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Sample records for connecting liquefaction reactors

  1. Investigation of the deposit formation in pipelines connecting liquefaction reactors; 1t/d PSU ni okeru ekika hanno tokan fuchakubutsu no seisei yoin ni kansuru ichikosatsu

    Energy Technology Data Exchange (ETDEWEB)

    Okada, Y.; Nogami, Y.; Inokuchi, K. [Mitsui SRC Development Co. Ltd., Tokyo (Japan); Mochizuki, M.; Imada, K. [Nippon Steel Corp., Tokyo (Japan)

    1996-10-28

    The liquefaction reaction system of an NEDOL process coal liquefaction 1t/d PSU was opened and checked to investigate the cause of the rise of differential pressure between liquefaction reactors of the PSU. The liquefaction test at a coal concentration of 50 wt% using Tanito Harum coal was conducted, and it was found that the differential pressure between reactors was on the increase. By the two-phase flow pressure loss method, deposition thickness of deposit in pipelines was estimated at 4.4mm at the time of end operation, which agreed with a measuring value obtained from a {gamma} ray. The rise of differential pressure was caused by deposit formation in pipelines connecting reactors. The main component of the deposit is calcite (CaCO3 60-70%) and is the same as the usual one. It is also the same type as the deposit on the reactor wall. Ca in coal ash is concerned with this. To withdraw solid matters deposited in the reactor, there are installed pipelines for the withdrawal at the reactor bottom. The solid matters are regularly purged by reverse gas for prevention of clogging. As the frequency of purge increases, the deposit at the reactor bottom decreases, but the deposit attaches strongly to pipelines connecting reactors. It is presumed that this deposit is what Ca to be discharged out of the system as a form of deposition solid matter naturally in the Ca balance precipitated as calcite in the pipeline connecting the reactor. 3 refs., 5 figs., 4 tabs.

  2. Production of Advanced Biofuels via Liquefaction - Hydrothermal Liquefaction Reactor Design: April 5, 2013

    Energy Technology Data Exchange (ETDEWEB)

    Knorr, D.; Lukas, J.; Schoen, P.

    2013-11-01

    This report provides detailed reactor designs and capital costs, and operating cost estimates for the hydrothermal liquefaction reactor system, used for biomass-to-biofuels conversion, under development at Pacific Northwest National Laboratory. Five cases were developed and the costs associated with all cases ranged from $22 MM/year - $47 MM/year.

  3. Studies on characteristics of fluid dynamics in the coal liquefaction reactor; Sekitan ekika hanno tonai no ryudo tokusei

    Energy Technology Data Exchange (ETDEWEB)

    Sakawaki, K.; Nogami, Y.; Inokuchi, K. [Mitsui SRC Development Co. Ltd., Tokyo (Japan); Mochizuki, M.; Imada, K. [Nippon Steel Corp., Tokyo (Japan); Tachikawa, N.; Moki, T.; Ishikawa, I. [Japan Atomic Energy Research Institute, Tokyo (Japan)

    1996-10-28

    To design the coal liquefaction reactor of large scale plant in future, it is important to understand characteristics of fluid dynamics within the coal liquefaction reactor. In this study, to measure the fluid dynamics of liquid phase within the coal liquefaction reactor operated under high temperature and high pressure coal liquefaction condition, neutron attenuating tracer (NAT) technique, one of the tracer test methods, was applied using 1 t/d coal treating PSU. The residence time of liquid phase within the reactor can be measured by utilizing property of neutron of being absorbed by materials. The tracer was injected at the inlets of first and third reactors, and the neutron was counted at each outlet. The concentration of tracer was derived from the discrete value, to determine the residence time distribution of liquid phase. The mean residence time of liquid phase in the single first reactor and in the total three reactors were prolonged under the severe operation conditions of liquefaction. The more severe the liquefaction operation condition was, the more active the mixing of liquid phase was in the first reactor. It was found that the progress of reaction was accelerated. 2 refs., 5 figs., 1 tab.

