status on the resolution of those issues that require further evaluation before authorizing operation of Unit 1 above 5% of rated power

  15. Safety-Evaluation Report related to the operation of Grand Gulf Nuclear Station, Units 1 and 2. Docket Nos. 50-416 and 50-417

    International Nuclear Information System (INIS)

    1983-05-01

    Supplement 4 to the Safety Evaluation Report for Mississippi Power and Light Company, et. al., joint application for licenses to operate the Grand Gulf Nuclear Station, Units 1 and 2, located on the east bank of the Mississippi River near Port Gibson in Claiborne County, Mississippi, has been prepared by the Office of Nuclear Reactor Regulation of the US Nuclear Regulatory Commission. This supplement reports the status on the resolution of those issues that required further evaluation before authorizing operation of Unit 1 above 5% rated power and other issues that were to be evaluated during the first cycle of power operation

  16. Integrated-plant-safety assessment Systematic Evaluation program. Millstone Nuclear Power Station, Unit 1, Northeast Nuclear Energy Company, Docket No. 50-245

    International Nuclear Information System (INIS)

    1982-11-01

    The Systematic Evaluation Program was initiated in February 1977 to review the designs of older operating nuclear reactor plants to reconfirm and document their safety. The review provides: (1) an assessment of how these plants compare with current licensing safety requirements relating to selected issues, (2) a basis for deciding on how these differences should be resolved in an integrated plant review, and (3) a documented evaluation of plant safety. This report documents the review of the Millstone Nuclear Power Station, Unit 1, operated by Northeast Nuclear Energy Company (located in Waterford, Connecticut). Millstone Nuclear Power Station, Unit 1, is one of ten plants reviewed under Phase II of this program. This report indicates how 137 topics selected for review under Phase I of the program were addressed. Equipment and procedural changes have been identified as a result of the review. It is expected that this report will be one of the bases in considering the issuance of a full-term operating license in place of the existing provisional operating license

  17. Measures to assess and to assure the integrity of RPV-internals at Isar, Unit 1 Nuclear Power Plant

    International Nuclear Information System (INIS)

    Erve, M.; Bouecke, R.; Leibold, F.; Marschke, D.; Senski, G.; Maier, V.

    1998-01-01

    As visual examinations carried out in autumn 1994 detected cracks in a German BWR plant due to intergranular stress corrosion cracking in several core shroud components manufactured from 1.4550 steel, precautionary examinations and assessments were performed for all other plants. In accordance with these analyses, it can be stated for Isar, Unit 1 that the heat treatment to which the components in question were subjected in the course of manufacture cannot have caused sensitization of the material, and that crack formation due to the damage mechanism primarily identified in the reactor pressure vessel internals at Wuergassen Nuclear Power Station need not be feared. Although the material and corrosion-chemical assessments performed to date did not give any indications for the other crack formation mechanisms that are theoretically relevant for reactor pressure vessel internals (IGSCC due to weld sensitization, IASCC), visual examinations with a limited scope will be carried out with the independent expert's agreement during the scheduled inservice inspections. The fluid-dynamic and structure-mechanical analyses showed that the individual components are subjected only to low loadings, even in the event of accidents, and that the safety objectives shutdown and residual heat removal can be fulfilled even in the case of large postulated cracks. The fracture-mechanics analyses indicated critical through-wall crack lengths which, however, can be promptly and reliably detected during random inservice inspections even when assuming stress corrosion cracking and irradiation-induced low-toughness material conditions. In addition, both the VGB and the Isar, Unit 1 licensee are pursuing further prophylactic measures such as alternative water chemistry modes and an appropriate repair and replacement concept. (author)

  18. Study on application of operating experience to new nuclear power plant

    International Nuclear Information System (INIS)

    Hong, Nam Pyo

    1991-01-01

    From the standpoint of designing the nuclear power plant, nine operating units have been designed and constructed as turn-key base by foreign Nuclear Steam Supply System (NSSS) Suppliers or as component base by foreign Architect/Engineer companies. In case of the component base project, the owner of electric company generally has merits that owner's operational experiences can be effectively incorporated from the beginning stage of design by A/E. Even though six nuclear units, Kori Units 3 and 4, Yonggwang Units 1 and 2, and Ulchin Units 1 and 2, were designed as component base by foreign A/E's, operational experience feedback from Kori Unit 1, such as design improvement and system upgrade, could not be reflected, because the design process of the following units started well ahead before Kori Unit 1 operating experience is obtained enough to reflect on future nuclear power plant design. It can be stated that foreign A/E's used their experience in designing nuclear projects on very limited basis

  19. Safety evaluation report related to the operation of Sequoyah Nuclear Plant, Units 1 and 2, Docket Nos. 50-327 and 50-328, Tennessee Valley Authority

    International Nuclear Information System (INIS)

    1982-12-01

    Supplement No. 6 to the Safety Evaluation Report (SER) related to the operation of the Tennessee Valley Authority's Sequoyah Nuclear Plant, Units 1 and 2, located in Hamilton County, Tennessee, has been prepared by the Office of Nuclear Reactor Regulation of the US Nuclear Regulatory Commission. The purpose of this supplement is to update the staff's evaluations of the issues related to the hydrogen mitigation system identified in the SER and previous supplements as needing resolution

  20. Safety Evaluation Report related to the operation of Diablo Canyon Nuclear Power Plant, Units 1 and 2 (Docket Nos. 50-275 and 50-323)

    International Nuclear Information System (INIS)

    1984-02-01

    Supplement 17 to the Safety Evaluation Report for Pacific Gas and Electric Company's application for licenses to operate Diablo Canyon Nuclear Power Plants, Units 1 and 2 (Docket Nos. 50-275 and 50-323) has been prepared by the Office of Nuclear Reactor Regulation of the US Nuclear Regulatory Commission. This supplement reports the status of certain items that had not been resolved at the time of publication of the Safety Evaluation Report and the previous supplements

  1. Software V and V of PPS for Shin-Hanul Nuclear Power Plant Units 1 and 2

    International Nuclear Information System (INIS)

    Park, Cheollak; Kang, Dongpa; Choe, Changhui; Sohn, Sedo; Beak, Seungmin

    2013-01-01

    Software V and V processes determine whether the development products of a given activity conform to the requirements of that activity and whether the software satisfies its intended use and user needs. This paper introduces the software V and V activities and tasks performed during the software development life cycle performed during the software development life cycle of the Plant Protection System (PPS) for Shin-Hanul Nuclear Power Plant Units 1 and 2 (SHN 1 and 2). The PPS generates signals to actuate Reactor Trip (RT) and Engineered Safety Features (ESF) whenever monitored processes exceed predetermined limits, and the PPS software is classified safety critical and an independent V and V is thus required according to regulations, code and standards. The software V and V efforts, sufficiently disciplined and rigorous, are quite essential to demonstrate that the software development process is of a high quality. The software V and V of PPS for SHN 1 and 2 has been accomplished successfully with systematic V and V procedures and methods established until test phase in compliance with related code and standards. In particular, the use of automated tools such as LDRA and DOORS greatly has contributed to an improvement of a software quality, and a reduction of a verification time and human errors

  2. Montague Nuclear Power Station, Units 1 and 2: Final environmental statement (Docket Nos. 50-496 and 50-497)

    International Nuclear Information System (INIS)

    1977-02-01

    The proposed action is the issuance of construction permits to the Northeast Nuclear Energy Company for the construction of the Montague Nuclear Power Station, Units 1 and 2, located on the Connecticut River in the Town of Montague, Massachusetts. The plant will employ two identical boiling-water reactors to produce up to 3579 megawatts thermal (MWt) each. Two steam turbine-generators will use this heat to provide 1150 MWe (net) of electrical power capacity from each turbine-generator. A design power level of 3759 MWt (1220 Mwe net) for each unit is anticipated at a future date and is considered in the assessments contained in this statement. The waste heat will be rejected through natural-draft cooling towers using makeup water obtained from and discharged to the Connecticut River. The 1900-acre site is about 90% forest, with the remaining acreage in transmission-line corridor and old-field vegetation. The total loss of mixed-age forest will be 1273 acres. Nodesignated scenic areas will be crossed. Sixty acres of public lands, State forests, and parks will be lost to transmission facilities as well as losses associated with crossings of 2.0 miles of water bodies and 11.9 miles of wetlands. The maximum estimated potential loss of salable wood products will be $849,600. A maximum of 85.8 cfs of cooling water will be withdrawn from the Connecticut River. A maximum of 17.2 cfs will be returned to the river with the dissolved solids concentration increased by a factor of about 5. A maximum of 68.6 cfs will be evaporated to the atmosphere by the cooling towers. 143 refs., 58 figs., 69 tabs

  3. Safety-evaluation report related to operation of McGuire Nuclear Station, Units 1 and 2. Docket Nos. 50-369 and 50-370

    International Nuclear Information System (INIS)

    1983-05-01

    This report supplements the Safety Evaluation Report Related to the Operation of McGuire Nuclear Station, Units 1 and 2 (SER (NUREG-0422)) issued in March 1978 by the Office of Nuclear Reactor Regulation of the US Nuclear Regulatory Commission with respect to the application filed by Duke Power Company, as applicant and owner, for licenses to operate the McGuire Nuclear Station, Units 1 and 2 (Docket Nos. 50-369 and 50-370). The facility is located in Mecklenburg County, North Carolina, about 17 mi north-northwest of Charlotte, North Carolina. This supplement provides information related to issuance of a full-power authorization for Unit 2. The staff concludes that the McGuire Nuclear Station can be operated by the licensee without endangering the health and safety of the public

  4. Public exposure from environmental release of radioactive material under normal operation of unit-1 Bushehr nuclear power plant

    International Nuclear Information System (INIS)

    Sohrabi, M.; Parsouzi, Z.; Amrollahi, R.; Khamooshy, C.; Ghasemi, M.

    2013-01-01

    Highlights: ► The unit-1 Bushehr nuclear power plant is a VVER type reactor with 1000 MWe power. ► Doses of public critical groups living around the plant were assessed under normal reactor operation conditions. ► PC-CREAM 98 computer code developed by the HPA was applied to assess the public doses. ► Doses are comparable with those in the FSAR, in the ER and doses monitored. ► The doses assessed are lower than the dose constraint of 0.1 mSv/y associated with the plant. - Abstract: The Unit-1 Bushehr Nuclear Power Plant (BNPP-1), constructed at the Hallileh site near Bushehr located at the coast of the Persian Gulf, Iran, is a VVER type reactor with 1000 MWe power. According to standard practices, under normal operation conditions of the plant, radiological assessment of atmospheric and aquatic releases to the environment and assessment of public exposures are considered essential. In order to assess the individual and collective doses of the critical groups of population who receive the highest dose from radioactive discharges into the environment (atmosphere and aquatic) under normal operation conditions, this study was conducted. To assess the doses, the PC-CREAM 98 computer code developed by the Radiation Protection Division of the Health Protection Agency (HPA; formerly called NRPB) was applied. It uses a standard Gaussian plume dispersion model and comprises a suite of models and data for estimation of the radiological impact assessments of routine and continuous discharges from an NPP. The input data include a stack height of 100 m annual radionuclides release of gaseous effluents from the stack and liquid effluents that are released from heat removal system, meteorological data from the Bushehr local meteorological station, and the data for agricultural products. To assess doses from marine discharges, consumption of sea fish, crustacean and mollusca were considered. According to calculation by PC-CREAM 98 computer code, the highest individual

  5. Technical evaluation of the electrical, instrumentation, and control design aspects of the low temperature overpressure protection system for the Salem nuclear power plant, Unit 1

    International Nuclear Information System (INIS)

    Laudenbach, D.H.

    1979-03-01

    The technical evaluation is presented for the electrical, instrumentation, and control design aspects of the low temperature overpressure protection system for the Salem nuclear power plant, Unit 1. Design basis criteria used to evaluate the acceptability of the system include operator action, system testability, single failure criterion, and seismic Category I and IEEE Std-279-1971 criteria

  6. Technical evaluation of the alternate to the keylock control to the bypass valves for the Davis-Besse nuclear power plant, Unit 1

    International Nuclear Information System (INIS)

    Ibarra, J.G.

    1979-09-01

    This report documents the technical evaluation of the alternate to the keylock control to the bypass valves for the Davis-Besse nuclear power plant, Unit 1. The review criteria are inferred from the NRC Reactor Safety Study (WASH-1400) and the Safety Evaluation Report for Davis-Besse. This report is supplied as part of the Selected Electrical, Instrumentation, and Control Systems Issues Program being conducted for the US Nuclear Regulatory Commission by Lawrence Livermore Laboratory

  7. Technical evaluation of the proposed deletion of a reactor trip on a turbine trip below 50-percent power for the Beaver Valley nuclear power plant, Unit 1

    International Nuclear Information System (INIS)

    Reeves, W.E.

    1979-12-01

    This report documents the technical evaluation of the Duquesne Light Company's proposed license amendment for the deletion of a reactor trip on a turbine trip below 50% power for the Beaver Valley nuclear power plant, Unit 1. This report is supplied as part of the Selected Electrical, Instrumentation, and Control Systems Issues Program being conducted for the US Nuclear Regulatory Commission by Lawrence Livermore Laboratory

  8. A pilot application of risk-based methods to establish in-service inspection priorities for nuclear components at Surry Unit 1 Nuclear Power Station

    International Nuclear Information System (INIS)

    Vo, T.; Gore, B.; Simonen, F.; Doctor, S.

    1994-08-01

    As part of the Nondestructive Evaluation Reliability Program sponsored by the US Nuclear Regulatory Commission, the Pacific Northwest Laboratory is developing a method that uses risk-based approaches to establish in-service inspection plans for nuclear power plant components. This method uses probabilistic risk assessment (PRA) results and Failure Modes and Effects Analysis (FEMA) techniques to identify and prioritize the most risk-important systems and components for inspection. The Surry Nuclear Power Station Unit 1 was selected for pilot applications of this method. The specific systems addressed in this report are the reactor pressure vessel, the reactor coolant, the low-pressure injection, and the auxiliary feedwater. The results provide a risk-based ranking of components within these systems and relate the target risk to target failure probability values for individual components. These results will be used to guide the development of improved inspection plans for nuclear power plants. To develop inspection plans, the acceptable level of risk from structural failure for important systems and components will be apportioned as a small fraction (i.e., 5%) of the total PRA-estimated risk for core damage. This process will determine target (acceptable) risk and target failure probability values for individual components. Inspection requirements will be set at levels to assure that acceptable failure probabilistics are maintained

  9. Fracture Toughness Evaluation of Kori-1 RPV Beltline Weld for a Long-Term Operation

    International Nuclear Information System (INIS)

    Lee, Bong-Sang; Kim, Min-Chul; Ahn, Sang-Bok; Kim, Byung-Chul; Hong, Jun-Hwa

    2007-01-01

    Irradiation embrittlement of RPV (reactor pressure vessel) material is the most important aging issue for a long-term operation of nuclear power plants. KORI unit 1, which is the first PWR in Korea, is approaching its initial licensing life of 30 years. In order to operate the reactor for another 10 years and more, it should be demonstrated that the irradiation embrittlement of the reactor will be adequately managed by ensuring that the fracture toughness properties have a certain level of the safety margin. The current regulation requires Charpy V-notch impact data through conventional surveillance tests. It is based on the assumption that Charpy impact test results are well correlated with the fracture toughness properties of many engineering steels. However, Charpy V-notch impact data may not be adequate to estimate the fracture toughness of certain materials, such as Linde 80 welds. During the last decade, a tremendous number of fracture toughness data on many RPV steels have been produced in accordance with the new standard test method, the so-called master curve method. ASTM E1921 represents a revolutionary advance in characterizing fracture toughness of RPV steels, since it permits establishing the ductile to brittle transition portion of the fracture toughness curve with direct measurements on a relatively small number of relatively small specimens, such as pre-cracked Charpy specimens. Actual fracture toughness data from many different RPV steels revealed that the Charpy test estimations are generally conservative with the exception of a few cases. Recent regulation codes in USA permit the master curve fracture toughness methodology in evaluating an irradiation embrittlement of commercial nuclear reactor vessels

  10. Point Beach Nuclear Plant, Units 1 and 2. Semiannual operating report No. 10, January--June 1975

    International Nuclear Information System (INIS)

    1975-01-01

    Unit 1 operated at an average capacity factor of 65.2 percent with a net efficiency of 31.41 percent. Unit 2 operted at an average capacity factor of 88.6 lpercent with a net efficiency of 32.28 percent. Unit 1 was essentially base loaded while Unit 2 operated on load follow. Information is presented concerning power generation, shutdowns, corrective maintenance, chemistry and radiochemistry, occupational radiation exposure, release of radioactive materials, abnormal occurrences, and environmental monitoring. (FS)

  11. Interim reliability-evaluation program: analysis of the Browns Ferry, Unit 1, nuclear plant. Appendix B - system descriptions and fault trees

    International Nuclear Information System (INIS)

    Mays, S.E.; Poloski, J.P.; Sullivan, W.H.; Trainer, J.E.; Bertucio, R.C.; Leahy, T.J.

    1982-07-01

    This report describes a risk study of the Browns Ferry, Unit 1, nuclear plant. The study is one of four such studies sponsored by the NRC Office of Research, Division of Risk Assessment, as part of its Interim Reliability Evaluation Program (IREP), Phase II. This report is contained in four volumes: a main report and three appendixes. Appendix B provides a description of Browns Ferry, Unit 1, plant systems and the failure evaluation of those systems as they apply to accidents at Browns Ferry. Information is presented concerning front-line system fault analysis; support system fault analysis; human error models and probabilities; and generic control circuit analyses

  12. Joint U.S./Russian Study on the Development of a Preliminary Cost Estimate of the SAFSTOR Decommissioning Alternative for the Leningrad Nuclear Power Plant Unit #1

    Energy Technology Data Exchange (ETDEWEB)

    SM Garrett

    1998-09-28

    The objectives of the two joint Russian/U.S. Leningrad Nuclear Power Plant (NPP) Unit #1 studies were the development of a safe, technically feasible, economically acceptable decom missioning strategy, and the preliminary cost evaluation of the developed strategy. The first study, resulting in the decommissioning strategy, was performed in 1996 and 1997. The preliminary cost estimation study, described in this report, was performed in 1997 and 1998. The decommissioning strategy study included the analyses of three basic RBM.K decommission- ing alternatives, refined for the Leningrad NPP Unit #1. The analyses included analysis of the requirements for the planning and preparation as well as the decommissioning phases.

  13. A pilot application of risk-informed methods to establish inservice inspection priorities for nuclear components at Surry Unit 1 Nuclear Power Station. Revision 1

    International Nuclear Information System (INIS)

    Vo, T.V.; Phan, H.K.; Gore, B.F.; Simonen, F.A.; Doctor, S.R.

    1997-02-01

    As part of the Nondestructive Evaluation Reliability Program sponsored by the US Nuclear Regulatory Commission, the Pacific Northwest National Laboratory has developed risk-informed approaches for inservice inspection plans of nuclear power plants. This method uses probabilistic risk assessment (PRA) results to identify and prioritize the most risk-important components for inspection. The Surry Nuclear Power Station Unit 1 was selected for pilot application of this methodology. This report, which incorporates more recent plant-specific information and improved risk-informed methodology and tools, is Revision 1 of the earlier report (NUREG/CR-6181). The methodology discussed in the original report is no longer current and a preferred methodology is presented in this Revision. This report, NUREG/CR-6181, Rev. 1, therefore supersedes the earlier NUREG/CR-6181 published in August 1994. The specific systems addressed in this report are the auxiliary feedwater, the low-pressure injection, and the reactor coolant systems. The results provide a risk-informed ranking of components within these systems

  14. Safety evaluation report related to the operation of Catawba Nuclear Station, Units 1 and 2 (Docket Nos. 50-413 and 50-414)

    International Nuclear Information System (INIS)

    1984-07-01

    The report supplements the Safety Evaluation Report (NUREG-0954) issued in February 1983 by the Office of Nuclear Reactor Regulation of the US Nuclear Regulatory Commission with respect to the application filed by Duke Power Company, North Carolina Municipal Power Agency Number 1, North Carolina Membership Corporation, and Saluda River Electric Cooperative, Inc. as applicants and owners, for licenses to operate the Catawba Nuclear Station, Units 1 and 2 (Docket Nos. 50-413 and 50-414, respectively). The facility is located in York County, South Carolina, approximately 9.6 km (6 mi) north of Rock Hill and adjacent to Lake Wylie. This supplement provides additional information supporting the license for fuel loading and precriticality testing for Unit 1

  15. Safety evaluation report related to the operation of Catawba Nuclear Station, Units 1 and 2 (Docket Nos. 50-413 and 50-414)

    International Nuclear Information System (INIS)

    1984-12-01

    This report supplements the Safety Evaluation Report (NUREG-0954) issued in February 1983 by the Office of Nuclear Reactor Regulation of the US Nuclear Regulatory Commission with respect to the application filed by Duke Power Company, North Carolina Municipal Power Agency Number 1, North Carolina Membership Corporation, and Saluda River Electric Cooperative, Inc., as applicants and owners, for licenses to operate the Catawba Nuclear Station, Units 1 and 2 (Docket Nos. 50-413 and 50-414, respectively). The facility is located in York County, South Carolina, approximately 9.6 km (6 mi) north of Rock Hill and adjacent to Lake Wylie. This supplement provides additional information supporting the license for initial criticality and power ascension to full-power opertion for Unit 1

  16. Safety evaluation report related to the operation of Diablo Canyon Nuclear Power Plant, Units 1 and 2 (Docket Nos. 50-275 and 50-323). Suppl. 22

    International Nuclear Information System (INIS)

    1984-03-01

    Supplement 22 to the Safety Evaluation Report for Pacific Gas and Electric Company's application for licenses to operate Diablo Canyon Nuclear Power Plants, Unit 1 and 2 (Docket Nos. 50-275 and 50-323), has been prepared jointly by the Office of Nuclear Reactor Regulation and the Region V Office of the US Nuclear Regulatory Commission. This supplement provides the criteria that were used by the staff to determine which of the allegations that have been evaluated and must be resolved prior to Unit 1 achieving criticality and operating at power level up to 5 percent of rated power (i.e., low power operation). The supplement also reports on the status of the staff's investigation, inspection and evaluation of 219 allegations or concerns that have been identified to the NRC as of March 9, 1984, excluding those recently received under 10 CFR 2.206 petitions

  17. Safety evaluation report related to the operation of Watts Bar Nuclear Plant, Units 1 and 2 (Docket Nos. 50-390 and 50-391). Supplement No. 14

    Energy Technology Data Exchange (ETDEWEB)

    Tam, P.S.

    1994-12-01

    Supplement No. 14 to the Safety Evaluation Report for the application filed by the Tennessee Valley Authority for license to operate Watts Bar Nuclear Plant, Units 1 and 2, Docket Nos. 50-390 and 50-391, located in Rhea County, Tennessee, has been prepared by the Office of Nuclear Reactor Regulation of the Nuclear Regulatory Commission. The purpose of this supplement is to update the Safety Evaluation with additional information submitted by the applicant since Supplement No. 13 was issued, and matters that the staff had under review when Supplement No. 13 was issued.

  18. Safety Evaluation Report related to the operation of Diablo Canyon Nuclear Power Plant, Units 1 and 2 (Docket Nos. 50-275 and 50-323)

    International Nuclear Information System (INIS)

    1991-06-01

    Supplement 34 to the Safety Evaluation Report for the application by Pacific Gas and Electric Company (PG ampersand E) for licenses to operate Diablo Canyon Nuclear Power Plant, Unit Nos. 1 and 2 (Docket Nos. 50-275 and 50-323, respectively) has been prepared by the Office of Nuclear Reactor Regulation of the US Nuclear Regulatory Commission. This supplement documents the NRC staff review of the Long-Term Seismic Program conducted by PG ampersand E in response to License Condition 2.C.(7) of Facility Operating License DPR-80, the Diablo Canyon Unit 1 operating license. 111 refs., 20 figs., 31 tabs

  19. Safety evaluation report related to the operation of Diablo Canyon Nuclear Power Plant, Units 1 and 2 (Docket Nos. 50-275 and 50-323)

    International Nuclear Information System (INIS)

    1984-06-01

    Supplement 23 to the Safety Evaluation Report for Pacific Gas and Electric Company's application for licenses to operate Diablo Canyon Nuclear Power Plants, Units 1 and 2 (Docket Nos. 50-275 and 50-323) has been prepared by the Office of Nuclear Reactor Regulation of the US Nuclear Regulatory Commission. This supplement addresses the applicant's requests for approval of 22 deviations from the requirements of Section III.G of Appendix R of Title 10 of the Code of Federal Regulations Part 50

  20. Safety evaluation report related to the operation of Watts Bar Nuclear Plant, Units 1 and 2 (Docket Nos. 50-390 and 50-391): Supplement No. 19

    International Nuclear Information System (INIS)

    1995-11-01

    Supplement No. 19 to the Safety Evaluation Report for the application filed by the Tennessee Valley Authority for license to operate Watts Bar Nuclear Plant, Units 1 and 2, Docket Nos. 50-390 and 50-391, located in Rhea County Tennessee, has been prepared by the Office of Nuclear Reactor Regulation of the Nuclear Regulatory Commission. The purpose of this supplement is to update the Safety Evaluation with (1) additional information submitted by the applicant since Supplement No. 18 was issued, and (2) matters that the staff had under review when Supplement No. 18 was issued

  1. Safety evaluation report related to the operation of Shearon Harris Nuclear Power Plant, Units 1 and 2. Docket Nos. STN 50-400 and STN 50-401

    International Nuclear Information System (INIS)

    1983-11-01

    The Safety Evaluation Report for the application filed by the Carolina Power and Light Company, as applicant and owner, for licenses to operate the Shearon Harris Nuclear Power Plant Units 1 and 2 (Docket Nos. 50-400 and 50-401) has been prepared by the Office of Nuclear Reactor Regulation of US Nuclear Regulatory Commission. The facility is located near Raleigh, North Carolina. Subject to favorable resolution of the items discussed in this report, the NRC staff concludes that the facility can be operated by the applicant without endangering the health and safety of the public

  2. Safety evaluation report related to the operation of Watts Bar Nuclear Plant, Units 1 and 2, Docket Nos. 50-390 and 50-391

    International Nuclear Information System (INIS)

    1992-01-01

    Supplement No. 8 to the Safety Evaluation Report for the application filed by the Tennessee Valley Authority for license to operate Watts Bar Nuclear plant, Units 1 and 2, Docket Nos. 50-390 and 50-391, located in Rhea County, Tennessee, has been prepared by the Office of Nuclear Reactor Regulation of the Nuclear Regulatory Commission. The purpose of this supplement is to update the Safety Evaluation of (1) additional information submitted by the applicant since Supplement No. 7 was issued, and (2) matters that the staff had under review when Supplement No. 7 was issued

  3. 76 FR 30206 - Southern Nuclear Operating Company, Inc., Vogtle Electric Generating Plant, Unit 1 and 2; Notice...

    Science.gov (United States)

    2011-05-24

    ... Operating Company, Inc., Vogtle Electric Generating Plant, Unit 1 and 2; Notice of Consideration of Issuance..., http://www.regulations.gov . Because your comments will not be edited to remove any identifying or... received from other persons for submission to the NRC inform those persons that the NRC will not edit their...

  4. Technical evaluation report on the proposed design modifications and technical-specification changes on grid voltage degradation for the San Onofre Nuclear Genetating Station, Unit 1

    International Nuclear Information System (INIS)

    Selan, J.C.

    1982-01-01

    This report documents the technical evaluation of the proposed design modifications and Technical Specification changes for protection of Class 1E equipment from grid voltage degradation for the San Onofre Nuclear Generating Station, Unit 1. The review criteria are based on several IEEE standards and the Code of Federal Regulations. The evaluation finds that the proposed design modifications and Technical Specification changes will ensure that the Class 1E equipment will be protected from sustained voltage degradation

  5. Influence of marine sediments in the distribution of the main radionuclides of the effluent from the nuclear power plant Almirante Alvaro Alberto (Unit 1)

    International Nuclear Information System (INIS)

    Brugnara, Miriam

    1977-01-01

    This study aimed to: 1) Characterize bottom sediments of the Angra dos Reis region, in the dispersion area of the effluent of the central Almirante Nuclear Alvaro Alberto, Unit 1. 2) Determining the adsorption capacity of these sediments to the long half-life and mean radionuclides to be released in the reactor effluent in a higher concentration. 3) Estimate the fraction of the different studied radionuclides that will be immobilized in sediments. 4) Identify critical radionuclides available for food chain

  6. Browns Ferry Nuclear Power Station, Units 1, 2, and 3. Annual operating report: January--December 1976

    International Nuclear Information System (INIS)

    1977-01-01

    Units 1 and 2 were down for the first half of the year caused by the fire of March 1975. Net electrical power generated by Unit 1 this year was 1,301,183 MWH with the generator on line 2,175.25 hrs. Unit 2 generated 1,567,170 MWH with the generator on line 2,548.73 hrs. Unit 3 began full power operation on November 20th and generated 1,416,891 MWH with the generator on line 2,058.20 hrs. Information is presented concerning operations, fuel performance, surveillance testing, containment leak testing, changes, power generation, shutdown and forced reductions, coolant chemistry, occupational radiation exposures, and maintenance

  7. Dresden Nuclear Power Station, Units 1, 2, and 3. Semiannual report on operating and maintenance, July--December 1974

    International Nuclear Information System (INIS)

    1975-01-01

    Unit 1 generated 388,882 MWH(e) and was on line 3111.2 hours, Unit 2 generated 1,204,106 MWH(e) and was on line 2013.4 hours, and Unit 3 generated 2,250,810 MWH(e) and was on line 3836 hours. Information is presented concerning operations, shutdowns, maintenance, changes, tests, and experiments for the three units. (U.S.)

  8. Technical evaluation report on the monitoring of electric power to the reactor protection system for the Nine Mile Point Nuclear Station, Unit 1 (Docket No. 50-220)

    International Nuclear Information System (INIS)

    Selan, J.C.

    1984-01-01

    This report documents the technical evaluation of the monitoring of electric power to the reactor protection system (RPS) at the Nine Mile Point Nuclear Station, Unit 1. The evaluation is to determine if the proposed design modification will protect the RPS from abnormal voltage and frequency conditions which could be supplied from the power supplies and will meet certain requirements set forth by the Nuclear Regulatory Commission. The proposed design modifications will protect the RPS from sustained abnormal voltage and frequency conditions from the supplying sources

  9. Technical evaluation of the electrical, instrumentation, and control design aspects of the low temperature overpressure protection system for the Point Beach Nuclear Power Plant, Units 1 and 2

    International Nuclear Information System (INIS)

    Laudenbach, D.H.

    1979-03-01

    The technical evaluation is presented for the electrical, instrumentation, and control design aspects of the low temperature overpressure protection system for the Point Beach nuclear power plant, Units 1 and 2. Design basis criteria used to evaluate the acceptability of the system included operator action, system testability, single failure criterion, and seismic Category I and IEEE Std-279-1971 criteria. This report is supplied as part of the Selected Electrical, Instrumentation, and Control Systems Issues Support Program being conducted for the U.S. Nuclear Regulatory Commission by Lawrence Livermore Laboratory

  10. Technical evaluation of the electrical, instrumentation, and control design aspects of the low temperature overpressure protection system for the Point Beach Nuclear Power Plant, Units 1 and 2

    Energy Technology Data Exchange (ETDEWEB)

    Laudenbach, D.H.

    1979-03-01

    The technical evaluation is presented for the electrical, instrumentation, and control design aspects of the low temperature overpressure protection system for the Point Beach nuclear power plant, Units 1 and 2. Design basis criteria used to evaluate the acceptability of the system included operator action, system testability, single failure criterion, and seismic Category I and IEEE Std-279-1971 criteria. This report is supplied as part of the Selected Electrical, Instrumentation, and Control Systems Issues Support Program being conducted for the U.S. Nuclear Regulatory Commission by Lawrence Livermore Laboratory.

  11. Palo Verde Nuclear Generating Station, Units 1, 2, and 3 (Docket Nos. STN 50-528, STN 50-529, and STN 50-530): Final environmental statement

    International Nuclear Information System (INIS)

    1982-02-01

    The proposed action is the issuance of operating licenses to the Arizona Public Service Company (APS, applicant) for the startup and operation of PVNGS, Units 1, 2, and 3, located in Maricopa County, about 24 km (15 mi) west of Buckeye, Arizona. The information in this statement represents the second assessment of the environmental impact associated with PVNGS Units 1, 2, and 3 pursuant to the guidelines of the National Environmental Policy Act of 1969 (NEPA) and Title 10 of the Code of Federal Regulations (10 CFR) Part 51 of the Commissions's Regulations. After receiving an application in July 1974 to construct this station, the staff carried out a review of impacts that would occur during its construction and operation. That evaluation was issued as a Final Environmental Statement/emdash/Construction Phase (FES-CP). After this environmental review, a safety review, an evaluation by the Advisory Committee on Reactor Safeguards, and public hearings in Phoenix, Arizona, the US Nuclear Regulatory Commission issued Construction Permits Nos. CPPR-141, CPPR-142, and CPPR-143 for the construction of PVNGS Units 1, 2, and 3. As of September 1981, the construction of Unit 1 was about 92 percent complete, Unit 2 was 68 percent complete, and Unit 3 was 26 percent complete. 11 figs., 21 tabs

  12. Risk-based assessment of the allowable outage times for the unit 1 leningrad nuclear power plant ECCS components

    International Nuclear Information System (INIS)

    Koukhar, Sergey; Vinnikov, Bronislav

    2009-01-01

    Present paper describes a method for risk - informed assessment of the Allowable Outage Times (AOTs). The AOT is the time, when components of a safety system allowed to be out of service during power operation or during shutdown operation off a plant. If the components are not restored during the time, the plant in operation must be shut down or the plant in a given shutdown mode has to go to safer shutdown mode. Application of the method is also provided for the equipment of the Unit 1 Leningrad NPP ECCS components. For solution of the problem it is necessary to carry out two series of computations using a Living PSA model, level 1. In the first series of the computations the core damage frequency (CDFb) for the base configuration of the plant is determined (there is no equipment out of service). Here the symbol 'b' means the base configuration of a plant. In the second series of the computations the core damage frequency (CDFi) for the configuration of the plant with the component (which is out of service) is calculated. That is here CDFi is determined for the failure probability of the component equal to 1.0 (component 'i' is unavailable). Then it is necessary to determine so called Risk Increase Factor (RIF) using the following ratio: RIFi = CDFi / CDFb. At last the AOT is calculated with the help of the ratio: AOTi = Tppr / RIFi, where Tppr is a period of time between two Planned Preventive Repairs (PPRs). 1. Using the risk based approach the AOTs were calculated for a set of the components of the Unit 1 Leningrad NPP ECCS components. 2. The main conclusion from the analysis is that the current deterministic AOTs for the ECCS components are conservative and should be extended. 3. The risk based extension of the AOTs for the ECCS components can prevent the Unit 1 Leningrad NPP to enter into the operating modes with increased risk. (author)

  13. Optimal inspection and replacement periods of the safety system in Wolsung Nuclear Power Plant Unit 1 with an optimized cost perspective

    International Nuclear Information System (INIS)

    Jinil Mok; Poong Hyun Seong

    1996-01-01

    In this work, a model for determining the optimal inspection and replacement periods of the safety system in Wolsung Nuclear Power Plant Unit 1 is developed, which is to minimize economic loss caused by inadvertent trip and the system failure. This model uses cost benefit analysis method and the part for optimal inspection period considers the human error. The model is based on three factors as follows: (i) The cumulative failure distribution function of the safety system, (ii) The probability that the safety system does not operate due to failure of the system or human error when the safety system is needed at an emergency condition and (iii) The average probability that the reactor is tripped due to the failure of system components or human error. The model then is applied to evaluate the safety system in Wolsung Nuclear Power Plant Unit 1. The optimal replacement periods which are calculated with proposed model differ from those used in Wolsung NPP Unit 1 by about a few days or months, whereas the optimal inspection periods are in about the same range. (author)

  14. Safety evaluation report related to the operation of Watts Bar Nuclear Plant, Units 1 and 2 (Docket Nos. 50-390 and 50-391). Supplement No. 17

    International Nuclear Information System (INIS)

    Tam, P.S.

    1995-10-01

    This report supplements the Safety Evaluation Report (SER), NUREG-0847 (June 1982), Supplement No. 1 (September 1982), Supplement No. 2 (January 1984), Supplement No. 3 (January 1985), Supplement No. 4 (March 1985), Supplement No. 5 (November 1990), Supplement No. 6 (April 1991), Supplement No. 7 (September 1991), 1991), Supplement No. 8 (January 1992), Supplement No. 9 (June 1992), Supplement No. 10 (October 1992), Supplement No. 11 (April.1993), Supplement No. 12 (October 1993), Supplement No. 13 (April 1994), Supplement No. 14 (December 1994), Supplement No. 15 (June 1995), and Supplement No. 16 (September 1995) issued by the Office of Nuclear Reactor Regulation of the US Nuclear Regulatory Commission with respect to the application filed by the Tennessee Valley Authority, as applicant and owner, for licenses to operate the Watts Bar Nuclear Plant, Units 1 and 2 (Docket Nos. 50--390 and 50--391). The facility is located in Rhea county, Tennessee, near the Watts Bar Dam on the Tennessee River. In this supplement, NRC examines the significant problems of construction quality and quality assurance effectiveness that led TVA to withdraw its certification in 1985 that Watts Bar Unit I was ready to load fuel. Also discussed are the extensive corrective actions performed by TVA according to its nuclear performance plans and other supplemental programs, and NRC's extensive oversight to determine whether the Watts Bar Unit 1 construction quality and TVA's operational readiness and quality assurance effectiveness are adequate for a low-power operating license to be issued. SSER 17 does not address Watts Bar Unit 2, except for the systems which are necessary to support Unit 1 operation

  15. A special information campaign on decommissioning of unit 1 at the Ignalina Nuclear Power Plant started in Lithuania

    International Nuclear Information System (INIS)

    Vitkiene, E.

    2000-01-01

    A lack of understanding is felt in Lithuania of the importance of informing the public about nuclear energy, its safety and decisions related with nuclear energy in general. our swedish colleagues have noticed this flaw in our work and a joined decision has been taken to start a series of publicity projects. It was decided to work along three lines: a series of programmes on the national TV, support to the media of the town of Visaginas and creating an Internet page on the Ignalina Nuclear Power Plant decommissioning

  16. 75 FR 24997 - FPL Energy Point Beach, LLC; Point Beach Nuclear Plant, Units 1 and 2; Environmental Assessment...

    Science.gov (United States)

    2010-05-06

    ... proposed action is necessary to correct a typographical error in Appendix C which incorrectly labels the... day of April 2010. For the Nuclear Regulatory Commission. Peter S. Tam, Senior Project Manager, Plant...

  17. Safety assessment of Olkiluoto NPP units 1 and 2. Decision of the Radiation and Nuclear Safety Authority regarding the periodic safety review of the Olkiluoto NPP

    International Nuclear Information System (INIS)

    2010-02-01

    In this safety assessment the Radiation and Nuclear Safety Authority (STUK) has evaluated the safety of the Olkiluoto Nuclear Power Plant units 1 and 2 in connection with the periodic safety review. This safety assessment provides a summary of the reviews, inspections and continuous oversight carried out by STUK. The issues addressed in the assessment and the related evaluation criteria are set forth in the nuclear energy and radiation safety legislation and the regulations issued thereunder. The provisions of the Nuclear Energy Act concerning the safe use of nuclear energy, security and emergency preparedness arrangements, and waste management are specified in more detail in the Government Decrees and Regulatory Guides issued by STUK. Based on the assessment, STUK consideres that the Olkiluoto Nuclear Power Plant units 1 and 2 meet the set safety requirements for operational nuclear power plants, the emergency preparedness arrangements are sufficient and the necessary control to prevent the proliferation of nuclear weapons has been appropriately arranged. The physical protection of the Olkiluoto nuclear power plant is not yet completely in compliance with the requirements of Government Decree 734/2008, which came into force in December 2008. Further requirements concerning this issue based also on the principle of continuous improvement were included in the decision relating to the periodic safety review. The safety of the Olkiluoto nuclear power plant was assessed in compliance with the Government Decree on the Safety of Nuclear Power Plants (733/2008), which came into force in 2008. The decree notes that existing nuclear power plants need not meet all the requirements set out for new plants. Most of the design bases pertaining to the Olkiluoto 1 and 2 nuclear power plant units were set in the 1970s. Substantial modernisations have been carried out at the Olkiluoto 1 and 2 nuclear power plant units since their commissioning to improve safety. This is in line with

  18. Investigation of cracking on a main steam isolation valve shaft from the Farley unit 1 nuclear power plant

    International Nuclear Information System (INIS)

    Czajkowski, C.J.