  4. Computational Fluid Dynamics simulation of hydrothermal liquefaction of microalgae in a continuous plug-flow reactor.

    Science.gov (United States)

    Ranganathan, Panneerselvam; Savithri, Sivaraman

    2018-06-01

    Computational Fluid Dynamics (CFD) technique is used in this work to simulate the hydrothermal liquefaction of Nannochloropsis sp. microalgae in a lab-scale continuous plug-flow reactor to understand the fluid dynamics, heat transfer, and reaction kinetics in a HTL reactor under hydrothermal condition. The temperature profile in the reactor and the yield of HTL products from the present simulation are obtained and they are validated with the experimental data available in the literature. Furthermore, the parametric study is carried out to study the effect of slurry flow rate, reactor temperature, and external heat transfer coefficient on the yield of products. Though the model predictions are satisfactory in comparison with the experimental results, it still needs to be improved for better prediction of the product yields. This improved model will be considered as a baseline for design and scale-up of large-scale HTL reactor. Copyright © 2018 Elsevier Ltd. All rights reserved.

  5. Sunshine Program for fiscal 1981. Research on direct coal-liquefaction reactor; 1981 nendo sekitan chokusetsu ekika hannoki no kenkyu seika hokokusho

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1982-04-17

    The research aims to develop a new-type high-efficiency reactor for direct coal-liquefaction from a reaction engineering viewpoint and, at the same time, to settle problems expected to occur in industrializing this technique. The research items are Item 1 on the analysis of characteristics of a tubular continuous reactor and Item 2 on high-activity catalysts. Under Item 1, on the assumption that liquefaction reaction is dominantly a reaction in a continuous phase, a reactor is selected in consideration of homogeneous-phase reaction, and operating conditions are set according to the selected reactor and to the liquefaction reaction characteristics. A somewhat large Re number is assigned to the paste. Since the hydrogen partial pressure lowers with the progress of reaction, hydrogen is resupplied at the middle of the reaction tube. The volume of gas increases toward the final stage of reaction, decreasing the continuous phase holdup. Since it is undesirable to let the decrease stand, a vapor-liquid separator is provided for the control of the gas volume. In this fiscal year, investigation is conducted into details so as to determine if the reactor is equipped with intended characteristics. Under Item 2, the iron ore is deemed to be the most promising as disposal catalysts for liquefaction. In this fiscal year, studies are conducted to disclose the activity etc. of catalysts of this type. (NEDO)

  6. Hydrothermal Liquefaction of Biomass

    Energy Technology Data Exchange (ETDEWEB)

    Elliott, Douglas C.

    2010-12-10

    collaboration with Canada to investigate kelp (seaweed) as a biomass feedstock. The collaborative project includes process testing of the kelp in HydroThermal Liquefaction in the bench-scale unit at PNNL. HydroThermal Liquefaction at PNNL is performed in the hydrothermal processing bench-scale reactor system. Slurries of biomass are prepared in the laboratory from whole ground biomass materials. Both wet processing and dry processing mills can be used, but the wet milling to final slurry is accomplished in a stirred ball mill filled with angle-cut stainless steel shot. The PNNL HTL system, as shown in the figure, is a continuous-flow system including a 1-litre stirred tank preheater/reactor, which can be connected to a 1-litre tubular reactor. The product is filtered at high-pressure to remove mineral precipitate before it is collected in the two high-pressure collectors, which allow the liquid products to be collected batchwise and recovered alternately from the process flow. The filter can be intermittently back-flushed as needed during the run to maintain operation. By-product gas is vented out the wet test meter for volume measurement and samples are collected for gas chromatography compositional analysis. The bio-oil product is analyzed for elemental content in order to calculate mass and elemental balances around the experiments. Detailed chemical analysis is performed by gas chromatography-mass spectrometry and 13-C nuclear magnetic resonance is used to evaluate functional group types in the bio-oil. Sufficient product is produced to allow subsequent catalytic hydroprocessing to produce liquid hydrocarbon fuels. The product bio-oil from hydrothermal liquefaction is typically a more viscous product compared to fast pyrolysis bio-oil. There are several reasons for this difference. The HTL bio-oil contains a lower level of oxygen because of more extensive secondary reaction of the pyrolysis products. There are less amounts of the many light oxygenates derived from the

  7. Coal conversion rate in 1t/d PSU liquefaction reactor; 1t/d PSU ekika hannoto ni okeru sekitan tenka sokudo no kento

    Energy Technology Data Exchange (ETDEWEB)

    Ikeda, K.; Imada, K. [Nippon Steel Corp., Tokyo (Japan); Nogami, Y.; Inokuchi, K. [Mitsui SRC Development Co. Ltd., Tokyo (Japan)

    1996-10-28

    To investigate the coal liquefaction characteristics, coal slurry samples were taken from the outlets of the reactors and slurry preheater of NEDOL process 1 t/d process supporting unit (PSU), and were analyzed. Tanito Harum coal was used for liquefaction, and the slurry was prepared with recycle solvent. Liquefaction was performed using synthetic iron sulfide catalyst at reaction temperatures, 450 and 465{degree}C. Solubility of various solid samples was examined against n-hexane, toluene, and tetrahydrofuran (THF). When considering the decrease of IMO (THF-insoluble and ash) as a characteristic of coal conversion reaction, around 20% at the outlet of the slurry preheater, around 70% within the first reactor, and several percents within the successive second and third reactors were converted against supplied coal. Increase of reaction temperature led to the increase of evaporation of oil fraction, which resulted in the decrease of actual slurry flow rate and in the increase of residence time. Thus, the conversion of coal was accelerated by the synergetic effect of temperature and time. Reaction rate constant of the coal liquefaction was around 2{times}10{sup -1} [min{sup -1}], which increased slightly with increasing the reaction temperature from 450 to 465{degree}C. 3 refs., 5 figs., 1 tab.

  8. Analysis of solvent extracts from coal liquefaction in a flowing solvent reactor

    Energy Technology Data Exchange (ETDEWEB)

    Li, Wen-Ying; Feng, Jie; Xie, Ke-Chang [Key Laboratory of Coal Science and Technology, Taiyuan University of Technology, Ministry of Education and Shanxi Province, No. 79 Yingze West Street, Taiyuan 030024 (China); Kandiyoti, R. [Department of Chemical Engineering and Chemical Technology, Imperial College, University of London, London SW7 2BY (United Kingdom)

    2004-10-15

    Point of Ayr coal has been extracted using three solvents, tetralin, quinoline and 1-methyl-2-pyrrolidinone (NMP) at two temperatures 350 and 450 C, corresponding approximately to before and after the onset of massive covalent bond scission by pyrolysis. The three solvents differ in solvent power and the ability to donate hydrogen atoms to stabilise free radicals produced by pyrolysis of the coal. The extracts were prepared in a flowing solvent reactor to minimise secondary thermal degradation of the primary extracts. Analysis of the pentane-insoluble fractions of the extracts was achieved by size exclusion chromatography, UV-fluorescence spectroscopy in NMP solvent and probe mass. With increasing extraction temperature, the ratio of the amount having big molecular weight to that having small molecular weight in tetralin extracts was increased; the tetralin extract yield increased from 12.8% to 75.9%; in quinoline, increasing extraction temperature did not have an effect on the molecular weight of products but there was a big increase in extract yield. The extracts in NMP showed the enhanced solvent extraction power at both temperatures, with a shift in the ratio of larger molecules to smaller molecules with increasing extraction temperature and with the highest conversion of Point of Ayr coal among these three solvents at both temperatures. Solvent adducts were detected in the tetralin and quinoline extracts by probe mass spectrometry; solvent products were formed from NMP at both temperatures.

  9. Report on 1981 result of Sunshine Project. Research on direct liquefaction reactor of coal; 1981 nendo sekitan no chokusetsu ekika hannoki no kenkyu seika hokokusho

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1981-07-01

    This paper explains the results of research on direct liquefaction reaction of coal in fiscal 1981. The direct liquefaction is a reaction of three phases, gas-liquid-solid, under high temperature and high pressure. A tube type was employed in order to increase volume efficiency of the reactor, the continuous phase disperse number was decreased in order to bring it close to plug flow, and the paste Re number was increased to some extent in order to prevent sedimentation of coal particles. Hydrogen was supplied from the tube halfway for the purpose of supplementing the lowering of hydrogen partial pressure with the progress of reaction. A gas-liquid separator was installed so that increase in gas quantity was controlled in the rear stage of the reactor. As for catalysts, iron ore-sulfur system was examined which was promising as a disposable catalyst in place of the conventional iron system. Effect of catalytic addition was clearly recognizable in comparison with non-catalytic, with an exothermic peak observed comparable to the coal hydrogenation reaction of 350-420 degree C. Its catalytic effect was also presumable from the high pressure differential thermal analysis curve. The catalytic mechanism in the case where sulfur is added to hematite and limonite is similar to that of Fe{sub 2}O{sub 3} - sulfur catalyst, with the center of activity supposed to be Fe{sub 1-x}S. The catalytic effect is largely dependent on the particle size. (NEDO)

  10. Analysis of recovered solvents from coal liquefaction in a flowing-solvent reactor by SEC and UV-fluorescence

    Energy Technology Data Exchange (ETDEWEB)

    Li, W.Y.; Feng, J.; Xie, K.C.; Kandiyoti, R. [Taiyuan University of Technology, Taiyuan (China)