    1985-01-01

    The chemical analysis of the Farley Unit 1 MSIV shaft (69C) showed that the chemical composition of the material was consistent with that expected of a Type 410 stainless steel. The microstructure observed in the base metal (tempered martensite) is consistent with that expected in a Type 410 stainless steel in the quenched and tempered condition. The hardness measurements (both Rsub(c) and Knoop) show that the hardness observed (Rsub(c) 41.3 with a KN max of 459) is significantly higher than that which was anticipated by the heat treatments performed. The cracking was intergranular in nature, occuring along prior austenite grain boundaries. There was no evidence of fatigue interaction on the fracture observed, and no definitive corrodent species identified. The cracking is considered to be an intergranular stress corrosion cracking phenomenon resulting from a high hardness-susceptible material under pressurized water reactor conditions

  19. Erie Nuclear Plant, Units 1 and 2. License application, preliminary safety analysis report, volume 1: chapter 1

    International Nuclear Information System (INIS)

    1977-01-01

    Erie 1 and 2 reactors will be located on a site consisting of 1,740 acres in Berlin Township about 2.4 miles south of Lake Erie and 8.9 miles southeast of Sandusky, Ohio. Lake Erie will provide makeup water. The ultimate heat sink will be a 40 acre cooling reservoir shared by both units. Each unit has a proposed core thermal power level of 3,760 MW(t) and a nominal net capacity of about 1282 MW(e). Unit 1 is scheduled for commercial operation by 4/1/84 and Unit 2 by 4/1/86. Fuel will be Zircaloy-4 clad tubes containing cylindrical fuel pellets of UO 2 . B and W pressurized water reactor units to be employed are described in DOCKET-STN-50561

  20. Safety evaluation report related to the operation of Catawba Nuclear Station, Units 1 and 2. Docket Nos. 50-413 and 50-414. Suppl. 1

    International Nuclear Information System (INIS)

    1983-04-01

    This reort supplements the Safety Evaluation Report (NUREG-0954) issued in February 1983 by the Office of Nuclear Reactor Regulation of the US Nuclear Regulatory Commission with respect to the application filed by Duke Power Company, North Carolina Municipal Power Agency Number 1, North Carolina Membership Corporation, and Saluda River Electric Cooperative, Inc. as applicants and owners, for licenses to operate the Catawba Nuclear Station, Units 1 and 2 (Docket Nos. 50-413 and 50-414, respectively). The facility is located in York County, South Carolina, approximately 9.6 km (6 mi) north of Rock Hill and adjacent to Lake Wylie. This supplement provides more recent information regarding resolution or updating of some of the open and confirmatory items and license conditions identified in the Safety Evaluation Report, and discusses the recommendations of the Advisory Committee on Reactor Safeguards in its report dated March 15, 1983

  1. Alteration in reactor installations (Unit 1 and 2 reactor facilities) in the Hamaoka Nuclear Power Station of The Chubu Electric Power Co., Inc. (report)

    International Nuclear Information System (INIS)

    1982-01-01

    A report by the Nuclear Safety Commission to the Ministry of International Trade and Industry concerning the alteration in Unit 1 and 2 reactor facilities in the Hamaoka Nuclear Power Station, Chubu Electric Power Co., Inc., was presented. The technical capabilities for the alteration of reactor facilities in Chubu Electric Power Co., Inc., were confirmed to be adequate. The safety of the reactor facilities after the alteration was confirmed to be adequate. The items of examination made for the confirmation of the safety are as follows: reactor core design (nuclear design, mechanical design, mixed reactor core), the analysis of abnormal transients in operation, the analysis of various accidents, the analysis of credible accidents for site evaluation. (Mori, K.)

  2. Safety Evaluation Report related to the operation of Perry Nuclear Power Plant, Units 1 and 2 (Docket Nos. 50-440 and 50-441). Supplement No. 6

    International Nuclear Information System (INIS)

    1985-04-01

    Supplement No. 6 to the Safety Evaluation Report (NUREG-0887) on the application filed by the Cleveland Electric Illuminating Company on behalf of itself and as agent for the Duquesne Light Company, the Ohio Edison Company, the Pennsylvania Power Company, and the Toledo Edison Company (the Central Area Power Coordination Group or CAPCO), as applicants and owners, for a license to operate the Perry Nuclear Power Plant, Units 1 and 2 (Docket Nos. 50-540 and 50-441), has been prepared by the Office of the Nuclear Reactor Regulation of the US Nuclear Regulatory Commission. The facility is located in Lake County, Ohio, approximately 35 miles northeast of Cleveland, Ohio. This supplement reports the status of certain issues that had not been resolved at the time of publication of the Safety Evaluation Report and Supplement Nos. 1 through 5 to that report

  3. Safety evaluation report related to the operation of Perry Nuclear Power Plant, Units 1 and 2 (Docket Nos. 50-440 and 50-441). Supplement No. 10

    International Nuclear Information System (INIS)

    1986-09-01

    Supplement No. 10 to the Safety Evaluation Report (NUREG-0887) on the application filed by the Cleveland Electric Illuminating Company on behalf of itself and as agent for the Duquesne Light Company, the Ohio Edison Company, the Pennsylvania Power Company, and the Toledo Edison Company (the Central Area Power Coordination Group or CAPCO), as applicants and owners for a license to operate the Perry Nuclear Power Plant, Units 1 and 2 (Docket Nos. 50-440 and 50-441), has been prepared by the Office of Nuclear Reactor Regulation of the US Nuclear Regulatory Commission. The facility is located in Lake County, Ohio, approximately 35 miles northeast of Cleveland, Ohio. This supplement reports the status of certain issues and action items that had not been resolved or completed at the time of publication of the Safety Evaluation Report and Supplements Nos. 1 through 9 to that report

  4. Safety Evaluation Report related to the operation of Perry Nuclear Power Plant, Units 1 and 2, (Docket Nos. 50-440 and 50-441)

    International Nuclear Information System (INIS)

    1984-02-01

    Supplement No. 4 to the Safety Evaluation Report on the application filed by the Cleveland Electric Illuminating Company on behalf of itself and as agent for the Duquesne Light Company, the Ohio Edison Company, the Pennsylvania Power Company, and the Toledo Edison Company (the Central Area Power Coordination Group or CAPCO), as applicants and owners, for a license to operate the Perry Nuclear Power Plant, Units 1 and 2 (Docket Nos. 50-440 and 50-441), has been prepared by the Office of Nuclear Reactor Regulation of the US Nuclear Regulatory Commission. The facility is located in Lake County, Ohio. This supplement reports the status of certain issues that had not been resolved at the time of publication of the Safety Evaluation Report and Supplement Nos. 1, 2 and 3 to that report

  5. Safety evaluation report related to the operation of Perry Nuclear Power Plant, Units 1 and 2: Docket Nos. 50-440 and 50-441

    International Nuclear Information System (INIS)

    1983-01-01

    Supplement No. 2 to the Safety Evaluation Report on the application filed by the Cleveland Electric Illuminating Company on behalf of itself and as agent for the Duquesne Light Company, the Ohio Edison Company, the Pennsylvania Power Company, and the Toledo Edison Company (the Central Area Power Coordination Group (CAPCO)), as applicants and owners, for a license to operate the Perry Nuclear Power Plant, Units 1 and 2 (Docket Nos. 50-440 and 50-441), has been prepared by the Office of Nuclear Reactor Regulation of the US Nuclear Regulatory Commission. The facility is located in Lake County, Ohio. This supplement reports the status of certain issues that had not been resolved at the time of publication of the Safety Evaluation Report and Supplement No. 1 to that report

  6. Safety Evaluation Report related to the operation of Cartawba Nuclear Station, Units 1 and 2 (Docket Nos. 50-413 and 50-414). Supplement No. 5

    International Nuclear Information System (INIS)

    1986-02-01

    This report supplements the Safety Evaluation Report (NUREG-0954) issued in February 1983 by the Office of Nuclear Reactor Regulation of the US Nuclear Regulatory Commission with respect to the application filed by Duke Power Company, North Carolina Municipal Power Agency Number 1, North Carolina Membership Corporation, Saluda River Electric Cooperative, Inc., and Piedmont Municipal Power Agency, as applicants and owners, for licenses to operate the Catawba Nuclear Station, Units 1 and 2 (Docket Nos. 50-413 and 50-414, respectively). The facility is located in York County, South Carolina, approximately 9.6 km (6 mi) north of Rock Hill and adjacent to Lake Wylie. This supplement provides additional information supporting the license for initial criticality and power ascension to full-power operation for Unit 2

  7. Safety Evaluation Report related to the operation of Perry Nuclear Power Plant, Units 1 and 2 (Docket Nos. 50-440 and 50-441). Supplement No. 7

    International Nuclear Information System (INIS)

    1985-11-01

    Supplement No. 7 to the Safety Evaluation Report (NUREG-0887) on the application filed by the Cleveland Electric Illuminating Company on behalf of itself and as agent for the Duquesne Light Company, the Ohio Edison Company, the Pennsylvania Power Company, and the Toledo Edison Company (the Central Area Power Coordination Group or CAPCO), as applicants and owners, for a license to operate the Perry Nuclear Power Plant, Units 1 and 2 (Docket No. 50-440 and 50-441) has been prepared by the Office of Nuclear Reactor Regulation of the US Nuclear Regulatory Commission. The facility is located in Lake County, Ohio, approximately 35 miles northeast of Cleveland, Ohio. This supplement reports the status of certain issues that had not been resolved at the time of publication of the Safety Evaluation Report and Supplement Nos. 1 through 6 to that report

  8. Safety Evaluation Report related to the operation of Watts Bar Nuclear Plant, Units 1 and 2 (Docket Nos. 50-390 and 50-391). Supplement No. 4

    International Nuclear Information System (INIS)

    1985-03-01

    This report supplements the Safety Evaluation Report, NUREG-0847 (June 1982), Supplement No. 1 (September 1982), Supplement No. 2 (January 1984), and Supplement No. 3 (January 1985) issued by the Office of Nuclear Reactor Regulation of the US Nuclear Regulatory Commission with respect to the application filed by the Tennessee Valley Authority, as applicant and owner, for licenses to operate the Watts Bar Nuclear Plant, Units 1 and 2 (Docket Nos. 50-390 and 50-391). The facility is located in Rhea County, Tennessee, near the Watts Bar Dam on the Tennessee River. This supplement provides recent information regarding resolution of some of the open and confirmatory items and license conditions identified in the Safety Evaluation Report

  9. Safety Evaluation Report related to the operation of Grand Gulf Nuclear Station, Units 1 and 2 (Docket Nos. 50-416 and 50-417)

    International Nuclear Information System (INIS)

    1984-10-01

    This report supplements the Safety Evaluation Report (NUREG-0831) issued in September 1981 by the Office of Nuclear Reactor Regulation of the US Nuclear Regulatory Commission with respect to the application filed by Mississippi Power and Light (MP and L) Company, Middle South Energy, Inc., and South Mississippi Electric Power Association as applicants and owners, for licenses to operate the Grand Gulf Nuclear Station, Units 1 and 2 (Docket Nos. 50-416 and 50-417, respectively). The facility is located on the east bank of the Mississippi River near Port Gibson in Claiborne County, Mississippi. This supplement provides information on the NRC staff's evaluation of requests for exemptions to NRC regulations pursuant to the Commission's direction in CLI-84-19, dated October 25, 1984

  10. Safety Evaluation Report related to the operation of Watts Bar Nuclear Plant, Units 1 and 2 (Docket Nos. 50-390 and 50-391). Supplement No. 3

    International Nuclear Information System (INIS)

    1985-01-01

    This report supplements the Safety Evaluation Report, NUREG-0847 (June 1982), Supplement No. 1 (September 1982), and Supplement No. 2 (January 1984) issued by the Office of Nuclear Reactor Regulation of the US Nuclear Regulatory Commission with respect to the application filed by the Tennessee Valley Authority, as applicant and owner, for licenses to operate the Watts Bar Nuclear Plant, Units 1 and 2 (Docket Nos. 50-390 and 50-391). The facility is located in Rhea County, Tennessee, near the Watts Bar Dam on the Tennessee River. This supplement provides recent information regarding resolution of some of the open and confirmatory items and license conditions identified in the Safety Evaluation Report

  11. Safety evaluation report related to the operation of Watts Bar Nuclear Plant, Units 1 and 2 (Docket Nos. 50--390 and 50--391)

    International Nuclear Information System (INIS)

    1990-11-01

    This report supplements the Safety Evaluation Report (SER), NUREG-0847 (June 1982), Supplement No. 1 (September 1982), Supplement No. 2 (January 1984), Supplement No. 3 (January 1985), and Supplement No. 4 (March 1985), issued by the Office of Nuclear Reactor Regulation of the US Nuclear Regulatory Commission with respect to the application filed by the Tennessee Valley Authority, as applicant and owner, for licenses to operate the Watts Bar Nuclear Plant, Units 1 and 2 (Docket Nos. 50-390 and 50-391). The facility is located in Rhea County, Tennessee, near the Watts Bar Dam on the Tennessee River. This supplement provides recent information regarding resolution of some of the outstanding and confirmatory items and proposed license conditions identified in the SER

  12. Safety evaluation report related to the operation of Watts Bar Nuclear Plant, Units 1 and 2, (Docket Nos. 50-390 and 50-391), Tennessee Valley Authority

    International Nuclear Information System (INIS)

    1992-06-01

    This report supplements the Safety Evaluation Report (SER), NUREG- 0847 (June 1982), Supplement No. 1 (September 1982), Supplement No. 2 (January 1984), Supplement No. 3 (January 1985), Supplement No. 4 (March 1985), Supplement No. 5 (November 1990), Supplement No. 6 (April 1991), Supplement No. 7 (September 1991), and Supplement No. 8 (January 1992) issued by the Office of Nuclear Reactor Regulation of the US Nuclear Regulatory Commission with respect to the application filed by the Tennessee Valley Authority, as applicant and owner, for licenses to operate the Watts Bar Nuclear Plant, Units 1 and 2 (Docket Nos. 50-390 and 50-391). The facility is located in Rhea County, Tennessee near the Watts Bar Dam on the Tennessee River. This supplement provides recent information regarding resolution of some of the outstanding and confirmatory items, and proposed license conditions identified in the SER

  13. Safety Evaluation Report related to the operation of Watts Bar Nuclear Plant, Units 1 and 2 (Docket Nos. 50-390 and 50-391)

    International Nuclear Information System (INIS)

    Tam, P.S.

    1991-04-01

    This report supplements the Safety Evaluation Report (SER), NUREG- 0847 (June 1982), Supplement No. 1' (September 1982), Supplement No. 2 (January 1984), Supplement No. 3 (January 1985), Supplement No. 4 (March 1985), and Supplement No. 5 (November 1990) issued by the Office of Nuclear Reactor Regulation of the US Nuclear Regulatory commission with respect to the application filed by the Tennessee Valley Authority, as applicant and owner, for licenses to operate the Watts Bar Nuclear Plant, Units 1 and 2 (Docket Nos. 50--390 and 50--391). The facility is located in Rhea County, Tennessee, near the Watts Bar Dam on the Tennessee River. This supplement provides recent information regarding resolution of some of the outstanding and confirmatory items, and proposed license conditions identified in the SER

  14. Safety Evaluation Report related to the operation of Catawba Nuclear Station, Units 1 and 2 (Docket Nos. 50-413 and 50-414). Supplement No. 6

    International Nuclear Information System (INIS)

    1986-05-01

    This report supplements the Safety Evaluation Report (NUREG-0954) issued in February 1983 by the Office of Nuclear Reactor Regulation of the US Nuclear Regulatory Commission with respect to the application filed by Duke Power Company, North Carolina Municipal Power Agency Number 1, North Carolina Membership Corporation, Saluda River Electric Cooperative, Inc., and Piedmont Municipal Power Agency, as applicants and owners, for licenses to operate the Catawba Nuclear Station, Units 1 and 2 (Docket Nos. 50-413 and 50-414, respectively). The facility is located in York County, South Carolina, approximately 9.6 km (6 miles) north of Rock Hill and adjacent to Lake Wylie. This supplement provides additional information supporting the license for operation above 5% power and power ascension to full-power operation for Unit 2

  15. Safety Evaluation Report related to the operation of Perry Nuclear Power Plant, Units 1 and 2 (Docket Nos. 50-440 and 50-441). Supplement No. 5

    International Nuclear Information System (INIS)

    1985-02-01

    Supplement No. 5 to the Safety Evaluation Report (NUREG-0887) on the application filed by the Cleveland Electric Illuminating Company on behalf of itself and as agent for the Duquesne Light Company, the Ohio Edison Company, The Pennsylvania Power Company, and the Toledo Edison Company (the Central Area Power Coordination Group or CAPCO), as applicants and owners, for a license to operate the Perry Nuclear Power Plant, Units 1 and 2 (Docket Nos. 50-440 and 50-441), has been prepared by the Office of Nuclear Reactor Regulation of the US Nuclear Regulatory Commission. The facility is located in Lake County, Ohio, approximately 35 miles northeast of Cleveland, Ohio. This supplement reports the status of certain issues that had not been resolved at the time of publication of the Safety Evaluation Report and Supplement Nos. 1 through 4 to that report

  16. Touchstone for Japan's Export of nuclear power plant system. Vinh Hai unit 1 and 2 project in the Ninh Thuan province in Viet Nam

    International Nuclear Information System (INIS)

    Mitsumata, Hiroki; Takekuro, Ichiro; Kaneko, Kumao; Suzuki, Hideaki; Saito, Shinzo

    2011-01-01

    'Japan-Viet Nam Joint Statement on the Strategic Partnership for Peace and Prosperity in Asia' issued after the meeting between Japan-Viet Nam Prime Ministers on October 31, affirmed that the Vietnamese Government had decided to choose Japan as the cooperation partner for building Vinh Hai Unit 1 and 2 Project in the Ninh Thuan Province, southern Viet Nam, which showed substantially an order of Japan was arranged informally. 'International Nuclear Energy Development of Japan Co., Ltd. (JINED)' set up by industry and government, would negotiate to decide fundamental parameters such as type and power of nuclear power plants with the start of operation scheduled in 2021. This special issue consisted of six articles on significance of the project of Japan's first export, feasibility studies and future perspective and regional effects with introduction of nuclear power station in Viet Nam. (T. Tanaka)

  17. Safety evaluation report related to the operation of Perry Nuclear Power Plant, Units 1 and 2. Docket Nos. 50-440 and 50-441

    International Nuclear Information System (INIS)

    1983-04-01

    Supplement No. 3 to the Safety Evaluation Report on the application filed by the Cleveland Electric Illuminating Company on behalf of itself and as agent for the Duquesne Light Company, the Ohio Edison Company, the Pennsylvania Power Company, and the Toledo Edison Company (the Central Area Power Coordination Group or CAPCO), as applicants and owners, for a license to operate the Perry Nuclear Power Plant, Units 1 and 2 (Docket Nos. 50-440/441), has been prepared by the Office of Nuclear Reactor Regulation of the US Nuclear Regulatory Commission. The facility is located in Lake County, Ohio. This supplement reports the status of certain issues that had not been resolved at the time of publication of the Safety Evaluation Report and Supplement Nos. 1 and 2 to that report

  18. Contributions to a methodology for periodical verification of the parameters of the control systems at Cernavoda Nuclear plant Unit 1

    International Nuclear Information System (INIS)

    Tapu, Cornel; Anescu, George

    1998-01-01

    A model identification methodology for periodical verification of the regulating system parameters at Cernavoda NPP Unit 1 was developed. As support to this methodology, the computer program MODELIDENT was implemented in the Java programming language. This program is used for off-line evaluation of the real regulating systems characteristic parameters using an identification algorithm which takes as input data the system response collected for different input excitation signals, a structurally similar model of the analyzed regulating system, and some starting guess value of the unknown parameters. The real values of the parameters are determined during MODELIDENT program execution by applying an iterative algorithm and afterwards are retained as nominal reference values. The success of the identification algorithm is strongly dependent on how appropriately the structure of model's transfer function is chosen. By repeating periodically the identification method, using newly collected data from the process, the current value of the parameters are determined. Any deviations of the new values relative to the nominal reference values are interpreted as de-calibration of the control equipment and in this case corrective maintenance actions have to be taken. With the implementation of the presented methodology at Cernavoda NPP Unit 1 we can make the statement that the preventive maintenance activity is gaining a predictive feature, which can lead to the elimination of major degradation possibilities in the performances of the RS equipment and consequently to increase the NPP availability. On the basis of the experience gained in the practical application of the presented methodology we expect that the identification method will also have beneficial effects in the optimal control of the process systems and also in the activity of Full Scope Simulator software maintenance (the reference values of the identified parameters being used for fine tuning of the simulation models

  19. Radiographic monitoring of the ossification of long bones in kori (Ardeotis kori) and white-bellied (Eupodotis senegalensis) bustards

    International Nuclear Information System (INIS)

    Naldo, J.L.; Samour, J.H.; Bailey, T.A.

    1998-01-01

    A serial radiographic study was conducted on eight kori bustard (Ardeotis kori) and four white-bellied bustard (Eupodotis senegalensis) chicks to determine the pattern of long bone development and to establish radiographic standards for assessing skeletal maturity. The ossification pattern, appearance of secondary ossification centres, and epiphyseal fusion of the long bones in kori and white-bellied bustards were similar to those in houbara bustards (Chlamydotis undulata macqueenii),rufous-crested bustards (Eupodotis ruficrista), domestic fowl (Gallusgallus), house wrens (Troglodytes aedon aedon), racing pigeons (Columba livia), and barn owls (Tyto alba). Secondary ossification centres were present at the proximal and distal tibiotarsus, proximal tarsometatarsus and proximal metacarpal III. The ossification of long bones occurred earlier in female kori bustards compared with males

  20. A Study on Determination of Proper Pressurizer Level for Kori Unit 1

    Energy Technology Data Exchange (ETDEWEB)

    Lee, Chang Sup; Song, Dong Soo [Korea Electric Power Research Institute, Taejon (Korea, Republic of)

    1996-12-31

    1. Determination of Proper Pressurizer Level. To determine operation level of pressurizer, LOFTRAN code is used with conservative model and assumption. 2. Performance Analysis. To simulate the plant, RETRAN computer code is used with realistic model and assumptions. The control and protection systems are fully credited. The turbine trip event is simulated at the condition of 47.62% of pressurizer level at full power. After that the same event as that with 55% of pressurizer level is simulated. And the FSAR requirements of pressurizer are verified with the new level setpoints. 3. Safety Analysis. As safety analyses, Loss of Normal Feedwater/Station Blackout which is significantly affected by the initial pressurizer water level is performed. Turbine Trip accident is also analyzed to verify if the peak primary side pressure is within the limit. LOFTRAN code is used with conservative mode and assumption. 3. Steam Generator Replacement. Relating to the steam generator replacement planed in 1998, safety analysis in terms of pressurizer level setpoint change. 4. Limit Condition for Operation. The LCO of pressurizer level is changed from 60% to 67.4% which is included pressurizer level uncertainty. (author). 13 refs., figs., tabs.

  1. Option managing for radioactive metallic waste from the decommissioning of Kori Unit 1

    Energy Technology Data Exchange (ETDEWEB)

    Kessel, David S.; Kim, Chagn Lak [KEPCO International Nuclear Graduate School (KINGS), Ulsan (Korea, Republic of)

    2017-06-15

    The purpose of this paper is to evaluate several leading options for the management of radioactive metallic waste against a set of general criteria including safety, cost effectiveness, radiological dose to workers and volume reduction. Several options for managing metallic waste generated from decommissioning are evaluated in this paper. These options include free release, controlled reuse, and direct disposal of radioactive metallic waste. Each of these options may involve treatment of the metal waste for volume reduction by physical cutting or melting. A multi-criteria decision analysis was performed using the Analytic Hierarchy Process (AHP) to rank the options. Melting radioactive metallic waste to produce metal ingots with controlled reuse or free release is found to be the most effective option.

  2. Technical evaluation of RETS-required reports for Zion Nuclear Power Station, Units 1 and 2 for 1983

    International Nuclear Information System (INIS)

    Young, T.E.; Magleby, E.H.

    1985-01-01

    A review was performed on the reports required by Federal regulations and the plant-specific Radiological Effluent Technical Specifications (RETS) for operations conducted at Commonwealth Edison's Zion Nuclear Power Station during 1983. The two periodic reports reviewed: (1) were the Effluent and Waste Disposal Semiannual Report, July-December 1983, and (2) the Radioactive Waste and Environmental Monitoring Annual Report - 1983. The principal review guidelines were the plant's specific RETS and NRC guidance given in NUREG-0133, ''Preparation of Radiological Effluent Technical Specifications for Nuclear Power Plants.'' The Licensee's submitted reports were found to be reasonably complete and consistent with the review guidelines

  3. Technical evaluation of RETS-required reports for the Edwin I. Hatch Nuclear Plant, Units 1 and 2

    International Nuclear Information System (INIS)

    Young, T.E.; Magleby, E.H.

    1985-01-01

    A review of the reports required by federal regulations and the plant-specific Radiological Effluent Technical Specifications (RETS) for operations conducted during 1983 was performed. The periodic reports reviewed for the Edwin I. Hatch Nuclear Plant were the Annual Radiological Environmental Operating Report for 1983 and the Semiannual Radioactive Effluent Release Reports for 1983. The principal review guidelines were the plant's specific RETS, NUREG-0133, ''Preparation of Radiological Effluent Technical Specifications for Nuclear Power Plants'', and NRC Guidance on the Review of the Process Control Programs. The Licensee's submitted reports were found to be reasonably complete and consistent with the review guidelines. 7 refs

  4. Analysis of core damage frequency: Nuclear power plant Dukovany, VVER/440 V-213 Unit 1, internal events. Volume 1: Main report

    International Nuclear Information System (INIS)

    Pugila, W.J.

    1994-01-01

    This report presents the final results from the Level 1 probabilistic safety assessment (PSA) for the Dukovany VVER/440 V-213 nuclear power plant, Unit 1. Section 1.1 describes the objectives of this study. Section 1.2 discusses the approach that was used for completing the Dukovany PSA. Section 1.3 summarizes the results of the PSA. Section 1.4 provides a comparison of the results of the Dukovany PSA with the results of other PSAs for different types of reactors worldwide. Section 1.5 summarizes the conclusions of the Dukovany PSA

  5. Technical evaluation of the noise and isolation testing of the safety features actuation system at the Davis Besse Nuclear Power Station, Unit 1

    International Nuclear Information System (INIS)

    Selan, J.C.

    1981-07-01

    This report documents the technical evaluation of the noise and isolation testing of the safety features actuation system at the Davis Besse Nuclear Power Station, Unit 1. The tests were to verify that faults on the non-Class 1E circuits would not propagate to the Class 1E circuits and degrade them below acceptable levels. The tests conducted demonstrated that the safety features actuation system did not degrade below acceptable levels nor was the system's ability to perform its protective functions affected

  6. Technical evaluation report on the proposed design modifications and technical specification changes on grid voltage degradation for the Millstone Nuclear Power Station, Unit 1

    International Nuclear Information System (INIS)

    Selan, J.C.

    1982-01-01

    This report documents the technical evaluation of the proposed design modifications and Technical Specification change for protection of Class 1E equipment from grid voltage degradation for the Millstone Nuclear Power Station, Unit 1. The review criteria are based on several IEEE standards and the Code of Federal Regulations. The evaluation finds that the licensee has not provided sufficient information on the undervoltage protection system to allow a complete evaluation into the adequacy of protecting the Class 1E equipment from sustained voltage degradation

  7. 75 FR 12312 - South Carolina Electric and Gas Company; Virgil C. Summer Nuclear Station, Unit 1; Exemption

    Science.gov (United States)

    2010-03-15

    ... cladding oxidation from the metal/water reaction shall be calculated using the Baker-Just equation. The... of energy release, hydrogen concentration, and cladding oxidation from the metal-water reaction shall... pressurized light-water nuclear power reactor fueled with uranium oxide pellets within cylindrical zircaloy or...

  8. 77 FR 66484 - PSEG Nuclear LLC; Hope Creek Generating Station and Salem Generating Station, Units 1 and 2...

    Science.gov (United States)

    2012-11-05

    ... Power Plant Personnel,'' endorses the Nuclear Energy Institute (NEI) report, NEI 06-11, Revision 1... exclusion, set forth in 10 CFR 51.22(c)(25). Pursuant to 10 CFR 51.22(b), no environmental impact statement... Commission (NRC or the Commission) now or hereafter in effect. The facilities consist of one boiling-water...

  9. 75 FR 9623 - Arizona Public Service Company, et al.; Palo Verde Nuclear Generating Station, Units 1, 2, and 3...

    Science.gov (United States)

    2010-03-03

    ... pressurized-water reactors located in Maricopa County, Arizona. 2.0 Request/Action Title 10 of the Code of... pressure boundary during normal operating and hydrostatic or leak rate testing conditions. Specifically, 10... NRC's March 16, 2001, SE, the staff noted, ``[t]he CE NSSS [nuclear steam supply system] methodology...

  10. 75 FR 77010 - Nextera Energy Point Beach, LLC; Point Beach Nuclear Plant, Units 1 and 2, Draft Environmental...

    Science.gov (United States)

    2010-12-10

    ... waste is low-level radioactive waste which includes sludge, oily waste, bead resin, spent filters, and... Impact of Transportation of Fuel and Waste to and from One Light-Water-Cooled Nuclear Power Reactor..., wetlands, and open areas. Each of the two units at PBNP use Westinghouse pressurized water reactors...

  11. In-service materials testing of selected components of unit 1 and 2 of V-1 nuclear power plant

    International Nuclear Information System (INIS)

    Cintula, J.

    1982-01-01

    The task of in-service nondestructive testing of nuclear installations is to confirm that the state of base material and welded joints has not changed owing to mechanical, thermal or radiation stress. Under the regulations of safe operation the first in-service inspection of all components of a WWER 440 reactor must be carried out after 15,000 to 2O,00O operating hours at the latest. Further in-service inspections are repeated after 30,000 hours (pressure vessels) and 40,000 hours (the main steam piping and the feedwater piping). Proceeding from experience gained so far, intervals are suggested for in-service checks of the other components of the V-1 nuclear power plant. Also briefly described are the main nondestructive methods used for such checks at this power plant. (Z.M.)

  12. Safety evaluation report related to the operation of Watts Bar Nuclear Plant, Units 1 and 2 (Docket Nos. 50-390 and 50-391). Supplement No. 18

    International Nuclear Information System (INIS)

    Tam, P.S.

    1995-10-01

    In June 1982, the Nuclear Regulatory Commission staff (NRC staff or staff) issued a Safety Evaluation Report, NUREG-0847, regarding the application by the Tennessee Valley Authority (TVA or the applicant) for licenses to operate the Watts Bar Nuclear Plant, Units 1 and 2. Each of the following sections and appendices of this supplement is numbered the same as the section or appendix of the SER that is being updated, and the discussions are supplementary to, and not in lieu of, the discussion in the SER, unless otherwise noted. Accordingly, Appendix A continues the chronology of the safety review. Appendix E lists principal contributors to this supplement. Appendix FF is added in this supplement. The other appendices are not changed by this supplement

  13. Modification and backfitting at the Barsebaeck Nuclear Power Plant Unit 1 and 2 in safety related systems

    International Nuclear Information System (INIS)

    Karlsson, Leif; Nilsson, Ove; Lidh, B.

    1995-05-01

    This report is intended for use by the Swedish Nuclear Power Inspectorate. It has been published to enable comparison of modification and backfitting implemented at Barsebaeck, with those implemented at other plants, both domestic and abroad. The report summarizes the more notable modifications and backfitting carried out on any safety-related equipment, or software, at Barsebaeck, and covers the decade 1984 to 1994. Modifications to hardware, and to some extent to software, are catalogued, but not described in any detail. No general procedures (operational or maintenance) are dealt with. 3 refs

  14. Determination of atmospheric dispersion factors in emergency situations in Almirante Alvaro Alberto nuclear power plant - unit 1

    International Nuclear Information System (INIS)

    Leao, I.L.B.

    1987-08-01

    The necessity of Knowing the atmospheric dispersion factor, used to obtain the first estimation dose in the public case for accidents with releasing of radioactive material to atmosphere in Almirante Alvaro Alberto nuclear power plant - unit I, lead to the development of a fast and efficient method to determine the dilution factors, in a pre-determined distance from the source, to be used in the dose estimate. The ACID computer program for pocket calculation allow to obtain the meteorological information to evaluate the dose. In this work the mathemathical models used and the program developed are described. (Author) [pt

  15. Cutset Quantification Error Evaluation for Shin-Kori 1 and 2 PSA model

    International Nuclear Information System (INIS)

    Choi, Jong Soo

    2009-01-01

    Probabilistic safety assessments (PSA) for nuclear power plants (NPPs) are based on the minimal cut set (MCS) quantification method. In PSAs, the risk and importance measures are computed from a cutset equation mainly by using approximations. The conservatism of the approximations is also a source of quantification uncertainty. In this paper, exact MCS quantification methods which are based on the 'sum of disjoint products (SDP)' logic and Inclusion-exclusion formula are applied and the conservatism of the MCS quantification results in Shin-Kori 1 and 2 PSA is evaluated

  16. Safety Evaluation Report related to the operation of Perry Nuclear Power Plant, Units 1 and 2 (Docket Nos. 50-440 and 50-441). Supplement No. 9

    International Nuclear Information System (INIS)

    1986-03-01

    Supplement No. 9 to the Safety Evaluation Report (NUREG-0887) on the application filed by the Cleveland Electric Illuminating Company on behalf of itself and as agent for the Duquesne Light Company, the Ohio Edison Company, the Pennsylvania Power Company, and the Toledo Edison Company (the Central Area Power Coordination Group or CAPCO) for a license to operate the Perry Nuclear Power Plant, Units 1 and 2 (Docket Nos. 50-440 and 50-441), has been prepared by the Office of Nuclear Reactor Regulation of the US Nuclear Regulatory Commission. The facility is located in Lake County, Ohio, approximately 35 miles northeast of Cleveland, Ohio. This supplement reports the staff's evaluation findings pertaining to the earthquake event that occurred in the vicinity of the Perry Nuclear Power Plant site on January 31, 1986, and is limited to that evaluation. Future supplemental reports will continue reporting on the status of new or unresolved issues since Supplement No. 8 was issued in January 1986

  17. Draft environmental statement related to the operation of Shearon Harris Nuclear Power Plant, Units 1 and 2. Docket Nos. STN 50-400 and STN 50-401

    International Nuclear Information System (INIS)

    1983-04-01

    This Draft Environmental Statement contains the second assessment of the environmental impact associated with the operation of the Shearon Harris Nuclear Power Plant, Units 1 and 2, pursuant to the National Environmental Policy Act of 1979 (NEPA) and 10 CFR 51, as amended, of the NRC regulations. This statement examines the environment, environmental consequences and mitigating actions, and environmental and economic benefits and costs. Land use and terrestrial and aquatic-ecological impacts will be small. Operational impacts to historic and archeological sites will be negligible. The effects of routine operations, energy transmission, and periodic maintenance of rights-of-way and transmission facilities should not jeopardize any populations of endangered or threatened species. No significant impacts are anticipated from normal operational releases of radioactivity. The risk of radiation exposure associated with accidental release of radioactivity is very low. The net socio-economic effects of the project will be beneficial. The action called for is the issuance of an operating license for Shearon Harris PLant, Units 1 and 2

  18. Safety evaluation report related to the operation of Catawba Nuclear Station, Units 1 and 2 (Docket Nos. 50-413 and 50-414). Supplement 2

    International Nuclear Information System (INIS)

    1984-06-01

    This report supplements the Safety Evaluation Report (NUREG-0954) and Supplement 1 with respect to the application filed by Duke Power Company, North Carolina Municipal Power Agency Number 1, North Carolina Membership Corporation, and Saluda River Electric Cooperative, Inc., as applicants and owners, for licenses to operate the Catawba Nuclear Station, Units 1 and 2 (Docket Nos., 50-413 and 50-414, respectively). The facility is located in York County, South Carolina, approximately 9.6 km (6 mi) north of Rock Hill and adjacent to Lake Wylie. This supplement provides more recent information regarding resolution or updating of some of the open and confirmatory issues and license conditions identified in the Safety Evaluation Report

  19. Final Environmental Statement related to the operation of Shearon Harris Nuclear Power Plant, Units 1 and 2 (Docket Nos. STN 50-400 and STN 50-401)

    International Nuclear Information System (INIS)

    1983-10-01

    This Final Environmental Statement contains the second assessment of the environmental impact associated with the operation of the Shoran Harris Nuclear Power Plant, Units 1 and 2, pursuant to the National Environmental Policy Act of 1969 (NEPA) and 10 CFR 51, as amended, of the NRC regulations. This statement examines the environment, environmental consequences and mitigating actions, and environmental economic benefits and costs. Land use and terrestrial and aquatic-ecological impacts will be small. Operational impacts to historic and archaeological sites will be negligible. The effects of routine operations, energy transmission, and periodic maintenance of rights-of-way and transmission facilities should not jeopardize any populations of endangered or threatened species. No significant impacts are anticipated from normal operational releases of radioactivity. The risk of radiation exposure associated with accidental release of radioactivity is very low. The net socioeconomic effects of the project will be beneficial. 19 figs., 21 tabs

  20. Integrated plant safety assessment: Systematic Evaluation Program, San Onofre Nuclear Generating Station, Unit 1 (Docket No. 50-206): Final report

    International Nuclear Information System (INIS)

    1986-12-01

    The Systematic Evaluation Program was initiated in February 1977 by the US Nuclear Regulatory Commission to review the designs of older operating nuclear reactor plants to reconfirm and document their safety. The review provides: (1) an assessment of how these plants compare with current licensing safety requirements relating to selected issues; (2) a basis for deciding on how these differences should be resolved in an integrated plant review; and (3) a documented evaluation of plant safety. This report documents the review of San Onofre Nuclear Generating Station, Unit 1, operated by Southern California Edison Company. The San Onofre plant is one of ten plants reviewed under Phase II of this program. This report indicates how 137 topics selected for review under Phase I of the program were addressed. Equipment and procedural changes have been identified as a result of the review. This report will be one of the bases in considering the issuance of a full-term operating license in place of the existing provisional operating license. This report also addresses the comments and recommendations made by the Advisory Committee on Reactor Safeguards in connection with its review of the draft report issued in April 1985

  1. Safety evaluation report related to operation of Sequoyah Nuclear Plant, Units 1 and 2, Docket nos. 50-327 and 50-328, Tennessee Valley Authority

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1979-03-01

    A safety evaluation of the Tennessee Valley Authority's application for a license to operate its Sequoyah Nuclear Plant, Units 1 and 2, located in Hamilton County, Tennessee, has been prepared by the Office of Nuclear Reactor Regulation of the Nuclear Regulatory Commission. It consists of a technical review and staff evaluation of applicant information on: (1) population density, land use, and physical characteristics of the site area; (2) design, fabrication, construction, testing criteria, and performance characteristics of plant structures, systems, and components important to safety; (3) expected response of the facility to anticipated operating transients, and to postulated design basis accidents; (4) applicant engineering and construction organization, and plans for the conduct of plant operations; and (5) design criteria for a system to control the plant's radiological effluents. The staff has concluded that the plant can be operated by the Tennessee Valley Authority without endangering the health and safety of the public provided that the outstanding matters discussed in the report are favorably resolved. (author)

  2. Simulation of the turbine trip of Unit 1 of the Laguna Verde nuclear power plant using the code Simulate-3K

    International Nuclear Information System (INIS)

    Alegria A, A.; Filio L, C.; Ortiz V, J.

    2017-09-01

    In order to compare the results obtained from the model developed in the Comision Nacional de Seguridad Nuclear y Salvaguardias (CNSNS) with the code Simulate-3K (S3K) with respect to those reported by the process computer of the Central (SIIP), the simulation of the turbine trip transient was carried out, caused by the firing of the main generator, the low differential pressure of oil of its seals and the automatic Scram of Unit 1 of the Laguna Verde nuclear power plant, at 87% of power nominal during the operation cycle 16. Since the reactor was brought to a safe stop due to Scram, was enough to simulate 20 seconds to observe the maximum increase in pressure with S3K. In this work, the following parameters are shown and compared: the neutron flux, the thermal power, the pressure in the dome, the flow at the entrance to the core, the steam flow that leaves the vessel and the minimal critical power ratio (MCPR). The neutron flux of the average power range monitors of the nuclear power plant was compared with the S3K detectors model. Finally, the MCPR was calculated with a different correlation to that of the fuel supplier and its deviation from its safety limit was determined. In conclusion, the results obtained show the current state of the model for the simulation of reactivity transients and the opportunity areas to consolidate this tool in support of the process of licensing refueling in the CNSNS. (Author)

  3. Safety evaluation report related to the operation of Watts Bar Nuclear Plant, Units 1 and 2 (Docket Nos. 50-390 and 50-391). Supplement No. 15

    International Nuclear Information System (INIS)

    Tam, P.S.

    1995-06-01

    This report supplements the Safety Evaluation Report (SER), NUREG-0847 (June 1982), Supplement No. 1 (September 1982), Supplement No. 2 (January 1984), Supplement No. 3 (January 1985), Supplement No. 4 (March 1985), Supplement No. 5 (November 1990), Supplement No. 6 (April 1991), Supplement No. 7 (September 1991), Supplement No. 8 (January 1992), Supplement No. 9 (June 1992), Supplement No. 10 (October 1992), Supplement No. 11 (April 1993), Supplement No. 12 (October 1993), Supplement No. 13 (April 1994), and Supplement No. 14 (December 1994) issued by the Office of Nuclear Reactor Regulation of the US Nuclear Regulatory Commission with respect to the application filed by the Tennessee Valley Authority, as applicant and owner, for licenses to operate the Watts Bar Nuclear Plant, Units 1 and 2 (Docket Nos. 50-390 and 50-391). The facility is located in Rhea County, Tennessee, near the Watts Bar Dam on the Tennessee River. This supplement provides recent information regarding resolution of some of the outstanding and confirmatory items, and proposed license conditions identified in the SER

  4. Safety Evaluation Report related to the operation of Watts Bar Nuclear Plant, Units 1 and 2 (Docket Numbers 50-390 and 50-391)

    International Nuclear Information System (INIS)

    1994-04-01

    This report supplements the Safety Evaluation Report (SER), NUREG-0847 (June 1982), Supplement No. 1 (September 1982), Supplement No. 2 (January 1984), Supplement No. 3 (January 1985), Supplement No. 4 (March 1985), Supplement No. 5 (November 1990), Supplement No. 6 (April 1991), Supplement No. 7 (September 1991), Supplement No. 8 (January 1992), Supplement No. 9 (June 1992), Supplement No. 10 (October 1992), Supplement No. 11 (April 1993), and Supplement No. 12 (October 1993), issued by the Office of Nuclear Reactor Regulation of the US Nuclear Regulatory Commission with respect to the application filed by the Tennessee Valley Authority, as applicant and owner, for licenses to operate the Watts Bar Nuclear Plant, Units 1 and 2 (Docket Nos. 50-390 and 50-391). The facility is located in Rhea County, Tennessee, near the Watts Bar Dam on the Tennessee River. This supplement provides recent information regarding resolution of some of the outstanding and confirmatory items, and proposed license conditions identified in the SER. These issues relate to: Design criteria -- structures, components, equipment, and systems; Reactor; Instrumentation and controls; Electrical power systems; Auxiliary systems; Conduct of operations; Accident analysis; and Quality assurance

  5. The 4th surveillance testing for Kori unit 3 reactor vessel materials

    Energy Technology Data Exchange (ETDEWEB)

    Chang, Kee Ok; Kim, Byoung Chul; Lee, Sam Lai; Choi, Kwun Jae; Gong, Un Sik; Chang, Jong Hwa; Joo, Yong Sun; Ahn, Sang Bok; Hong, Joon Hwa [Korea Atomic Energy Research Institute, Taejeon (Korea)

    2000-10-01

    Surveillance testing for reactor vessel materials is performed in order to evaluate the irradiation embrittlement due to neutrons during operation and set the condition of safe operation of nuclear reactor. The 4th surveillance testing was performed completely by Korea Atomic Energy Research Institute at Taejeon after the capsule was transported from Kori site including its removal from reactor. Fast neutron fluences for capsules were calculated and various testing including mechanical and chemistry analysis were performed in order to evaluate the integrity of Kori unit 3 reactor vessel during the operation until life time. The evaluation results are as follows; Fast neutron fluences for capsules U, V, X and W are 4.983E+18, 1.641E+19, 3.158E+19, and 4.469E+19n/cm{sup 2}, respectively. The bias factor, the ratio of calculation/measurement, was 0.840 for the 1st through 4th testing and the calculational uncertainty, 12% satisfied the requirement of USNRC Reg.Guide DG-1053, 20%. The best estimated neutron fluence for reactor vessel inside surface was 1.362E+19n/cm{sup 2} based on the end of 12th fuel cycle and it was predicted that the fluences of vessel inside surface at 32, 40, 48 and 56EFPY would reach 3.481E+19, 4.209E+19, 5.144E+19 and 5.974E+19n/cm{sup 2} based on the current calculation. The result through this analysis for Kori unit 3 showed that there would be no problem for the pressurized thermal shock(PTS) during the operation until design life. 48 refs., 35 figs., 41 tabs. (Author)

  6. The 5th surveillance testing for Kori unit 2 reactor vessel materials

    Energy Technology Data Exchange (ETDEWEB)

    Chang, Kee Ok; Kim, Byoung Chul; Lee, Sam Lai; Choi, Kwon Jae; Gong, Un Sik; Chang, Jong Hwa; Joo, Yong Sun; Ahn, Sang Bok; Hong, Joon Hwa [Korea Atomic Energy Research Institute, Taejeon (Korea)

    2001-03-01

    Surveillance testing for reactor vessel materials is performed in order to evaluate the irradiation embrittlement due to neutrons during operation and set the condition of safe operation of nuclear reactor. The 5th surveillance testing was performed completely by Korea Atomic Energy Research Institute at Taejeon after the capsule was transported from Kori site including its removal from reactor. Fast neutron fluences for capsules were calculated and various testing including mechanical and chemistry analysis were performed in order to evaluate the integrity of Kori unit 2 reactor vessel during the operation until life time. The evaluation results are as follows; Fast neutron fluences for capsules V, R, P, T and N are 2.837E+18, 1.105E+19, 2.110E+19, 3.705E+19 and 4.831E+19n/cm{sup 2}, respectively. The bias factor, the ratio of measurement/calculation, was 0.918 for the 1st through 5th testing and the calculational uncertainty, 11.6% satisfied the requirement of USNRC Reg.Guide DG-1053, 20%. The best estimated neutron fluence for reactor vessel inside surface was 1.898E+19n/cm{sup 2} based on the end of 15th fuel cycle and it was predicted that the fluences of vessel inside surface at 32, 40, 48 and 56EFPY would reach 4.203E+19, 5.232E+19, 6.262E+19 and 7.291E+19n/cm{sup 2} based on the current calculation. The result through this analysis for Kori unit 2 showed that there would be no problem for the pressurized thermal shock(PTS) during the operation until design life. 49 refs., 35 figs., 48 tabs. (Author)

  7. Application of a Virtual Ovation System to the ShinKori-3 Simulator

    International Nuclear Information System (INIS)

    Hong, Jin Hyuk; Lee, Myeong Soo; Chung, Kyung Hun

    2011-01-01

    The Ovation system for the Shin-Kori Unit 3 Simulator is essentially a non-redundant, repackaged subset of the actual plant I and C equipment, with additional interface computers (SimStations). This system also present in the simulator to provide communication between the plant model computer and the stimulated Ovation equipment. The stimulated Ovation equipment in the simulator system includes Operator HMI (Human- Machine Interface) equipment and Ovation virtual controllers hosted by Virtual Controller Host workstations, which are not present in the actual plant DCS system. The simulator for the Shin-Kori Unit 3 and 4 is being developed by Korea Hydro and Nuclear Power's Central Research Institute (KHNP CRI). One of the features of the simulator is its application of a virtual Ovation system capable of simulated functionalities such as run, freeze, snapshot, backtrack and others required by ANSI/ANS-3.5 in addition to the original functionality for the actual Ovation system applied at the plant. This is the first application of a virtual Ovation system to a full-scope simulator for a nuclear power plant in Korea. The purpose of this paper is to provide the overall architecture of the communication system between the virtual system and the simulator model and to describe the current situation of the development of the system and recent relevant studies

  8. Locating the Source of Atmospheric Contamination Based on Data From the Kori Field Tracer Experiment

    Directory of Open Access Journals (Sweden)

    Piotr Kopka

    2015-01-01

    Full Text Available Accidental releases of hazardous material into the atmosphere pose high risks to human health and the environment. Thus it would be valuable to develop an emergency reaction system which can recognize the probable location of the source based only on concentrations of the released substance as reported by a network of sensors. We apply a methodology combining Bayesian inference with Sequential Monte Carlo (SMC methods to the problem of locating the source of an atmospheric contaminant. The input data for this algorithm are the concentrations of a given substance gathered continuously in time. We employ this algorithm to locating a contamination source using data from a field tracer experiment covering the Kori nuclear site and conducted in May 2001. We use the second-order Closure Integrated PUFF Model (SCIPUFF of atmospheric dispersion as the forward model to predict concentrations at the sensors' locations. We demonstrate that the source of continuous contamination may be successfully located even in the very complicated, hilly terrain surrounding the Kori nuclear site. (original abstract

  9. Final environmental statement related to construction of Skagit Nuclear Power Project Units 1 and 2: (Docket Nos. 50-522 and 50-523)

    International Nuclear Information System (INIS)

    1975-05-01

    The proposed action is the issuance of construction permits to the Pudget Sound Power and Light Company, Pacific Power and Light Company, Washington Water Power Company and the Washington Public Power Supply System, for the construction of Skagit Nuclear Power Projects Units 1 and 2 (Docket Nos. 50-522 and 50-523) in Skagit County, Washington (about 64 miles north of Seattle and 6 miles ENE of Sedro Woolley). These units are scheduled for commercial service in 1982 and 1985, respectively. Each unit will employ a boiling-water nuclear reactor with a maximum expected thermal power level of 4100 MWt, which is considered in the assessments contained in this statement. At the 3800 MWt power level initially to be licensed, the net electrical capacity of each unit will be 1288 MWe. The exhaust steam from the turbine-generators will be cooled in condensers which will utilize one hyperbolic-type natural-draft cooling tower per unit to dissipate heat to the atmosphere. Water (106 cfs max.) for the cooling tower makeup (82.4 cfs) and other plant uses will be withdrawn from the Skagit River through Ranney Collectors embedded in the north bank of the river and pumped to the plant through a pipeline about 35,000 ft. long. Cooling tower blowdown (7 cfs max.) from the project and dilution water (20 cfs max.) will flow through a pipeline back to the river where it will be discharged through a diffuser

  10. Safety evaluation report related to the operation of Diablo Canyon Nuclear Power Plant, Units 1 and 2 (Docket Nos. 50-275 and 50-323). Supplement No. 26

    International Nuclear Information System (INIS)

    1984-07-01

    Supplement 26 to the Safety Evaluation Report for Pacific Gas and Electric Company's application for licenses to operate Diablo Canyon Nuclear Power Plants, Units 1 and 2 (Docket Nos. 50-275 and 50-323), has been prepared jointly by the Office of Nuclear Reactor Regulation and the Region V Office of the US Nuclear Regulatory Commission. The supplement reports on the status of the staff's investigation, inspection and evaluation of those allegations or concerns that have been identified to the NRC as of July 8, 1984. The report specifically addresses those allegations which the staff determined must be satisfactorily resolved prior to full power operation of Diablo Canyon Unit 1

  11. Safety-evaluation report related to the operation of Diablo Canyon Nuclear Power Plants, Units 1 and 2. Docket Nos. 50-275 and 50-323. Supplement No. 18

    International Nuclear Information System (INIS)

    1983-08-01

    Supplement 18 to the Safety Evaluation Report for Pacific Gas and Electric Company's application for licenses to operate Diablo Canyon Nuclear Power Plants, Units 1 and 2 (Docket Nos. 50-275 and 50-323), has been prepared by the Office of Nuclear Reactor Regulation of the US Nuclear Regulatory Commission. This supplement reports on the verification effort for Diablo Canyon Unit 1 that was performed between November 1981 and the present in response to Commission Order CLI-81-30 and an NRC letter to the licensee

  12. The 4th surveillance test and evaluation of the reactor pressure vessel material (capsule W) of Younggwang nuclear power plant unit1

    Energy Technology Data Exchange (ETDEWEB)

    Kim, Byoung Chul; Lee, Sam Lai; Choi, Kwon Jae [Korea Atomic Energy Research Institute, Taejeon (Korea)

    2001-08-01

    Surveillance testing for reactor vessel materials is performed in order to evaluate the irradiation embrittlement due to neutrons during operation and set the condition of safe operation of nuclear reactor. The 4th surveillance testing was performed completely by Korea Atomic Energy Research Institute at Taejeon after the capsule was transported from Yonggwang site including its removal from reactor. Fast neutron fluences for capsules were calculated and various testing including mechanical and chemistry analysis were performed in order to evaluate the integrity of Yonggwang unit 1 reactor vessel during the operation until life time. The evaluation results are as follows; Fast neutron fluences for capsules U, V, X and W are 5.555E+18, 1.662E+19, 3.358E+19, and 4.521E+19 n/cm{sup 2}, respectively. The bias factor, the ratio of measurement versus calculation, was 0.859 for the 1st through 4th testing and the calculational uncertainty, 11.80% satisfied the requirement of USNRC Reg.Guide 1.190, 20%. The best estimated neutron fluence for reactor vessel inside surface was 1.551E+19 n/cm{sup 2} based on the end of 12th fuel cycle and it was predicted that the fluences of vessel inside surface at 32, 40, 48 and 56EFPY would reach 3.929E+19, 4.880E+19, 5.831E+19 and 6.782E+19 n/cm{sup 2} based on the current calculation. The result through this analysis for Yonggwang unit 1 showed that there would be no problem for the pressurized thermal shock(PTS) during the operation until design life. 4 refs., 41 figs., 35 tabs. (Author)

  13. Actinides inventory of the nuclear power plant of Laguna Verde Unit 1; Inventario de actinidos de la Central Nuclear Laguna Verde Unidad 1

    Energy Technology Data Exchange (ETDEWEB)

    Martinez C, E.; Ramirez S, J. R. [ININ, Carretera Mexico-Toluca s/n, 52750 Ocoyoacac, Estado de Mexico (Mexico); Alonso V, G., E-mail: eduardo.martinez@inin.gob.mx [IPN, Escuela Superior de Fisica y Matematicas, Av. Instituto Politecnico Nacional s/n, U. P. Adolfo Lopez Mateos, Col. San Pedro Zacatenco, 07738 Mexico D. F. (Mexico)

    2013-10-15

    At the present time 435 nuclear power reactors exist for the electricity generation operating in the world and 63 in construction. Mexico has two reactors type BWR in the nuclear power plant of Laguna Verde. The nuclear fuel that is used in the nuclear reactors is retired of the reactor core when the energy that this contained has been extracted. This used fuel is known as spent nuclear fuel, the problem with this fuel is that was irradiated inside the reactor and continuous emitting a high radiation, as well as a significant heat quantity when being extracted, for what is necessary to maintain it in cooling and with some shielding to be protected of the radiation that emits. This objective is achieved confining the fuel in the spent nuclear fuel pool, where it is cooled and the same pool provides the necessary shielding to maintain the surroundings in safety radiation levels for the personnel that work in the power plant. An inconvenience of the pools is its limited storage capacity and that after certain time is necessary to remove the fuel, according to the established regulation to continue operating. To correct this inconvenience, two alternatives of spent fuel disposition exist, 1) the final disposition in deep geologic repositories and 2) the reprocessing and recycled of spent fuel. Each alternative presents its particularities and specific problems; however taking many years to be able to implement anyone of them. To carry out the second option, is indispensable to estimate the total mass of actinides generated in the spent nuclear fuel, that which represents to develop a methodology for it, this action is the main purpose of the present work. Inside our calculation method was necessary to appeal to diverse computation tools as the codes Origin-S and Keno V.a. Later on the obtained were compared with a problem type Benchmark, being obtained a smaller absolute error to 1.0%. (Author)

  14. Development of radiation protection technology for application of the retired steam generator, Kori Unit no. 1

    Energy Technology Data Exchange (ETDEWEB)

    Kim, J. H.; Jang, D. C.; Song, K. S.; Lee, S. J.; Ahn, C. S.; Kim, D. H.; Im, Y. K.; Kim, H. D. [Hanil Nuclear Co., Ltd., Anyang (Korea, Republic of)

    2005-04-15

    It is a field study to develop and verify maintenance technologies such as verification and technology development of ECT (Eddy current test) using failure, heat tube excavation and field pressure test regarding the utilization of retired steam generator using 2 units of Retired Steam Generator in Kori 1 that was replaced for the first time in Korea in 1998. Since May, 2003, our team has investigated Retired Steam Generator which was stored in Radioactive waste warehouse in Korea Hydro and Nuclear Power Kori unit no.1 Branch, in order to study natural fault ECT signal acquisition, maintenance technology verification, small tubes/samples abstraction. A temporal task zone was made focusing on 'Man Way at the bottom of Chamber 'A'.' The purpose of the study is to establish Radiological Protection and Radioactive Waste Treatment Plan by setting ALARA (As Low As Reasonably Achievable) goal systematically, which is the basic concept of Radiological Protection and reduction in exposure of radiological workers to radioactive materials with proper Radiological Protection countermeasures according to the changes in radioactivity, to prevent expansion from contamination and to manage 'Radioactive Waste Reduction Activities' effectively.

  15. Marble Hill Nuclear Generating Station, Units 1 and 2: Final environmental statement (Docket Nos. STN 50-546 and STN 50-547)

    International Nuclear Information System (INIS)

    1976-09-01

    The proposed action is the issuance of construction permits to the Public Service Company of Indiana, Inc., Northern Indiana Public Service Company, Inc., East Kentucky Power Cooperative, Inc., and Wabash Valley Power Association for the construction of the Marble Hill Nuclear Generating Station, Units 1 and 2 (MH 1and2). The 987-acre site is predominately forest and cropland. Construction-related activities on the site would disturb about 250 acres. The portion of this land not be used for the plant facilities, parking lots, roads, etc., will be restored by seeding and landscaping. The temporary removal of vegetation will tend to promote erosion. Increased siltation and turbidity can be expected in local streams during construction, but measures will be taken to minimize these effects. A maximum of 69 cfs of cooling water will be withdrawn from the Ohio River of which cfs will be returned to the river via pipeline with the dissolved solids concentration increased by a factor of about 6. About cfs will be evaporated to the atmosphere by the cooling towers. The volume of discharge (9 cfs) is very small compared with the river flow (annual mean is about 110,000 cfs) and the thermal effect on the river ecosystem is not expected to be significant. Chemical discharges from the plant will be diluted to concentrations below those which might adversely affect aquatic biota. The risk associated with accidental radiation exposure will be very low. 43 figs., 115 tabs

  16. Draft environmental statement related to the proposed Jamesport Nuclear Power Station, Units 1 and 2: (Docket Nos. STN-50-516 and STN-50-517)

    International Nuclear Information System (INIS)

    1975-02-01

    The proposed action is the issuance of construction permits to the Long Island Lighting Company for the construction of the Jamesport Nuclear Power Station, Units 1 and 2, located on Long Island Sound in the Town of Riverhead, New York. Operation of the proposed once-through cooling system will result in the heating of 4180 cfs of water by 18/degree/F. Phytoplankton, zooplankton, and ichthyoplankton will be entrained by the cooling system. The organisms in approximately 40 /times/ 10 9 ft 3 of water per year will suffer direct mortality due to chlorination and heat shock. The risk associated with accidental radiation exposure will be very low. A bottom area of some 105.5 acres will be affected by dredging and jetty construction. Of this total, 4.35 acres will be permanently replaced by jetties, and 101.15 acres will be temporarily (a total of four years) disrupted by dredging. This impact will be temporary, since the dredged areas will be recolonized by the benthic community upon completion of work. There is a potential for substantial impingement loss of fishes on the intake screens which will require additional data to quantify. Approximately 39 miles of transmission lines will be constructed. Ninety-two percent of the total routings utilize existing rights-of-way, railroad rights-of-way, or new rights-of-way immediately adjacent to railroad rights-of-way. The rights-of-way will require approximately 621 acres. 65 refs., 64 tabs

  17. Perkins Nuclear Station, Units 1, 2, and 3: Final environmental statement (Docket Nos. STN 50-488, STN 50-489, and STN 50-490

    International Nuclear Information System (INIS)

    1975-10-01

    The proposed action is the issuance of a construction permit to the Duke Power Company for the construction of the Perkins Nuclear Station (PNS) Units 1, 2, and 3 located in Davie County, North Carolina. A total of 2402 acres will be used for the PNS site; another 1401 acres will be used for the Carter Creek Impoundment. Construction-related activities on the primary site will disturb about 617 acres. Approximately 631 acres of land will be required for transmission line right-of-way, and a railroad spur will affect 77 acres. This constitutes a minor local impact. The heat dissipation system will require a maximum water makeup of 55,816 gpm, of which 50,514 gpm will be consumed due to drift and evaporative losses. This amount represents 4% of the mean monthly flow of the Yadkin River. The cooling tower blowdown and chemical effluents from the station will increase the dissolved solids concentration in the Yadkin River by a maximum of 18 ppm. The thermal alterations and increases in total dissolved solids concentration will not significantly affect the aquatic productivity of the Yadkin River. 26 figs., 51 tabs

  18. Palo Verde Nuclear Generating Station, Units 1, 2 and 3 (Docket Nos. STN 50-528, STN 50-529 and STN 50-530): Final environmental statement

    International Nuclear Information System (INIS)

    1975-09-01

    The proposed action is the issuance of construction permits to the Arizona public Service Company for the construction of the Palo Verde Nuclear Generating Station, Units 1, 2, and 3. Preparation of the 3800-acre site will involve the clearing of up to 2500 acres of land, 1500 of which will be prominently devoted to station facilities. An additional 1200- to 1300-acre evaporation pond will ultimately be developed during the lifetime of the station. About 2200 site acres, previously devoted to agriculture, will be excluded from this land use. Soil disturbance during construction of the station, transmission lines, and water conveyance pipeline will tend to promote erosion and increase siltation in local ephemeral water courses. Stringent measures will be taken to minimize these effects. The total radiation dose to construction workers is estimated to be 15 man-rem. This dose is a small fraction of the approximately 470 man-rem which will be received by the construction force over the same period from natural background radiation. Station, transmission line, and water pipeline construction will kill, remove, displace, or otherwise disturb involved flora and fauna, and will eliminate varying amounts of wildlife breeding, nesting, and forage habitat. These will not be important permanent impacts to the population stability and structure of the involved local ecosystems of the Sonoran desert; however, measures will be taken to minimize such effects as do result form the proposed action

  19. Operation of Grand Gulf Nuclear Station, Units 1 and 2, Dockets Nos. 50-416 and 50-417: Mississippi Power and Light Company, Middle South Energy, Inc., South Mississippi Electric Power Association. Final environmental statement

    International Nuclear Information System (INIS)

    1981-09-01

    The information in this Final Environmental Statement is the second assessment of the environmental impacts associated with the construction and operation of the Grand Gulf Nuclear Station, Units 1 and 2, located on the Mississippi River in Claiborne County, Mississippi. The Draft Environmental Statement was issued in May 1981. The first assessment was the Final Environmental Statement related to construction, which was issued in August 1973 prior to issuance of the Grand Gulf Nuclear Station construction permits. In September 1981 Grand Gulf Unit 1 was 92% complete and Unit 2 was 22% complete. Fuel loading for Unit 1 is scheduled for December 1981. The present assessment is the result of the NRC staff review of the activities associated with the proposed operation of the Station, and includes the staff responses to comments on the Draft Environmental Statement

  20. Final environmental statement for William B. McGuire Nuclear Station, Units 1 and 2: (Docket Nos. 50-369 and 50-370)

    International Nuclear Information System (INIS)

    1976-04-01

    The proposed action is the issuance of operating licenses to the Duke Power Company for the startup and operation of the William B. McGuire Nuclear Station, Units 1 and 2 (the plant) located on the Lake Norman in Mecklenburg County, 17 miles north-northwest of Charlotte, North Carolina. The units will be cooled by once-through flow of water from Lake Norman. Two units, each with a net electrical capacity of 1180 MWe will be added to the resources of the Duke Power Company. This will have a favorable effect on reserve margins and provide a cost savings of $77 to $122 million in production costs in 1979 if the units come on line as scheduled, and cost savings in subsequent years. Approximately 200 acres of rural, partially wooded land owned by the applicant will be unavailable for other uses during the 40-year life of the plant. Approximately 61.6 acres of additional land will be utilized for transmission line corridors and/or switchyard and maintained under controlled conditions. Land-use patterns will necessarily conform to the needs of the application but will not be changed significantly from present usage. At full power, condenser cooling water could be heated to as high as 96/degree/F (35.6/degree/C) as a monthly average and will be discharged at a rate of up to 4492 cfs. The temperature rise of the water will be 16/degree/F (8.8/degree/C) to 32/degree/F (17.8/degree/C) above ambient. The heated water will mix with the cooler water of Lake Norman, where the heat will be dissipated to the atmosphere. The increase in temperature will cause a loss of approximately 31 cfs of water as a result of increased evaporation. 26 figs., 46 tabs

  1. Closure simulation of the MSIV of Unit 1 of the Laguna Verde nuclear power plant using the Simulate 3K code

    International Nuclear Information System (INIS)

    Alegria A, A.

    2015-09-01

    In this paper the simulation of closure transient of all main steam isolation valves (MSIV) was performed with the Simulate-3K (S-3K) code for the Unit 1 of the Laguna Verde nuclear power plant (NPP-LV), which operates to thermal power of 2317 MWt, corresponding to the cycle 15 of operation. The set points for the performance of systems correspond to those set out in transient analysis: 3 seconds for the closure of all MSIV; the start of Scram when 121% of the neutron flux is reached, respect from baseline before the transient; the opening by peer of safety relief valves (SRV) in relief mode when the set point of the pressure is reached, the shoot of the feedwater flow seconds after the start of closing of the MSIV and the shoot of the recirculation water pumps when the pressure is reached in the dome of 1048 psig. The simulation time was of 57 seconds, with the top 50 to reach the steady state, from which the closure of all MSIV starts. In this paper the behavior of the pressure in the dome are analyzed, thermal power, neutron flux, the collapsed water level, the flow at the entrance of core, the steam flow coming out of vessel and the flow through of the SRV; the fuel temperature, the minimal critical power ratio, the readings in the instrumentation systems and reactivities. Instrumentation systems were implemented to analyze the neutron flux, these consist of 96 local power range monitors (LPRM) located in different radial and axial positions of the core and 4 channels of average power range monitors, which grouped at 24 LPRM each one. LPRM response to the change of neutron flux in the center of the core, at different axial positions is also shown. Finally, the results show that the safety limit MCPR is not exceeded. (Author)

  2. Palo Verde Nuclear Generating Station Units 1, 2, and 3: Draft environmental statement (Docket Nos. STN 50-528, 529, and 530)

    International Nuclear Information System (INIS)

    1975-04-01

    The proposed action is the issuance of construction permits to the Arizona Public Service Corporation for the construction of the Palo Verde Nuclear Generating Station, Units 1, 2 and 3. Preparation of the 3880-acre site will involve the clearing of up to 2500 acres of land, 1500 of which will be permanently devoted to station facilities. An additional 1200- to 1300-acre evaporation pond will ultimately be developed during the lifetime of the station. About 2200 site acres, previously devoted to agriculture, will be excluded from this land use (Sec. 4. 1). Soil disturbance during construction of the station, transmission lines, and water conveyance pipeline will tend to promote erosion and increase siltation in local ephemeral water courses. Stringent measures will be taken to minimize these effects (Sec. 4.5). Station, transmission line, and water pipeline construction will kill, remove displace, or otherwise disturb involved flora and fauna, and will eliminate varying amounts of wildlife breeding, nesting, and forage habitat. These will not be important impacts to the population stability and structure of the involved local ecosystems of the Sonoran desert; however, measures will be taken to minimize such effects (Sec. 4.3 and 4.5). Approximately 60 acres of agricultural land will be temporarily affected by construction in transmission corridors. The great majority can be returned to that use upon completion of construction, thus the impact is considered minor. Similarly, most grazing lands affected along these corridors, as well as along the water pipeline corridor, can eventually be returned to that use. New archaeological resources could be discovered along the path of final transmission corridor alignments. The applicant will take measures to locate and protect such resources if they exist. 75 refs., 24 figs., 65 tabs

  3. Alan R. Barton Nuclear Plant Units 1, 2, 3 and 4: Draft environmental statement (Docket Nos. 50-524, 525, 526 and 527)

    International Nuclear Information System (INIS)

    1975-04-01

    The proposed action is the issuance of construction permits to the Alabama Power Company for the construction of the Alan R. Barton Nuclear Plant Units 1, 2, 3 and 4. The Barton Plant, located on the Coosa River in Chilton and Elmore Counties, Alabama, will employ boiling water reactors to produce up to 3579 megawatts thermal (MWt) from each unit. A steam turbine-generator will use the heat to provide 1159 MWe (net) of electrical power capacity. A stretch power level of 3758 MWt (1209 MWe) is anticipated from design data and is considered in the assessments contained in this statement. The exhaust steam will be cooled in a closed cycle mode by mechanical cooling towers with water from the Coosa River. Construction of the plant and adjacent facilities will disturb an area of about 1025 acres. the land presently consists of forest land and some cropland. The impact is considered minor. About 18,460 acres will be required for the transmission line routes. The land presently consists of forest, pasture and cropland. No unique land usage is involved in the routes selected. The impacts are considered minor. Station construction will involve some community impacts. Highway congestion, due to increased traffic associated with construction and commuting activities, will have a moderate adverse impact on the local area. The number of construction workers moving into the area is expected to place a strain on the local school systems, housing and community services. Noise, dust, and odor during construction will have a minor adverse effect upon nearby residents in the sparsely populated area. 125 refs., 25 figs., 56 tabs

  4. Final environmental statement related to the proposed construction of Douglas Point Nuclear Generating Station, Units 1 and 2: (Docket Nos. 50-448 and 50-449)

    International Nuclear Information System (INIS)

    1976-03-01

    The proposed action is the issuance of construction permits to the Potomac Electric Power Company for the construction of the Douglas Point Nuclear Generating Station, Units 1 and 2, located in Charles County, Maryland. The exhaust steam will be cooled via a closed-cycle mode incorporating natural-draft wet cooling towers. The water used in the cooling system will be obtained from the Potomac River. Construction-related activities on the site will convert about 290 acres of the 1390 acres of forested land at the Douglas Point site to industrial use. In addition to acreage at the site, approximately 4.5 miles of transmission corridor will require about 211 acres of land for rights-of-way. This corridor will connect with 27 miles of existing rights-of-way over which a line connecting Possum Point to Burches Hill has already been approved. The installation of new transmission line, uniquely identified with Douglas Point, along the existing right-of-way will involve approximately 464 additional acres. As described in the application, the maximum river water intake will be about 97,200 gpm. Of this, a maximum of about 28,000 gpm will be lost in drift or evaporation from the cooling towers. About 700 gpm maximum of fresh well water will be consumed. It is conservatively assumed that all aquatic organisms entrained in the service water system will be killed due to thermal and mechanical shock. It is further estimated that at 97,200 gpm maximum total river water intake, the maximum impact on the striped bass fishery will be a reduction of <5%. The risk associated with accidental radiation exposure is very low. 32 figs., 59 tabs

  5. Final environmental statement: Related to the operation of Davis-Besse Nuclear Power Station, Unit 1 (Docket No. 50-346)

    International Nuclear Information System (INIS)

    1975-10-01

    The proposed action is the issuance of an operating license to the Toledo Edison Company and the Cleveland Electric Illuminating Company for the startup and operation of the Davis-Besse Nuclear Power Station Unit 1 (the station) located near Port Clinton in Ottawa County, Ohio. The total site area is 954 acres of which 160 acres have been removed from production of grain crops and converted to industrial use. Approximately 600 acres of the area is marshland which will be maintained as a wildlife refuge. The disturbance of the lake shore and lake bottom during construction of the station water intake and discharge pipes resulted in temporary turbidity, silting, and destruction of bottom organisms. Since completion of these activities, evidence of improvement in turbidity and transparency measurements, and the reestablishment of the bottom organism has been obtained. The cooling tower blowdown and service water which the station discharges to Lake Erie, via a submerged jet, will be heated no more than 20/degrees/F above the ambient lake water temperature. Although some small fish and plankton in the discharge water plume will be disabled as a result of thermal shock, exposure to chlorine and buffeting, few adult fish will be affected. The thermal plume resulting from the maximum thermal discharge is calculated to have an area of less than one acre within the 3/degrees/F isotherm (above lake ambient). Approximately 101 miles of transmission lines have been constructed, primarily over existing farmland, requiring about 1800 acres of land for the rights-of-way. Land use will essentially be unchanged since only the land required for the base of the towers is removed from production. Herbicides will not be used to maintain the rights-of-way. 14 figs., 34 refs

  6. Draft environmental statement related to construction of Erie Nuclear Plant, Units 1 and 2: (Docket Nos. STN 50-580 and STN 50-581)

    International Nuclear Information System (INIS)

    1977-11-01

    The proposed action is the issuance of construction permits to the Ohio Edison Company, acting on behalf of itself, the Cleveland Electric Illuminating Company, Duquesne Light Company, Pennsylvania Power Company, and the Toledo Edison Company, for the construction of the Erie Nuclear Plant Units 1 and 2, located in Erie County, Ohio. A total of 704 hectares (ha) (1740 acres) will be used for the Erie plant site. Construction-related activities on the primary site will disturb about 223 ha (551 acres). Approximately 641 ha (1584 acres) will be required for transmission line rights-of-way. The 3.86-km (2.4-mile) intake and discharge pipeline land corridor will involve alteration of approximately 13 ha (32 acres) of corridor and 1 ha (2.5 acres) for shore facilities. Also, 3.9 ha (9.6 acres) of lake bottom will be disturbed to provide 15-m-wide (50-ft-wide) trenches and an additional 15-m-wide (50-ft-wide) area for storage of excavated material for subsequent backfill for the 701-m (2300-ft) intake and 579-m (1900-ft) discharge lines. Plant construction will involve some community impacts. No residents will be displaced from the site property. Traffic on local roads will increase due to construction and commuting activities. The influx of construction workers' families (a peak work force of about 2700) is expected to cause no major housing or school problems. It is assumed that aquatic organisms entrained in the circulating water system will be killed due to thermal and mechanical shock. The maximum impact based on the population densities of phytoplankton and zooplankton organisms in the adjacent lake area will be the destruction of 0.1% of the entrainable organisms from the lake water. The entrainment of fish larvae will not constitute a significant impact on the lake fishery. 62 figs., 32 tabs

  7. Draft environmental statement related to construction of Yellow Creek Nuclear Plant, Units 1 and 2: (Docket Nos. STN 50-566 and STN 50-567)

    International Nuclear Information System (INIS)

    1977-06-01

    The proposed action is the issuance of construction permits to the Tennessee Valley Authority for the construction of the Yellow Creek Nuclear Plant Units 1 and 2. The 470-hectare site is predominantly wooded. Construction-related activities on the site would disturb about 59 hectares. The portion of this land not to be used for plant facilities, parking lots, roads, etc., will be restored by seeding and landscaping. The temporary removal of vegetation will tend to promote erosion. Increased siltation and turbidity can be expected in the Yellow Creek embayment during construction, but measures will be taken to minimize these effects. A maximum of 237.6 m 3 /min of make-up water will be withdrawn from the Yellow Creek embayment, of which 106 m 3 /min will be returned to Pickwick Lake via a pipeline with the dissolved solids concentration increased by a factor of about two. About 106 m 3 /min will be evaporated to the atmosphere by the cooling towers. The volume of thermal discharge (106 m 3 /min) is small compared with the flow in Pickwick Lake (minimum daily average flow of 7812 m 3 /min) and the effect on the Pickwick Lake ecosystem is not expected to be significant. During periods of average flow the plant could use about 24% of the flow through Yellow Creek embayment. Chemical discharges (with the possible exception of copper) from the plant will be diluted to concentrations below those which might adversely affect aquatic biota. The risk associated with accidental radiation exposure will be very low. 42 figs., 100 tabs

  8. Study of bark of chestnut tree Aesculus hippocastanum L. by two-dimensional decomposition of nuclear relax application; Badanie kory kasztanowca (Aesculus hippocastanum L.) metoda dwuwymiarowej dekompozycji funkcji relaksacji jadrowej

    Energy Technology Data Exchange (ETDEWEB)

    Weglarz, W.; Haranczyk, H. [Inst. Fizyki, Uniwersytet Jagiellonski, Cracow (Poland)

    1994-12-31

    Water bound in the bark of Aesculus hippocastanum L. was studied by two-dimensional decomposition of nuclear relaxation function. The aim of the work was to increase accuracy of relaxation function measurement. The work shows three components of relaxation function. 6 refs, 4 figs, 4 tabs.

  9. HRD System and Experience in the Korean Nuclear Industry

    Energy Technology Data Exchange (ETDEWEB)

    Kang, Byoungkook [KHNP Nuclear Power Education Institute, Busan (Korea, Republic of)

    2012-03-15

    Korea began to nurture its nuclear energy pioneers in the 1950s when the government dispatched personnel in research and policy-making areas to foreign institutions. Then in 1959, KAERI was established and now plays a leading role in nuclear technology R and D. In addition, Korea's first research reactor, TRIGA Mark-II, was built and put into operation in 1962. This paved the way for advancements in operation and technical development of nuclear reactors. In turn, these accomplishments led to the birth of Korea's first commercial reactor, Kori Unit 1, in the 1970s, and HRD in the nuclear industry was put on the right track. However, the Korean nuclear industry remained heavily dependent on nuclear exporting countries such as the US, Canada, and France. Already confident in construction, Korea took the lead in building Kori Units 3 and 4 and Ulchin Units 1 and 2 in the 1980s, but the country was still in need of technological self-reliance. In order to achieve this, Korea proactively launched systematic HRD programs and dispatched nuclear professionals to overseas nuclear facilities to secure individuals competent in the areas of NPP operations, plant design, and major equipment manufacturing. Thanks to its diligent endeavors, Korea's nuclear entities established independent nuclear training institutes in the 1990s and began producing a large number of competent personnel. This allowed the country to ensure not only the best operation and maintenance engineers but also the essential nuclear technology required for plant design and equipment manufacturing. Since the beginning of the 21{sup st} century, Korea has been producing its nuclear personnel on its own and exchanging nuclear training instructors and trainees with other organizations in fields where specialized knowledge is needed. Furthermore, Korea is taking comprehensive nuclear HRD measures in response to the rising demand for human resources that result from ongoing construction of NPPs in

  10. HRD System and Experience in the Korean Nuclear Industry

    International Nuclear Information System (INIS)

    Kang, Byoungkook

    2012-01-01

    Korea began to nurture its nuclear energy pioneers in the 1950s when the government dispatched personnel in research and policy-making areas to foreign institutions. Then in 1959, KAERI was established and now plays a leading role in nuclear technology R and D. In addition, Korea's first research reactor, TRIGA Mark-II, was built and put into operation in 1962. This paved the way for advancements in operation and technical development of nuclear reactors. In turn, these accomplishments led to the birth of Korea's first commercial reactor, Kori Unit 1, in the 1970s, and HRD in the nuclear industry was put on the right track. However, the Korean nuclear industry remained heavily dependent on nuclear exporting countries such as the US, Canada, and France. Already confident in construction, Korea took the lead in building Kori Units 3 and 4 and Ulchin Units 1 and 2 in the 1980s, but the country was still in need of technological self-reliance. In order to achieve this, Korea proactively launched systematic HRD programs and dispatched nuclear professionals to overseas nuclear facilities to secure individuals competent in the areas of NPP operations, plant design, and major equipment manufacturing. Thanks to its diligent endeavors, Korea's nuclear entities established independent nuclear training institutes in the 1990s and began producing a large number of competent personnel. This allowed the country to ensure not only the best operation and maintenance engineers but also the essential nuclear technology required for plant design and equipment manufacturing. Since the beginning of the 21 st century, Korea has been producing its nuclear personnel on its own and exchanging nuclear training instructors and trainees with other organizations in fields where specialized knowledge is needed. Furthermore, Korea is taking comprehensive nuclear HRD measures in response to the rising demand for human resources that result from ongoing construction of NPPs in Korea and the UAE

  11. Analysis of a station blackout transient at the Kori units 3/4

    International Nuclear Information System (INIS)

    Bang, Young Seok; Kim, Hho Jung

    1992-01-01

    A transient analysis of station blackout accident is performed to evaluate the plant specific capability to cope with the accident at the Kori Units 3/4. The RELAP5/MOD3/5m5 code and full three loop modelling scheme are used in the calculation. The leak flow from reactor coolant system due to a failure of reactor coolant pump seal following the accident is assumed to be 25 gpm and the turbine driven aux feedwater unavailable. As a result, it is found that no core uncovery occurs in the plant until 7100 sec following a station blackout, the steam generator has a decay heat removal capability until 3100 sec, and the natural circulation over the reactor coolant loop until the complete loop seal voiding are observed. And the Nuclear Plant Analyzer is used and found to be effective in improving the phenomenological understanding on the accident

  12. Safety Evaluation Report related to the operation of Diablo Canyon Nuclear Power Plant, Units 1 and 2 (Docket Nos. 50-275 and 50-323). Supplement No. 33

    International Nuclear Information System (INIS)

    1986-05-01

    Supplement 33 to the Safety Evaluation Report for the Pacific Gas and Electric Company's Diablo Canyon Nuclear Power Plant, Units 1 and 2 (Docket Nos. 50-275 and 50-323) has been prepared jointly by the Office of Nuclear Reactor Regulation and the Region V Office of the US Nuclear Regulatory Commission. The supplement reports on the status of the staff's investigation, inspection, and evaluation of allegations and concerns that have been identified to the NRC through March 1986. The report includes a complete listing of all allegations and concerns, indicating the status of their resolution. The NRC staff concludes that the technical issues raised in the allegations with regard to the design, construction, and safe operation of Diablo Canyon Units 1 and 2 have been satisfactorily resolved and no further action is required

  13. Safety Evaluation Report related to the operation of Diablo Canyon Nuclear Power Plant, Units 1 and 2 (Docket Nos. 50-275 and 50-323). Supplement No. 30

    International Nuclear Information System (INIS)

    1985-04-01

    Supplement 30 to the Safety Evaluation Report for the application by the Pacific Gas and Electric Company (PG and E) to operate the Diablo Canyon Nuclear Power Plant - Unit 2 (Docket No. 50-323) has been prepared by the Office of Nuclear Reactor Regulation of the US Nuclear Regulatory Commission. SSER 30 reports on the staff's technical review and evaluation of the design and analysis of Unit 2 piping systems and pipe supports. The staff effort includes an evaluation of PG and E's treatment of issues raised during the Unit 1 design verification, actions resulting from low power License Condition 2.C.(11) in the Unit 1 low power license DPR-76 and the Unit 2 applicability and resolution of certain allegations related to piping and supports

  14. A Preliminary Study on the Containment Integrity following BIT Removal for Kori NPP Unit 3,4

    Energy Technology Data Exchange (ETDEWEB)

    Song, Dong Soo; Byun, Choong Sup [KEPRI, Nuclear Power Generation Laboratory, Daejeon (Korea, Republic of); Jo, Jong Young [ENERGEO Inc., Sungnam (Korea, Republic of)

    2008-05-15

    The Boron Injection Tank (BIT) is to provide high concentrated boric acid to the reactor in order to mitigate the consequences of postulated Main Steam Line Break accidents (MSLB). Although BIT plays an important role in mitigating the accident, high concentration of 20,000ppm causes valve leakage, pipe clog, precipitation and continuous heat tracing have to be provided. This paper is for the feasibility study of containment integrity using CONTEMPT code for BIT removal of Kori Nuclear Power Plant (NPP) Unit 3, 4.