    2005-08-01

    Point of Ayr coal has been extracted using three solvents: tetralin, quinoline and 1-methyl-2-pyrrolidinone (NMP); at two temperatures: 350 {sup o}C and 450{sup o}C, corresponding approximately to before and after the onset of massive covalent bond scission by pyrolysis. These solvents differ in solvent power and the ability to donate hydrogen atoms to stabilize free radicals produced by pyrolysis of the coal. Analysis of the fresh solvents and recovered solvents from coal liquefaction was achieved by size exclusion chromatography and UV-fluorescence spectroscopy. In the blank run, it was testified that the filling material sand and the steel powder did not react with solvent with increasing reaction temperature. The role of hydrogen donation in the tetralin extracts was to increase the proportion of large molecules with increasing extraction temperature. Quinoline and NMP both have the powerful extracting capability to get more materials out of coal with increasing extraction temperature.

  11. Analysis of recovered solvents from coal liquefaction in a flowing-solvent reactor by SEC and UV-fluorescence

    Energy Technology Data Exchange (ETDEWEB)

    Wen-Ying Li; Jie Feng; Ke-Chang Xie; R. Kandiyoti [Taiyuan University of Technology, Taiyuan (China). Key Laboratory of Coal Science and Technology for Ministry of Education and Shanxi Province

    2005-08-01

    Point of Ayr coal has been extracted using three solvents: tetralin, quinoline and 1-methyl-2-pyrrolidinone (NMP); at two temperatures: 350{sup o}C and 450{sup o}C, corresponding approximately to before and after the onset of massive covalent bond scission by pyrolysis. These solvents differ in solvent power and the ability to donate hydrogen atoms to stabilize free radicals produced by pyrolysis of the coal. Analysis of the fresh solvents and recovered solvents from coal liquefaction was achieved by size exclusion chromatography and UV-fluorescence spectroscopy. In the blank run, it was testified that the filling material sand and the steel powder did not react with solvent with increasing reaction temperature. The role of hydrogen donation in the tetralin extracts was to increase the proportion of large molecules with increasing extraction temperature. Quinoline and NMP both have the powerful extracting capability to get more materials out of coal with increasing extraction temperature.

  12. Two-stage coal liquefaction without gas-phase hydrogen

    Science.gov (United States)

    Stephens, H.P.

    1986-06-05

    A process is provided for the production of a hydrogen-donor solvent useful in the liquefaction of coal, wherein the water-gas shift reaction is used to produce hydrogen while simultaneously hydrogenating a donor solvent. A process for the liquefaction of coal using said solvent is also provided. The process enables avoiding the use of a separate water-gas shift reactor as well as high pressure equipment for liquefaction. 3 tabs.

  13. Design of generic coal conversion facilities: Process release---Direct coal liquefaction

    Energy Technology Data Exchange (ETDEWEB)

    1991-09-01

    The direct liquefaction portion of the PETC generic direct coal liquefaction process development unit (PDU) is being designed to provide maximum operating flexibility. The PDU design will permit catalytic and non-catalytic liquefaction concepts to be investigated at their proof-of-the-concept stages before any larger scale operations are attempted. The principal variations from concept to concept are reactor configurations and types. These include thermal reactor, ebullating bed reactor, slurry phase reactor and fixed bed reactor, as well as different types of catalyst. All of these operating modes are necessary to define and identify the optimum process conditions and configurations for determining improved economical liquefaction technology.

  14. Liquefaction of Lignocellulose in Fractionated Light Bio-Oil: Proof of Concept and Techno-Economic Assessment

    NARCIS (Netherlands)

    Kumar, S.; Lange, Jean Paul; van Rossum, G.; Kersten, Sascha R.A.

    2015-01-01

    The direct thermal liquefaction of lignocellulose can provide a biocrude that could be used as a precursor for biofuels. However, earlier attempts to use the whole reactor effluent as a liquefaction medium, by recycling it to the liquefaction reactor, were hampered by the buildup of heavy products.

  15. Nuclear reactor incorporating locking device for threaded bolt connections

    International Nuclear Information System (INIS)

    Blaushild, R.M.

    1987-01-01

    A nuclear reactor having a pressure vessel and a first element is described comprising a core barrel situated within the pressure vessel. The core barrel has a baffle former secured in and to the core barrel by bolted connections, and a second element comprising baffle plates secured to the inner surface of the baffle former by bolted connections, with a locking device to prevent loosening of bolted connections between the baffle former and at least one of the elements. The baffle former and at least one element are held together by a headed, threaded bolt engaged in a bore coaxially extending in the baffle former and at least one element and threadedly engaged in a threaded section in at least the baffle former. The threaded section has first threaded of a first direction, with the head of the bolt engaged with a shoulder about the bore in at least one element to hold the baffle formed and at least one element together, the head of the bolt having a first diameter and a cavity, having an unsymmetrical wall thereabout, in the end surface thereof. It comprises a recess in at least one element coaxial with the bore forming a wall thereabout and extending inwardly from the outer surface of at least one element, the recess having a second diameter greater than the first diameter, with at least one element having second threads in the wall of a direction opposite the direction of the first threads of the threaded bore; a locking nut having a base with a downwardly depending cylindrical wall thereabout

  16. Hydrothermal liquefaction of biomass

    DEFF Research Database (Denmark)

    Toor, Saqib; Rosendahl, Lasse; Rudolf, Andreas

    2011-01-01

    This article reviews the hydrothermal liquefaction of biomass with the aim of describing the current status of the technology. Hydrothermal liquefaction is a medium-temperature, high-pressure thermochemical process, which produces a liquid product, often called bio-oil or bi-crude. During...... the hydrothermal liquefaction process, the macromolecules of the biomass are first hydrolyzed and/or degraded into smaller molecules. Many of the produced molecules are unstable and reactive and can recombine into larger ones. During this process, a substantial part of the oxygen in the biomass is removed...... by dehydration or decarboxylation. The chemical properties of bio-oil are highly dependent of the biomass substrate composition. Biomass constitutes of various components such as protein; carbohydrates, lignin and fat, and each of them produce distinct spectra of compounds during hydrothermal liquefaction...

  17. A connection-disconnection device for the nuclear reactor control rods

    International Nuclear Information System (INIS)

    Drean, H.; Breant, C.

    1992-01-01

    An automatic and relatively light system is developed to connect and disconnect the control rods in a nuclear reactor; it is designed to apply, in a controlled manner, constraints on the rods and to detect a possible misalignment of the connection-disconnection means in the corresponding butt

  18. Reactor

    International Nuclear Information System (INIS)

    Toyama, Masahiro; Kasai, Shigeo.

    1978-01-01

    Purpose: To provide a lmfbr type reactor wherein effusion of coolants through a loop contact portion is reduced even when fuel assemblies float up, and misloading of reactor core constituting elements is prevented thereby improving the reactor safety. Constitution: The reactor core constituents are secured in the reactor by utilizing the differential pressure between the high-pressure cooling chamber and low-pressure cooling chamber. A resistance port is formed at the upper part of a connecting pipe, and which is connect the low-pressure cooling chamber and the lower surface of the reactor core constituent. This resistance part is formed such that the internal sectional area of the connecting pipe is made larger stepwise toward the upper part, and the cylinder is formed larger so that it profiles the inner surface of the connecting pipe. (Aizawa, K.)

  19. Mongolian coal liquefaction test; Mongorutan no ekika tokusei

    Energy Technology Data Exchange (ETDEWEB)

    Yamamoto, H.; Kubo, H. [Mitsui SRC Development Co. Ltd., Tokyo (Japan); Tsedevsuren, T. [National Research Center of Chemistry and Technology of Coal in Mongoria (Mongolia)

    1996-10-28

    This paper describes the results of liquefaction tests of Mongolian coals using an autoclave and a flow micro reactor. Uvdughudag coal, Hootiinhonhor coal, and Shivee-Ovoo coal were used for liquefaction tests with an autoclave. Oil yields of Uvdughudag and Hootiinhonhor coals were 55.56 wt% and 55.29 wt%, respectively, which were similar to that of Wyoming coal. Similar results were obtained, as to produced gas and water yields. These coals were found to be suitable for coal liquefaction. Lower oil yield, 42.55 wt% was obtained for Shivee-Ovoo coal, which was not suitable for liquefaction. Liquefaction tests were conducted for Uvdughudag coal with a flow micro reactor. The oil yield was 55.7 wt%, which was also similar to that of Wyoming coal, 56.1 wt%. Hydrogen consumption of Uvdughudag coal was also similar to that of Wyoming coal. From these, Uvdughudag coal can be a prospective coal for liquefaction. From the distillation distribution of oil, distillate fraction yield below 350{degree}C of Uvdughudag coal was 50.7 wt%, which was much higher than that of Wyoming coal, 35.6 wt%. Uvdughudag coal is a coal with high light oil fraction yield. 2 figs., 5 tabs.