  15. A Preliminary Study on the Containment Integrity following BIT Removal for Kori NPP Unit 3,4

    International Nuclear Information System (INIS)

    Song, Dong Soo; Byun, Choong Sup; Jo, Jong Young

    2008-01-01

    The Boron Injection Tank (BIT) is to provide high concentrated boric acid to the reactor in order to mitigate the consequences of postulated Main Steam Line Break accidents (MSLB). Although BIT plays an important role in mitigating the accident, high concentration of 20,000ppm causes valve leakage, pipe clog, precipitation and continuous heat tracing have to be provided. This paper is for the feasibility study of containment integrity using CONTEMPT code for BIT removal of Kori Nuclear Power Plant (NPP) Unit 3, 4

  16. Safety evaluation report related to the operation of Diablo Canyon Nuclear Power Plant, Units 1 and 2 (Docket Nos. 50-275 and 50-323). Supplement No. 25

    International Nuclear Information System (INIS)

    1984-07-01

    Supplement 25 to the Safety Evaluation Report for Pacific Gas and Electric Company's application for licenses to operate Diablo Canyon Nuclear Power Plants, Unit 1 and Unit 2 (Docket Nos. 50-275 and 50-323) has been prepared by the Office of Nuclear Reactor Regulation (NRR) of the US Nuclear Regulatory Commission. This supplement reports on the staff's inspection and evaluation efforts on the matter of piping and piping supports as related to the seven technical license conditions in an Order Modifying License issued by NRR on April 18, 1984

  17. Safety evaluation report related to the operation of Grand Gulf Nuclear Station, Units 1 and 2. Dockets Nos. 50-416 and 50-417, Mississippi Power and Light Company; Middle South Energy, Inc., South Mississippi Electric Power Association

    International Nuclear Information System (INIS)

    1982-06-01

    Supplement 2 to the Safety Evaluation Report for Mississippi Power and Light Company, et. al, joint application for licenses to operate the Grand Gulf Nuclear Station, Units 1 and 2, located on the east bank of the Mississippi River near Port Gibson, in Claiborne County, Mississippi, has been prepared by the Office of Nuclear Reactor Regulation of the US Nuclear Regulatory Commission. This supplement reports the status of certain items that had not been resolved at the time of publication of the Safety Evaluation Report

  18. Safety Evaluation Report related to the operation of Palo Verde Nuclear Generating Station, Units 1, 2, and 3 (Docket Nos. STN 50-528, STN 50-529, and STN 50-530)

    International Nuclear Information System (INIS)

    1984-10-01

    Supplement No. 6 to the Safety Evaluation Report for the application filed by Arizona Public Service Company, et al., for licenses to operate the Palo Verde Nuclear Generating Station, Units 1, 2, and 3 (Docket Nos. STN 50-528/529/530), located in Maricopa County, Arizona, has been prepared by the Office of Nuclear Reactor Regulation of the Nuclear Regulatory Commission. The purpose of this supplement is to update the Safety Evaluation Report by providing an evaluation of (1) additional information submitted by the applicant since Supplement No. 5 was issued and (2) matters that the staff had under review when Supplement No. 5 was issued

  19. Safety Evaluation Report related to the operation of Palo Verde Nuclear Generating Station, Units 1, 2, and 3 (Docket Nos. STN 50-528, STN 50-529, and STN 50-530). Supplement No. 7

    International Nuclear Information System (INIS)

    1984-12-01

    Supplement No. 7 to the Safety Evaluation Report for the application filed by Arizona Public Service Company et al. for licenses to operate the Palo Verde Nuclear Generating Station, Units 1, 2, and 3 (Docket Nos. STN 50-528/529/530), located in Maricopa County, Arizona, has been prepared by the Office of Nuclear Reactor Regulation of the Nuclear Regulatory Commission. The purpose of this supplement is to update the Safety Evaluation Report by providing an evaluation of: (1) additional information submitted by the applicant since Supplement No. 6 was issued; and (2) matters that the staff had under review when Supplement No. 6 was issued

  20. Safety Evaluation Report related to the operation of Diablo Canyon Nuclear Power Plant, Units 1 and 2 (Docket Nos. 50-275 and 50-323). Supplement No. 28

    International Nuclear Information System (INIS)

    1985-04-01

    Supplement 28 to the Safety Evaluation Report for the Pacific Gas and Electric Company's application for licenses to operate Diablo Canyon Nuclear Power Plant, Units 1 and 2 (Docket Nos. 50-275 and 50-323) has been prepared jointly by the Office of Nuclear Reactor Regulation and the Region V Office of the US Nuclear Regulatory Commission. The supplement reports on the status of the staff's investigation, inspection, and evaluation of those allegations or concerns that have been identified to the NRC as of March 1, 1985

  1. Pickering Unit 1 chemical cleaning

    International Nuclear Information System (INIS)

    Smee, J.L.; Fiola, R.J.; Brennenstuhl, K.R.; Zerkee, D.D.; Daniel, C.M.

    1995-01-01

    The secondary sides of all 12 boilers at Pickering Unit 1 were chemically cleaned in 1994 by the team of Ontario Hydro, B and W International (Cambridge, Ontario) and B and W Nuclear Technologies (Lynchburg, Virginia). A multi-step EPRI/SGOG process was employed in a similar manner to previous clearings at Units 5 and 6 in 1992 and 1993, respectively. A major innovation with the Unit 1 cleaning was the incorporation of a crevice cleaning step, the first time this had been done on Ontario Hydro plants. In addition, six boilers were cleaned in parallel compared to three at a time in previous Pickering cleanings. This significantly reduced cleaning time. A total of 6,770 kg of sludge was removed through direct chemical dissolution. It consisted of 66% iron/nickel oxides and 28% copper metal. A total of 1,600,000 L (420,000 US gallons) of liquid waste was produced. It was processed through the spent solvent treatment facility located at the Bruce Nuclear Power Development site. Visual inspection performed after the cleaning indicated that the crevices between the boiler tubes and the tube support structure were completely clear of deposit and the general condition of the tubing and lattice bars appeared to be in 'as new' condition. (author)

  2. Final Environmental Statement related to the operation of Perry Nuclear Power Plant, Units 1 and 2 Docket Nos. 50-440 and 50-441, Cleveland Electric Illuminating Company

    International Nuclear Information System (INIS)

    1982-08-01

    The information in this Final Environmental Statement is the second assessment of the environmental impact associated with the construction and operation of the Perry Nuclear Power Plant, Units 1 and 2, located on Lake Erie in Lake County, about 11 km (7 mi) northeast of Painesville, Ohio. The first assessment was the Final Environmental Statement related to the construction of the plant issued in April 1974, prior to issuance of the construction permits (CPRR-148 and CPPR-149). Plant construction for Unit 1 is currently about 83% complete, and Unit 2 about 43% complete. Fuel loading for Units 1 and 2 currently estimated by the licensee (Cleveland Electric Illuminating Company) for November 1983, with Unit 2 fuel load scheduled for May 1987. The present assessment is the result of the NRC staff review of the activities associated with the proposed operation of the plant

  3. The application experience of ethanol amine at KORI unit 4

    International Nuclear Information System (INIS)

    Lee, Sang-hak; Park, Jong-il; Lee, Jae-won; Kim, Guem-Soo

    2004-01-01

    The secondary system water chemistry in the KORI PWR units has been well controlled by reducing the corrosion in the tubes of the steam generators; the pH agent has been changing from ammonia to ethanol amine (ETA) (1.8 to 2.0 ppm). For example, the iron concentration in the system was reduced by 40 to 70% compared with ammonia treatment. The paper presents the detailed information, such as ETA injection concentration and the variation of pH, concentration of organic acid products, and irons in the system, and a significant change on sludge after ETA application. (S. Ohno)

  4. Analysis of internal events for the Unit 1 of the Laguna Verde Nuclear Power Station. Appendixes; Analisis de eventos internos para la Unidad 1 de la Central Nucleoelectrica de Laguna Verde. Apendices

    Energy Technology Data Exchange (ETDEWEB)

    Huerta B, A; Lopez M, R [Comision Nacional de Seguridad Nuclear y Salvaguardias, 03000 Mexico D.F. (Mexico)

    1995-07-01

    This volume contains the appendices for the accident sequences analysis for those internally initiated events for Laguna Verde Unit 1, Nuclear Power Plant. The appendix A presents the comments raised by the Sandia National Laboratories technical staff as a result of the review of the Internal Event Analysis for Laguna Verde Unit 1 Nuclear Power Plant. This review was performed during a joint Sandia/CNSNS multi-day meeting by the end 1992. Also included is a brief evaluation on the applicability of these comments to the present study. The appendix B presents the fault tree models printed for each of the systems included and.analyzed in the Internal Event Analysis for LVNPP. The appendice C presents the outputs of the TEMAC code, used for the cuantification of the dominant accident sequences as well as for the final core damage evaluation. (Author)

  5. Proposed design modifications and technical specification changes on grid voltage degradation for the Point Beach Nuclear Plant, Units 1 and 2 (Docket Nos. 50-266 and 50-301). Technical evaluation report

    International Nuclear Information System (INIS)

    White, R.L.

    1981-01-01

    This report documents the technical evaluation of the proposed design mofifications and Technical Specification changes for protection of Class 1E equipment from grid voltage degradation for the Point Beach Nuclear Plant, Units 1 and 2. The review criteria are based on several IEEE standards and the Code of Federal Regulations. The evaluation compares the submittals made by the licensee with the NRC staff positions and the review criteria and presents the reviewer's conclusion on the acceptability of the proposed system

  6. Technical evaluation report on the adequacy of station electric-distribution-system voltages for the Millstone Nuclear Power Station, Units 1 and 2. Docket Nos. 50-245, 50-336

    International Nuclear Information System (INIS)

    Selan, J.C.

    1983-01-01

    This report documents the technical evaluation of the adequacy of the station electric-distribution-system voltages for the Millstone Nuclear Power Station, Units 1 and 2. The evaluation is to determine if the onsite distribution system, in conjunction with the offsite power sources, has sufficient capacity to automatically start and operate all Class 1E loads within the equipment voltage ratings under certain conditions established by the Nuclear Regulatory Commission. The analyses submitted demonstrate that adequate voltages will be supplied to the Class 1E equipment under the worst-case conditions analyzed

  7. Technical evaluation of the susceptibility of safety-related systems to flooding caused by the failure of non-category 1 systems for the San Onofre Nuclear Power Plant, Unit 1

    International Nuclear Information System (INIS)

    Latorre, V.R.; Victor, R.A.

    1980-11-01

    This report documents the technical evaluation of Southern California Edison Company's San Onofre Nuclear Power Plant, Unit 1, to determine whether the failure of any non-Category 1 (seismic) equipment could result in a condition, such as flooding, that might potentially adversely affect the performance of safety-related equipment required for the safe shutdown of the facility or to mitigate the consequences of an accident. Criteria developed by the US Nuclear Regulatory Commission were used to evaluate the acceptability of the existing protection as well as measures taken by Southern California Edison Company to minimize the danger of flooding and to protect safety-related equipment

  8. Technical evaluation report on the adequacy of station electric distribution system voltages for the Point Beach Nuclear Plant, Units 1 and 2. (Docket Nos. 50-266, 50-301)

    International Nuclear Information System (INIS)

    White, R.L.

    1983-01-01

    This report documents the technical evaluation of the adequacy of the station electric distribution system voltages for the Point Beach Nuclear Plant, Units 1 and 2. The evaluation is to determine if the onsite distribution system, in conjunction with the offsite power sources, has sufficient capacity to automatically start and operate all Class 1E loads within the equipment voltage ratings under certain conditions established by the Nuclear Regulatory Commission. For the worst case conditions study submitted by the licensee, it was shown that the station electric distribution system voltages would be adequate to start and operate 4160-volt and 480-volt Class 1E loads and their associated low voltage controls

  9. Reevaluation of Kori Unit 4 Natural Circulation Test

    Energy Technology Data Exchange (ETDEWEB)

    Yassin, Nassir [Korea Advanced Institute of Science and Technology, Daejeon (Korea, Republic of); Woo, Sweng Woong [Korea Institute of Nuclear Safety, Daejeon (Korea, Republic of)

    2013-10-15

    The simulation results showed that the natural circulation flow developed by density difference was capable of removing decay heat from the fuel rod. The maximum pellet centerline temperature of the hot channel showed large margin to the pellet melting temperature. The maximum coolant temperature in the hot channel was well below the saturation temperature. If steam generators provide heat sink to the primary coolant system and thus natural circulation is maintained, the integrity of the fuel in the core can be sustained with large margin. Passive cooling of reactor is inevitable in case of failures in forced cooling system such as loss of electric power for cooling pumps. Fukushima accident showed the importance of the passive core cooling. During the commissioning test of PWRs, natural circulation test is performed to demonstrate the passive core cooling by natural convection. The driving force for coolant flow is developed by the density deference along the loop multiplied by the gravitation. Using the data from 'natural circulation test' and 'RCS flow coast down test' of Kori Unit 4, fuel behavior was reevaluated by FRAPTRAN code. RCS natural circulation test of Kori Unit 4 was reevaluated by FRAPTYRAN simulation to study the fuel behavior during the flow coast down transient and at the equilibrium condition in which decay heat transport and RCS flow were stabilized.

  10. Field measurement of the piping system vibration of Ko-Ri unit 4 during the load-following operation

    International Nuclear Information System (INIS)

    Chung, Tae-Young; Hong, Sung-Yull; Kim, Bum-Nyun.

    1989-01-01

    During the load-following operation of nuclear power plants, flow rate, temperature, and pressure in the piping system can be varied by changing the electric power output level, and these variations can cause different vibration phenomena in the piping system. The piping system vibration is important because it is directly related to the dynamic stress of the piping system and can affect the life of the piping system through structural fatigue. An assessment of vibration levels for the classes II and III piping systems of the Ko-Ri Unit 4950-MW nuclear power plant was performed according to the given pattern of the load-following operation to study its feasibility from the viewpoint of piping system vibration. The classes II and III piping system vibration of the Ko-Ri Unit 4 may not cause any potential problem under the given pattern of the load-following operation; however, it is recommended that long-term operation in the 85 to 95% power range be avoided as much as possible

  11. NRC Fact-Finding Task Force report on the ATWS event at Salem Nuclear Generating Station, Unit 1, on February 25, 1983

    International Nuclear Information System (INIS)

    1983-03-01

    An NRC Region I Task Force was established on March 1, 1983 to conduct fact finding and data collection with regard to the circumstances which led to an anticipated transient without scram (ATWS) event at the Public Service Electric and Gas Company's Salem Generating Station, Unit 1 on February 25, 1983. The charter of the Task Force was to determine the factual information pertinent to management and administrative controls which should have ensured proper operation of the reactor trip breakers in the solid state protection system. This report documents the findings of the Task Force along with its conclusions

  12. Unit 1 and Unit 2 Nuclear Power Plant Mochovce construction finishing from primary contractor of technological part. Skoda Praha a. s. point of view

    International Nuclear Information System (INIS)

    Horky, F.

    2000-01-01

    In this paper the history of delivery of technological part for NPP V-1 Mochovce as well as of reconstruction and safety improvements by the Skoda Praha a.s. is presented. Primary contractor of technological part Skoda Praha together with its final suppliers proved ability to realize under hard conditions such a complicated work what was indisputedly Units 1 and 2 finishing. Company proved capability to conform itself flexibly in the course of work to requirements of customer for realization of safety measures which means that Units 1 and 2 fully satisfy international standards. By fulfilment of primary contractor of technology obligations and above all by takeover of complex responsibility for both Units putting in operation including responsibility for 'past' Skoda Praha put away one of basic problems which occurred in decision making to whom will be assigned construction finishing contract. These facts fully qualify Skoda Praha to be selected for possible Units 3 and 4 construction finishing as one of chief construction finishing participant

  13. Safety evaluation report related to the construction of Skagit/Hanford Nuclear Project, Units 1 and 2. Docket Nos. STN 50-522 and 50-523

    International Nuclear Information System (INIS)

    1982-12-01

    Supplement 3 to the Safety Evaluation Report for the application filed by Puget Sound Power and Light Company on behalf of itself, the Pacific Power and Light Company, The Washington Water Power Company, and the Portland General Electric Company for construction permits to build the Skagit/Hanford Nuclear Project has been issued by the Office of Nuclear Reactor Regulation of the United States Nuclear Regulatory Commission. This supplement is an evaluation of the site relocation amendment to the Preliminary Safety Analysis Report. The proposed site has been relocated from Skagit County, Washington, to the Department of Energy's Hanford Reservation

  14. Integrated safety assessment report: Integrated Safety Assessment Program: Millstone Nuclear Power Station, Unit 1 (Docket No. 50-245): Draft report

    International Nuclear Information System (INIS)

    1987-04-01

    The Integrated Safety Assessment Program (ISAP) was initiated in November 1984, by the US Nuclear Regulatory Commission to conduct integrated assessments for operating nuclear power reactors. The integrated assessment is conducted in a plant-specific basis to evaluate all licensing actions, licensee initiated plant improvements and selected unresolved generic/safety issues to establish implementation schedules for each item. In addition, procedures will be established to allow for a periodic updating of the schedules to account for licensing issues that arise in the future. This report documents the review of Millstone Nuclear Power Station, Unit No. 1, operated by Northeast Nuclear Energy Company (located in Waterford, Connecticut). Millstone Nuclear Power Station, Unit No. 1, is one of two plants being reviewed under the pilot program for ISAP. This report indicates how 85 topics selected for review were addressed. This report presents the staff's recommendations regarding the corrective actions to resolve the 85 topics and other actions to enhance plant safety. The report is being issued in draft form to obtain comments from the licensee, nuclear safety experts, and the Advisory Committee for Reactor Safeguards (ACRS). Once those comments have been resolved, the staff will present its positions, along with a long-term implementation schedule from the licensee, in the final version of this report

  15. Safety Evaluation Report related to the operation of Palo Verde Nuclear Generating Station, Units 1, 2, and 3 (Dockets Nos. STN 50-528, STN 50-529, and STN 50-530)

    International Nuclear Information System (INIS)

    1987-03-01

    Supplement No. 11 to the Safety Evaluation Report for the application filed by Arizona Public Service Company et al. for licenses to operate the Palo Verde Nuclear Generating Station, Units 1, 2, and 3 (Docket Nos. STN 50-528/529/530), located in Maricopa County, Arizone, has been prepared by the Office of Nuclear Reactor Regulation of the Nuclear Regulatory Commission. The purpose of this supplement is to update the Safety Evaluation Report by providing an evaluation of (1) additional information submitted by the applicant since Supplement No. 10 was issued and (2) other matters requiring staff review since Supplenent No. 10 was issued, specifically those issues that required resolution before Unit 3 low-power licensing

  16. Safety evaluation report related to the operation of Catawba Nuclear Station, Units 1 and 2. Docket Nos. 50-413 and 50-414, Duke Power Company, et al

    International Nuclear Information System (INIS)

    1983-02-01

    The Safety Evaluation Report for the application filed by Duke Power Company, North Carolina Municipal Power Agency Number 1, North Carolina Electric Membership Corporation, and Saluda River Electric Cooperative, Inc. as applicants and owners, for licenses to operate the Catawba Nuclear Station, Units 1 and 2 (Docket Nos. 50-413 and 50-414), has been prepared by the Office of Nuclear Reactor Regulation of the US Nuclear Regulatory Commission. The facility is located in York County, South Carolina, approximately 9.6 km (6 mi) north of Rock Hill and adjacent to Lake Wylie. Subject to favorable resolution of the items discussed in this report, the staff concludes that the facility can be operated by the applicant without endangering the health and safety of the public

  17. Safety Evaluation Report related to the operation of Palo Verde Nuclear Generating Station, Units 1, 2, and 3 (Docket Nos. STN 50-528, STN 50-529, and STN 50-530). Supplement No. 9

    International Nuclear Information System (INIS)

    1985-12-01

    Supplement No. 9 to the Safety Evaluation Report for the application filed by Arizona Public Service Company et al. for licenses to operate the Palo Verde Nuclear Generating Station, Units 1, 2 and 3 (Docket Nos. STN 50-528/529/530), located in Maricopa County, Arizona, has been prepared by the Office of Nuclear Reactor Regulation of the Nuclear Regulatory Commission. The purpose of this supplement is to update the Safety Evaluation Report by providing an evaluation of: (1) additional information submitted by the applicant since Supplement No. 8 was issued; and (2) matters that the staff had under review when Supplement No. 8 was issued, specifically those issues which required resolution prior to Unit 2 fuel loading and testing up to 5% of full power

  18. Safety evaluation report: related to the operation of Perry Nuclear Power Plant, Units 1 and 2, Docket Nos. 50-440 and 50-441, Cleveland Electric Illuminating Company

    International Nuclear Information System (INIS)

    1982-08-01

    Supplement No. 1 to the Safety Evaluation Report on the application filed by the Cleveland Electric Illuminating Company on behalf of itself and as agent for the Duquesne Light Company, the Ohio Edison Company, the Pennsylvania Power Company, and the Toledo Edison Company (the Central Area Power Coordination Group, CAPCO), as applicants and owners, for a license to operate the Perry Nuclear Power Plant, Units 1 and 2 (Docket Nos. 50-440 and 441). The facility is located near Lake Erie in Lake County, Ohio. This supplement has been prepared by the Office of Nuclear Reactor Regulation of the US Nuclear Regulatory Commission and reports the status of certain items that had not been resolved at the time of publication of the Safety Evaluation Report

  19. Safety Evaluation Report related to the operation of Watts Bar Nuclear Plant, Units 1 and 2 (Docket Nos. 50-390 and 50-391)

    International Nuclear Information System (INIS)

    Tam, P.S.

    1992-10-01

    This report supplements the Safety Evaluation Report (SER), NUREG-0847 (June 1982), Supplement No. 1 (September 1982), Supplement No. 2 (January 1984), Supplement No. 3 (January 1985), Supplement No. 4 (March 1985), Supplement No. 5 (November 1990), Supplement No. 6 (April 1991), Supplement No. 7 (September 1991), Supplement No. 8 (January 1992), and Supplement No. 9 (June 1992) issued by the Office of Nuclear Reactor Regulation of the US Nuclear Regulatory Commission with respect to the application filed by the Tennessee Valley Authority, as applicant and owner, for licenses to operate the Watts Bar Nuclear Plant, Units I and 2 (Docket Nos. 50-390 and 50-391). The facility is located in Rhea County, Tennessee, near the Watts Bar Dam on the Tennessee River. This supplement provides recent information regarding resolution of some of the outstanding and confirmatory items, and proposed license conditions identified in the SER

  20. Safety Evaluation Report related to the operation of Perry Nuclear Power Plant, Units 1 and 2 (Docket Nos. 50-440 and 50-441). Supplement No. 8

    International Nuclear Information System (INIS)

    1986-01-01

    Supplement No. 8 to the Safety Evaluation Report (NUREG-0887) on the application filed by the Cleveland Electric Illuminating Company on behalf of itself and as agent for the Duquesne Light Company, the Ohio Edison Company, the Pennsylvania Power Company, and the Toledo Edison Company (the Central Area Power Coordination Group or CAPCO), as applicants and owners, for a license to operate the Perry Nuclear Power Plant, Units and 1 and 2 (Docket Nos. 50-440 and 50-441), has been prepared by the Office of Nuclear Reactor Regulation of the US Nuclear Regulatory Commission. The facility is located in Lake County, Ohio, approximately 35 miles northeast of Cleveland, Ohio. This supplement reports the status of certain issues that has not been resolved at the time of publication of the Safety Evaluation Report and Supplement Nos. 1 through 7 to that report

  1. Report of the OSART (Operational Safety Review Team) mission to the Ignalina, units 1 and 5 nuclear power plant Republic of Lithuania 4 to 22 September 1995

    International Nuclear Information System (INIS)

    1996-03-01

    This report presents the results of the IAEA Operational Safety Review Team (OSART) review of Ignalina nuclear power plant in Lithuania. It describes recommendations and suggestions for improvements affecting operational safety provided to the responsible Lithuanian authorities for consideration and also describes a good practice for consideration by other nuclear power plants. Distribution of this OSART report is at the discretion of the Government of Lithuania and, until it is derestricted, the IAEA will make the report available to third parties only with the express permission of the Government of Lithuania. Any use of, or reference to, this report that may be made by the competent Lithuanian organizations is solely their responsibility

  2. Design concepts for the reactor protection and control process instrumentation digital upgrade project at the Donald C. Cook Nuclear Plant units 1 and 2

    International Nuclear Information System (INIS)

    Carruth, R.C.; Sotos, W.G.

    1996-01-01

    As the nation's nuclear power plants age, the need to consider upgrading of their electronic protection and control systems becomes more urgent. Hardware obsolescence and mechanical wear out resulting from frequent calibration and surveillance play a major role in defining their useful life. At Cook Nuclear Plant, a decision was made to replace a major portion of the plant's protection and control systems with newer technology. This paper describes the engineering processes involved in this successful upgrade and explains the basis for many decisions made while performing the digital upgrade

  3. Safety evaluation report related to the full-term operating license for San Onofre Nuclear Generating Station, Unit 1 (Docket No. 50-206)

    International Nuclear Information System (INIS)

    1991-07-01

    The safety evaluation report for the full-term operating license application filed by the Southern California Edison Company and the San Diego Gas and Electric Company has been prepared by the Office of Nuclear Reactor Regulation of the US Nuclear Regulatory Commission. The facility is located in San Diego County, California. The staff has evaluated the issues related to the conversion of the provisional operating license to a full-term operating license and concluded that the facility can continue to be operated without endangering the health and safety of the public following the license conversion. 43 refs., 3 figs., 3 tabs

  4. Order of 21 October 1988 withdrawing the licence for the release of liquid radioactive effluents by the Cattenom nuclear production centre (units 1 and 2)

    International Nuclear Information System (INIS)

    1988-01-01

    The Court of Justice of the European Communities decided on 22 September 1988 that the Commission of the European Communities had to be notified and give its opinion before the competent authorities of Member States authorised the release of radioactive effluents from a nuclear installation. In compliance with that judgment, this Order repeals an Order of 21 February 1986 licensing such release (NEA) [fr

  5. Rehabilitation and modernization project of units 1 and 2 of Laguna Verde Nuclear Power Plant. A strengthening project to 120%. (2nd phase)

    International Nuclear Information System (INIS)

    Liebana, B.; Merino, A.; Garcia, J. L.; Gomez, M.; Martinez, I.; Ruiz, L.

    2010-01-01

    The power increase of the Laguna Verde Nuclear Power Plant is a project for the rehabilitation and modernization of the turbo and associated equipment to get an increase of its power and of its service life. The project scope includes the design, the engineering, the equipment supply, the installation, the testing and the commissioning. This article presents the work of the second phase.

  6. Technical evaluation of the proposed design modifications and technical specification changes on grid voltage degradation (Part A) for the Pilgrim Nuclear Power Station, Unit 1

    International Nuclear Information System (INIS)

    White, R.L.

    1980-01-01

    This report documents the technical evaluation of the proposed design modifications and Technical Specification changes for protection of Class 1E equipment from grid voltage degradation for the Pilgrim Nuclear Power Station. The review criteria are based on several IEEE standards and the Code of Federal Regulations. The evaluation compares the submittals made by the licensee with the NRC staff positions and the review criteria and presents the reviewer's conclusion on the acceptability of the proposed system

  7. Report of the international fire safety mission to Temelin, unit 1 nuclear power plant Czech Republic 4 to 14 February 1996

    International Nuclear Information System (INIS)

    1996-01-01

    This report presents the results of an IAEA Fire Safety Mission conducted within the scope of Technical Co-operation Project CZR/9/005 to assess the licensing process, design, analysis and operational management of the Temelin Nuclear Power Plant with regards to fire safety of the plant. The Temelin Nuclear Power Plant currently has two units under construction. Each unit is equipped with a pressurized water reactor of the WWER design with a net electrical output of about MWe. The plant has already made significant upgrading in fire protection from the original design. The Team's evaluation is based on the IAEA Safety Series No. 50-SG-D2 (Rev.1), Fire Protection in Nuclear Power Plants, and other fire protection guidelines currently produced by the IAEA. The evaluation, conclusions and recommendations presented in this report reflect the views of the Fire Safety Mission experts. The recommendations are provided for consideration by the responsible authorities in the Czech Republic towards enhancing fire safety at the Temelin plant

  8. Preliminary development of an integrated approach to the evaluation of pressurized thermal shock as applied to the Oconee Unit 1 Nuclear Power Plant

    Energy Technology Data Exchange (ETDEWEB)

    Burns, T J; Cheverton, R D; Flanagan, G F; White, J D; Ball, D G; Lamonica, L B; Olson, R

    1986-05-01

    An evaluation of the risk to the Oconee-1 nuclear plant due to pressurized thermal shock (PTS) has been Completed by Oak Ridge National Laboratory (ORNL). This evaluaion was part of a Nuclear Regulatory Commission (NRC) program designed to study the PTS risk to three nuclear plants: Oconee-1, a Babcock and Wilco reactor plant owned and operated by Duke Power Company; Calvert Cliffs-1, a Combustion Engineering reactor plant owned and operated by Baltimore Gas and Electric company; and H.B. Robinson-2, a Westinghouse reactor plant owned and operated by Carolina Power and Light Company. Studies of Calvert Cliffs-1 and H.B. Robinson-2 are still underway. The specific objectives of the Oconee-1 study were to: (1) provide a best estimate of the probability of a through-the-wall crack (TWC) occurring in the reactor pressure vessel as a result of PTS; (2) determine dominant accident sequences, plant features, operator and control actions and uncertainty in the PTS risk; and (3) evaluate effectiveness of potential corrective measures.

  9. Lessons learnt from the resin release into the primary circuit of the Fessenheim NPP unit 1 in January 2004. Impact on the nuclear safety

    International Nuclear Information System (INIS)

    Georgescu, M.

    2004-01-01

    On January the 24 th , at the Fessenheim NPP unit 1, a human error was committed during a boron demineralizer line-up, caused by lack of preparation. Consequently, a quantity of resin estimated at about 300 liters was released from this demineralizer, through its safety valve, into the head-tank of the chemical and volume control (CVC) system and after that, into the primary circuit. The incident had a real impact on the unit: the CVC filters were clogged, the seal injection flow of the primary circuit main pumps was lost, the primary circuit main pump 2 tripped four days after the incident, as the rate of the recirculated seal leak flow (downstream the seal 1) increased up to the automatic trip set point, the shaft of the running primary circuit feed pump was found seized into the rear hydrostatic bearing following the pump stop (after ten days of successful operation), the thimble plugs were jammed into their guide tubes, the small diameter pipes were plugged. The unit shutdown for over five months was necessary to clean the primary circuit components, repair or replace the affected equipment items and carry out inspections and tests. The reinforced unit in-service monitoring program, set up during the unit start-up, confirms that, up to now, the unit operation has not been adversely affected by the residual amounts of resin which subsist in certain areas of the primary circuit. Nevertheless, it remains to verify that, in the long term, these deposits will have no negative chemical effect in the potential confined areas, such as the thermal barriers of the primary circuit main pumps. Finally, the occurrence of this incident underlines, once more, the importance of normal operating activity preparing and checking. It also reveals the implementation of an ''unforgiving'' design change allowing the installation of a boron demineralizer safety valve having its outlet connected to the primary circuit. (orig.)

  10. Safety evaluation report related to the operation of Sequoyah Nuclear Plant, Units 1 and 2, Docket Nos. 50-327 and 50-328, Tennessee Valley Authority. Supplement No. 4

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1981-01-01

    On September 17, 1980, the Nuclear Regulatory Commission (NRC) issued the facility operating license DPR-77 to the Tennessee Valley Authority for the Sequoyah Nuclear Plant, Unit 1, located in Hamilton County, Tennessee. The license authorized operation of Unit 1 at 100 percent power; however, a license condition regarding the adequacy of the hydrogen control system was included that required resolution by January 31, 1981. The purpose of Supplement No. 4 to the SER is to further update our Safety Evaluation Reports on the hydrogen control measures (Section 22.2, II.B.7), and to comply with the license condition which is as follows: 'By January 31, 1981, TVA shall by testing and analysis show to the satisfaction of the NRC staff that an interim hydrogen control system will provide with reasonable assurance protection against breach of containment in the event that a substantial quantity of hydrogen is generated.' TVA submitted on December 11, 1980, the first quarterly report on the research program for hydrogen control. Also, TVA revised volume 2 of the Sequoyah Core Degradation Program Report to incorporate additional information on the overall program. Section II.B.7 of Supplement No. 4 responds to the license condition. Each section is supplementary to and not in lieu of discussion in the Safety Evaluation Report and Supplements Nos. 1, 2, and 3, except where specifically noted. Supplements No. 2 and 3 to the Safety Evaluation Report provided a basis for concluding that the full-power licensing of Sequoyah Unit 1 need not await completion of ongoing work on hydrogen control measures. This supplement concludes that operation of the IDIS for an interim period of one year is appropriate.

  11. TMI-1 restart: an evaluation of the licensee's management integrity as it affects restart of Three Mile Island Nuclear Station (Unit 1 Docket 50-289). Supplement 5

    International Nuclear Information System (INIS)

    1984-07-01

    Supplement 5 to the Safety Evaluation Report (SER) on TMI-1 Restart documents the review by the Nuclear Regulatory Commission (NRC) staff of nine investigations conducted by the NRC Office of Investigations into matters identified as relevant and material to an evaluation of the licensee's management integrity. The staff has included, as part of its evaluation, materials from its review of the GPU v. B and W lawsuit record (NUREG-1020LD, GPU, v. B and W Lawsuit Review and Its Effect on TMI-1) as well as other relevant materials developed since the close of the record in the TMI-1 Restart proceeding. In developing its position on General Public Utilities Nuclear Corporation's character (i.e., management integrity), the staff evaluated matters that cast doubt on the licensee's character, individually and collectively; considered the remedial actions taken by the licensee; and balanced past improper conduct of the licensee against its subsequent record of remedial actions and performance and record of current senior management of the licensee. The staff concluded that, while the past improper conduct was grave, the remedial actions taken, the subsequent record of performance, and the record of current senior management support a finding that GPUN can and will operate TMI-1 without undue risk to the health and safety of the public

  12. Impact on the bar value in hot by the introduction of advanced control bars in the Unit 1 of the Laguna Verde Nuclear power plant

    International Nuclear Information System (INIS)

    Montes, J.L.; Perusquia, R.; Ortiz, J.J.; Hernandez, J.L.; Ramirez, J.R.

    2004-01-01

    In recent dates the Laguna Verde Nuclear Power station (CNLV) has acquired new designs of control bars, this new type of bars presents modifications important in their design. For what is important to analyze their performance inside those reactors of this nuclear power station. Presently work is shown the behavior of the nucleus of the reactor in hot condition (HFP) when three different types of control bar are used. The first of them corresponds the one that initially has been used in this power station and that we will call original. The second type of control bars, it corresponds to an advanced type and it is the first design different from the original and it corresponds to a bar design that it includes Hafnium (Hf) like one of their neutronic absorption characteristics. The third, denoted as 2AV, include besides the material of the second type new design characteristics, and it is the last finish bar type that it has been introduced in the operation of the reactors of the CNLV. With base in the studied cases is found that the bars 2AV have a total power value, 7.6 % bigger respect the bars 1AV; and in turn the bars 1AV, 6.1 % bigger with respect the ORG control bars. (Author)

  13. Safety Evaluation Report related to the restart of Davis-Besse Nuclear Power Station, Unit 1, following the event of June 9, 1985 (Docket No. 50-346)

    International Nuclear Information System (INIS)

    1986-06-01

    On June 9, 1985, the Davis-Besse Nuclear Power Station, operated by the Toledo Edison Company, experienced a partial loss of main feedwater while the plant was at 90% power. The ensuing reactor trip was followed by spurious isolation of the steam geneators which initiated a chain of events involving a number of equipment malfunctions and several operator errors ultimately interrupting all feedwater for a short period of time. By the time operators were able to restore feedwater, both steam generators had dried out. A letter from the Director of the Office of Nuclear Reactor Regulation, pursuant to 10 CFR 50.54(f) of the Commission's regulations, confirmed that the Davis-Besse facility would not be restarted without NRC approval. The letter also requested that Toledo Edison submit its program for resolving numerous concerns identified by the staff. In response, the license submitted the Davis-Besse Course of Action report. The staff has reviewed that document and other supporting material submitted by the licensee; the staff's evaluation of that information is presented in this report

  14. Pretreatment Process for performance Improvement of SIES at Kori Unit 2 in Korea

    International Nuclear Information System (INIS)

    Lee, Sang Jin; Yang, Ho Yeon; Shin, Sang Woon; Song, Myung Jae

    1994-01-01

    Pretreatment process consisted of submerged hollow-fiber microfiltration(HMF) membrane and spiral-wound nanofiltration(SNF) membrane has been developed by NETEC, KHNP for the purpose of improving the impurities of liquid radioactive waste before entering Selective Ion Exchange System(SIES). The lab-scale combined system was installed at Kori NPP no. 2 nuclear power plant and demonstration tests using actual liquid radioactive waste were carried out to verify the performance of the combined system. The submerged HMF membrane was adopted for removal of suspended solid in liquid radioactive waste and the SNF membrane was used for removal of particulate radioisotope such as, Ag-110m and oily waste because ion exchange resin can not remove particulate radioisotopes. The liquid waste in Waste Holdup Tank(WHT) was processed with HMF and SNF membrane, and SIES. The initial SS concentration and total activity of actual waste were 38,000ppb and 1.534x10 -3 μCi/cc, respectively. The SS concentration and total activity of permeate were 30ppb and lower than LLD(Lower Limit of Detection), respectively

  15. User's guide for PRISM (Plant Risk Status Information Management System) Arkansas Nuclear One-Unit 1: Volume 1, Program for inspectors

    International Nuclear Information System (INIS)

    Campbell, D.J.; Guthrie, V.H.; Kirchner, J.R.; Kirkman, J.Q.; Paula, H.M.; Ellison, B.C.; Dycus, F.M.; Farquharson, J.A.; Flanagan, G.F.

    1988-03-01

    This user's guide is a two-volume document designed to teach NRC inspectors and NRC regulators how to access probabilistic risk assessment information from the two Plant Risk Status Information Management System (PRISIM) programs developed for Arkansas Nuclear One -- Unit One (ANO-1). This document, Volume 1, describes how the PRA information available in Version 1.0 of PRISIM is useful for planning inspections. Using PRISIM, inspectors can quickly access PRA information and use that information to update risk analysis results, reflecting a plant's status at any particular time. Both volumes are stand-alone documents, and each volume presents several sample computer sessions designed to lead the user through a variety of PRISIM applications used to obtain PRA-related information for monitoring and controlling plant risk

  16. User's guide for PRISIM (Plant Risk Status Information Management System) Arkansas Nuclear One--Unit 1: Volume 2, Program for regulators

    Energy Technology Data Exchange (ETDEWEB)

    Campbell, D.J.; Guthrie, V.H.; Kirchner, J.R.; Kirkman, J.Q.; Paula, H.M.; Ellison, B.C.; Dycus, F.M.; Farquharson, J.A.; Flanagan, G.F.

    1988-03-01

    This user's guide is a two-volume document designed to teach NRC inspectors and NRC regulators how to access probabilistic risk assessment information from the two Plant Risk Status Information Management System (PRISIM) programs developed for Arkansas Nuclear One--Unit One (ANA-1). This document, Volume 2, describes how the PRA information available in Version 2.0 of PRISIM is useful as an evaluation tool for regulatory activities. Using PRISIM is useful as an evaluation tool for regulatory activities. Using PRISIM, regulators can both access PRA information and modify the information to assess the impact these changes may have on plant safety. Each volume is a stand-alone document.

  17. User's guide for PRISM (Plant Risk Status Information Management System) Arkansas Nuclear One-Unit 1: Volume 1, Program for inspectors

    Energy Technology Data Exchange (ETDEWEB)

    Campbell, D.J.; Guthrie, V.H.; Kirchner, J.R.; Kirkman, J.Q.; Paula, H.M.; Ellison, B.C.; Dycus, F.M.; Farquharson, J.A.; Flanagan, G.F.

    1988-03-01

    This user's guide is a two-volume document designed to teach NRC inspectors and NRC regulators how to access probabilistic risk assessment information from the two Plant Risk Status Information Management System (PRISIM) programs developed for Arkansas Nuclear One -- Unit One (ANO-1). This document, Volume 1, describes how the PRA information available in Version 1.0 of PRISIM is useful for planning inspections. Using PRISIM, inspectors can quickly access PRA information and use that information to update risk analysis results, reflecting a plant's status at any particular time. Both volumes are stand-alone documents, and each volume presents several sample computer sessions designed to lead the user through a variety of PRISIM applications used to obtain PRA-related information for monitoring and controlling plant risk.