  20. Hydrothermal liquefaction of biomass

    DEFF Research Database (Denmark)

    Toor, Saqib; Rosendahl, Lasse; Hoffmann, Jessica

    2014-01-01

    Biomass is one of the most abundant sources of renewable energy, and will be an important part of a more sustainable future energy system. In addition to direct combustion, there is growing attention on conversion of biomass into liquid en-ergy carriers. These conversion methods are divided...... into biochemical/biotechnical methods and thermochemical methods; such as direct combustion, pyrolysis, gasification, liquefaction etc. This chapter will focus on hydrothermal liquefaction, where high pressures and intermediate temperatures together with the presence of water are used to convert biomass...... into liquid biofuels, with the aim of describing the current status and development challenges of the technology. During the hydrothermal liquefaction process, the biomass macromolecules are first hydrolyzed and/or degraded into smaller molecules. Many of the produced molecules are unstable and reactive...

  1. Raw materials problems in connection with fast breeder type reactors

    International Nuclear Information System (INIS)

    Hirsch, H.; Kreusch, J.

    1981-01-01

    The power supply by the FBR type reactors which depends upon the availability of essential raw materials such as Cr and Mo for structural and special steels is supposed to be less ensured than supply by fossil-fueled power plants. This contribution tries to verify this statement by means of estimates of the annual Cr and Mo demand, of the resources, production and consumption as well as by a study of the possibilities of recycling and substituting Cr and Mo. The only realistic alternative to the fast breeder type reactor is supposed to be a soft path of development according to the principle of decentralization, utilization of renewable energy sources regard to environmental protection, and use of less sophisticated technology. (DG) [de

  2. Coal liquefaction becomes viable

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    2005-11-15

    In 2003 the May/June issue of CoalTrans International speculated that coal liquefaction would become viable due to falling coal prices. This has not proved the case but the sustained high oil price is sparking new interest. A survey by Energy Intelligence and Marketing Research during November 2005 revealed a growth in the number of projects under development or at the feasibility stage. The article reports projects in China, the USA, Australia, New Zealand, the Philippines and India. China is commissioning the first wave of large liquefaction plants. The key question is whether other countries, particularly the USA, will follow.

  3. Liquefaction of uranium tailings

    International Nuclear Information System (INIS)

    1992-02-01

    Numerical methods for assessing the liquefaction potential of soils are reviewed with a view to their application to uranium tailings. The method can be divided into two categories: total stress analysis, where changes in pore pressure are not considered in the soil model, and effective stress analysis, where changes in pore pressure are included in the soil model. Effective stress analysis is more realistic, but few computer programs exist for such analysis in two or three dimensions. A simple linearized, two-dimensional, finite element effective stress analysis which incorporates volumetric compaction due to shear motion is described and implemented. The new program is applied to the assessment of liquefaction potential of tailings in the Quirke Mine tailings area near Elliot Lake, Ontario. The results are compared with those of a total stress analysis. Both analyses indicate liquefaction would occur if a magnitude 6.0 earthquake were to occur near the area. However, the extent of liquefaction predicted by the effective stress analysis is much less than that predicted by the total stress analysis. The results of both methods are sensitive to assumed material properties and to the method used to determine the cyclic shear strength of the tailings. Further analysis, incorporating more in situ and/or laboratory data, is recommended before conclusions can be made concerning the dynamic stability of these tailings

  4. Preloading of bolted connections in nuclear reactor component supports

    Energy Technology Data Exchange (ETDEWEB)

    Yahr, G T

    1984-10-01

    A number of failures of threaded fasteners in nuclear reactor component supports have been reported. Many of those failures were attributed to stress corrosion cracking. This report discusses how stress corrosion cracking can be avoided in bolting by controlling the maximum bolt preloads so that the sustained stresses in the bolts are below the level required to cause stress corrosion cracking. This is a basic departure from ordinary bolted joint design where the only limits on preload are on the minimum preload. Emphasis is placed on the importance of detailed analysis to determine the acceptable range of preload and the selection of a method for measuring the preload that is sufficiently accurate to ensure that the preload is actually within the acceptable range. Procedures for determining acceptable preload range are given, and the accuracy of various methods of measuring preload is discussed.

  5. Preloading of bolted connections in nuclear reactor component supports

    International Nuclear Information System (INIS)

    Yahr, G.T.