  18. Some causes of vibrations recorded by in-service diagnostic systems in steam generators of units 1 and 2 of Dukovany nuclear power plant

    International Nuclear Information System (INIS)

    Sadilek, J.; Matal, O.

    1989-01-01

    A brief description is presented of the design of the steam generators of the first and second units of the Dukovany nuclear power plant. Attention is also given to the feed water systems and the diagnostic systems. The causes are analyzed of the irregularly occurring vibrations in the steam generators in service. It is demonstrated that the source of the vibrations transmitted to the steam generators are the valves in the feeding tract. The vibrations are induced by dynamic forces from the feed water. Reducing the water pressure at the delivery of the electric feed pumps by reducing the size of the rotor, etc., does not remove all vibrations. It is therefore recommended that valves be ins+alled with better regulating characteristics. (Z.M.). 6 figs., 1 tab., 3 refs

  19. A study of the annual doses to man from routine gaseous effluent releases of the Philippine Nuclear Power Plant Unit 1 (PNPP-1)

    International Nuclear Information System (INIS)

    Noriel, M.C.J.

    1983-01-01

    Individual and population integrated doses from radioactive gaseous releases of the Philippine Nuclear Power Plant 1 (PNPP-1) were calculated using a modified GASPAR Code. Input data consisted of meteorological and site data gathered from the PNPP-1 Final Analysis Report (FASR) population and agricultural data from the National Economic and Development Authority (NEDA) and the National Census and Statistics Office (NCSO). Usage factors were calculated based on Food and Nutrition Research Institute (FNRI) recommended dietary allowances for Filipinos. Results of population integrated dose calculations were used in identifying the critical nuclides, the critical body organs, and the critical pathway. Results from individual dose calculation were used in determining compliance with the dose limits set forth in Appendix D of Part 7 Code of Philippine Atomic Energy Commission (PAEC) regulations. (Author). 23 tabs.; 5 figs

  20. Internal event analysis of Laguna Verde Unit 1 Nuclear Power Plant. System Analysis; Analisis de Eventos Internos para la Unidad 1 de la Central Nucleoelectrica de Laguna Verde. Analisis de sistemas

    Energy Technology Data Exchange (ETDEWEB)

    Huerta B, A; Aguilar T, O; Nunez C, A; Lopez M, R [Comision Nacional de Seguridad Nuclear y Salvaguardias, 03000 Mexico D.F. (Mexico)

    1993-07-01

    The Level 1 results of Laguna Verde Nuclear Power Plant PRA are presented in the {sup I}nternal Event Analysis of Laguna Verde Unit 1 Nuclear Power Plant{sup ,} CNSNS-TR-004, in five volumes. The reports are organized as follows: CNSNS-TR-004 Volume 1: Introduction and Methodology. CNSNS-TR-004 Volume 2: Initiating Event and Accident Sequences. CNSNS-TR-004 Volume 3: System Analysis. CNSNS-TR-004 Volume 4: Accident Sequence Quantification and Results. CNSNS-TR-004 Volume 5: Appendices A, B and C. This volume presents the results of the system analysis for the Laguna Verde Unit 1 Nuclear Power Plant. The system analysis involved the development of logical models for all the systems included in the accident sequence event tree headings, and for all the support systems required to operate the front line systems. For the Internal Event analysis for Laguna Verde, 16 front line systems and 5 support systems were included. Detailed fault trees were developed for most of the important systems. Simplified fault trees focusing on major faults were constructed for those systems that can be adequately represent,ed using this kind of modeling. For those systems where fault tree models were not constructed, actual data were used to represent the dominant failures of the systems. The main failures included in the fault trees are hardware failures, test and maintenance unavailabilities, common cause failures, and human errors. The SETS and TEMAC codes were used to perform the qualitative and quantitative fault tree analyses. (Author)

  1. Safety Evaluation Report related to the restart of Rancho Seco Nuclear Generating Station, Unit 1, following the event of December 26, 1985 (Docket No. 50-312)

    International Nuclear Information System (INIS)

    1987-10-01

    On December 26, 1985, the Rancho Seco Nuclear Generating Station, owned and operated by the Sacramento Municipal Utility District (SMUD), experienced a loss of dc power within the integrated control system (ICS) while the plant was at 76% power. The ensuing reactor trip was followed by a rapid overcooling transient and automatic initiation of the safety features actuation system (SFAS). The overcooling transient continued until ICS dc power was restored 26 minutes after its loss. Two letters from the NRC Region V Administrator (dated December 26, 1985) confirmed that the Rancho Seco plant would not be returned to power operation until SMUD (the licensee) had provided the NRC with an assessment of the root cause of the transient and a justification as to why the Rancho Seco facility is ready to resume power operation. In response, the licensee submitted the ''Rancho Seco Action Plan for Performance Improvement'' on July 3, 1986; revisions to that action plan were submitted on December 15, 1986 and February 28, 1987. The NRC staff has reviewed the action plan and numerous other supporting documents submitted by the licensee. The staff's evaluation of the information supporting restart of Rancho Seco is presented in this safety evaluation report

  2. Results and insights of internal fire and internal flood analyses of the Surry Unit 1 Nuclear Power Plant during mid-loop operations

    International Nuclear Information System (INIS)

    Chu, Tsong-Lun; Musicki, Z.; Kohut, P.

    1995-01-01

    During 1989, the Nuclear Regulatory Commission (NRC) initiated an extensive program to carefully examine the potential risks during low power and shutdown operations. Two plants, Surry (pressurized water reactor) and Grand Gulf (boiling water reactor), were selected as the plants to be studied by Brookhaven National Laboratory (BNL) and Sandia National Laboratories (SNL). The objectives of the program are to assess the risks of severe accidents initiated during plant operational states (POSs) other than full power operation and to compare the estimated core damage frequencies (CDFs), important accident sequences and other qualitative and quantitative results with those accidents initiated during full power operation as assessed in NUREG-1150. The scope of the program includes that of a Level 3 PRA for internal events and a Level 1 PRA for seismically induced and internal fire and flood induced core damage sequences. This paper summarizes the results and highlights of the internal fire and flood analysis documented in Volumes 3 and 4 of NUREG/CR-6144 performed for the Surry plant during mid-loop operation

  3. Final environmental statement related to the operation of Catawba Nuclear Station, Units 1 and 2. Docket Nos. 50-413 and 50-414, Duke Power Company, et al

    International Nuclear Information System (INIS)

    1983-01-01

    This Final Environmental Statement contains the second assessment of the environmental impact associated with the operation of the Catawba Nuclear Station, Units 1 and 2, pursuant to the National Environmental Policy Act of 1969 (NEPA) and 10 CFR 51, as amended, of the NRC regulations. This statement examines: the affected environment, environmental consequences and mitigating actions, and environmental and economic benefits and costs. Land use and terrestrial and aquatic-ecological impacts will be small. Operational impacts to historic and archeological sites will be negligible. The effects of routine operations, energy transmission, and periodic maintenance of rights-of-way and transmission facilities should not jeopardize any populations of endangered or threatened species. No significant impacts are anticipated from normal operational releases of radioactivity. The risk associated with accidental radiation exposure is very low. The net socioeconomic effects of the project will be beneficial

  4. Safety evaluation report related to the operation of Watts Bar Nuclear Plant, Units 1 and 2, Docket Nos. 50-390 and 50-391, Tennessee Valley Authority. Supplement number 20

    International Nuclear Information System (INIS)

    1996-02-01

    This report supplements the Safety Evaluation Report (SER), NUREG-0847 (June 1982), Supplement No. 1 (September 1982), Supplement No. 2 (January 1984), Supplement No. 3 (January 1985), Supplement No. 4 (March 1985), Supplement No. 5 (November 1990), Supplement No. 6 (April 1991), Supplement No. 7 (September 1991), Supplement No. 8 (January 1992), Supplement No. 9 (June 1992), Supplement No. 10 (October 1992), Supplement No. 11 (April 1993), Supplement No. 12 (October 1993), Supplement No. 13 (April 1994), Supplement No. 14 (December 1994), Supplement No. 15 (June 1995), Supplement No. 16 (September 1995), Supplement No. 17 (October 1995), Supplement No. 18 (October 1995), and Supplement No. 19 (November 1995) issued by the Office of Nuclear Reactor Regulation of the US Nuclear Regulatory Commission with respect to the application filed by the Tennessee Valley Authority, as applicant and owner, for licenses to operate the Watts Bar Nuclear Plant, Units 1 and 2 (Docket Nos. 50-390 and 50-391). The facility is located in Rhea County, Tennessee, near the Watts Bar Dam on the Tennessee River. This supplement provides recent information regarding resolution of some of the issues identified in the SER

  5. Relaxation of inservice test frequency requirement for Kori 1 ASME code pumps

    International Nuclear Information System (INIS)

    Sohn, Gap Heon; Choi, Hae Yoon; Min, Kyung Sung; Rim, Nam Jin

    1994-08-01

    The objective of this investigation is to evaluate the technical and regulational requirements to justify the relaxation of the test frequency of Kori 1 pumps through reviewing the related rules and codes and standards, technical specifications of Kori 1 and other similar plants, standard technical specifications, research results for tech. spec. improvements and site test records. It is concluded that the relaxation of test frequency to quarterly be justified based on the conformance with rules and codes and standard, quarterly test cases in similar plants and standard tech. spec., recommendations of research result and stable site test records. (Author) 16 refs., 26 figs., 13 tabs

  6. Internal event analysis for Laguna Verde Unit 1 Nuclear Power Plant. Accident sequence quantification and results; Analisis de eventos internos para la Unidad 1 de la Central Nucleoelectrica de Laguna Verde. Cuantificacion de secuencias de accidente y resultados

    Energy Technology Data Exchange (ETDEWEB)

    Huerta B, A; Aguilar T, O; Nunez C, A; Lopez M, R [Comision Nacional de Seguridad Nuclear y Salvaguardias, 03000 Mexico D.F. (Mexico)

    1994-07-01

    The Level 1 results of Laguna Verde Nuclear Power Plant PRA are presented in the {sup I}nternal Event Analysis for Laguna Verde Unit 1 Nuclear Power Plant, CNSNS-TR 004, in five volumes. The reports are organized as follows: CNSNS-TR 004 Volume 1: Introduction and Methodology. CNSNS-TR4 Volume 2: Initiating Event and Accident Sequences. CNSNS-TR 004 Volume 3: System Analysis. CNSNS-TR 004 Volume 4: Accident Sequence Quantification and Results. CNSNS-TR 005 Volume 5: Appendices A, B and C. This volume presents the development of the dependent failure analysis, the treatment of the support system dependencies, the identification of the shared-components dependencies, and the treatment of the common cause failure. It is also presented the identification of the main human actions considered along with the possible recovery actions included. The development of the data base and the assumptions and limitations in the data base are also described in this volume. The accident sequences quantification process and the resolution of the core vulnerable sequences are presented. In this volume, the source and treatment of uncertainties associated with failure rates, component unavailabilities, initiating event frequencies, and human error probabilities are also presented. Finally, the main results and conclusions for the Internal Event Analysis for Laguna Verde Nuclear Power Plant are presented. The total core damage frequency calculated is 9.03x 10-5 per year for internal events. The most dominant accident sequences found are the transients involving the loss of offsite power, the station blackout accidents, and the anticipated transients without SCRAM (ATWS). (Author)

  7. Upgrade of KNPEC no.2 Simulator for Kori Unit 3 Power Uprating

    Energy Technology Data Exchange (ETDEWEB)

    Hong, Jin-Hyuk; Lee, Seung-Ho [KEPRI, Daejeon (Korea, Republic of)

    2007-07-01

    Kori-Unit 3 and 4 is preparing the operation of the power-uprating (2900MWt), and therefore the Korea regulatory body(KINS) requested the operator training with the simulator reflecting the power-uprating. As a result of the intensive research and expertise of KEPRI on the simulators, KEPRI accomplished the upgrade project of KNPEC no.2 simulator for Kori-Unit 3 power-uprating. This project includes various high-tech methods incorporating - realtime neutronics model based on MASTER (Multi-purpose Analyzer for Static and Transient Effects of Reactors) code, best-estimate neutronics code by the KINS, (By using the RMASTER, the precision of the simulation of the neutron behaviors in the core is highly improved.) - betterment of the reactor coolant system and the balance-of-plant system - modification of the corresponding setpoints due to the power-uprating And the acceptance test procedure (ATP) was successfully carried out through the integration of system models and its performance tests. Through the success of this project, the operator training for the power uprating of the Kori-Unit 3 will be accomplished before its power operation and, after all, this simulator will contribute to the safe operation for the power-uprating of the Kori-Unit 3 and 4.

  8. Development of Severe Accident Management Strategies for Shin-Kori 3 and 4

    International Nuclear Information System (INIS)

    Lee, Youngseung; Kim, Hyeongtaek; Shin, Jungmin

    2013-01-01

    Shin-Kori units 3 and 4 are new reactors under construction as an APR 1400 type reactor. The plants which considered coping with severe accident from design phase are different from other operating plants in view of severe accident management strategies. The purpose of this paper is to establish optimal strategies for Shin-Kori 3 and 4. A scheme for optimized severe accident management was drawn up with the object of achieving core cooling, containment integrity, and decreased release of fission product. Shin-Kori units 3 and 4 are a new reactor and designed to add mitigating systems for coping with severe accident such as ECSBS, PAR, and CFS. Also the plants are reflected as a part of Fukushima followup measures The strategies of SAMG for Shin-Kori 3 and 4 were developed. The strategic approach was based on the concept of defense in depth. Firstly, strategies for core cooling were chosen such as RCS depressurization, injection to SG, injection to RCS, and injection to reactor cavity. Secondly, the plans for containment integrity were developed for controlling pressure and hydrogen in containment. Lastly, reduced release of fission product was considered for protection of the public after containment failure. The achieved strategies meet the needs of effective methods for severe accident management and enhancement of safety

  9. Final supplement to the final environmental statement related to construction of Palo Verde Nuclear Generating Station Units 1, 2 and 3 (Docket Nos. STN 50-528, STN 50-529, and STN 50-530)

    International Nuclear Information System (INIS)

    1976-02-01

    The proposed action is the issuance of construction permits to the Arizona Public Service Company for the construction of the Palo Verde Nuclear Generating Station, Units 1, 2, and 3. Preparation of the 3800-acre site will involve the clearing of up to 2500 acres of land, 1500 of which will ultimately be developed during the lifetime of the station. About 2200 site acres, previously devoted to agriculture, will be excluded from this land use. Soil disturbance during construction of the station, transmission lines, and water conveyance pipeline will tend to promote erosion and increase siltation local ephemeral water courses. Stringent measures will be taken to minimize these effects (Sec. 4.5). Station, transmission line, and water pipeline construction will kill, remove, displace, or otherwise disturb involved flora and fauna, and will eliminate varying amounts of wildlife breeding, nesting, and forage habitat. These will not be important permanent impacts to the population stability and structure of the involved local ecosystems of the Sonoran desert; however, measures will be taken to minimize such effects as do results from the proposed action. 26 refs., 1 fig., 20 tabs

  10. Palo Verde Nuclear Generating Station, Units 1, 2 and 3 (Docket Nos. STN 50-528, STN 50-529 and STN 50-530): Draft supplement to the Final environmental satement

    International Nuclear Information System (INIS)

    1975-11-01

    The proposed action is the issuance of construction permits to the Arizona Public Service Company for the construction of the Palo Verde Nuclear Generating Station, Units 1, 2, and 3. Preparation of the 3800-acre site will involve the clearing of up to 2500 acres of land, 1500 of which will be permanently devoted to station facilities. An additional 1200- to 1300-acre evaporation pond will ultimately be developed during the lifetime of the station. About 2200 site acres, previously devoted to agriculture, will be excluded from this land use. Soil disturbance during construction of the station, transmission lines, and water conveyance pipeline will tend to promote erosion and increase siltation in local ephemeral water courses. Stringent measures will be taken to minimize these effects. Station, transmission line, and water pipeline construction will kill, remove, displace, or otherwise disturb involved flora and fauna, and will eliminate varying amounts of wildlife breeding, nesting, and forage habitat. These will not be important permanent impacts to the population stability and structure of the involved local ecosystems of the Sonoran desert; however, measures will be taken to minimize such effects as do result from the proposed action. The pumping of groundwater will cause a local drawdown of about 1 ft/yr, less than that currently occurring; hence, the impact is considered acceptable. 1 fig., 20 tabs

  11. Report on the Fourth Reactor Refueling. Laguna Verde Nuclear Central. Unit 1. April-May 1995; Informe de la Cuarta Recarga de Combustible. Central Laguna Verde. Unidad 1. Abril-Mayo 1995

    Energy Technology Data Exchange (ETDEWEB)

    Mendoza L, A; Flores C, E; Lopez G, C P.F.

    1996-12-31

    The fourth refueling of the Unit 1 of Laguna Verde Nuclear Central was executed in the period of April 17 to May 31 of 1995 with the participation of a task group of 358 persons, included technicians and radiation protection officials and auxiliaries.The radiation monitoring and radiological surveillance to the workers was present length ways the refueling process and always attached to the ALARA criteria. The check points for radiation levels were set at: primary container or dry well, reloading floor, decontamination room (level 10.5), turbine building and radioactive waste building. To take advantage of the refueling process, rooms 203 and 213 of the turbine buildings were subject to inspection and maintenance work in valves, heaters and drains of heaters. Management aspects as personnel selection and training, costs, and countable are also presented in this report. Owing to the high cost of man-hour of the members of the ININ staff, its participation in the refueling process was in smaller number than years before. (Author).

  12. IAEA International Peer Review Mission on Mid-and-Long-Term Roadmap Towards the Decommissioning of TEPCO's Fukushima Daiichi Nuclear Power Station Units 1-4, Tokyo and Fukushima Prefecture, Japan, 15-22 April 2013. Mission Report

    International Nuclear Information System (INIS)

    2013-01-01

    Following the accident at TEPCO's Fukushima Daiichi Nuclear Power Station (NPS) on 11 March 2011, the ''Mid-and-Long-Term Roadmap towards the Decommissioning of TEPCO's Fukushima Daiichi Nuclear Power Station Units 1-4'' was adopted by the Government of Japan and TEPCO Council on Mid-to-Long-Term Response for Decommissioning in December 2011 and revised in July 2012. The Roadmap, which is scheduled for an additional update in June 2013, describes the main steps and activities to be implemented for the decommissioning of the Fukushima Daiichi NPS through the combined efforts of the Government of Japan and TEPCO. Within the framework of the IAEA Action Plan on Nuclear Safety, the Government of Japan invited the IAEA to conduct an independent peer review of the Roadmap with two main objectives: - To improve the decommissioning planning and the implementation of pre-decommissioning activities at TEPCO's Fukushima Daiichi NPS; and - To share with the international community the good practices and lessons learned by the review. The review has been organized in two steps, and the IAEA conducted the first part in Japan from 15 to 22 April 2013. The objective of the first mission was to undertake an initial review of the Roadmap, including assessments of decommissioning strategy, planning and timing of decommissioning phases and a review of several specific short-term issues and recent challenges. Specifically, it covered the assessment of current reactor conditions, assessment of management of radioactive releases and associated doses, control of radioactive exposure of employees and decontamination within the site for improvement of working environment, structural integrity of reactor buildings and other constructions. The incidents recently experienced at the site, related with failures of the power supply and leakages of water from the underground reservoirs, were also included in the review of the specific short-term issues. The Government of Japan and TEPCO have

  13. Feasibility study of passive gamma spectrometry of molten core material from Fukushima Daiichi Nuclear Power Station unit 1, 2, and 3 cores for special nuclear material accountancy - low-volatile FP and special nuclear material inventory analysis and fundamental characteristics of gamma-rays from fuel debris

    International Nuclear Information System (INIS)

    Sagara, Hiroshi; Tomikawa, Hirofumi; Watahiki, Masaru; Kuno, Yusuke

    2014-01-01

    The technologies applied to the analysis of the Three Mile Island accident were examined in a feasibility study of gamma spectrometry of molten core material from the Fukushima Daiichi Nuclear Power Station unit 1, 2, and 3 cores for special nuclear material accountancy. The focus is on low-volatile fission products and heavy metal inventory analysis, and the fundamental characteristics of gamma-rays from fuel debris with respect to passive measurements. The inventory ratios of the low-volatile lanthanides, "1"5"4Eu and "1"4"4Ce, to special nuclear materials were evaluated by the entire core inventories in units 1, 2, and 3 with an estimated uncertainty of 9%-13% at the 1σ level for homogenized molten fuel material. The uncertainty is expected to be larger locally owing to the use of the irradiation cycle averaging approach. The ratios were also evaluated as a function of burnup for specific fuel debris with an estimated uncertainty of 13%-25% at the 1σ level for units 1 and 2, and most of the fuels in unit 3, although the uncertainty regarding the separated mixed oxide fuel in unit 3 would be significantly higher owing to the burnup dependence approach. Source photon spectra were also examined and cooling-time-dependent data sets were prepared. The fundamental characteristics of high-energy gamma-rays from fuel debris were investigated by a bare-sphere model transport calculation. Mass attenuation coefficients of fuel debris were evaluated to be insensitive to its possible composition in a high-energy region. The leakage photon ratio was evaluated using a variety of parameters, and a significant impact was confirmed for a certain size of fuel debris. Its correlation was summarized with respect to the leakage photopeak ratio of source "1"5"4Eu. Finally, a preliminary study using a hypothetical canister model of fuel debris based on the experience at Three Mile Island was presented, and future plans were introduced. (author)

  14. Final environmental statement related to construction of Cherokee Nuclear Station, Units 1, 2, and 3: (Docket Nos. STN 50-491, STN 50-492, and STN 50-493)

    International Nuclear Information System (INIS)

    1975-10-01

    The proposed action is the issuance of a construction permit to the Duke Power Company for the construction of the Cherokee Nuclear Station (CNS) Units 1, 2, and 3 located in Cherokee County, South Carolina. A total of 2263 acres will be removed from public use for the CNS site. Construction-related activities on the site will disturb about 751 acres. Approximately 654 acres of land will be required for transmission line right-of-way, and a railroad spur will affect 83 acres. This constitutes a minor regional impact. No significant environmental impacts are anticipated from normal operational releases of radioactive materials. The total annual dose to the US population (total body plus thyroid) from operation of the plant is 210 man-rems which is less than the normal fluctuations in the background dose this population would receive. The occupational dose is approximately 1400 man-rems/year. The heat dissipation system will require a maximum water makeup of 55,814 gpm, of which 50,514 gpm will be consumed due to drift and evaporative losses. This amount represents 4.5% of the mean monthly flow and 23.8% of the low flow of the Broad River. The cooling tower blowdown and chemical effluents from the station will increase the dissolved solids concentration in the river by a maximum of 44 ppM. The thermal alterations and increases in total dissolved solids concentration will not significantly affect the aquatic productivity of the river. 114 refs., 25 figs., 46 tabs

  15. Analysis of internal events for the Unit 1 of the Laguna Verde nuclear power station; Analisis de eventos internos para la Unidad 1 de la Central Nucleolelectrica de Laguna Verde

    Energy Technology Data Exchange (ETDEWEB)

    Huerta B, A.; Aguilar T, O.; Nunez C, A.; Lopez M, R. [Comision Nacional de Seguridad Nuclear y Salvaguardias, 03000 Mexico D.F. (Mexico)

    1993-07-01

    This volume presents the results of the starter event analysis and the event tree analysis for the Unit 1 of the Laguna Verde nuclear power station. The starter event analysis includes the identification of all those internal events which cause a disturbance to the normal operation of the power station and require mitigation. Those called external events stay beyond the reach of this study. For the analysis of the Laguna Verde power station eight transient categories were identified, three categories of loss of coolant accidents (LOCA) inside the container, a LOCA out of the primary container, as well as the vessel break. The event trees analysis involves the development of the possible accident sequences for each category of starter events. Events trees by systems for the different types of LOCA and for all the transients were constructed. It was constructed the event tree for the total loss of alternating current, which represents an extension of the event tree for the loss of external power transient. Also the event tree by systems for the anticipated transients without scram was developed (ATWS). The events trees for the accident sequences includes the sequences evaluation with vulnerable nucleus, that is to say those sequences in which it is had an adequate cooling of nucleus but the remoting systems of residual heat had failed. In order to model adequately the previous, headings were added to the event tree for developing the sequences until the point where be solved the nucleus state. This process includes: the determination of the failure pressure of the primary container, the evaluation of the environment generated in the reactor building as result of the container failure or cracked of itself, the determination of the localization of the components in the reactor building and the construction of boolean expressions to estimate the failure of the subordinated components to an severe environment. (Author)

  16. Final supplement to the final environmental statement related to construction of Skagit Nuclear Power Project, Units 1 and 2: (Docket Nos. STN 50-522 and STN 50-523)

    International Nuclear Information System (INIS)

    1977-04-01

    The proposed action is the issuance of construction permits to the Puget Sound Power and Light Company, Pacific Power and Light Company, Washington Water Power Company and the Portland General Electric Company, for the construction of Skagit Nuclear Power Projects Units 1 and 2 in Skagit County, Washington (about 64 miles north of Seattle and 6 miles ENE of Sedro Woolley). These units are scheduled for commercial service in 1984 and 1986, respectively. The exhaust steam from the turbine-generators will be cooled in condensers which will utilize one hyperbolic-type natural-draft cooling tower per unit to dissipate heat to the atmosphere. Water (106 cfs max.) for the cooling tower makeup (82.4 cfs) and other plant uses will be withdrawn from the Skagit River through Ranney Collectors embedded in the north bank of the river and pumped to the plant through a pipeline about 35,000 ft. long. Cooling tower blowdown (7 cfs max.) from the project and dilution water (20 cfs max.) will flow through a pipeline back to the river where it will be discharged through a diffuser. Approximately 1750 acres of forested and agricultural land will be removed from harvesting for the life of the power plant; 360 acres of this land will be diverted to industrial use. This will affect less than 0.5% of standing forest in Skagit County and 16 acres in cultivated crops and pasturage. Increased siltation of onsite creeks and the Skagit River from construction work and the small amounts of heat and chemicals discharged to the river during plant operation will have insignificant impacts on water quality and aquatic biota due to erosion control efforts and dilution by the large river flow. (16,200 cfs average; 4740 cfs 7-day, 10-yr low). 18 figs

  17. Status of Korean nuclear industry and Romania-Korea cooperation in nuclear field

    International Nuclear Information System (INIS)

    Myung-Key, Lee

    2005-01-01

    Current status of electric power in Korea is characterized by the end of August 2004 by a total installed capacity of about 62,000 MW while the total electricity generation is about 342,000 GWh. The installed capacity of nuclear power is 17,716 MW, sharing 29% of total installed capacity and presenting 38% of total electricity generation in Korea. In accordance with the provisions of the Long Term Energy Plan during the past 40 years, the installed capacity in Korea has been drastically increased. In the 1960's, major sources of electricity generation were locally-mined anthracite coal and hydro, but in the 1970's it was the imported oil. However, through diversification policy the dependence of the imported oil has been rapidly reduced and the share of coal , gas and nuclear generation has been steadily increased. According to the long-term power development plan updated last year, which is extended to 2017, the installed capacity in the year 2017 will be about 88,000 MW. At that time nuclear power will become the largest, sharing 30% and the shares of coal and gas fired power will be steadily decreased. Concerning the Nuclear Power Projects, there are four different nuclear power sites along the coast of Korean peninsula, Yonggwang, Kori, Wolsong and Ulchin. In addition to the currently operating 20 nuclear power plants, there are 6 more nuclear power plants under construction at Shin-Wolsong and Shin-Kori sites. Our efforts to enhance the technology, economy and safety of the nuclear power plants will be continuously pursued. Wolsong unclear power units 1, 2, 3 and 4 are CANDU type reactors which are same type as Romanian Cernavoda nuclear power plants. Operational performance, in terms of capacity factor of NPPs, has remained well above the world average and recorded 91.4% last year. Also, last year, the frequency of unplanned trip was 0.6 time per reactor. In 2004, ten NPPs achieved OCTF, which stands for One Cycle Trouble Free in 2004. Wolsong unit 1

  18. Calculation of risk-based detection limits for radionuclides in the liquid effluents from Korean nuclear power plants

    International Nuclear Information System (INIS)

    Cheong, Jae Hak

    2017-01-01

    In order to review if present detection limits of radionuclides in liquid effluent from nuclear power plants are effective enough to warrant compliance with regulatory discharge limits, a risk-based approach is developed to derive a new detection limit for each radionuclide based on radiological criteria. Equations and adjustment factors are also proposed to discriminate the validity of the detection limits for multiple radionuclides in the liquid effluent with or without consideration of the nuclide composition. From case studies to three nuclear power plants in Korea with actual operation data from 2006 to 2015, the present detection limits have turned out to be effective for Hanul Unit 1 but may not be sensitive enough for Kori Unit 1 (8 out of 14 radionuclides) and Wolsong Unit 1 (9 out of 42 radionuclides). However, it is shown that the present detection limits for the latter two nuclear power plants can be justified, if credit is given to the radionuclide composition. Otherwise, consideration should be given to adjustment of the present detection limits. The risk-based approach of this study can be used to determine the validity of established detection limits of a specific nuclear power plant. (author)

  19. ALARA review of the maintenance and repair jobs of repetitive high radiation dose at Kori Unit 3 and 4

    International Nuclear Information System (INIS)

    Cho, Y.H.; Moon, J.H.; Kang, C.S.; Lee, J.S.; Lee, D.H.

    2003-01-01

    The policy of maintaining occupational radiation dose (ORD) as low as reasonably achievable (ALARA) requires the effective reduction of ORD in the phases of design as well as operation of nuclear power plants. It has been identified that a predominant portion of ORD arises during maintenance and repair operations at nuclear power plants. The cost-effective reduction of ORD cannot be achieved without a comprehensive analysis of accumulated ORD data of existing nuclear power plants. To identify the jobs of repetitive high ORD, the ORD data of Kori Units 3 and 4 over 10-year period from 1986 to 1995 were compiled into the PC-based ORD database program. As the radiation job classification structure, 26 main jobs are considered, most of which are further subdivided into detailed jobs. According to the order of the collective dose values for 26 main jobs, 10 jobs of high collective dose are identified. As an ALARA review, then, top 10 jobs of high collective dose are statistically analyzed with regard to 1) dose rate, 2) crew number and 3) job frequency that are the factors determining the collective dose for the radiation job of interest. Through the ALARA review, main reasons causing to high collective dose values are identified as follows. The high collective dose of RCP maintenance job is mainly due to the large crew number and the high job frequency. The characteristics of refueling job are similar to those of RCP maintenance job. However, the high collective doses of SG-related jobs such as S/G nozzle dam job, S/G man-way job and S/G tube maintenance job are mainly due to high radiation dose rate. (author)

  20. Chemical Decontamination at Browns Ferry Unit 1

    International Nuclear Information System (INIS)

    Hartwig, Ed; Reid, Richard

    2003-01-01

    In May, 2002, the Tennessee Valley Authority's (TVA) Board of Directors approved the recovery and restart of Unit 1 at Browns Ferry Nuclear Station. As an initial step in the site characterization and restart feasibility review, a majority of the primary reactor circuit was chemically decontaminated. Close cooperation between TVA and vendor personnel resulted in project completion ahead of schedule with outstanding results. The final average decontamination factors were excellent, and the final dose rates were very low, with contact readings on most points between one and three mRem/hr. In addition to allowing TVA to do a complete and thorough job of determining the feasibility of the Unit 1 restart, the decontamination effort will greatly reduce personnel exposure during plant recovery, both whole body exposure to gamma radiation and airborne exposure during pipe replacement efforts. The implementation of lessons learned from previous decontamination work performed at Browns Ferry, as well as decontamination efforts at other plants aided greatly in the success. Specific items of note are: (1) The initial leak check of the temporary decontamination system should include ancillary systems such as the spent resin system, as well as the main circulation loop. This could save time and dose exposure if leaks are discovered before the use of such systems is required. (2) Due to the quick turnaround time from the award of contract, a vendor representative was onsite early in the project to help with engineering efforts and procedures. This aided greatly in completing preparations for the decontamination. (3) The work was performed under a single maintenance activity. This resulted in great craft and plant support. (4) The constant coverage by the site's decontamination flush directors provided timely plant support and interface. (5) The FPC system isolation and back flushing to prevent residual chemicals from being left in the FPC system should have been addressed in more

  1. Safety Evaluation Report related to the operation of Palo Verde Nuclear Generating Station, Units 1, 2, and 3 (Docket Nos. STN 50-528, STN 50-529, and STN 50-530). Supplement No. 8

    International Nuclear Information System (INIS)

    1985-05-01

    Purpose of this supplement is to update the Safety Evaluation Report by providing an evaluation of additional information submitted by the applicant since Supplement No. 7 was issued and matters that the staff had under review when Supplement No. 7 was issued, specifically those issues which required resolution prior to plant operation of Unit 1 above 5% full power

  2. Study on the improvement of nuclear fuel cladding reliability

    International Nuclear Information System (INIS)

    Rheem, Karp Soon; Han, Jung Ho; Jeong, Yong Hwan; Lee, Deok Hyun

    1987-12-01

    In order to improve the nuclear fuel cladding reliability for high burn-up fuels, the corrosion resistance of laser beam surface treated and β-quenched zircaloys and the mechanical characteristics including fatigue, burst, and out-of-pile PCMI characteristics of heat treated zircaloys were investigated. In addition, the inadiation characteristics of Ko-Ri reactor fuel claddings was examined. It was found that the wasteside corrosion resistance of commercial zircaloys was improved remarkably by laser beam surface treatment. The out-of-pile transient cladding failures were investigated in terms of hoop stress versus time-to-failures by means of mandrel loading units at 25 deg C and 325 deg C. Fatigue characteristics of the β-quenched and as-received zircaloy cladding were investigated by using an internal oil pressurization method which can simulate the load-following operation cycle. The results were in good agreement with the existing data obtained by conventional methods for commercial zircaloys. Burst tests were performed with commercial and the β-quenched zircaloys in high pressure argon gas atmosphere as a function of burst temperature. The burst stress decreased linearly in the α phase region up to 600 deg C and hereafter the decrement of the burst stress decreased gradually with temperature in the β-phase region. For the first time, the burst characteristic of the irradiated zircaloy-4 cladding tubes released from Ko-Ri nuclear power unit 1 was investigated, and attempts were made to trace the cause of cladding failures by examining the failed structure and fret marks by debris. (Author)

  3. Svakodnevna militarizacija života: etički aspekti korištenja djece u ratu

    OpenAIRE

    Rupčić, Darija

    2017-01-01

    Namjera je rada ukazati na problematiku izmijenjene naravi ratovanja u posljednjih nekoliko desetljeća 20. i 21. stoljeća, s osobitim naglaskom na problem korištenja sve većeg broja djece ratnika. Osnovna je teza rada ta da je praksa korištenja i regrutiranja djece u oružanim sukobima diljem svijeta najmanje prepoznata i najviše zanemarena forma zlostavljanja djece u suvremenom društvu te da je ona manje stvar kulture i nepostojanja stave društva prema vrijednostima djeteta, a više stvar prag...

  4. Report of the ASSET (Assessment of Safety Significant Events Team) mission to the Cernavoda nuclear power plant in Romania 8-12 August 1994 Division of Nuclear Safety. Root cause analysis of a significant event that occurred during commissioning of unit 1

    International Nuclear Information System (INIS)

    1994-01-01

    The IAEA Assessment of Safety Significant Events Team (ASSET) report presents the results of the team's investigation of a significant event that occurred during commissioning of Unit 1 of Cernavoda nuclear power plant. The results, conclusions and suggestions presented herein reflect the views of the ASSET experts. They are provided for consideration by the responsible authorities in Romania. The ASSET team's views presented in this report are based on visits to the plant, on review of documentation made available by the operating organization and on discussions with utility personnel. The report is intended to enhance operational safety at Cernavoda by proposing improvements to the policy for the prevention of incidents at the plant. The report includes, as a usual practice, the official response of the Regulatory Body and Operating Organization to the ASSET recommendations. Figs

  5. Simulation of the turbine trip of Unit 1 of the Laguna Verde nuclear power plant using the code Simulate-3K; Simulacion del disparo de turbina de la Unidad 1 de la central nuclear Laguna Verde empleando el codigo Simulate-3K

    Energy Technology Data Exchange (ETDEWEB)

    Alegria A, A. [Comision Nacional de Seguridad Nuclear y Salvaguardias, Dr. Barragan 779, Col. Narvarte, 03020 Ciudad de Mexico (Mexico); Filio L, C. [IPN, Escuela Superior de Fisica y Matematicas, Av. IPN s/n, 07738 Ciudad de Mexico (Mexico); Ortiz V, J., E-mail: aalegria@cnsns.gob.mx [ININ, Carretera Mexico-Toluca s/n, 52750 Ocoyoacac, Estado de Mexico (Mexico)

    2017-09-15

    In order to compare the results obtained from the model developed in the Comision Nacional de Seguridad Nuclear y Salvaguardias (CNSNS) with the code Simulate-3K (S3K) with respect to those reported by the process computer of the Central (SIIP), the simulation of the turbine trip transient was carried out, caused by the firing of the main generator, the low differential pressure of oil of its seals and the automatic Scram of Unit 1 of the Laguna Verde nuclear power plant, at 87% of power nominal during the operation cycle 16. Since the reactor was brought to a safe stop due to Scram, was enough to simulate 20 seconds to observe the maximum increase in pressure with S3K. In this work, the following parameters are shown and compared: the neutron flux, the thermal power, the pressure in the dome, the flow at the entrance to the core, the steam flow that leaves the vessel and the minimal critical power ratio (MCPR). The neutron flux of the average power range monitors of the nuclear power plant was compared with the S3K detectors model. Finally, the MCPR was calculated with a different correlation to that of the fuel supplier and its deviation from its safety limit was determined. In conclusion, the results obtained show the current state of the model for the simulation of reactivity transients and the opportunity areas to consolidate this tool in support of the process of licensing refueling in the CNSNS. (Author)

  6. Cernavoda NPP Unit 1 - a plant of several generations

    International Nuclear Information System (INIS)

    Rotaru, I.; Metes, M.; Anghelescu, M.S.

    2000-01-01

    Cernavoda NPP Unit 1, the first nuclear power unit in Romania, has a long and tormented history. It represents a rather unique case in Eastern Europe. The project started well before 1989 (the construction phase lasted 17 years and generations were involved in its completion), but it is effectively based on western technology (Candu). Meanwhile, the national nuclear program underwent many changes, affecting the lives and careers of Romanian nuclear professionals. Finally, on December 2 nd 1996, the unit began its c ommercial operation , being operated at its nominal power rating of 706 MW e . It now provides a reliable source of electricity for Romanian economy, supplying to the national grid about 10% of the country's average annual demand. The paper reflects some aspects related to the shift of generations during the project's development, including the present stage. The operational performances achieved 'in service' by Cernavoda NPP Unit 1 up to the end of 1999 , are also presented. Reference to the electrical energy production, performance indicators, production costs, nuclear safety, radiation protection, radioactive wastes, nuclear fuel consumption and nuclear fuel performances are included. Comparisons are performed with similar indicators reported by other worldwide nuclear power plants, in order to assess our results. (authors)

  7. The licensing practice on nuclear power plants in Korea

    Energy Technology Data Exchange (ETDEWEB)

    Moon, S P

    1994-12-31

    The evolution of Korean regulatory system has tightly coupled with development ot Korean nuclear power program. The nuclear power plant licensing has become a major regulatory function of the government when the construction of the Kori NPP Unit 1 started in early 1970s. During this period, domestic laws and regulations applicable to the licensing of NPP were not yet fully developed. Therefore the vendor countries` laws and regulations were applied as mandatory requirement. Beginning in the early 19808, component approach was used and contracts were awarded separately for major components of the plants, thus enabling more domestic industries to participate in the projects. The two-step licensing system was incorporated into the law. In the third phase from 1987, major efforts have been concentrated on the maximum participation of local industries. The overriding priority for selecting suppliers was the condition of higher nuclear technology transfer to Korea. The Korea Institute of Nuclear Safety (KINS) was established in 1990 as an independent regulatory expert organization. 1 tab., 4 figs.

  8. The licensing practice on nuclear power plants in Korea

    International Nuclear Information System (INIS)

    Moon, S. P.

    1994-01-01

    The evolution of Korean regulatory system has tightly coupled with development ot Korean nuclear power program. The nuclear power plant licensing has become a major regulatory function of the government when the construction of the Kori NPP Unit 1 started in early 1970s. During this period, domestic laws and regulations applicable to the licensing of NPP were not yet fully developed. Therefore the vendor countries' laws and regulations were applied as mandatory requirement. Beginning in the early 19808, component approach was used and contracts were awarded separately for major components of the plants, thus enabling more domestic industries to participate in the projects. The two-step licensing system was incorporated into the law. In the third phase from 1987, major efforts have been concentrated on the maximum participation of local industries. The overriding priority for selecting suppliers was the condition of higher nuclear technology transfer to Korea. The Korea Institute of Nuclear Safety (KINS) was established in 1990 as an independent regulatory expert organization

  9. Determination of ABOS 1-3+ system components belonging to the scope of license application of Paks Nuclear Power Plant Unit 1 for extension of service life, designated for the review, and verification of completeness of the scope

    International Nuclear Information System (INIS)

    Biro, Agnes Janosine; Tanits, Katalin Baumann-ne; Gosi, Peter; Kovacs, Andras; Ratkai, Sandor

    2012-01-01

    It is one major requirement of licensing the extension of design service life to determine the systems, structures and components that belong to the scope of licensing. According to the domestic regulatory requirements the ABOS 1-3 safety class components, the non safety system components of seismic safety class 3 and those non safety class components whose failure would occur due to its unmanaged ageing process and which may jeopardize safety class components with the released medium shall be involved into the scope of licensing of service life extension (SLE). In the task the components for the scope of SLE licensing of Unit 1 was determined using and, if necessary, further developing the tools provided by and exploiting, verifying and, as appropriate, supplementing the data included in the central technical database (IMR/MDM) of the NPP. As basis for determination of the scope the systems, structures and individual components categorized into safety class in the Final Safety Report were taken. Digitalized mechanical technological schemes were also used in determining the components of the systems fulfilling safety functions and in verifying the completeness. In order to assign the components belonging to the fulfillment of the function of the systems and to review the scope, the digitalization of the ABOS 2-3 electric and the ABOS 2 I and C circuit diagrams and distributor single-line diagrams and the processing and analysis of the digitalized data was performed. The ABOS + scope components were verified by walkdown. The completed component lists were compared to the components of the SLE licensing scope of the IMR/MDM database and the necessary supplementation, correction of the IMR/MDM data was also performed. In order to identify the components requiring review during licensing, also the active/passive safety function fulfillment modes were determined for every component of the licensing scope for Unit 1, which is now regarded as complete. As the results of

  10. Present status of nuclear containments in Korea

    International Nuclear Information System (INIS)

    Park, Jihong; Hong, Jaekeun; Lee, Byunghoon; Son, Youngho

    2007-01-01

    Since the first nuclear power plant in Korea, Kori unit no.1, was started in commercial service in 1978, 20 units including Kori unit no.1 have been operated and maintained until now in Korea. Recently several units were started to be constructed and also, additionally more than 4 units were planned to be constructed in the near future. The importance of nuclear containments has been always one of the hottest issues for the safety and protection of nuclear power plants until now. At the beginning of nuclear power plants construction in Korea, several typed nuclear containment systems were adopted. For those reasons, various codes, standards, and inspection technologies are applied to nuclear containment systems differently. In this study, the status of inservice inspection performed for the safety and maintenance of nuclear containments in Korea was researched. Overall nuclear containment systems and inspections performed up to recently in Korea including trends, inspection items, periods, and regulations were described briefly. (author)

  11. Cernavoda NPP Unit 1 - a plant of several generations

    International Nuclear Information System (INIS)

    Rotaru, I.; Metes, M.; Anghelescu, M.S.

    2001-01-01

    The paper reflects some key aspects related to the shift of generations during the project's development, including the present stage. Further, the place of Cernavoda NPP Unit 1 in the Romanian power sector and among other nuclear stations in the world is presented. The operational performances achieved 'in service' up to the end of 1999, with reference to the performance indicators for electrical energy production, nuclear safety, radiation protection, radioactive wastes and nuclear fuel are illustrated. For all of these items, comparisons are performed with similar indicators reported by other worldwide nuclear power plants, in order to assess our results. Finally, some comments about Cernavoda NPP Unit 2 project status and need to completion and commissioning it are included. (authors)

  12. Technical evaluation of the electrical, instrumentation, and control design aspects of the proposed license amendment Revision 1 for single-loop operation of Browns Ferry Nuclear Plants (Docket No. 50-259, Unit 1; Docket No. 50-260, Unit 2; Docket No. 50-296, Unit 3)

    International Nuclear Information System (INIS)

    Donich, T.R.

    1983-01-01

    This report documents the technical evaluation of the proposed changes to the plant reactor protection system by the licensee of Browns Ferry Nuclear Power Station, Units 1, 2, and 3, to account for single-loop plant operation. This evaluation is restricted to only the electrical, instrumentation and control design aspects of proposed changes to the plant technical specifications for single-loop operation beyond 24 hours. Conclusion is that the license amendment for single-loop operation has met the review criteria provided sufficient administrative controls are in effect, and any anomalous control room indicators are corrected or warning-tagged for the duration of single-loop operation

  13. Analysis of inadvertent safety injection incident at Kori unit 3 on september 6, 1990

    International Nuclear Information System (INIS)

    Kim, Kyun Tae; Chung, Bub Dong; Kim, In Goo; Kim, Hho Jung

    1992-01-01

    The inadvertent safety injection incident occurred at Kori Unit 3 on September 6, 1990 is analyzed using RELAP5/MOD3 code. The event was initiated by a failure of main feedwater control valve in one of three steam generators. The actual sequence of plant transient with the proper estimations of the operator actions is investigated in the present calculation. The calculational results are compared with the plant transient data. It is shown that the results of the plant behaviors are in good agreement with the plant data. The emergency response guidelines is assessed for the time of the SI termination and the establishment of natural circulation. The changes in the time of the SI termination do not significantly affect the overall plant behaviors, and the natural circulation is established

  14. Metallurgical characteristics and fracture mechanical properties of unirradiated Kori-1 RPV weld: Linde 80, WF-233

    International Nuclear Information System (INIS)

    Hong, Jun Hwa; Lee, B. S.; Oh, Y. J.; Chi, S. H.; Kim, J. H.; Park, D. G.; Yoon, J. H.; Oh, J. M.

    2000-07-01

    The fracture toughness transition properties of the low upper shelf weld, Linde 80 WF-233, of Kori-1 RPV were evaluated by the master curve method, which is designated by ASTM E 1921, 'Standard test method for determination of reference temperature, T o , for ferritic steels in the transition range'. The reference temperature, T o =-83 deg C, was determined by PCVN specimens at -90 deg C. This value is similar to that of other high copper welds. The initial RT NDT was conservatively estimated as -26 deg F from the current fracture toughness results. From the studies on the chemistry and microstructure, the fracture mechanical properties of WF-233 weld is convincingly not worse than WF-70 and 72W welds

  15. Comparison of APR1400 safety between brake site and shin-Kori site Due to the difference in the climate conditions

    International Nuclear Information System (INIS)

    Yoon, Ho Joon; Lee, Jeong Ik; Lee, Jeong Ik

    2012-01-01

    Brake Nuclear Power Plant (BNPP) is now under the construction based on APR1400 designed by Korean Electric Power Corporation (KEPCO). APR1400 is a two loop pressurized water reactor, the nuclear steam supply system (NSSS) US designed for about put of 4,000 MWt, with a corresponding electrical output of approximately 1,390 MWe. The first APR1400 (SKN 3 and 4) constructed in Shin-Kori, Korea has been modified according to the surrounding environment of the United Arab Emirates. In this paper, authors would like to compare safety issues between B NPP and Skin due to the changes of surroundings, since the site characteristics are very different. For instance, the mean annual air temperature in the UAE is 28 .deg. C and the peak air temperature was recorded as 48.8 .deg. C. Sea temperatures are varying from 17. deg. C in January to 35. deg. C in August, while that of Korea is in 9-16. deg. C range. Hot climate of UAE and the malfunction of HVAC system can lead the increasing of the water temperature in safety injection system (SIS). The heated water in SIS may affect the safety margin of the peak cladding temperature (PCT). The change of PCT and response time according to design basis accident scenarios such as large break LOCA are analyzed in detail. To evaluate such effect, Mars code was utilized to evaluate assumed condition by KAIST and the analyses of the results were carried out by Khalifa Univ.

  16. Safety evaluation report related to the operation of Palo Verde nuclear generating station, Units 1, 2, and 3. Docket Nos. STN 50-528, STN 50-529, and STN 50-530, Arizona Public Service Company

    International Nuclear Information System (INIS)

    1982-05-01

    On November 13, 1981, the Nuclear Regulatory Commission (NRC) staff issued its Safety Evaluation Report (SER) relating to the application for licenses to operate the Palo Verde Nuclear Generating Station, Unit Nos. 1, 2 and 3 (PVNGS 1-3); Supplement No. 1 to the SER was issued on February 4, 1982. In the SER and Supplement No. 1, the staff identified certain issues where either further information was required of the applicant or additional staff effort was necessary to complete the review of the application. The purpose of this supplement is to update the SER by providing (1) the evaluation of additional information submitted by the applicant since Supplement No. 1 to the SER was issued, and (2) the evaluation of the matters that the staff had under review and Supplement No. 1 was issued

  17. The current status and future prospects of the Korean nuclear power industry

    International Nuclear Information System (INIS)

    Lee, J. J.

    2006-01-01

    Recently, countries all over the world are becoming aware of the values and importance of nuclear energy which can help respond to energy crises caused by a sharp rise in oil prices and protect the earth from global warming. Since 1978, when Kori Unit 1(587MW), opened the nuclear generation era as a semi-domestic energy resource in Korea which is absolutely in short supply of energy, nuclear power generation in Korea has developed continuously for the past 28 years. Four new units including the Yonggwang 5 and 6 and Ulchin 5 and 6 have been successfully completed, raising the total nuclear installed capacity to 17,716MW from 20 units. At present, the nuclear generation in Korea is stably supplying about 40% of total electric generation, which is the fundamental energy of the nation, supporting the dynamic economic growth of Korea. In particular, Korean nuclear industry has been achieving excellent performance in nuclear power plant operation. The average capacity factor in 2005 hit the record of 95.5%, surpassing the previous record of 94.2% in 2003 in two years. Kori Unit 4 and another four units were listed at the top five in the capacity factor rating list of 2005 released by Nucleonics Week. In 2005, the site for radioactive waste disposal, which had been a long-cherished hope and the largest pending issue of the nuclear industry, was successfully selected in Korea through resident ballot as the first case of a national policy project, and as such, a national agenda was solved after 19 long years. Such a method in site selection has a significant meaning and establishes an excellent precedence; a large national policy project was decided upon by the residents themselves. As one of the model countries of building and operating nuclear power plants and technological independence, Korea is willing to contribute to the common goals of the world nuclear circle which can be summarized into energy security and environment preservation, by sharing accumulated

  18. Evaluation of River Bend Station Unit 1 Technical Specifications

    International Nuclear Information System (INIS)

    Baxter, D.E.; Bruske, S.J.

    1985-08-01

    This document was prepared for the Nuclear Regulatory Commission (NRC) to assist them in determining whether the River Bend Station Unit 1 Technical Specifications (T/S), which govern plant systems configurations and operations, are in conformance with the requirements of the Final Safety Analysis Report (FSAR) as amended, and the requirements of the Safety Evaluation Report (SER) as supplemented. A comparative audit of the FSAR as amended, and the SER as supplemented was performed with the River Bend T/S. Several discrepancies were identified and subsequently resolved through discussions with the cognizant NRC reviewer, NRC staff reviewers and/or utility representatives. The River Bend Station Unit 1 T/S, to the extent reviewed, are in conformance with the FSAR and SER

  19. Final environmental statement related to the operation of Watts Bar Nuclear Plant, Units 1 and 2: Docket Numbers 50-390 and 50-391, Tennessee Valley Authority. Supplement Number 1

    International Nuclear Information System (INIS)

    1995-04-01

    The Final Environmental Statement-Operating License (FES-OL) issued in 1978 represents the Nuclear Regulatory Commission's (NRC's) previous environmental review related to the operation of Watts Bar Nuclear (WBN) Plant. The NRC staff has determined that it is appropriate to re-examine the issues associated with the environmental review before issuance of an operating license. The purpose of this NRC review is to discuss the effects of observed changes in the environment and to evaluate the changes in environmental impacts that have occurred as a result of changes in the WBN Plant design and proposed methods of operations since the last environmental review. A full scope of environmental topics has been evaluated, including regional demography, land and water use, meteorology, terrestrial and aquatic ecology, radiological and non-radiological impacts on humans and the environment, socioeconomic impacts, and environmental justice. The staff concluded that there are no significant changes in the environmental impacts since the NRC 1978 FES-OL from changes in plant design, proposed methods of operations, or changes in the environment. The Tennessee Valley Authority's (TVA's) preoperational and operational monitoring programs were reviewed and found to be appropriate for establishing baseline conditions and ongoing assessments of environmental impacts. The staff also conducted an analysis of plant operation with severe accident mitigation design alternatives (SAMDAs) and concluded that none of the SAMDAs, beyond the three procedural changes that the TVA committed to implement, would be cost-beneficial for further mitigating environmental impacts

  20. Trace of nuclear energy with pictures

    International Nuclear Information System (INIS)

    1992-05-01

    This book traces the history of development over nuclear energy with pictures, which contains preface, development history of the world, development history of Korea, nuclear power plant in Kori, nuclear power plant in Wolseong, nuclear power plant in Yeonggwang, nuclear power plant in Uljin, nuclear fuel, using of radiation and radioactive isotope, development of nuclear energy in the world and a Chronological table of nuclear energy. This book is written to record the development history of Korea through pictures of the nuclear power plants in Korea.

  1. Uslovi korišćenja plovnih dizalica za dizanje potonulih objekata na unutrašnjim plovnim putevima

    OpenAIRE

    Radojević M. Slobodan

    2012-01-01

    U radu se prikazuju uslovi korišćenja plovnih dizalica za dizanje potonulih plovnih i drugih objekata na unutrašnjim plovnim putevima. Prikazani su osnovni načini podizanja plovnim dizalicama i osnovni tehnički podaci sa proračunskim pojedinostima za predložen postupak dizanja. Ukazano je na značaj dizanja potonulih objekata i njihovog uklanjanja iz unutrašnjih plovnih puteva u Republici Srbiji.

  2. Sludge Lancing and Visual Inspection of Steam Generator for KORI Nuclear Power Plant Unit 3

    Energy Technology Data Exchange (ETDEWEB)

    Jeong, Woo-Tae [Korea Hydro and Nuclear Power Co. Ltd. Central Research Institute, Daejeon(Korea, Republic of); Kim, Sang-Tae; Hong, Jae-Yung; Jeong, Yun-Soon [Sae-An Engineering Corporation, Seoul (Korea, Republic of)

    2015-05-15

    Annulus, tube-lane, and in-bundle area of the steam generators were searched for possible foreign objects. No new foreign objects were found. Two foreign objects which were found during previous outage were impossible to remove. Mock-up training before the operation was helpful to finish the service as scheduled. Sludge lancing of the three steam generators was made using FOLAS-I lancing system. FOSAR operations were done using video probe and special tools of Sae-An Engineering Cooperation. The weight of sludge removed from SG 'A', 'B', and 'C' was 177kg, 134kg, 117kg respectively. Bag filters for and cartridge filters consumed for SG 'A', 'B', and 'C' was (53,414), (75,243), and (61,171) respectively. Foreign object search operation for the annulus, the tube lane, and in-bundle area of the steam generators found nothing. Retrieval of the two remaining foreign objects from the previous outage was tried but failed.

  3. Sludge Lancing and Visual Inspection of Steam Generator for KORI Nuclear Power Plant Unit 3

    International Nuclear Information System (INIS)

    Jeong, Woo-Tae; Kim, Sang-Tae; Hong, Jae-Yung; Jeong, Yun-Soon

    2015-01-01

    Annulus, tube-lane, and in-bundle area of the steam generators were searched for possible foreign objects. No new foreign objects were found. Two foreign objects which were found during previous outage were impossible to remove. Mock-up training before the operation was helpful to finish the service as scheduled. Sludge lancing of the three steam generators was made using FOLAS-I lancing system. FOSAR operations were done using video probe and special tools of Sae-An Engineering Cooperation. The weight of sludge removed from SG 'A', 'B', and 'C' was 177kg, 134kg, 117kg respectively. Bag filters for and cartridge filters consumed for SG 'A', 'B', and 'C' was (53,414), (75,243), and (61,171) respectively. Foreign object search operation for the annulus, the tube lane, and in-bundle area of the steam generators found nothing. Retrieval of the two remaining foreign objects from the previous outage was tried but failed

  4. Audit Technical of Kori Rubber Dam in the River of Keyang District of Ponorogo East Java Province

    Science.gov (United States)

    Murnianto, E.; Suprapto, M.; Ikhsan, C.

    2018-03-01

    The development of science and technology for the utilization and protection of rivers has embodied various types of river infrastructure. Without proper maintenance, rapid river sediments undergo physical degradation and function. Problems that occur in Kori Rubber Dam, among others, the damage to the body of the rubber dam that is made of rubber, so that the function of flower deflection is not optimal. This happens because of limited operational and maintenance activities (OM). A technical audit is a process of identifying problems, analyzing, and evaluating ones conducted independently, objectively and professionally on the basis of examination, to assess the truth, accuracy, credibility, and reliability of information about a job. In this case an assessment of the Kori Rubber Dam, which is basically a benchmarking activity. Assessment of rubber dam components includes the physical conditions and functions that affect the weir. This research is expected to know the performance of Kori rubber Dam as a recommendation material in the implementation of OM Rubber Dam activities.

  5. Closure simulation of the MSIV of Unit 1 of the Laguna Verde nuclear power plant using the Simulate 3K code; Simulacion del cierre de las MSIV de la Unidad 1 de la central nuclear Laguna Verde empleando el codigo Simulate-3K

    Energy Technology Data Exchange (ETDEWEB)

    Alegria A, A., E-mail: aalegria@cnsns.gob.mx [Comision Nacional de Seguridad Nuclear y Salvaguardias, Dr. Barragan 779, Col. Narvarte, 03020 Ciudad de Mexico (Mexico)

    2015-09-15

    In this paper the simulation of closure transient of all main steam isolation valves (MSIV) was performed with the Simulate-3K (S-3K) code for the Unit 1 of the Laguna Verde nuclear power plant (NPP-LV), which operates to thermal power of 2317 MWt, corresponding to the cycle 15 of operation. The set points for the performance of systems correspond to those set out in transient analysis: 3 seconds for the closure of all MSIV; the start of Scram when 121% of the neutron flux is reached, respect from baseline before the transient; the opening by peer of safety relief valves (SRV) in relief mode when the set point of the pressure is reached, the shoot of the feedwater flow seconds after the start of closing of the MSIV and the shoot of the recirculation water pumps when the pressure is reached in the dome of 1048 psig. The simulation time was of 57 seconds, with the top 50 to reach the steady state, from which the closure of all MSIV starts. In this paper the behavior of the pressure in the dome are analyzed, thermal power, neutron flux, the collapsed water level, the flow at the entrance of core, the steam flow coming out of vessel and the flow through of the SRV; the fuel temperature, the minimal critical power ratio, the readings in the instrumentation systems and reactivities. Instrumentation systems were implemented to analyze the neutron flux, these consist of 96 local power range monitors (LPRM) located in different radial and axial positions of the core and 4 channels of average power range monitors, which grouped at 24 LPRM each one. LPRM response to the change of neutron flux in the center of the core, at different axial positions is also shown. Finally, the results show that the safety limit MCPR is not exceeded. (Author)

  6. Preliminary study on the analysis of alpha emitters at working places in nuclear power plants

    Energy Technology Data Exchange (ETDEWEB)

    Kim, Hanna; Kim, Jeong In; Lee, Byoungil [Korea Hydro and Nuclear Power Co., Seoul (Korea, Republic of); Yoon, Suk Won [Korea Institute of Radiological and Medical Sciences National Radiation Emergency Medical Center, Seoul (Korea, Republic of)

    2012-10-15

    Over sea nuclear power plants have been reported cases of internal contamination by alpha nuclides. In many cases, stations encountered significant alpha contamination when aged/legacy equipment was disturbed or handled. Under normal operating conditions, transuranic radionuclides are contained within the fuel rods and therefore are not a contributor to radioactive contamination within a facility. However, transuranic radionuclides result from the presence of tramp-uranium contamination on the exterior of fuel elements. Fuel failures may develop during operating cycles due to a variety of causes, ranging from manufacturing defects to mechanical or abrasive damage. In case of domestic nuclear power plants, the pressure tube replacements in Wolsong Unit 1 and steam generator replacements in Kori Unit 1 were done. Due to deterioration of equipment in accordance with the long-term operation, the domestic nuclear power plants are expected to improve the facilities and the probability of internal exposure from alpha emitters is increasing. The domestic nuclear power plants are only keeping alpha radionuclides of the effluent from the exterior under constant surveillance. The representative areas of CV are just carried out continuous alpha monitoring in during a unit outage. So far, there is no other case with alpha nuclides analysis. As the domestic nuclear power plants are expected to improve the facilities, it is the time to take proactive measures to deal with internal contamination by alpha emitting radioactive elements. In this paper, the possible risk of internal exposure is based on preliminary experiments on the analysis of alpha emitting radioactive elements at working places in nuclear power plants.

  7. Present and future of Korean nuclear power

    International Nuclear Information System (INIS)

    Min, K-H

    2014-01-01

    'Full text:' The Korean nuclear power industry has devoted itself to technological development and self-reliance over the last 30 years since Kori unit 1, the first nuclear power plant commenced its commercial operation in 1978. As a result of such efforts and accumulated experiences, the Korean nuclear power industry has developed the OPR 1000 and APR 1400 units and is almost completing the development of the APR+ as a 1,500MW class reactor with its own technologies of design and manufacturing. Also, the Korean nuclear power industry has been able to build a strong supply chain from engineering, manufacturing, construction, and fuel supply, to operation and maintenance. At present, Korea is operating 23 commercial power reactors with a total installed capacity of 20,716 MW, accounting for 25 percent of the installed capacity and one third of the nation's total electricity generation. Also, the share of nuclear power generation capacity will be 29 percent by 2035 in the Long Term Energy Development Plan and 43 GW of nuclear energy capacity will be needed. Thanks to nuclear power generation as an essential driving force, Korea has been able to supply cheap and stable electricity. However, amid the growing public concerns about nuclear safety after the Fukushima accident, the Korean government and related organizations are exerting its utmost effort in all areas, for example, enhancing nuclear safety and safety culture, carrying out management innovation, and communicating with the public in order to enhance transparency. Also, the Korean government launched the Public Engagement Commission on spent nuclear fuel (SNF) management in 2013, which is tasked to initiate public consultation & discussion and submit recommendation to government after in-depth review and analysis on SNF management options by the end of 2014. Nuclear power has become very essential part of national economy in Korea because Korea has virtually no indigenous energy resources and

  8. Present and future of Korean nuclear power

    Energy Technology Data Exchange (ETDEWEB)

    Min, K-H [Korea Atomic Industrial Forum, Inc., Seoul (Korea, Republic of)

    2014-07-01

    'Full text:' The Korean nuclear power industry has devoted itself to technological development and self-reliance over the last 30 years since Kori unit 1, the first nuclear power plant commenced its commercial operation in 1978. As a result of such efforts and accumulated experiences, the Korean nuclear power industry has developed the OPR 1000 and APR 1400 units and is almost completing the development of the APR+ as a 1,500MW class reactor with its own technologies of design and manufacturing. Also, the Korean nuclear power industry has been able to build a strong supply chain from engineering, manufacturing, construction, and fuel supply, to operation and maintenance. At present, Korea is operating 23 commercial power reactors with a total installed capacity of 20,716 MW, accounting for 25 percent of the installed capacity and one third of the nation's total electricity generation. Also, the share of nuclear power generation capacity will be 29 percent by 2035 in the Long Term Energy Development Plan and 43 GW of nuclear energy capacity will be needed. Thanks to nuclear power generation as an essential driving force, Korea has been able to supply cheap and stable electricity. However, amid the growing public concerns about nuclear safety after the Fukushima accident, the Korean government and related organizations are exerting its utmost effort in all areas, for example, enhancing nuclear safety and safety culture, carrying out management innovation, and communicating with the public in order to enhance transparency. Also, the Korean government launched the Public Engagement Commission on spent nuclear fuel (SNF) management in 2013, which is tasked to initiate public consultation & discussion and submit recommendation to government after in-depth review and analysis on SNF management options by the end of 2014. Nuclear power has become very essential part of national economy in Korea because Korea has virtually no indigenous energy resources and

  9. A study on optimization of environmental qualification envelope for Kori 3 and 4 NPP

    International Nuclear Information System (INIS)

    Song, Dong Soo; Byun, Choong Sup; Jo, Jong Young

    2009-01-01

    The purpose of this study is to present the reevaluation of the Main Steam Line Break (MSLB) applied Boron Injection Tank (BIT) removal and to optimize the environmental qualification (EQ) temperature envelope with thermal lag analysis and liquid entrainment method. BIT alleviates the reactor power excursion during Main Steam Line Break (MSLB) accident. Thermal lag analysis methods by NUREG-0588 is using four times condensing heat transfer coefficient on the passive heat sink surface, the forced convection heat transfer coefficient whenever the condensing is not occurring and during blowdown stage. And the entrainment model is that the all of the break regions within the secondary side are represented by non-homogeneous vapor volumes in which the liquid and steam are uniformly mixed throughout. These methods are focused on making higher the surface temperature of the safety equipment. For the analysis, amount of released mass and energy is calculated using the LOFTRAN code and containment temperature is predicted by CONTEMPT-LT 28 code. These two codes are used to for safety analysis. In accordance with the analysis result, a plant specific EQ test envelope was proposed for Kori 3 and 4 NPP

  10. A study on optimization of environmental qualification envelope for Kori 3 and 4 NPP

    Energy Technology Data Exchange (ETDEWEB)

    Song, Dong Soo; Byun, Choong Sup; Jo, Jong Young [Korea Electric Power Research Institute, Daejeon (Korea, Republic of)

    2009-07-01

    The purpose of this study is to present the reevaluation of the Main Steam Line Break (MSLB) applied Boron Injection Tank (BIT) removal and to optimize the environmental qualification (EQ) temperature envelope with thermal lag analysis and liquid entrainment method. BIT alleviates the reactor power excursion during Main Steam Line Break (MSLB) accident. Thermal lag analysis methods by NUREG-0588 is using four times condensing heat transfer coefficient on the passive heat sink surface, the forced convection heat transfer coefficient whenever the condensing is not occurring and during blowdown stage. And the entrainment model is that the all of the break regions within the secondary side are represented by non-homogeneous vapor volumes in which the liquid and steam are uniformly mixed throughout. These methods are focused on making higher the surface temperature of the safety equipment. For the analysis, amount of released mass and energy is calculated using the LOFTRAN code and containment temperature is predicted by CONTEMPT-LT 28 code. These two codes are used to for safety analysis. In accordance with the analysis result, a plant specific EQ test envelope was proposed for Kori 3 and 4 NPP.

  11. Estimation of stature from different anthropometric measurements in Kori population of North India

    Directory of Open Access Journals (Sweden)

    Renu Kamal

    2016-12-01

    Full Text Available In medico-legal cases, most often the personal identity of the deceased is a mystery. The stature, sex and other parameters in such scenarios are ascertained using the physical evidence present at the crime scene. One of the key methods of ascertaining the sex and stature is by using the human bones. The method of achieving accuracy in estimation of stature from bones has been well established in past. There are several regression formulae for conducting such estimation. However, it must be kept in mind that these regression equations can vary depending upon the population and region. Thus, it is very necessary to study a particular population thoroughly before formulating regression equations for that specific population patch. In this paper, we have penned down the study of KORI POPULATION, who are native to Kanpur region of Uttar Pradesh state, in India. In this study, we have observed the statistics of 202 individuals (106 females and 96 males. In totality, eight bone dimensions including stature, total arm length, length of the middle finger, knee length, foot length, foot breadth, maximum head length and maximum head breadth have been recorded in this research paper. The regression formulae for females and males have been derived separately. Further, there are various parameters that have been compared to find which parameter provides the best results in terms of accuracy in stature estimation.

  12. Technical specifications: Seabrook Station, Unit 1 (Docket No. 50-443)

    International Nuclear Information System (INIS)

    1990-03-01

    The Seabrook Station, Unit 1 Technical Specifications were prepared by the US Nuclear Regulatory Commission to set forth the limits, operating conditions, and other requirements applicable to a nuclear reactor facility as set forth in Section 50.36 of 10 CFR Part 50 for the protection of the health and safety of the public

  13. Status of Korean nuclear industry and Romania-Korea cooperation in the field of nuclear power

    International Nuclear Information System (INIS)

    Lee, Myung Key

    2005-01-01

    The Kyoto Protocol on climate change has urged the world to explore ways of cutting down the greenhouse emissions, and it also boosted a number of nuclear power projects that is so-called the renaissance of nuclear power. Nuclear power has proven to be the cleanest energy source and one of the cheapest types of energies, compared with other energy sources. Korea began developing its nuclear power projects from the early 1970's. Since the first nuclear power plant Kori Unit 1, started commercial operation in 1978, Korea has continuously promoted the development of nuclear power projects, and today it operates 20 nuclear power units (17,716 MW), including 4 units of CANDU plants. Korea ranked No. 6 in the world in terms of installed capacity of nuclear power plants, and 40% of its domestic electricity generation comes from nuclear power plants. The average plant capacity factor was 95.5% in 2005, which is about 16% than the world average of around 79%. All the Korean nuclear power projects are led and implemented by Korea Hydro and Nuclear Power Co. (KHNP) which is the sole state-owned nuclear power project company spun off from Korea Electric Power Corporation (KEPCO) in 2001 as part of the government's program for electric industry restructuring. The cooperation between Romania and Korea in the nuclear power field began in March 2001. At industrial level a technical agreement between the Romanian Company Nuclearelectrica S.A. (SNN) and KHNP was signed in July 2003 for cooperation in Cernavoda NPP projects. The joint development of the Cernavoda NPP unit 3 was one of the major topics. Heavy water produced by Romanian Heavy Water plant at Drobeta Turnu Severin was supplied to KHNP (16 tones in 2001 and another 16 tones in 2004). The feasibility study for units 3 and 4 is being performed in two phases under leadership of SNN in cooperation with KHNP, AECL, ANSALDO and Deloitte and Touche as a financial advisor in Phase 2. It is expected that the appropriate securities

  14. Earth and Sky, Unit 1A

    DEFF Research Database (Denmark)

    Gammelgaard Nielsen, Anders

    2011-01-01

    The assignment known as ‘Earth and sky’ is the final first year course at Unit 1a. The aim of the assignment is to strengthen the student’s abilities to manage a project process individu- ally. The process involves develop- ing the ability to make independent decisions.The point of departure...... for the ‘Earth and sky’ assignment is ex- perience students acquired during their group study tour to Austra- lia. Building in particular on the re- search conducted on the Sydney Opera House and the architectur- al principles of spatial creation that this building represents....

  15. Study on the Operating Strategy of HVAC Systems for Nuclear Decommissioning Plant

    Energy Technology Data Exchange (ETDEWEB)

    Kim, Sung-hwan; Han, Sung-heum; Lee, Jae-gon [KHNP CRI, Daejeon (Korea, Republic of)

    2016-10-15

    According as Kori nuclear power plant unit 1 was determined to be defueled in 2017, various studies on nuclear plant decommissioning have been performed. In nuclear decommissioning plant, HVAC systems with large fan and electric coil have to be operated for long periods of time to support various types of work from defueled phase to final dismantling phase. So, in view of safety and utility costs, their overall operating strategy need to be established prior to defueled phase. This study presents HVAC system operating strategy at each decommissioning phase, that is, defueled plant operating phase, SSCs(systems, structures, components) decontamination and dismantling phases. In defueled plant operating phase, all fuel assemblies in reactor vessel are transferred to spent fuel pool(SFP) permanently. In defueled plant operation phase, reduction of the operating system trains is more practicable than the introduction of new HVAC components with reduced capacity. And, based on the result of the accident analyses for this phase, HVAC design bases such as MCR habitability requirement can be mitigated. According to these results, associated SSCs also can be downgraded. In similar approach, at each phase of plant decommissioning, proper inside design conditions and operating strategies should be re-established.

  16. Pilgrim Nuclear Power Station, Unit 1. Annual operating report, 1975

    International Nuclear Information System (INIS)

    1976-01-01

    Net electric power generated in 1975 was 1,074,401 MW(e) with the generator on line 4,680.7 hrs. Information is presented concerning operations, maintenance, radioactive effluents and waste shipments, health physics, shutdowns, and personnel exposures

  17. Pilgrim Nuclear Power Station, Unit 1. Annual operating report, 1975

    International Nuclear Information System (INIS)

    1976-01-01

    Net electrical power generated was 2,587,248 MWH(e) with the reactor on line 6,242.4 hr. Information is presented concerning operations, power generation, shutdowns, corrective maintenance, chemistry and radiochemistry, occupational radiation exposure, release of radioactive materials, and reportable occurrences

  18. Reactor pressure vessel integrity of Genkai Unit 1

    International Nuclear Information System (INIS)

    Nakamuta, Y.; Nozaki, G.; Saruwatari, T.; Watanabe, S.; Yamashita, Y.

    2015-01-01

    The structural integrity of reactor pressure vessels (RPVs) of commercial nuclear power plants in Japan has to be confirmed for the continuing operation according to the Japanese technical standards, JEAC4206-2007 and JEAC4201-2007, which specify the procedures to evaluate the structural integrity of RPVs and the embrittlement of RPV materials, respectively. The structural integrity analysis of Genkai Unit 1 RPV was performed based on the 4. surveillance data. Even though the ΔRT(NDT) obtained for the base metal was larger than the prediction of the current embrittlement correlation method of JEAC4201-2007, the structural integrity of the RPV during PTS event was confirmed with a sufficient margin. The reason of the large ΔRT(NDT) in the base metal was investigated thoroughly in terms of the microstructural changes caused by the neutron irradiation. The study showed that the microstructural changes are all as expected for this class of material, no grain boundary fracture occurred, the material is homogeneous in terms of chemical composition, and the chemical compositions which are important for the evaluation of embrittlement are correct. All these results suggested room for improvement of the current embrittlement correlation method in JEAC4201-2007. Using Genkai Unit 1 data as well as other recent surveillance data, the embrittlement correlation method has been modified so that the recent high fluence data can be predicted with higher accuracy, and was issued as JEAC4201-2007, 2013 addendum. It has been demonstrated that the RPV materials of the Genkai Unit 1 meet the requirements of JEAC4206-2007 and can be used for the continuing safe operation up to 60 years

  19. 78 FR 44603 - Byron Nuclear Station, Units 1 and 2, and Braidwood Nuclear Station, Units 1 and 2; Exelon...

    Science.gov (United States)

    2013-07-24

    ... Documents Access and Management System (ADAMS): You may access publicly available documents online in the... order to serve documents through the Electronic Information Exchange System, users will be required to... of acceptance for docketing and notice of opportunity for hearing regarding the renewal of operating...

  20. Life extension of the St. Lucie unit 1 reactor vessel

    International Nuclear Information System (INIS)

    Rowan, G.A.; Sun, J.B.; Mott, S.L.

    1991-01-01

    In late 1989, Florida Power and Light Company (FP and L) established the policy that St. Lucie unit 1 should not be prevented from achieving a 60-yr operating life by reactor vessel embrittlement. A 60-yr operating life means that the plant would be allowed to operate until the year 2036, which is 20 years beyond the current license expiration date of 2016. Since modifications to the reactor vessel and its components are projected to be expensive, the desire of FP and L management was to achieve this lifetime extension through the use of fuel management and proven technology. The following limitations were placed on any acceptable method for achieving this lifetime extension capability: low fuel cycle cost; low impact on safety parameters; very little or no operations impact; and use of normal reactor materials. A task team was formed along with the Advanced Nuclear Fuels Company (ANF) to develop a vessel-life extension program

  1. Evaluation of severe accident risks, Grand Gulf, Unit 1: Appendices

    International Nuclear Information System (INIS)

    Brown, T.D.; Breeding, R.J.; Jow, H.N.; Higgins, S.J.; Shiver, A.W.; Helton, J.C.; Amos, C.N.

    1990-12-01

    In support of the Nuclear Regulatory Commission's (NRC's) assessment of the risk from severe accidents at commercial nuclear power plants in the US report in NUREG-1150, the Severe Accident Risk Reduction Program (SARRP) has completed a revised calculation of the risk to the general public from severe accidents at the Grand Gulf Nuclear Station, Unit 1. This power plant, located in Port Gibson, Mississippi, is operated by the System Energy Resources, Inc. (SERI). The emphasis in this risk analysis was not on determining a ''so-called'' point estimate of risk. Rather, it was to determine the distribution of risk, and to discover the uncertainties that account for the breadth of this distribution. Off-site risk initiated by events internal to the power plant was assessed. This document provides Appendices A through E for this report. Topics included are, respectively: supporting information for the accident progression analysis; supporting information for the source term analysis; supporting information for the consequence analysis; risk results; and sampling information

  2. Analysis of core damage frequency: Surry, Unit 1 internal events

    International Nuclear Information System (INIS)

    Bertucio, R.C.; Julius, J.A.; Cramond, W.R.

    1990-04-01

    This document contains the accident sequence analysis of internally initiated events for the Surry Nuclear Station, Unit 1. This is one of the five plant analyses conducted as part of the NUREG-1150 effort by the Nuclear Regulatory Commission. NUREG-1150 documents the risk of a selected group of nuclear power plants. The work performed and described here is an extensive of that published in November 1986 as NUREG/CR-4450, Volume 3. It addresses comments form numerous reviewers and significant changes to the plant systems and procedures made since the first report. The uncertainty analysis and presentation of results are also much improved. The context and detail of this report are directed toward PRA practitioners who need to know how the work was performed and the details for use in further studies. The mean core damage frequency at Surry was calculated to be 4.05-E-5 per year, with a 95% upper bound of 1.34E-4 and 5% lower bound of 6.8E-6 per year. Station blackout type accidents (loss of all AC power) were the largest contributors to the core damage frequency, accounting for approximately 68% of the total. The next type of dominant contributors were Loss of Coolant Accidents (LOCAs). These sequences account for 15% of core damage frequency. No other type of sequence accounts for more than 10% of core damage frequency. 49 refs., 52 figs., 70 tabs

  3. Comparison of the Radionuclides Dispersion at the UAE Barakah Site with that at the ROK Shin-Kori Site - Comparison of the radionuclides dispersion in Barakah site with that in Shin-Kori site

    Energy Technology Data Exchange (ETDEWEB)

    Kim, Sung-yeop; Lee, Kun Jai; Chang, Soon Heung [Korea Advanced Institute of Science and Technology, 291 Daehak-ro, Yuseong-gu, Daejeon, 305-701 (Korea, Republic of); Beeley, Philip A. [Khalifa University of Science, Technology and Research, P.O. Box 127788, Abu Dhabi (United Arab Emirates)

    2014-07-01

    In order to understand the characteristics of atmospheric dispersion of radionuclides in the desert environment of Barakah site in UAE, comparison research with the results of other environments could be an appropriate way to facilitate it. Shin-Kori site is the proper comparison target because same reactor type of APR1400 with that in Barakah site is under construction. Hypothetical accident scenario was considered and accident source term which had been developed in previous research has been applied as releasing source. After reviewing several computation codes, ADMS5 has been selected as an atmospheric dispersion modeling tool which is installing advanced Gaussian plum model and plentiful options. The climate data of both Barakah and Shin-Kori were acquired and the environments of both sites have been simulated considering wind speed, wind direction, temperature, humidity, ground surface roughness and etc. Near field final human doses on the maps have been schematised regarding statistical meteorological data of both sites and dose conversion factors from the publications of ICRP and federal guidance report of EPA. The results of this research are expected to enhance the understanding about differences between two environments which have same reactor type and to improve the comprehension of desert environment of Barakah site as well. Applying different dose conversion factors to Barakah site considering the desert biosphere could be further study to obtain more accurate results. (authors)

  4. Cold weather effects on Dresden Unit 1

    Energy Technology Data Exchange (ETDEWEB)

    Anagnostopoulos, H. [Commonwealth Edison Co., Morris, IL (United States)

    1995-03-01

    Dresden Unit 1 is in the final stages of a decommissioning effort directed at preparing the unit to enter a SAFSTOR status. Following an extended sub-zero cold wave, about 55,000 gallons of water were discovered in the lowest elevation of the spherical reactor enclosure. Cold weather had caused the freezing and breaking of several service water lines that had not been completely isolated. Two days later, at a regularly scheduled decommissioning meeting, the event was communicated to the decommissioning team, who quickly recognized the potential for freezing of a 42 inches diameter Fuel Transfer Tube that connects the sphere to the Spent Fuel Pool. The team directed that the pool gates between the adjacent Spent Fuel Pool and the Fuel Transfer Pool be installed, and a portable source of heat was installed on the Fuel Transfer Tube. It was later determined that, with the fuel pool gates removed, and with a worst case freeze break at the 502 elevation on the Fuel Transfer Tube (in the Sphere), the fuel in the Spent Fuel Pool could be uncovered to a level 3 below the top of active fuel.