    1984-10-01

    A number of failures of threaded fasteners in nuclear reactor component supports have been reported. Many of those failures were attributed to stress corrosion cracking. This report discusses how stress corrosion cracking can be avoided in bolting by controlling the maximum bolt preloads so that the sustained stresses in the bolts are below the level required to cause stress corrosion cracking. This is a basic departure from ordinary bolted joint design where the only limits on preload are on the minimum preload. Emphasis is placed on the importance of detailed analysis to determine the acceptable range of preload and the selection of a method for measuring the preload that is sufficiently accurate to ensure that the preload is actually within the acceptable range. Procedures for determining acceptable preload range are given, and the accuracy of various methods of measuring preload is discussed

  6. Detachable connection for a nuclear reactor fuel assembly

    International Nuclear Information System (INIS)

    Christiansen, D.W.; Karnesky, R.A.

    1986-01-01

    This patent describes a connection for releasably attaching a socket member to a tube. It consists of: a tube defined by a wall provided with circumferentially spaced openings adjacent one end; a housing having an internal thread formation and laterally spaced fingers at one end. The fingers have pins engagable within the tube openings, a socket member threadably received within the housing and have a tapered portion at one end for urging the fingers radially outwardly. It also contains a split retaining ring interposed between the housing and the socket member and completely encapsulated

  7. Expansion connection of socket in flow distributed cabin of heavy water research reactor inner shell

    International Nuclear Information System (INIS)

    Jiang Zhiliang; Li Yanshui

    1995-01-01

    Expansion connection of aluminium alloy LT21 socket in flow distributed cabin of Heavy Water Research Reactor (HWRR) inner shell is described systematically. The expansion connection technology parameters of products are determined through tests. They are as following: bounce value of inner diameter after expansion, expansion degree, space between socket and plate hole, device for expanding pipes, selection of tools for enlarging or reaming holes, manufacture for socket inner hole and cleaning after expansion

  8. U.S. DOE indirect coal liquefaction program: An overview

    Energy Technology Data Exchange (ETDEWEB)

    Shen, J.; Schmetz, E.; Winslow, J.; Tischer, R. [Dept. of Energy, Germantown, MD (United States); Srivastava, R.

    1997-12-31

    Coal is the most abundant domestic energy resource in the United States. The Fossil Energy Organization within the US Department of Energy (DOE) has been supporting a coal liquefaction program to develop improved technologies to convert coal to clean and cost-effective liquid fuels to complement the dwindling supply of domestic petroleum crude. The goal of this program is to produce coal liquids that are competitive with crude at $20 to $25 per barrel. Indirect and direct liquefaction routes are the two technologies being pursued under the DOE coal liquefaction program. This paper will give an overview of the DOE indirect liquefaction program. More detailed discussions will be given to the F-T diesel and DME fuels which have shown great promises as clean burning alternative diesel fuels. The authors also will briefly discuss the economics of indirect liquefaction and the hurdles and opportunities for the early commercial deployment of these technologies. Discussions will be preceded by two brief reviews on the liquid versus gas phase reactors and the natural gas versus coal based indirect liquefaction.

  9. Residual Liquefaction under Standing Waves

    DEFF Research Database (Denmark)

    Kirca, V.S. Ozgur; Sumer, B. Mutlu; Fredsøe, Jørgen

    2012-01-01

    This paper summarizes the results of an experimental study which deals with the residual liquefaction of seabed under standing waves. It is shown that the seabed liquefaction under standing waves, although qualitatively similar, exhibits features different from that caused by progressive waves....... The experimental results show that the buildup of pore-water pressure and the resulting liquefaction first starts at the nodal section and spreads towards the antinodal section. The number of waves to cause liquefaction at the nodal section appears to be equal to that experienced in progressive waves for the same...

  10. Releasing method of connection of control rod and its drive mechanism in a reactor

    International Nuclear Information System (INIS)

    Ishida, Kazuo; Futatsugi, Masao.

    1976-01-01

    Object: To disengage a control rod from a control rod drive device in a boiling water reactor with a minimal failure of the device, when connection there between cannot be released in a normal manner. Structure: First, a part of a piston tube in the control rod drive device is withdrawn externally of a control rod housing and cut. Next, a discharge tool, which is designed to be connected with the cut piston tube, is connected to the remainder of the piston tube within the housing and the aforesaid piston tube is pushed into the index tube. The index tube is then cut by the discharge tool. Thus, the control rod drive device and the control rod may be separated. Thereafter, the control rod may be removed from the top of the reactor container whereas the control rod drive device removed from the bottom thereof. (Ikeda, J.)