  5. A Study on the Construct Validity of Safety Culture Oversight Model for Nuclear Power Operating Organization

    International Nuclear Information System (INIS)

    Jung, Su Jin; Choi, Young Sung; Oh, Jang Jin

    2015-01-01

    In Korea, the safety policy statement declared in 1994 by government stressed the importance of safety culture and licensees were encouraged to manage and conduct their self-assessments. A change in regulatory position about safety culture oversight was made after the event of SBO cover-up in Kori unit 1 and several subsequent falsification events. Since then KINS has been developing licensee's safety culture oversight system including conceptual framework of oversight, prime focus area for oversight, and specific details on regulatory expectations, all of which are based on defence-in-depth (DiD) safety enhancement approach. Development and gathering of performance data which is related to actual 'safety' of nuclear power plant are needed to identify the relationship between safety culture and safety performance. Authors consider this study as pilot which has a contribution on verifying the construct validity of the model and the effectiveness of survey based research. This is the first attempt that the validity of safety culture oversight model has been investigated with empirical data obtained from Korean nuclear power operating organization

  6. Development of Soil Derived Concentration Guidance Levels for Decommissioning at Overseas Nuclear Power Plants

    Energy Technology Data Exchange (ETDEWEB)

    Sohn, Wook; Yoon, Suk Bon; Kim, Jeongju [KHNP CRI, Daejeon (Korea, Republic of)

    2016-10-15

    In Korea, the criteria are expected to be given in terms of dose as in US and Spain. However, since dose cannot be measured, corresponding measurable concentration limits, so-called Derived Concentration Guidance Levels (DCGLs), should be developed for each radionuclide which is expected to be present in the site. Also, as they serve as a goal of decommissioning and direct dismantling and decontamination methods applicable to the site, DCGLs should be developed in the early phase of decommissioning. This paper describes how each overseas nuclear power plant developed its site-specific Soil DCGLs: what kind of post closure use of the site (scenario) was assumed and how the site-specific Soil DCGLs were calculated based on the scenario assumed for each plant. Through this, it is intended to derive lessons learned which will be instructive for future decommissioning of domestic nuclear power plants including Kori Unit 1. It is very important to have as good under-standing as possible of characteristics of the site by collection of relevant information and data in order to apply a scenario which is most foreseeable and plausible for a site to be decommissioned and to provide site-specific inputs to the calculation of the Soil DCGLs. These efforts will help to have not-overly conservative values for the Soil DCGLs, thus thereby reducing the costs and time needed for performing the decommissioning.

  7. A Study on the Construct Validity of Safety Culture Oversight Model for Nuclear Power Operating Organization

    Energy Technology Data Exchange (ETDEWEB)

    Jung, Su Jin; Choi, Young Sung; Oh, Jang Jin [Korea Institute of Nuclear Safety, Daejeon (Korea, Republic of)

    2015-05-15

    In Korea, the safety policy statement declared in 1994 by government stressed the importance of safety culture and licensees were encouraged to manage and conduct their self-assessments. A change in regulatory position about safety culture oversight was made after the event of SBO cover-up in Kori unit 1 and several subsequent falsification events. Since then KINS has been developing licensee's safety culture oversight system including conceptual framework of oversight, prime focus area for oversight, and specific details on regulatory expectations, all of which are based on defence-in-depth (DiD) safety enhancement approach. Development and gathering of performance data which is related to actual 'safety' of nuclear power plant are needed to identify the relationship between safety culture and safety performance. Authors consider this study as pilot which has a contribution on verifying the construct validity of the model and the effectiveness of survey based research. This is the first attempt that the validity of safety culture oversight model has been investigated with empirical data obtained from Korean nuclear power operating organization.

  8. Development of a Pilot Program for Human Factors Management in Operating Nuclear Power plants

    International Nuclear Information System (INIS)

    Lee, Jung-Woon; Lee, Yong-Hee; Jang, Tong-Il; Kim, Dae-Ho

    2007-01-01

    The human factors of operating NPPs have been reviewed as a part of Periodic Safety Reviews (PSRs). This human factors PSR covers a wide range of human factors including control room man-machine interfaces (MMIs), procedures, working conditions, qualification, training, information requirements and workload. Korea Atomic Energy Research Institute (KAERI) has performed human factors PSRs from the first PSR for Kori 1. It was determined in 2005 that for a Continuous Operation of the Korean NPPs an enhanced PSR should be performed and issues raised from the PSRs should be resolved. From the results of the PSR for Kori 1, several safety enhancement issues related to human factors were raised. KAERI is working on a resolution of some of the human factors issues for the Korea Hydro and Nuclear Power Co. (KHNP). As a part of the resolution, we are developing a human factors management program (HFMP) for Kori 1. This paper introduces the status of our development of HFMP

  9. Analysis on Isolation Condenser Operation by Fukushima Daiichi Unit 1 Operators

    International Nuclear Information System (INIS)

    Kim, Man Cheol

    2014-01-01

    Fukushima Daiichi nuclear accident resulted in the core damage in three reactors and the release of considerable amount of radioactive material to the environment, not to mention significant social impact and anti-nuclear atmosphere all around the world. This paper provides a review of the findings related to shift operators' operation of the isolation condenser in Unit 1 to examine shift operators' response to the situation. Based on the review of the findings, a situation assessment model was developed to analyze shift operators' understanding on whether core cooling was successfully performed in Unit 1 through the operation of isolation condenser. It was found that lack of information could be one of the main causes for the failure in core cooling by the IC in Unit 1. It is also recommended that the differences in the mathematical model for the situation assessment and that of the real operator need to be further investigated

  10. Analysis on Isolation Condenser Operation by Fukushima Daiichi Unit 1 Operators

    Energy Technology Data Exchange (ETDEWEB)

    Kim, Man Cheol [Chungang University, Seoul (Korea, Republic of)

    2014-08-15

    Fukushima Daiichi nuclear accident resulted in the core damage in three reactors and the release of considerable amount of radioactive material to the environment, not to mention significant social impact and anti-nuclear atmosphere all around the world. This paper provides a review of the findings related to shift operators' operation of the isolation condenser in Unit 1 to examine shift operators' response to the situation. Based on the review of the findings, a situation assessment model was developed to analyze shift operators' understanding on whether core cooling was successfully performed in Unit 1 through the operation of isolation condenser. It was found that lack of information could be one of the main causes for the failure in core cooling by the IC in Unit 1. It is also recommended that the differences in the mathematical model for the situation assessment and that of the real operator need to be further investigated.

  11. Decommissioning the Dresden Unit 1 Spent Fuel Pool

    International Nuclear Information System (INIS)

    Demmer, R.L.; Bargelt, R.J.; Panozzo, J.B.; Christensen, R.J.

    2006-01-01

    The Dresden Nuclear Power Station, Unit 1 Spent Fuel Pool (SFP) (Exelon Generation Co.) was decommissioned using a new underwater coating strategy developed in cooperation with the Idaho National Laboratory (INL). This was the first time that a commercial nuclear power plant (NPP) SFP was decommissioned using this underwater coating approach. This approach has advantages in many aspects, particularly in reducing airborne contamination and in safer, more cost effective deactivation. The process was pioneered at the INL and used to decommission three SFPs with a total combined pool volume of over 900,000 gallons. The INL provided engineering support and shared project plans to successfully initiate the Dresden project. This report outlines the steps taken by the INL and Exelon on the pathway for this activity. The rationale used to select the underwater coating option and the advantages and disadvantages are shown. Special circumstances, such as the use of a remotely operated underwater vehicle to map (visually and radiologically) the pool areas that were not readily accessible, are discussed. Several specific areas where special equipment was employed are given and a lessons learned evaluation is included. (authors)

  12. Bruce A units 1 and 2 restart project

    International Nuclear Information System (INIS)

    Routledge, K.

    2006-01-01

    This presentation provides an overview of the Bruce A Units 1 and 2 Restart project from the vantage point of the Project Management Contractor (PMC). The presentation will highlight the unique structure of the project, which has been designed to maximize project efficiencies while minimizing the impact to the Bruce Power operational reactors. Efficiency improvements covered in the presentation includes: support services provided to the direct work contractors, radiation protection, worker protection, engineering, field execution, maintenance and facilities. The presentation focusses on the roles of the PMC in helping to ensure the successful outcome of this ambitious reactor refurbishment project. In addition, the Construction Island concept that has been implemented on the project will be presented, with some of the innovative thinking that has gone into its creation. The organization of the PMC and an overview of the project schedule is also presented. AMEC NCL is a privately held consultancy in the Canadian nuclear industry which provides experienced and flexible multi-disciplined resources to support full project management, engineering solutions and safety consultancy services throughout the life cycle of nuclear facilities in Canada, and for customers in related markets in North America and overseas. AMEC NCL is a wholly-owned subsidiary of AMEC plc

  13. Dispersant Application during SG Wet Layup at SK Unit 1

    Energy Technology Data Exchange (ETDEWEB)

    Kwon, Hyukchul; Lee, Dooho; Sung, Kibang [KHNP Central Institute, Daejeon (Korea, Republic of)

    2014-05-15

    The corrosion products in the feedwater are deposited onto the steam generators (SGs) despite the effort to control them within limit of impurity. This deposit is one of causes for occurrence of SCC (Stress Corrosion Cracking), water level fluctuation and further corrosion of SGs. To minimize corrosion and remove deposit, the nuclear power plants apply high pH to the secondary system and SG chemical cleaning, respectively. But these methods can be costly and carry risks of extended outages or incomplete cleaning. Another method is an on-line dispersant application. The role of dispersant is to make deposit suspended in the SGs. Then, the suspended deposit is discharged to the blowdown system. The iron removal is increased in the blowdown system during the dispersant application. Additional significant benefit in the form of reduced corrosion product transport may be obtained through applying dispersant in the SGs wet lay operational mode. This method helps to reduce the total SGs loading without affecting critical outage activities and with minimal additional effort on the part of the utilities. This study provides the results of the dispersant application trial during the SG wet layup at SK Unit 1. As the PAA concentrations were increased, the corrosion rates of Alloy 690 and SA 106 Gr.B were increased. The corrosion rate of Alloy 690 was 2 times less than that of SA 106 Gr.B at 100 ppm of PAA based on the electrochemical experimental. There were no significant feasibility problems with application of PAA during the SG wet layup. The reasonable estimation of the additional mass removed by the presence of PAA during SGs wet layup is 460 g. The iron removal depended on PAA concentration injected based on the comparative results of the SK Unit 1 and TMI-1. It is expected that injection of PAA into the SG result in a significant decrease in the amount of iron transported to the SGs during the startup.

  14. Lessons learned from the SONGS Unit 1 water hammer event

    International Nuclear Information System (INIS)

    Chiu, C.

    1987-01-01

    On November 21, 1985, a water hammer event occurred in horizontal feedwater line B at San Onofre Nuclear Generation Site (SONGS) Unit 1. The SONGS Unit 1 is a three-loop pressurized water reactor designed by Westinghouse Electric Corp. The event was initiated by a differential current trip on the bus of auxiliary transformer C. The root cause of the event was a simultaneous failure of five check valves in the feedwater system. Two of them are located downstream of the feedwater pump, and three of them are located further downstream and on the lines to the steam generators. The failure mechanism was determined to be flow-induced vibration, which caused repeated impact between the disk stud and the disk stop. The water hammer occurred in feedwater line B during the refilling of feedwater lines A, B, and C with auxiliary feedwater. The thermal-hydraulic process to initiate the water hammer and the reason that the water hammer only happened in line B have been fully investigated and explained. A root cause analysis after the event was prompted to answer the following two questions: (1) why did these five check valves fail at that time and not in the preceding 15 yr? (2) why did only these five check valves fail? The scope of the root cause analysis involves an investigation of the valve vibration characteristics, plant operation history, and the maintenance history of the valves. The paper answers these two questions, after a brief study of the vibration characteristics of a check valve

  15. Introduction to Nuclear Power Plant Environment Supervisory Committee

    International Nuclear Information System (INIS)

    Lee, Byung Il

    2008-01-01

    In Korea, there are five nuclear power plant sites, located at Yongkwang, Kori, Shin Kori, Uljin, and Wolsong. Each administrative district has its own NESC (Nuclear plant Environment Public Supervisory Committee) which consists of a steering committee and a center. The purpose of NESC is to let the public survey and inspect nuclear plant environment and then improve a clarity and confidence in plant construction and operation by themselves. In order to understand the situation of NESC and explore ways toward a better role of NESC, in this paper we try to enumerate a few major facts related to a current status of NESC. As a summary, there must be a great role of NESC in the relationship between the residents, a nuclear industry company and the related government division. Furthermore, NESC would certainly do its role for all sides provided that more strong definition of NESC in law, more financial supporting and more philosophical speculation for the being of NESC

  16. Technical Specifications, Comanche Peak Steam Electric Station, Unit 1 (Docket No. 50-445)

    International Nuclear Information System (INIS)

    1990-04-01

    The Technical Specifications for Comanche Peak Steam Electric Station, Unit 1 were prepared by the US Nuclear Regulatory Commission. They set forth the limits, operating conditions, and other requirements applicable to a nuclear reactor facility, as set forth in Section 50.36 of Title 10 of the Code of Federal Regulations Part 50, for the protection of the health and safety of the public

  17. A study on Requirements of Data Base Translator for APR1400 Computerized Procedure System at Shin-Hanul unit 1 and 2

    International Nuclear Information System (INIS)

    Seong, Nokyu; Lee, Sungjin

    2015-01-01

    The CPS is one of the Man Machine Interface (MMI) resources and the CPS can directly display plant graphic objects which are in the Digital Control System (DCS). And the CPS can send a request to DCS to provide DCS screen which is called step support display through DCS link button on a computerized procedure. The procedure writers can insert DCS graphic information to computerized procedure through data base which is provided by CPS Editing System (CPSES). The data base which is provided by CPSES conforms to the naming rule of DCS graphic objects. The naming rule of DCS graphic objects is defined by vendor thus status of DCS graphic objects which are in computerized procedure at Shin-Kori plant cannot be displayed on CPS at Shin-Hanul plant. To use computerized procedure which is written by other plant procedure writer, DCS graphic objects shall be translated by its plant data base. This paper introduces requirements of data base translator to reduce translation and re-inserting graphic objects burden. This paper introduces the requirements of data base translator of CPSES for APR1400 CPS at Shin-Hanul unit 1 and 2. The translator algorithms shall be tested to update data base of CPSES effectively. The prototype of translator is implemented and is being tested using real plant DB. This translator can be applied to Shin- Hanul unit1 and 2 through software V and V

  18. A study on Requirements of Data Base Translator for APR1400 Computerized Procedure System at Shin-Hanul unit 1 and 2

    Energy Technology Data Exchange (ETDEWEB)

    Seong, Nokyu; Lee, Sungjin [KHNP, Daejeon (Korea, Republic of)

    2015-05-15

    The CPS is one of the Man Machine Interface (MMI) resources and the CPS can directly display plant graphic objects which are in the Digital Control System (DCS). And the CPS can send a request to DCS to provide DCS screen which is called step support display through DCS link button on a computerized procedure. The procedure writers can insert DCS graphic information to computerized procedure through data base which is provided by CPS Editing System (CPSES). The data base which is provided by CPSES conforms to the naming rule of DCS graphic objects. The naming rule of DCS graphic objects is defined by vendor thus status of DCS graphic objects which are in computerized procedure at Shin-Kori plant cannot be displayed on CPS at Shin-Hanul plant. To use computerized procedure which is written by other plant procedure writer, DCS graphic objects shall be translated by its plant data base. This paper introduces requirements of data base translator to reduce translation and re-inserting graphic objects burden. This paper introduces the requirements of data base translator of CPSES for APR1400 CPS at Shin-Hanul unit 1 and 2. The translator algorithms shall be tested to update data base of CPSES effectively. The prototype of translator is implemented and is being tested using real plant DB. This translator can be applied to Shin- Hanul unit1 and 2 through software V and V.

  19. Safety Evaluation of Full Digital Plant Protection System of Shin-Kori 3 and 4 in Korea

    International Nuclear Information System (INIS)

    Koh, J. S.; Kim, D. I.; Jeong, C. H.; Park, H. S.; Ji, S. H.; Kang, Y. D.; Park, G. Y.

    2009-01-01

    Keeping pace with the emerging trend of digital computer technologies, KHNP has utilized full digital plant protection system into the design of I and C systems at SKN 3 and 4. This paper presents safety review activities and results related to digital plant protection systems during the licensing of construction permit for the Shin-Kori 3 and 4(SKN 3 and 4) in Korea. The major licensing issues regarding the digital systems were software quality and cyber security during planning stage, system integrity with fail-safe design, EMI equipment qualification of digital systems, FPGA qualification and communication independence between safety and non-safety System. This paper addresses our approach to evaluate full digital protection systems with revised safety review guidelines and the resulting discussion to resolve the licensing issues

  20. Effect of Containment Spray Additives on the Chemical Effect after a Loss of Coolant Accident in Nuclear Power Plants

    Energy Technology Data Exchange (ETDEWEB)

    Lee, Seung Chan; Park, Jong Woon; Lee, Guen Sung [KOREA HYDRO and NUCLEAR POWER Co., Daejeon (Korea, Republic of)

    2007-10-15

    As a part of USNRC GSI-191, evaluation of Kori Unit 1 ECCS recirculation sump performance has been carried out in 2006. The work is derived from the result of first PSR(Periodic Safety Review) of Kori Unit1. In this work, we have considered the replacement of spray additive in containment building to solve issues of GSI-191 and GL2004-02. We estimated the chemical effect of changing NaOH into TSP(Trisodium Phosphate) based on SRP(Standard Review Plan) 6.5.2. Rev.02. WCAP-16530 methodology is used to compare chemical effects of spray additive(or buffering agents). In the other side, chemical thermodynamic simulation can be utilized. Herein, the results using WCAP-16530 methodology and chemical simulation are presented.

  1. Reactor Core Internals Replacement of Ikata Units 1 and 2

    International Nuclear Information System (INIS)

    Ikeda, K.; Ishikawa, T.; Miyoshi, T.; Takagi, T.

    2012-01-01

    This paper presents an overview of the reactor core internals replacement project carried out at the Ikata Nuclear Power Station in Japan, which was the first of its kind among PWRs in the world. Failure of baffle former bolts was first reported in 1989 at Bugey 2 in France. Since then, similar incidents have been reported in Belgium and in the U.S., but not in Japan. However, the possibility of these bolts failing in Japanese plants cannot be denied in the future as operating hours increase. Ageing degradation mechanisms for the reactor core internals include irradiation-assisted stress corrosion cracking of baffle former bolts and mechanical wear of control rod guide cards. Two different approaches can be taken to address these ageing issues: to inspect and repair whenever a problem is found; and to replace the entire core internals with those of a new design having advanced features to prevent ageing degradation problems. The choice of our company was the latter. This paper explains the reasons for the choice and summarizes the replacement project activities at Ikata Units 1 and 2 as well as the improvements incorporated in the new design. (author)

  2. Snubber reduction program at the Byron Station, Unit 1

    International Nuclear Information System (INIS)

    Arterburn, J.; Bakhtiari, S.

    1987-01-01

    Commonwealth Edison Company's (CECo's) Byron Station, unit 1, was originally designed with approximately 1200 snubbers supporting the plant's large- and small-bore piping systems. This relatively large number of snubbers is attributed to excessive conservatism in nuclear piping codes and regulations effective during the original piping design. A recent pilot program at CECo's LaSalle County Station, a boiling water reactor plant, demonstrated that a 50% or greater reduction in total snubber population is achievable in plants of this design vintage. Based on the successful results of the pilot program, CECo initiated a full scale snubber reduction program at Byron, a pressurized water reactor plant of the same vintage at the LaSalle County Station. The benefits from a reduced snubber population are described. To realize the maximum potential benefits, all snubbers in the plant were prioritized in order of desirability for removal. The priority designations are discussed. The major results from phase 1 of the Byron program are summarized. The NRC inspection of the project addressed a variety of issues and is discussed. The conclusions that can be drawn from the phase 1 program are summarized

  3. Results of zinc injection test for Hamaoka Unit-1

    International Nuclear Information System (INIS)

    Kani, K.; Masuda, H.; Hayashi, Y.; Sudo, S.; Yamazaki, K.

    1998-01-01

    A zinc injection test was preformed at Hamaoka Nuclear Power Station Unit-1 for suppressing radiation dose rate on primary coolant recirculation piping after the replacement of piping. Zinc ion was injected by using injection system where Depleted Zinc Oxide was dissolved in carbonated water. Controllability of the system was sufficient to maintain concentration of zinc in primary water. The concentration of zinc in the primary coolant was controlled from 1 ppb to 5 ppb gradually. The increasing trend of concentration of Co-60 in the coolant was suppressed at zinc concentration of 3 ppb. It is evaluated that the deposition coefficient of Co-60 onto the surface of primary coolant recirculation piping was suppressed to one-third of previous cycle in average, and one-fourth of that just before injection start at zinc concentration of 5 ppb. We concluded that zinc injection is effective for suppressing dose rate on the primary coolant piping and no adverse effect occurs by zinc injection up to 5 ppb in the primary coolant. (J.P.N.)

  4. Technical Specifications, Seabrook Station, Unit 1 (Docket No. 50-443): Appendix ''A'' to License No. NPF-67

    International Nuclear Information System (INIS)

    1989-05-01

    The Seabrook Station, Unit 1 Technical Specifications were prepared by the US Nuclear Regulatory Commission to set forth the limits, operating conditions, and other requirements applicable to a nuclear reactor facility as set forth in Section 50.36 of 10 CFR Part 50 for the protection of the health and safety of the public

  5. 77 FR 35079 - License Renewal Application for Seabrook Station, Unit 1 ; NextEra Energy Seabrook, LLC

    Science.gov (United States)

    2012-06-12

    ... NUCLEAR REGULATORY COMMISSION [Docket No. 50-443; NRC-2010-0206] License Renewal Application for Seabrook Station, Unit 1 ; NextEra Energy Seabrook, LLC AGENCY: Nuclear Regulatory Commission. ACTION: License renewal application; intent to prepare supplement to draft [[Page 35080

  6. Final report for the 1st ex-vessel neutron dosimetry installations and evaluations for Kori unit 2 reactor pressure vessel

    Energy Technology Data Exchange (ETDEWEB)

    Kim, Byoung Chul; Yoo, Choon Sung; Lee, Sam Lai; Chang, Kee Ok; Gong, Un Sik; Choi, Kwon Jae; Chang, Jong Hwa; Lim, Nam Jin; Hong, Joon Wha; Cheon, Byeong Jin

    2006-11-15

    This report describes a neutron fluence assessment performed for the Kori unit 2 pressure vessel belt line region based on the guidance specified in regulatory guide 1.190. In this assessment, maximum fast neutron exposures expressed in terms of fast neutron fluence (E>1 MeV) and iron atom displacements (dpa) were established for the belt line region of the pressure vessel. During cycle 20 of reactor operation, an ex-vessel neutron dosimetry program was instituted at Kori unit 2 to provide continuous monitoring of the belt line region of the reactor vessel. The use of the ex-vessel neutron dosimetry program coupled with available surveillance capsule measurements provides a plant specific data base that enables the evaluation of the vessel exposure and the uncertainty associated with that exposure over the service life of the unit. Ex-vessel neutron dosimetry has been evaluated at the conclusion of cycle 20.

  7. Final report for the 1st ex-vessel neutron dosimetry installation and evaluations for Kori unit 4 reactor pressure vessel

    Energy Technology Data Exchange (ETDEWEB)

    Kim, Byoung Chul; Yoo, Choon Sung; Lee, Sam Lai; Chang, Kee Ok; Gong, Un Sik; Choi, Kwon Jae; Chang, Jong Hwa; Lim, Nam Jin; Hong, Joon Wha; Cheon, Byeong Jin

    2006-11-15

    This report describes a neutron fluence assessment performed for the Kori unit 4 pressure vessel belt line region based on the guidance specified in regulatory guide 1.190. In this assessment, maximum fast neutron exposures expressed in terms of fast neutron fluence (E>1 MeV) and iron atom displacements (dpa) were established for the belt line region of the pressure vessel. During cycle 16 of reactor operation, an ex-vessel neutron dosimetry program was instituted at Kori unit 4 to provide continuous monitoring of the belt line region of the reactor vessel. The use of the ex-vessel neutron dosimetry program coupled with available surveillance capsule measurements provides a plant specific data base that enables the evaluation of the vessel exposure and the uncertainty associated with that exposure over the service life of the unit. Ex-vessel neutron dosimetry has been evaluated at the conclusion of cycle 16.

  8. Nuclear Regulatory Commission issuances, March 1975

    International Nuclear Information System (INIS)

    1975-04-01

    Reactor licensing actions taken by the Nuclear Regulatory Commission, the Atomic Safety and Licensing Appeal Board and the Atomic Safety and Licensing Boards for March 1975 are presented. Action was included for the following reactors: Big Rock Point Nuclear Plant; West Valley Reprocessing Plant; Limerick Generating Station, Units 1 and 2; Midland Plants, Units 1 and 2; Wolf Creek Generating Station, Unit 1; Monticello Nuclear Generating Plant, Unit 1; Douglas Point Nuclear Generating Station, Units 1 and 2; Seabrook Station, Units 1 and 2; Vermont Yankee Nuclear Power Station; and WPPSS Hanford Units 1 and 4. (U.S.)

  9. Nuclear Regulatory Commission issuances. Volume 17, No. 3

    International Nuclear Information System (INIS)

    1983-03-01

    This report contains the Issuances received during March 1983 from the Commission (CLI), the Atomic Safety and Licensing Appeal Boards (ALAB), the Atomic Safety and Licensing Boards (LBP), the Administrative Law Judge (ALJ), the Directors Decisions (DD), and the Denials of Petition for Rulemaking (DPRM). The Issuances concerned the following facilities: Three Mile Island Nuclear Station, Unit No. 1; Comanche Peak Steam Electric Station, Units 1 and 2; Vallecitos Nuclear Center; Floating Nuclear Power Plants; San Onofre Nuclear Generating Station, Units 2 and 3; Point Beach Nuclear Plant, Unit 1; Perry Nuclear Power Plant, Units 1 and 2; Shoreham Nuclear Power Station, Unit 1; Western New York Nuclear Service Center; Limerick Generating Station, Units 1 and 2; Seabrook Station, Units 1 and 2; Black Fox Station, Units 1 and 2; WmH Zimmer Nuclear Power Station, Unit 1; WPPSS Nuclear Project No. 1; Zion Nuclear Plant, Units 1 and 2; and South Texas Project, Units 1 and 2

  10. Strategy of nuclear power in Korea, non-nuclear-weapon state and peaceful use of nuclear power

    International Nuclear Information System (INIS)

    Nagasaki, Takao

    2005-01-01

    The nuclear power plant started at Kori in Korea in April, 1978. Korea has carried out development of nuclear power as a national policy. The present capacity of nuclear power plants takes the sixes place in the world. It supplies 42% total power generation. The present state of nuclear power plant, nuclear fuel cycle facility, strategy of domestic production of nuclear power generation, development of next generation reactor and SMART, strategy of export in corporation with industry, government and research organization, export of nuclear power generation in Japan, nuclear power improvement project with Japan, Korea and Asia, development of nuclear power system with nuclear diffusion resistance, Hybrid Power Extraction Reactor System, radioactive waste management and construction of joint management and treatment system of spent fuel in Asia are stated. (S.Y.)

  11. Analysis of core damage frequency from internal events: Surry, Unit 1

    International Nuclear Information System (INIS)

    Harper, F.T.

    1986-11-01

    This document contains the accident sequence analyses for Surry, Unit 1; one of the reference plants being examined as part of the NUREG-1150 effort by the Nuclear Regulatory Commission (NRC). NUREG-1150 will document the risk of a selected group of nuclear power plants. As part of that work, this report contains the overall core damage frequency estimate for Surry, Unit 1, and the accompanying plant damage state frequencies. Sensitivity and uncertainty analyses provide additional insights regarding the dominant contributors to the Surry core damage frequency estimate. The numerical results are driven to some degree by modeling assumptions and data selection for issues such as reactor coolant pump seal LOCAs, common cause failure probabilities, and plant response to station blackout and loss of electrical bust initiators. The sensitivity studies explore the impact of alternate theories and data on these issues

  12. Chemical cleaning of Dresden Unit 1: Final report

    International Nuclear Information System (INIS)

    1986-05-01

    The introduction of NS-1 solvent into the full primary system of Dresden Unit-1 nuclear power reactor on September 12, 1984, represented the culmination of several years of development, testing, planning, and construction. The requirement was to dissolve the highly radioactive deposits of primarily nickel ferrite without any corrosion which might compromise the reactor systems. During the actual cleaning with the NS-1 solvent, the chemical condition of the circulating solvent was measured. Iron, nickel, and radioactive cobalt all dissolved smoothly. The amount of copper in solution decreased in concentration, verifying expectations that metallic copper would plate on to clean metal surfaces. A special rinse formulation was employed after the primary cleaning steps and the ''lost'' copper was thus redissolved and removed from the system. After the cleaning was complete and the reactor had been refilled with pure water, radiation levels were measured. The most accurate of these measurements gave decontamination factors ranging well above 100, which indicated a significant removal of the radioactive deposits, and demonstrated the success of this project. Treatment of the radioactive liquid wastes from this operation required volume reduction and water purification. The primary method of processing the spent cleaning solvent and rinse water was evaporation. The resulting concentrate has been stored as a liquid, awaiting solidification to allow burial at a designated site. Water which was separated during evaporation, along with the dilute rinses, was processed by various chemical means, reevaporated, treated with activated carbon, and/or demineralized before its radionuclide and chemical content was low enough to allow it to be returned to Dresden Station for treatment or disposal. 60 figs., 31 tabs

  13. Failure Mode Estimation of Wolsong Unit 1 Containment Building with respect to Severe Accident Condition

    International Nuclear Information System (INIS)

    Hahm, Dae Gi; Choi, In Kil

    2009-01-01

    The containment buildings in a nuclear power plant (NPP) are final barriers against the exposure of harmful radiation materials at severe accident condition. Since the accident at Three Mile Island nuclear plant in 1979, it has become necessary to evaluate the internal pressure capacity of the containment buildings for the assessment of the safety of nuclear power plants. According to this necessity, many researchers including Yonezawa et al. and Hu and Lin analyzed the ultimate capacity of prestressed concrete containments subjected to internal pressure which can be occurred at sever accident condition. Especially in Wolsong nuclear power plant, the Unit 1 containment structures were constructed in the late 1970 to early 1980, so that the end of its service life will be reached in near future. Since that the complete decommission and reconstruction of the NPP may cause a huge expenses, an extension of the service time can be a cost-effective alternative. To extend the service time of NPP, an overall safety evaluation of the containment building under severe accident condition should be performed. In this study, we assessed the pressure capacity of Wolsong Unit 1 containment building under severe accident, and estimated the responses at all of the probable critical areas. Based on those results, we found the significant failure modes of Wolsong Unit 1 containment building with respect to the severe accident condition. On the other hand, for the aged NPP, the degradation of their structural performance must also be explained in the procedure of the internal pressure capacity evaluation. Therefore, in this study, we performed a parametric study on the degradation effects and evaluated the internal pressure capacity of Wolsong Unit 1 containment building with considering aging and degradation effects

  14. Fuel failure at the Laguna Verde unit 1- during Cycle 4

    International Nuclear Information System (INIS)

    Espinosa Vega, Juan Manuel

    1996-01-01

    The present work describes the event occurred at the Laguna Verde nuclear power plants Unit 1 during its fourth cycle ensembles; the first failure, by means of a test of power suppression, and the second one, during the sipping accomplished in the four refuelling of the unit. Also it describes the re-evaluation of the event accomplished by the licenser, the manufacturer and the Mexican agency

  15. A Nuclear Safety System based on Industrial Computer

    International Nuclear Information System (INIS)

    Kim, Ji Hyeon; Oh, Do Young; Lee, Nam Hoon; Kim, Chang Ho; Kim, Jae Hack

    2011-01-01

    The Plant Protection System(PPS), a nuclear safety Instrumentation and Control (I and C) system for Nuclear Power Plants(NPPs), generates reactor trip on abnormal reactor condition. The Core Protection Calculator System (CPCS) is a safety system that generates and transmits the channel trip signal to the PPS on an abnormal condition. Currently, these systems are designed on the Programmable Logic Controller(PLC) based system and it is necessary to consider a new system platform to adapt simpler system configuration and improved software development process. The CPCS was the first implementation using a micro computer in a nuclear power plant safety protection system in 1980 which have been deployed in Ulchin units 3,4,5,6 and Younggwang units 3,4,5,6. The CPCS software was developed in the Concurrent Micro5 minicomputer using assembly language and embedded into the Concurrent 3205 computer. Following the micro computer based CPCS, PLC based Common-Q platform has been used for the ShinKori/ShinWolsong units 1,2 PPS and CPCS, and the POSAFE-Q PLC platform is used for the ShinUlchin units 1,2 PPS and CPCS. In developing the next generation safety system platform, several factors (e.g., hardware/software reliability, flexibility, licensibility and industrial support) can be considered. This paper suggests an Industrial Computer(IC) based protection system that can be developed with improved flexibility without losing system reliability. The IC based system has the advantage of a simple system configuration with optimized processor boards because of improved processor performance and unlimited interoperability between the target system and development system that use commercial CASE tools. This paper presents the background to selecting the IC based system with a case study design of the CPCS. Eventually, this kind of platform can be used for nuclear power plant safety systems like the PPS, CPCS, Qualified Indication and Alarm . Pami(QIAS-P), and Engineering Safety

  16. A Nuclear Safety System based on Industrial Computer

    Energy Technology Data Exchange (ETDEWEB)

    Kim, Ji Hyeon; Oh, Do Young; Lee, Nam Hoon; Kim, Chang Ho; Kim, Jae Hack [Korea Electric Power Corporation Engineering and Construction, Daejeon (Korea, Republic of)

    2011-05-15

    The Plant Protection System(PPS), a nuclear safety Instrumentation and Control (I and C) system for Nuclear Power Plants(NPPs), generates reactor trip on abnormal reactor condition. The Core Protection Calculator System (CPCS) is a safety system that generates and transmits the channel trip signal to the PPS on an abnormal condition. Currently, these systems are designed on the Programmable Logic Controller(PLC) based system and it is necessary to consider a new system platform to adapt simpler system configuration and improved software development process. The CPCS was the first implementation using a micro computer in a nuclear power plant safety protection system in 1980 which have been deployed in Ulchin units 3,4,5,6 and Younggwang units 3,4,5,6. The CPCS software was developed in the Concurrent Micro5 minicomputer using assembly language and embedded into the Concurrent 3205 computer. Following the micro computer based CPCS, PLC based Common-Q platform has been used for the ShinKori/ShinWolsong units 1,2 PPS and CPCS, and the POSAFE-Q PLC platform is used for the ShinUlchin units 1,2 PPS and CPCS. In developing the next generation safety system platform, several factors (e.g., hardware/software reliability, flexibility, licensibility and industrial support) can be considered. This paper suggests an Industrial Computer(IC) based protection system that can be developed with improved flexibility without losing system reliability. The IC based system has the advantage of a simple system configuration with optimized processor boards because of improved processor performance and unlimited interoperability between the target system and development system that use commercial CASE tools. This paper presents the background to selecting the IC based system with a case study design of the CPCS. Eventually, this kind of platform can be used for nuclear power plant safety systems like the PPS, CPCS, Qualified Indication and Alarm . Pami(QIAS-P), and Engineering Safety

  17. Accidental safety analysis methodology development in decommission of the nuclear facility

    Energy Technology Data Exchange (ETDEWEB)

    Park, G. H.; Hwang, J. H.; Jae, M. S.; Seong, J. H.; Shin, S. H.; Cheong, S. J.; Pae, J. H.; Ang, G. R.; Lee, J. U. [Seoul National Univ., Seoul (Korea, Republic of)

    2002-03-15

    Decontamination and Decommissioning (D and D) of a nuclear reactor cost about 20% of construction expense and production of nuclear wastes during decommissioning makes environmental issues. Decommissioning of a nuclear reactor in Korea is in a just beginning stage, lacking clear standards and regulations for decommissioning. This work accident safety analysis in decommissioning of the nuclear facility can be a solid ground for the standards and regulations. For source term analysis for Kori-1 reactor vessel, MCNP/ORIGEN calculation methodology was applied. The activity of each important nuclide in the vessel was estimated at a time after 2008, the year Kori-1 plant is supposed to be decommissioned. And a methodology for risk analysis assessment in decommissioning was developed.

  18. Pressure tube replacement in Pickering NGS A units 1 and 2

    International Nuclear Information System (INIS)

    Irvine, H.S.; Bennett, E.J.; Talbot, K.H.

    1986-10-01

    Being able to technically and economically replace the most radioactive components (excluding the nuclear fuel) in operating reactors will help to ensure the ongoing acceptance of nuclear power as a viable energy source for the future. Ontario Hydro is well along the path to meeting the above objective for its CANDU-PHW reactors. Following the failure of a Zircaloy-II pressure tube in unit 2 of Pickering NGS A in August, 1983, Ontario Hydro has embarked on a program to replace all Zircaloy-II pressure tubes in units 1 and 2 at Pickering. This program integrates the in-house research, design, construction, and operating skills of a large utility (Ontario Hydro) with the skills of a national nuclear organization (Atomic Energy of Canada Limited) and the private engineering sector of the Canadian nuclear industry. The paper describes the background to the pressure tube failure in Pickering unit 2 and to the efforts incurred in understanding the failure mechanism and how similar failures are not expected for the zirconium-niobium pressure tube material used in all other large CANDU-PHW units after units 1 and 2 of Pickering NGS A. The tooling developed for the pressure tube replacement program is described as well as the organization to undertake the program in an operating nuclear station. The retubing of units 1 and 2 at Pickering NGS A is nearing a successful completion and shows the benefits of being able to integrate the various skills required for this success. Pressure tube replacement in a CANDU-PHW reactor is equivalent to replacement of the reactor vessel in a LWR. The fact that this replacement can be done economically and with acceptable radiation dose to workers augurs well for the continued viability of the use of nuclear energy for the benefit of mankind. (author)

  19. NPP Mochovce units 1 and 2 diagnostic systems

    International Nuclear Information System (INIS)

    Heidenreich, S.

    1997-01-01

    In this paper the diagnostic systems (leak detection monitoring, vibration monitoring, lose parts monitoring, fatigue monitoring) of NPP Mochovce units 1 and 2 are presented. All of the designed diagnostic systems are personal computer based systems

  20. Improvement and test of alarm cause tracking system for Kori nuclear power plant units 3 and 4

    International Nuclear Information System (INIS)

    Lee, Jung Woon; Park, Jae Chang; Lee, Jung Woon; Kim, Jung Taek; Lyu, Sung Pil; Kim, Eun Ju; Park, Joong Pal

    2003-05-01

    The proposed system, ACTS(Alarm Cause Tracking System), in the 1st development period(2002. 7 ∼ 2003. 6), tracks and displays the causes of alarms on-line from computerized logic diagrams. And the system highlights the specific procedures related the causes in the procedure of the alarm. But, some problems were found in ACTS on editing logic diagram and logic processing in realtime for 2000 logic diagrams. In 2nd development period, we improved the data structure of graphic information for logic diagram and changed function oriented programming to object oriented programming for logic elements. Also, the display of precedent alarms which introduce many following alarms is provided to avoid confusion from the followed nuisance alarms. And logic input signal generator was developed to test the ACTS which generates input signal in time sequence of events acquired from simulator or real plant

  1. Nuclear Power Plant Lifetime Management Study (I)

    Energy Technology Data Exchange (ETDEWEB)

    Hong, Sung Yull; Jeong, Ill Seok; Jang, Chang Heui; Song, Taek Ho; Song, Woo Young [Korea Electric Power Research Institute, Taejon (Korea, Republic of); Jin, Tae Eun [Korea Power Engineering Company Consulting and Architecture Engineers, (Korea, Republic of); Kim, Woo Chul [Korea Atomic Energy Research Institute, Taejon (Korea, Republic of)

    1997-12-31

    As the operation-year of nuclear power plant increases and finding sites for new nuclear power plant becomes harder, a comprehensive and systematic nuclear plant lifetime management(PLIM) program including life extension has to be established for stable and safe supply of electricity. A feasibility study was conducted to systematically evaluate technical, economic and regulatory aspect of plant lifetime managements and plant life extension for Kori-1 nuclear power plant. For technical evaluation of nuclear power plant, 13 major components were selected for lifetime evaluation by screening system. structure, and components(SSCs) of the plant. It was found that except reactor pressure vessel, which needs detailed integrity analysis, and low pressure turbine, which is scheduled to be replaced, 11 out of 13 major components have sufficient service life, for more than 40 years. Because domestic rules and regulations related to license renewal has not yet been written, review on the regulatory aspect of life extensions was conducted using US NRC rules and regulations. A cooperative effort with nuclear regulatory body is needed for early completion of license renewal rules and regulations. For economic evaluation of plant lifetime extension, a computer program was developed and used. It was found that 10 to 20 year of extension operation of Kori-1 nuclear power plant was proved. Based on the results, next phase of plant lifetime management program for detailed lifetime evaluation and presenting detailed implementation schedule for plant refurbishment for lifetime extension should be followed. (author). 74 refs., figs.

  2. Nuclear Power Plant Lifetime Management Study (I)

    Energy Technology Data Exchange (ETDEWEB)

    Hong, Sung Yull; Jeong, Ill Seok; Jang, Chang Heui; Song, Taek Ho; Song, Woo Young [Korea Electric Power Research Institute, Taejon (Korea, Republic of); Jin, Tae Eun [Korea Power Engineering Company Consulting and Architecture Engineers, (Korea, Republic of); Kim, Woo Chul [Korea Atomic Energy Research Institute, Taejon (Korea, Republic of)

    1996-12-31

    As the operation-year of nuclear power plant increases and finding sites for new nuclear power plant becomes harder, a comprehensive and systematic nuclear plant lifetime management(PLIM) program including life extension has to be established for stable and safe supply of electricity. A feasibility study was conducted to systematically evaluate technical, economic and regulatory aspect of plant lifetime managements and plant life extension for Kori-1 nuclear power plant. For technical evaluation of nuclear power plant, 13 major components were selected for lifetime evaluation by screening system. structure, and components(SSCs) of the plant. It was found that except reactor pressure vessel, which needs detailed integrity analysis, and low pressure turbine, which is scheduled to be replaced, 11 out of 13 major components have sufficient service life, for more than 40 years. Because domestic rules and regulations related to license renewal has not yet been written, review on the regulatory aspect of life extensions was conducted using US NRC rules and regulations. A cooperative effort with nuclear regulatory body is needed for early completion of license renewal rules and regulations. For economic evaluation of plant lifetime extension, a computer program was developed and used. It was found that 10 to 20 year of extension operation of Kori-1 nuclear power plant was proved. Based on the results, next phase of plant lifetime management program for detailed lifetime evaluation and presenting detailed implementation schedule for plant refurbishment for lifetime extension should be followed. (author). 74 refs., figs.

  3. Fukushima Daiichi Unit 1 power plant containment analysis using GOTHIC

    International Nuclear Information System (INIS)

    Ozdemir, Ozkan Emre; George, Thomas L.; Marshall, Mervin D.

    2015-01-01

    Highlights: • The inclusion of vent heat transfer had a significant impact on the overall containment response. • The vent heat transfer and condensation results in lower containment pressure. • The reduced gas transfer to the wetwell via the vents results in higher hydrogen concentration in the drywell. - Abstract: This paper is a part of Fukushima Technical Evaluation Project (EPRI, 2013a, 2014a, 2015) which investigates various aspects of the Fukushima Daiichi event using the GOTHIC code. The analysis takes advantage of the capability of GOTHIC to model certain aspects of the system geometry and behavior in more detail than typically considered in containment performance analysis. GOTHIC is a general purpose thermal hydraulics code that is used extensively in the nuclear industry for system design support, licensing support and safety analysis. It has the capability to model 3-dimensional flow behavior including the effects of turbulence, diffusion and buoyancy (EPRI, 2014b). This allows GOTHIC to be used in cases where mixing effects and stratification are important. The analysis presented here considers the events at Fukushima Daiichi Unit 1 (1F1) following the tsunami and leading up to the time of the hydrogen detonation in the 1F1 Reactor Building. The 1F1 MAAP5 Baseline Scenario (EPRI, 2013b) is used to define the steam, hydrogen and carbon-monoxide source terms from the primary system and the core concrete interaction. The model incorporates three dimensional modeling of the drywell, wetwell and connecting vent system that can predict the 3-dimensional flow patterns and the temperature and gas distributions. The model also includes leakage to the surrounding reactor building and the wetwell vent to the stack. The 3D containment model includes models for the heat transfer from the steam and gas in the drywell vent system to the torus room, wetwell gas space and pool. Inclusion of vent heat transfer had a significant impact on the overall containment

  4. Fessenheim 2: ASN's green light for continuing operation - Beginning of the works for unit 1

    International Nuclear Information System (INIS)

    Anon.

    2013-01-01

    Every 10 years a nuclear power plant operator has to make a re-assessment of the nuclear safety standard of his plant. This re-assessment is made of 2 parts: first the review of the safety conformity and secondly a thorough re-examination of the safety that takes into account today's safety standards and feedback experience from similar plants. This detailed assessment of the safety aims at checking that the consequences of the different aging phenomena are well mastered for the next 10 years at least. At the end of this re-assessment, the ASN (French Nuclear Safety Authorities) decide or not the continuation of plant activity or can prescribe safety improvements. In the case of the unit 2 of the Fessenheim plant that has just finished its third decennial safety re-assessment, the ASN has prescribed the same improvements as for the unit 1, that is to say the reinforcement of the resistance to corium of the foundation raft and an improvement on the emergency cooling system. The works on the unit 1 have begun despite contestation from anti-nuclear associations that question the cost of the safety upgrading (20 to 30 millions euros) while the unit is expected to be decommissioned by end 2016. (A.C.)

  5. Audit of Wolf Creek Generating Station, Unit 1 technical specifications. Final technical evaluation report

    International Nuclear Information System (INIS)

    Stromberg, H.M.

    1985-07-01

    This document was prepared for the Nuclear Regulatory Commission (NRC) to assist them in determining whether the Wolf Creek Generating Station Unit 1 Technical Specifications (T/S), which govern plant systems configurations and operations, are in conformance with the assumptions of the Final Safety Analysis Report (FSAR) as amended, the requirements of the Safety Evaluation Report (SER) as supplemented, and the Comments and Responses to the Wolf Creek Technical Specification Draft Inspection Report. A comparative audit of the FSAR as amended, the SER as supplemented, and the Draft Inspection Report was performed with the Wolf Creek T/S. Several discrepancies were identified and subsequently resolved through discussions with the cognizant NRC reviewer, NRC staff reviewers and/or utility representatives. The Wolf Creek Generating Station Unit 1 T/S, to the extent reviewed, are in conformance with the FSAR, SER, and Draft Inspection Report

  6. Development of Regulatory Audit Programs for Wolsong Unit 1 Continued Operation

    Energy Technology Data Exchange (ETDEWEB)

    Kim, Hong Key; Nho, Seung Hwan; Song, Myung Ho [Korea Institute of Nuclear Safety, Daejeon (Korea, Republic of)

    2012-05-15

    Wolsong Unit 1 (PHWR type) design life expires on November 20, 2010. In relation to it, KHNP submitted its application to get approval of the MEST on December 30, 2009 and KINS is under review to confirm the appropriateness of continued operation. For the comprehensive review of Wolsong Unit 1 continued operation, KINS has developed the review guidelines for PHWR type reactor including a total of 39 aging management program (AMP) items and 7 time limited aging analysis (TLAA) items. Evaluations or calculations to verify the integrity of nuclear components are required for plant specific AMP and TLAA items as well as the ones specified in the guidelines. In this paper, audit calculation programs developed for KINS staff use in reviewing applicant's submitted evaluation results are presented

  7. Evaluation of severe accident risks, Grand Gulf, Unit 1: Main report

    International Nuclear Information System (INIS)

    Brown, T.D.; Breeding, R.J.; Jow, H.N.; Higgins, S.J.; Shiver, A.W.; Helton, J.C.; Amos, C.N.

    1990-12-01

    In support of the Nuclear Regulatory Commission's (NRC's) assessment of the risk from severe accidents at commercial nuclear power plants in the US report in NUREG-1150, the Severe Accident Risk Reduction Program (SARRP) has completed a revised calculation of the risk to the general public from severe accidents at the Grand Gulf Nuclear Station, Unit 1. This power plant, located in Port Gibson, Mississippi, is operated by the System Energy Resources, Inc. (SERI). The emphasis in this risk analysis was not on determining a ''so-called'' point estimate of risk. Rather, it was to determine the distribution of risk, and to discover the uncertainties that account for the breadth of this distribution. Off-site risk initiated by events internal to the power plant was assessed. 42 refs., 51 figs., 52 tabs

  8. Newman Unit 1 advanced solar repowering. Final report

    Energy Technology Data Exchange (ETDEWEB)

    None

    1982-04-01

    The five appendices give the selection process and system specification of the Newman Unit 1 solar repowering system, including the conceptual design drawings and diagrams; input data for the simulation program; and a review of the most important characteristics of the existing plant. (LEW)

  9. Balancing preventive and corrective maintenance in Cernavoda Unit 1 NPP

    International Nuclear Information System (INIS)

    Riedel, M.; Marinescu, S.

    2000-01-01

    The paper presents a short reminder of Romania's Cernavoda NPP entering commercial operation and a brief description of the CANDU-6 project on which Unit 1 is based. The short term objectives of the maintenance management, the status of the existing maintenance programmes as well as future predictable maintenance programmes are outlined together with the Government plan to complete the balance of NPP. (author)

  10. Current status and future prospects of Korean standardized nuclear power plant design

    International Nuclear Information System (INIS)

    Rieh, C.-H.; Park, S.-K.; Lee, B.-R.

    1992-01-01

    The authors reviewed a brief history of Korean nuclear industry since the first Kori-1 plant operation in 1978 with special emphasis on the NSSS and BOP design and engineering, and the design approaches for nuclear power plants in the future. Continued effort to enhance plant economy and operational safety has been made by increasing plant size, and improving safety features, systems and component reliability in various design aspects. Korean nuclear industry is now trying to be one of the major contributors to the world nuclear field in sharing nuclear technology gained from past experience and developed through internation technical cooperation programs

  11. Review of the Shearon Harris Unit 1 auxiliary feedwater system reliability analysis

    International Nuclear Information System (INIS)

    Fresco, A.; Youngblood, R.; Papazoglou, I.A.

    1986-02-01

    This report presents the results of a review of the Auxiliary Feedwater System Reliability Analysis for the Shearon Harris Nuclear Power Plant (SHNPP) Unit 1. The objective of this report is to estimate the probability that the Auxiliary Feedwater System will fail to perform its mission for each of three different initiators: (1) loss of main feedwater with offsite power available, (2) loss of offsite power, (3) loss of all ac power except vital instrumentation and control 125-V dc/120-V ac power. The scope, methodology, and failure data are prescribed by NUREG-0611 for other Westinghouse plants

  12. Evaluation of power commissioning of the Mochovce Unit 1 demonstration run

    International Nuclear Information System (INIS)

    Sarvaic, I.; Miskolci, M.

    1998-01-01

    The document contains evaluation of the 144 hour demonstration run of the Mochovce Unit 1. In the document, the courses and results of additional tests in this phase of power commissioning are summarized, evaluation of the performance of important systems and equipment of the unit is carried out, as well as of the compliance with Limits and Conditions in the course of the demonstration run. On this basis, conclusions are drawn and recommendations given for the unit to by ready for trial operation. The evaluation was developed by the scientific management of the Mochovce commissioning providing an independent support for the operators for supervising the commissioning tasks from the point of nuclear safety

  13. Control room habitability Analysis and Testing for Wolsong Unit 1

    Energy Technology Data Exchange (ETDEWEB)

    Lee, J. B. [KHNP Central Research Institute, Daejeon (Korea, Republic of)

    2013-05-15

    In response to this recommendation, KHNP has established CRH program and performed tracer gas in leakage tests. These activities are described herein including the emergency ventilation system analysis, acceptance criteria calculation for the test and Control Room Envelope (CRE) discrimination, and the results of the tracer gas tests are presented. CRH analysis including unfiltered in leakage tests according to the methodology in ASTM E741 was performed for Wolsong Unit 1. The results show that the integrity of the control room of Wolsong Unit 1 is in good condition to maintain the reactor in a safe condition under accident conditions, which complies with the US NRC regulatory guides 1.78, 1.196 and 1.197.

  14. Bruce unit 1 moderator to end shield cooling leak repairs

    Energy Technology Data Exchange (ETDEWEB)

    Boucher, P; Ashton, A [Ontario Hydro, Tiverton, ON (Canada). Bruce Nuclear Generating Station-A

    1996-12-31

    In October 1994, a leak developed between the heavy water Moderator System and the light water End Shield Cooling System at Ontario Hydro`s Bruce A Generating Station Unit 1. The interface between these two systems consists of numerous reactor components all within the reactor vessel. This paper describes the initial discovery and determination of the leak source. The techniques used to pinpoint the leak location are described. The repair strategies and details are outlined. Flushing and refilling of the Moderator system are discussed. The current status of the Unit 1 End Shield Cooling System is given with possible remedial measures for clean-up. Recommendations and observations are provided for future references. (author). 7 figs.

  15. Flux distribution measurements in the Bruce A unit 1 reactor

    International Nuclear Information System (INIS)

    Okazaki, A.; Kettner, D.A.; Mohindra, V.K.

    1977-07-01

    Flux distribution measurements were made by copper wire activation during low power commissioning of the unit 1 reactor of the Bruce A generating station. The distribution was measured along one diameter near the axial and horizontal midplanes of the reactor core. The activity distribution along the copper wire was measured by wire scanners with NaI detectors. The experiments were made for five configurations of reactivity control mechanisms. (author)

  16. Rehabilitation and modernization project of units 1 and 2 of Laguna Verde Nuclear Power Plant. A strengthening project to 120%. (2nd phase); Proyecto de rehabilitacion y modernizacion de las Unidades 1and 2 de la CNLV. Un proyecto de reponteciacion al 120% (2ª Fase)

    Energy Technology Data Exchange (ETDEWEB)

    Liebana, B.; Merino, A.; Garcia, J. L.; Gomez, M.; Martinez, I.; Ruiz, L.

    2010-07-01

    The power increase of the Laguna Verde Nuclear Power Plant is a project for the rehabilitation and modernization of the turbo and associated equipment to get an increase of its power and of its service life. The project scope includes the design, the engineering, the equipment supply, the installation, the testing and the commissioning. This article presents the work of the second phase.

  17. Neutron embrittlement of the Kozloduy NPP unit 1 reactor

    International Nuclear Information System (INIS)

    Vodenicharov, S.; Kamenova, Tz.

    1996-01-01

    Activities made in the period 1989-1996 according to the Program for metal state monitoring of the Kozloduy NPP Unit 1 are described. Data on P and Cu content in the welded joint 4 are reported. Determination is made by wet chemical analysis of shavings taken out from the inner side of the wall, direct spectral analysis of the vessel itself and spectroscopy of the inner and outer side of 6 templates. The results obtained from 4 different study teams showed a good agreement. The real average P content is 0.046% and tends to diminish in depth. Microstructural investigation does not show any expressed inter-crystalline mechanism of brittle failure at low temperatures. The data on real P and Cu content, as well as the experimental values of the initial critical temperature of embrittlement (Tk o ), the residual part of temperature shift (Tk r ) and the re-embrittlement temperature after annealing at 475 o (Tk) allow to predict the change in Tk o of the joint 4 during the next refueling cycles. The measured low value of Tk after 18-th refueling cycle is considerably lower than that forecasted by lateral re-embrittlement law. This means that the forecasting of Tk for the next cycles is made with big enough conservatisms, and that a second annealing of the vessel until 26-th cycle is not necessary. So according to the most conservative estimate, the Unit 1 can operate safely until the end of the 26-th refueling cycle. It is also concluded, that in terms of radiation degradation of the vessel metal the operation life time of the Unit 1 can reach and exceed the designed one. 2 tab., 7 ref

  18. Steam generator leak detection at Bruce A Unit 1

    International Nuclear Information System (INIS)

    Maynard, K.J.; McInnes, D.E.; Singh, V.P.

    1997-01-01

    A new steam generator leak detection system was recently developed and utilized at Bruce A. The equipment is based on standard helium leak detection, with the addition of moisture detection and several other capability improvements. All but 1% of the Unit 1 Boiler 03 tubesheet was inspected, using a sniffer probe which inspected tubes seven at a time and followed by individual tube inspections. The leak search period was completed in approximately 24 hours, following a prerequisite period of several days. No helium leak indications were found anywhere on the boiler. A single water leak indication was found, which was subsequently confirmed as a through-wall defect by eddy current inspection. (author)

  19. Startup physics tests at Temelin NPP, Unit 1

    International Nuclear Information System (INIS)

    Sedlacek, M.; Minarcin, M.; Toth, L.; Elko, M.; Hascik, R.

    2002-01-01

    The objective, scope and proceedings of the physics tests of Temelin NPP, Unit 1 physical commissioning are given in this paper. Furthermore, some results of selected physics tests are presented: reactor initial criticality test, determination of reactor power range for physics testing, measurement of control rod cluster assembly group no. 10 reactivity worth in case of limitation system LS(a) actuation, control rod cluster assembly system reactivity worth measurement with single rod cluster assembly of greatest reactivity worth stuck in fully withdrawn position, measurement of differential reactivity worth of control rod cluster assembly group no. 9, boron 'endpoint' determination and measurement of power reactivity coefficient (Authors)

  20. Steam generator replacement in Bruce A Unit 1 and Unit 2

    International Nuclear Information System (INIS)

    Hart, R.S.

    2006-01-01

    The Bruce A Generating Station consists of four 900 MW class CANDU units. The reactor and Primary Heat Transport System for each Unit are housed within a reinforced concrete reactor vault. A large duct running below the reactor vaults accommodates the shared fuel handling system, and connects the four reactor vaults to the vacuum building. The reactor vaults, fuelling system duct and the vacuum building constitute the station vacuum containment system. Bruce A Unit 2 was shut down in 1995 and Bruce A Units 1, 3 and 4 were shutdown in 1997. Bruce A Units 3 and 4 were returned to service in late 2003 and are currently operating. Units 1 and 2 remain out of service. Bruce Power is currently undertaking a major rehabilitation of Bruce A Unit 1 and Units 2 that will extend the in-service life of these units by at least 25 years. Replacement of the Steam Generators (eight in each unit) is required; this work was awarded to SNC-Lavalin Nuclear (SLN). The existing steam drums (which house the steam separation and drying equipment) will be retained. Unit 2 is scheduled to be synchronized with the grid in 2009, followed by Unit 1 in 2009. Each Bruce A unit has two steam generating assemblies, one located above and to each end of the reactor. Each steam generating assembly consists of a horizontal cylindrical steam drum and four vertical Steam Generators. The vertical Steam Generators connect to individual nozzles that are located on the underside of the Steam Drum (SD). The steam drums are located in concrete shielding structures (steam drum enclosures). The lower sections of the Steam Generators penetrate the top of the reactor vaults: the containment pressure boundary is established by bellows assemblies that connect between the reactor vault roof slab and the Steam Generators. Each Steam Generators is supported from the bottom by a trapeze that is suspended from the reactor vault top structure. The Steam Generator Replacement (SGR) methodology developed by SLN for Unit 1

  1. MINAC radiography performed on susquehanna Steam Electric Station Unit 1

    International Nuclear Information System (INIS)

    Bognet, J.C.

    1986-01-01

    Ten welds were volumetrically examined with a manual and automated ultrasonic (UT) system during a Susquehanna Steam Electric Station (SES) Unit 1 preservice inspection. The automated system had been recently developed and several problems were encountered in this first field application. The ten welds examined had a Sweepolet-to-Risor weld configuration, which further complicated the examination effort. This weld configuration has corrosion-resistant cladding applied to the outside and inside circumference and, as a result of an installation/removal/reinstallation sequence during plant construction, is often referred to as the double weld. After several attempts to obtain interpretable UT data failed (e.g., repeatable data), the examination effort was terminated. PP and L opted to pursue using the Miniature Linear Accelerator (MINAC) to perform radiographic examination. The results were referenced in the Susquehanna SES Unit 1 outage summary report and submitted to the NRC. The total effort was viewed as a complete success with no impact to the overall outage duration. All welds previously attempted by automated and manual UT were successfully examined using the MINAC

  2. Safety Evaluation for the Impact of Strom Surges on Nuclear Facilities considering the Climate Change

    International Nuclear Information System (INIS)

    Hyun, Seung Gyu; Jin, So Beom

    2012-01-01

    Twenty one units of Nuclear Power Plants(hereinafter NPPs) are operating and five units are under construction in Korea. In particular, Kori unit 1 has been operating for over 30 years. All of the interior NPPs are located in coastal areas and use the sea water for the cooling system. Therefore, the change of sea level seem to affect the safety of NPPs in case of a flood(Hyun et al., 2009). The IPCC 4 th Report(2007) showed that the climate change induced by the high CO 2 effluent scenario results in rise of the sea level (+ 26 to 59 cm), increase in wind strength and more increase of typhoon intensity in the period between 2090 and 2099 and the rate of global mean sea level rise was up to 1.8 ± 0.5 mm/yr from 1961 to 2003. Kang et al.(2005) reported that the rise rate of sea level was 5.4 ± 0.3 mm/yr at the entire East Sea and was 6.6 ± 0.4 mm/yr for the southern part of East Sea from 1992 to 2002. These results are approximately four times greater than the results of the IPCC 4 th Report. The IAEA recommends that some safety margin related with climate change should be taken into consideration in the design basis flood for constructing new NPPs considering the entire plant lifetime and for periodic safety reviewing of operating NPPs referring to the interval between two consecutive reviews(2003). This paper, therefore, summarized the current regulatory activities related with the safety assessment of the impact of storm surge on the NPPs with climate change

  3. Safety Evaluation for the Impact of Strom Surges on Nuclear Facilities considering the Climate Change

    Energy Technology Data Exchange (ETDEWEB)

    Hyun, Seung Gyu; Jin, So Beom [Korea Institute of Nuclear Safety, Daejeon (Korea, Republic of)

    2012-05-15

    Twenty one units of Nuclear Power Plants(hereinafter NPPs) are operating and five units are under construction in Korea. In particular, Kori unit 1 has been operating for over 30 years. All of the interior NPPs are located in coastal areas and use the sea water for the cooling system. Therefore, the change of sea level seem to affect the safety of NPPs in case of a flood(Hyun et al., 2009). The IPCC 4{sup th} Report(2007) showed that the climate change induced by the high CO{sub 2} effluent scenario results in rise of the sea level (+ 26 to 59 cm), increase in wind strength and more increase of typhoon intensity in the period between 2090 and 2099 and the rate of global mean sea level rise was up to 1.8 {+-} 0.5 mm/yr from 1961 to 2003. Kang et al.(2005) reported that the rise rate of sea level was 5.4 {+-} 0.3 mm/yr at the entire East Sea and was 6.6 {+-} 0.4 mm/yr for the southern part of East Sea from 1992 to 2002. These results are approximately four times greater than the results of the IPCC 4{sup th} Report. The IAEA recommends that some safety margin related with climate change should be taken into consideration in the design basis flood for constructing new NPPs considering the entire plant lifetime and for periodic safety reviewing of operating NPPs referring to the interval between two consecutive reviews(2003). This paper, therefore, summarized the current regulatory activities related with the safety assessment of the impact of storm surge on the NPPs with climate change

  4. Prevention of nuclear fuel cladding materials corrosion

    International Nuclear Information System (INIS)

    Yang, K.R.; Yang, J.C.; Lee, I.C.; Kang, H.D.; Cho, S.W.; Whang, C.K.

    1983-01-01

    The only way which could be performed by the operator of nuclear power plant to minimizing the degradation of nuclear fuel cladding material is to control the water quality of primary coolant as specified standard conditions which dose not attack the cladding material. If the water quality of reactor coolant does not meet far from the specification, the failure will occure not only cladding material itself but construction material of primary system which contact with the coolant. The corrosion product of system material are circulate through the whole primary system with the coolant and activated by the neutron near the reactor core. The activated corrosion products and fission products which released from fuel rod to the coolant, so called crud, will repeate deposition and redeposition continuously on the fuel rod and construction material surface. As a result we should consider heat transfer problem. In this study following activities were performed; 1. The crud sample was taken from the spent fuel rod surface of Kori unit one and analized for radioactive element and non radioactive chemical species. 2. The failure mode of nuclear fuel cladding material was estimated by the investigation of releasing type of fission products from the fuel rod to the reactor coolant using the iodine isotopes concentration of reactor coolants. 3. A study was carried out on the sipping test results of spent fuel and a discussion was made on the water quality control records through the past three cycle operation period of Kori unit one plant. (Author)

  5. Aging management strategy for reactor internals of Korean nuclear power plants

    International Nuclear Information System (INIS)

    Hwang, Seong Sik; Kim, Soung Woo; Lee, Sam Lai; Hong, Seung Mo; Kim, Hong Pyo; Kim, Dong Jin; Lim, Yun Soo; Kim, Joung Soo; Jung, Man Kyo; Park, Jang Yul

    2010-01-01

    This report describes various factors on the IASCC of reactor internals in terms of fluence, stress, water chemistries and materials. Materials of each components of Korean nuclear power plants have been surveyed. A technical report for a management of reactor internals issued by EPRI was reviewed for a selection of most susceptible area among many components. Baffle former bolts are considered to be the most susceptible parts due to high irradiation level(fluence) and high tensile stress. Neutron fluence of Kori-1 and Kori-2 was calculated based on fuel exchange history, fuel performance and plant operation history. This report will be used for more advanced inspection and maintenance guidelines development by supplying inspection intervals and components (most susceptible regions) for the long term operation plants

  6. An integrated framework for effective reduction of occupational radiation exposure in a nuclear power plant

    International Nuclear Information System (INIS)

    Joo, Hyun Moon; Hak, Soo Kim; Young, Ho Cho; Chang, Sun Kang

    1998-01-01

    For effective reduction of occupational radiation exposure in a nuclear power plant, it is necessary to identify repetitive high radiation jobs during maintenance and refueling operation and comprehensively assess them. An integrated framework for effective reduction of occupational radiation exposure is proposed in this study. The framework consists of three parts; data collection, statistical analysis, and ALARA findings. A PC-based database program, INSTORE, is used for data collection and reduction, and the Rank Sum Method is used in identifying high radiation jobs. As a case study, the data accumulated in Kori Units 3 and 4 have been analyzed. The results of this study show that the radiation job classifications of SG related work have much effect on annual ORE collective dose in Kori Units 3 and 4. As an example of ALARA findings, hence, the improvements for the radiation job classifications of SG related work are summarized

  7. Wolsong Unit 1 restart chemistry procedures during retubing outage

    International Nuclear Information System (INIS)

    Yun, Hyunran; Lee, Sarang; Moon, Yunyong; Kim, Seoyul

    2015-01-01

    Lay-up is aimed at protecting systems from degradation during outage, mainly by minimizing corrosion and particularly, when the outage is longer than 16 weeks. Due to the intrinsic design of CANDU reactors, their horizontal fuel channels should be replaced for another service life time. This poster presents the lay-up guidelines and methods recommended for re-tubing outage based on the first re-tubing operation made in Korea (at the Wolsung Unit 1). It is shown that dry lay-up with specific gas blanket was the sole choice for the primary heat transfer system, the moderator system and the steam cycle system while wet lay-up under circulation was recommended for the end shield cooling system and the liquid zone control system. The water filled part of steam generators, of the liquid zone control system and of the end shield cooling system was maintained normal

  8. Impact on the bar value in hot by the introduction of advanced control bars in the Unit 1 of the Laguna Verde Nuclear power plant; Impacto sobre el valor de barra en caliente por la introduccion de barras de control avanzadas en la U1 de la CNLV

    Energy Technology Data Exchange (ETDEWEB)

    Montes, J.L.; Perusquia, R.; Ortiz, J.J.; Hernandez, J.L.; Ramirez, J.R. [ININ, Carretera Mexico-Toluca Km. 36.5, 52045 Estado de Mexico (Mexico)]. e-mail: jlmt@nuclear.inin.mx

    2004-07-01

    In recent dates the Laguna Verde Nuclear Power station (CNLV) has acquired new designs of control bars, this new type of bars presents modifications important in their design. For what is important to analyze their performance inside those reactors of this nuclear power station. Presently work is shown the behavior of the nucleus of the reactor in hot condition (HFP) when three different types of control bar are used. The first of them corresponds the one that initially has been used in this power station and that we will call original. The second type of control bars, it corresponds to an advanced type and it is the first design different from the original and it corresponds to a bar design that it includes Hafnium (Hf) like one of their neutronic absorption characteristics. The third, denoted as 2AV, include besides the material of the second type new design characteristics, and it is the last finish bar type that it has been introduced in the operation of the reactors of the CNLV. With base in the studied cases is found that the bars 2AV have a total power value, 7.6 % bigger respect the bars 1AV; and in turn the bars 1AV, 6.1 % bigger with respect the ORG control bars. (Author)

  9. Development of diagnostic process for abnormal conditions of Ulchin units 1 and 2

    Energy Technology Data Exchange (ETDEWEB)

    Choi, Hyun Soo; Kwak, Jeong Keun; Yun, Jung Hyun; Kim, Jong Hyun [KEPCO International Nuclear Graduate School, Ulsan (Korea, Republic of)

    2012-10-15

    Diagnosis of abnormal conditions during operation is one of difficult tasks to nuclear power plant operators. Operators may have trouble in handling abnormal conditions due to various reasons such as 1) many alarms (around 2,000 alarms in the Ulchin units 1 and 2 each) and multi alarms occurrences, 2) the same alarms occurrences in different abnormal conditions, and 3) a number of Abnormal Operating Procedures (AOPs). For these reasons, the first diagnosis on abnormal conditions largely relies on operator's experiences and pattern recognition. Then, this difficulty may be highlighted for inexperienced operators. This paper suggests an approach to develop the optimal diagnostic process for appropriate selection of AOPs by using the Elimination by Aspect (EBA) method. The EBA method uses a heuristic followed by decision makers during a process of sequential choice and which constitutes a good balance between the cost of a decision and its quality. At each stage of decision, the individuals eliminate all the options not having an expected given attribute, until only one option remains. This approach is applied to steam generator level control system abnormal procedure for Ulchin units 1 and 2. The result indicates that the EBA method is applicable to the development of optimal process on diagnosis of abnormal conditions.

  10. Level 1 shutdown and low power operation of Mochovce NPP, Unit 1, Slovakia

    International Nuclear Information System (INIS)

    Halada, P.; Cillik, I.; Stojka, T.; Kuzma, M.; Prochaska, J.; Vrtik, L.

    2004-01-01

    The paper presents general approach, used methods and form of documentation of the results that have been applied within the shutdown and low power PSA (SPSA) study for Mochovce NPP, Unit 1, Slovakia. The SPSA project was realized by VUJE Trnava Inc., Slovakia in 2001-2002 years. The Level 1 SPSA study for Mochovce NPP Unit 1 covers internal events as well as internal (fires, floods and heavy load drop) and external (aircraft crash, extreme meteorological conditions, seismic event and influence of surrounding industry) hazards. Mochovce NPP consists of two operating units equipped with VVER 440/V213 reactors safety upgraded before construction finishing and operation start. 87 safety measures based on VVER 440 operational experience and international mission insights were implemented to enhance its operational and nuclear safety. The SPSA relates to full power PSA (FPSA) as a continuation of the effort to create a harmonized level 1 PSA model for all operational modes of the plant with the goal to use it for further purposes as follows: Real Time Risk Monitor, Maintenance Optimization, Technical Specifications Optimization, Living PSA. (author)

  11. Report of the ASSET (Assessment of Safety Significant Events Team) follow-up mission to the Bohunice (units 1-2) nuclear power plant in Slovakia 5-9 July 1993. Root cause analysis of operational events with a view to enhancing the prevention of accidents

    International Nuclear Information System (INIS)

    1993-01-01

    This Report of the IAEA Assessment of Safety Significant Events Team (ASSET) presents the results of the team's review of the status of implementation of the recommendations made by the 1988 ASSET mission to Bohunice nuclear power plant in Slovakia, and of progress made by plant management in prevention of incidents. The findings, conclusions and suggestions presented herein reflect the views of the ASSET experts. They are provided for consideration by the responsible Slovakian authorities. The ASSET team's views presented in this report are based on review of the documentation made available and on the discussions with plant staff. The report includes the official response of the operating and regulatory organizations of Slovakia to the ASSET findings and conclusions. Figs, tabs

  12. Nuclear Regulatory Commission Issuances, September 1981

    International Nuclear Information System (INIS)

    1981-01-01

    Contents include: Issuances of the Nuclear Regulatory Commission--Commonwealth Edison Company (Dresden Nuclear Power Station, Unit 1), Consolidated Edison Company of New York (Indian Point, Unit 2), Metropolitan Edison Company, et al. (Three Mile Island Nuclear Station, Unit 1), Pacific Gas and Electric Company (Diablo Canyon Nuclear Power Plant, Units 1 and 2), Pacific Gas and Electric Company (Diablo Canyon Nuclear Power Plant, Units 1 and 2), Power Authority of the State of New York (Indian Point, Unit 3), Texas Utilities Generating Company, et al. (Comanche Peak Steam Electric Station, Units 1 and 2); Issuances of Atomic Safety and Licensing Appeal Boards--Pacific Gas and Electric Company (Diablo Canyon Nuclear Power Plant, Units 1 and 2), Philadelphia Electric Company, et al. (Peach Bottom Atomic Power Statin, Units 2 and 3), Metropolitan Edison Company, et al. (Three Mile Island Nuclear Statin, Unit No. 2), Public Service Electric and Gas Company (Hope Creek Generating Station, Units 1 and 2), The Toledo Edison Company, et al. (Davis-Besse Nuclear Power Station, Units 2 and 3); Issuances of the Atomic Safety Licensing Boards--Cleveland Electric Illuminating Company, et al. (Perry Nuclear Power Plant, Units 1 and 2), Commonwealth Edison Company (Dresden Station, Units 2 and 3), Houston Lighting and Power Company (Allens Creek Nuclear Generating Station, Unit 1), Southern California Edison Company, et al. (San Onofre Nuclear Generating Station, Units 2 and 3), Texas Utilities Generating Company, et al. (Comanche Peak Steam Electric Station, Units 1 and 2), Texas Utilities Generating Company, et al

  13. Radiological Effluent Technical Specifications (RETS) implementation: Zion Generating Station Units 1 and 2

    International Nuclear Information System (INIS)

    Serrano, W.; Akers, D.W.; Duce, S.W.; Mandler, J.W.; Simpson, F.B.; Young, T.E.

    1985-06-01

    A review of the Radiological Effluent Technical Specifications (RETS) of the Zion Generating Station Units 1 and 2 was performed. The principal review guidelines used were NUREG-0133, ''Preparation of Radiological Effluent Technical Specifications for Nuclear Power Plants,'' and Draft 7 of NUREG-0472, Revision 3, ''Radiological Effluent Technical Specifications for Pressurized Water Reactors.'' Draft submittals were discussed with the Licensee by both EG and G and the NRC staff until all items requiring changes to the Technical Specifications were resolved. The Licensee then submitted final proposed RETS to the NRC which were evaluated and found to be in compliance with the NRC review guidelines. The proposed Offsite Dose Calculation Manual was reviewed and generally found to be consistent with the NRC review guidelines. 35 refs., 2 figs., 1 tab

  14. Fukushima Daiichi unit 1 uncertainty analysis--Preliminary selection of uncertain parameters and analysis methodology

    Energy Technology Data Exchange (ETDEWEB)

    Cardoni, Jeffrey N.; Kalinich, Donald A.

    2014-02-01

    Sandia National Laboratories (SNL) plans to conduct uncertainty analyses (UA) on the Fukushima Daiichi unit (1F1) plant with the MELCOR code. The model to be used was developed for a previous accident reconstruction investigation jointly sponsored by the US Department of Energy (DOE) and Nuclear Regulatory Commission (NRC). However, that study only examined a handful of various model inputs and boundary conditions, and the predictions yielded only fair agreement with plant data and current release estimates. The goal of this uncertainty study is to perform a focused evaluation of uncertainty in core melt progression behavior and its effect on key figures-of-merit (e.g., hydrogen production, vessel lower head failure, etc.). In preparation for the SNL Fukushima UA work, a scoping study has been completed to identify important core melt progression parameters for the uncertainty analysis. The study also lays out a preliminary UA methodology.

  15. Evaluation of power commissioning of the Mochovce Unit 1 power level up to 100 % Nnom

    International Nuclear Information System (INIS)

    Sarvaic, I.; Mickolci, M.

    1998-01-01

    The document contains an evaluation of the power phase of power commissioning of the Mochovce Unit 1 in the phase up to the power level of 100 % N nom .In the document, the courses and results of tests in this phase of power commissioning are summarized, evaluation of the performance of important systems and equipment of the unit is carried out, and the compliance with Limits and Conditions in the course of the phase is assessed. On this basis, conclusions are drawn and recommendations for the unit to be ready for subsequent phases of the power commissioning. The evaluation was developed by the scientific management of the Mochovce commissioning providing an independent support for the operators for supervising the commissioning tasks from the point of nuclear safety

  16. Level 1 PSA study of Mochovce unit 1 NPP (SM AA 10 and 08)

    International Nuclear Information System (INIS)

    Cillik, I.

    1997-01-01

    This paper presents genesis of Level 1 PSA project preparation for all operational modes of Mochovce NPP unit 1 including the description of its' main objectives, scope and working method. The PSA study which includes full power (FPSA) as well as shutdown and low power conditions (SPSA) Level 1 PSA has to support the nuclear safety improvements of the unit. They evaluate the basic design and the benefits of all improvements, which were found necessary to be incorporated before the start-up of the unit. The study includes internal events (transients and under-loss of coolant accident, LOCAs), internal hazards as fires and floods and selected external hazards as earthquake, influence of external industry, extreme meteorological conditions and aircraft crash.The PSA (both FPSA and SPSA) models is developed using the RISK SPECTRUM PSA code. (author)

  17. Analysis of core damage frequency, Surry, Unit 1 internal events appendices

    International Nuclear Information System (INIS)

    Bertucio, R.C.; Julius, J.A.; Cramond, W.R.

    1990-04-01

    This document contains the appendices for the accident sequence analyses of internally initiated events for the Surry Nuclear Station, Unit 1. This is one of the five plant analyses conducted as part of the NUREG-1150 effort by the Nuclear Regulatory Commission. NUREG-1150 documents the risk of a selected group of nuclear power plants. The work performed is an extensive reanalysis of that published in November 1986 as NUREG/CR-4450, Volume 3. It addresses comments from numerous reviewers and significant changes to the plant systems and procedures made since the first report. The uncertainty analysis and presentation of results are also much improved. The context and detail of this report are directed toward PRA practitioners who need to know how the work was performed and the details for use in further studies. The mean core damage frequency at Surry was calculated to be 4.0E-5 per year, with a 95% upper bound of 1.3E-4 and 5% lower bound of 6.8E-6 per year. Station blackout type accidents (loss of all AC power) were the largest contributors to the core damage frequency, accounting for approximately 68% of the total. The next type of dominant contributors were Loss of Coolant Accidents (LOCAs). These sequences account for 15% of core damage frequency. No other type of sequence accounts for more than 10% of core damage frequency

  18. Specific aspects for Cernavoda - Unit 1 NPP life assurance

    International Nuclear Information System (INIS)

    Rucareanu, R.

    2002-01-01

    Full text: The main scope of a Plant Life Management Program is to operate the NPP in a safe manner and at a competitive cost during the reactor life. To achieve this goal, it is important to continuously evaluate the degradation of the main structures and components of the NPP. Background -Cernavoda NPP design life is 30 years. Compared with this target, the operation history is not long (Unit 1 is in commercial operation since 1997). It is still important to begin a plant life management program early to identify the critical components and structures, to establish the data needed for their monitoring and to find methods to mitigate their degradation. A specific aspect for Cernavoda NPP - Unit 1 is the long delay between the fabrication of the main components and the start-up. Most components were procured 10-15 years before start-up. First criticality was achieved in 1996, but the containment perimeter wall sliding was complete in 1983, the Calandria vessel was installed in 1985, the Steam Generators were in position in 1987, the fuel channels were installed in 1989. In evaluating the history of these components, the preservation period must be observed. For Unit 2, which will be in service around 2005, the delay will be longer. For this reason, CNCAN (the Romanian Regulatory Authority) imposed, as a condition to resume the work, to evaluate the ageing of the existing components and structures in order to establish their acceptability for use in the plant. The results of this evaluation can be used as references for subsequent evaluations. Plant Life Assurance Programme - The first step of a PLIM programme is to identify the components and structures that are important for the plant life management. Critical components and structures selection is done using the following criteria: safety criteria - components and structures whose failure can cause a release of radioactivity or which have to mitigate the release of radioactivity in case of a failure of other

  19. Nuclear

    International Nuclear Information System (INIS)

    2014-01-01

    This document proposes a presentation and discussion of the main notions, issues, principles, or characteristics related to nuclear energy: radioactivity (presence in the environment, explanation, measurement, periods and activities, low doses, applications), fuel cycle (front end, mining and ore concentration, refining and conversion, fuel fabrication, in the reactor, back end with reprocessing and recycling, transport), the future of the thorium-based fuel cycle (motivations, benefits and drawbacks), nuclear reactors (principles of fission reactors, reactor types, PWR reactors, BWR, heavy-water reactor, high temperature reactor of HTR, future reactors), nuclear wastes (classification, packaging and storage, legal aspects, vitrification, choice of a deep storage option, quantities and costs, foreign practices), radioactive releases of nuclear installations (main released radio-elements, radioactive releases by nuclear reactors and by La Hague plant, gaseous and liquid effluents, impact of releases, regulation), the OSPAR Convention, management and safety of nuclear activities (from control to quality insurance, to quality management and to sustainable development), national safety bodies (mission, means, organisation and activities of ASN, IRSN, HCTISN), international bodies, nuclear and medicine (applications of radioactivity, medical imagery, radiotherapy, doses in nuclear medicine, implementation, the accident in Epinal), nuclear and R and D (past R and D programmes and expenses, main actors in France and present funding, main R and D axis, international cooperation)

  20. Annealing of the RPV of unit 1 in Loviisa 1996

    International Nuclear Information System (INIS)

    Ahlstrand, R.; Kohopaeae, J.

    1997-01-01

    The critical circumferential core area weld of Loviisa 1 reactor pressure vessel was successfully annealed during the refueling and maintenance outage in August 1996. The weld was heated up to the annealing temperature of 475 deg.C and this temperature was maintained for 100 hours. The work was implemented by Skoda Nuclear Machinery Ltd as a main supplier representing consortium of Skoda Nuclear machinery Ltd from Czech Republic and Bohunice Nuclear Power Plant from Slovak Republic. Comprehensive material testing programs have been carried out to ensure the licensing of the annealing. Part of these programs have not yet been finished and are still going on. In the domestic programs sophisticated testing techniques including electric discharge machining and reconstitution techniques were used. Thus already tested surveillance specimens halves could be used as authentic material. The licensing work has been carried out mainly by VTT in Finland and Moht Otjig RM in Russia. A new comprehensive surveillance program has started to follow the embrittlement of the RPV after annealing. (author)