  11. New control strategy for grid connecting of wind turbine inverter without converter reactor

    DEFF Research Database (Denmark)

    Rasmussen, Tonny Wederberg; Sørensen, Kasper B.; Bjørneboe, Daniel

    2013-01-01

    Wind turbines and the belonging converters increase in size and price. A reduction in the number of main components is desirable while it reduces need of space, investments and increases the efficiency. A wind turbine contains both a converter reactor and a step up transformer. The paper presents...... theory and laboratory measurements for a new control strategy which make it possibly to connect a wind turbine converter to the utility grid without using the converter reactor or make measurements at the high voltage side of the transformer. The capability to control the DC voltage and reactive power...

  12. High flux testing reactor Petten. Replacement of the reactor vessel and connected components. Overall report

    International Nuclear Information System (INIS)

    Chrysochoides, N.G.; Cundy, M.R.; Von der Hardt, P.; Husmann, K.; Swanenburg de Veye, R.J.; Tas, A.

    1985-01-01

    The project of replacing the HFR originated in 1974 when results of several research programmes confirmed severe neutron embrittlement of aluminium alloys suggesting a limited life of the existing facility. This report contains the detailed chronology of events concerning preparation and execution of the replacement. After a 14 months' outage the reactor resumed routine operation on 14th February, 1985. At the end of several years of planning and preparation the reconstruction proceded in the following steps: unloading of the old core, decay of short-lived radioactivity in December 1983, removal of the old tank and of its peripheral equipment in January-February 1984, segmentation and waste disposal of the removed components in March-April, decontamination of the pools, bottom penetration overhauling in May-June, installation of the new tank and other new components in July-September, testing and commissioning, including minor modifications in October-December, and, trials runs and start-up preparation in January-February 1985. The new HFR Petten features increased and improved experimental facilities. Among others the obsolete thermal columns was replaced by two high flux beam tubes. Moreover the new plant has been designed for future increases of reactor power and neutron fluxes. For the next three to four years the reactor has to cope with a large irradiation programme, claiming its capacity to nearly 100%

  13. Cooperative research in coal liquefaction

    Energy Technology Data Exchange (ETDEWEB)

    Huffman, G.P.; Sendlein, L.V.A. (eds.)

    1991-05-28

    Significant progress was made in the May 1990--May 1991 contract period in three primary coal liquefaction research areas: catalysis, structure-reactivity studies, and novel liquefaction processes. A brief summary of the accomplishments in the past year in each of these areas is given.

  14. Case studies on direct liquefaction of low rank Wyoming coal

    Energy Technology Data Exchange (ETDEWEB)

    Adler, P.; Kramer, S.J.; Poddar, S.K. [Bechtel Corp., San Francisco, CA (United States)

    1995-12-31

    Previous Studies have developed process designs, costs, and economics for the direct liquefaction of Illinois No. 6 and Wyoming Black Thunder coals at mine-mouth plants. This investigation concerns two case studies related to the liquefaction of Wyoming Black Thunder coal. The first study showed that reducing the coal liquefaction reactor design pressure from 3300 to 1000 psig could reduce the crude oil equivalent price by 2.1 $/bbl provided equivalent performing catalysts can be developed. The second one showed that incentives may exist for locating a facility that liquifies Wyoming coal on the Gulf Coast because of lower construction costs and higher labor productivity. These incentives are dependent upon the relative values of the cost of shipping the coal to the Gulf Coast and the increased product revenues that may be obtained by distributing the liquid products among several nearby refineries.

  15. The direct liquefaction proof of concept program

    Energy Technology Data Exchange (ETDEWEB)

    Comolli, A.G.; Lee, L.K.; Pradhan, V.R.; Stalzer, R.H. [New York & Puritan Avenues, Lawrenceville, NJ (United States)

    1995-12-31

    The goal of the Proof of Concept (POC) Program is to develop Direct Coal Liquefaction and associated transitional technologies towards commercial readiness for economically producing premium liquid fuels from coal in an environmentally acceptable manner. The program focuses on developing the two-stage liquefaction (TSL) process by utilizing geographically strategic feedstocks, commercially feasible catalysts, new prototype equipment, and testing co-processing or alternate feedstocks and improved process configurations. Other high priority objectives include dispersed catalyst studies, demonstrating low rank coal liquefaction without solids deposition, improving distillate yields on a unit reactor volume basis, demonstrating ebullated bed operations while obtaining scale-up data, demonstrating optimum catalyst consumption using new concepts (e.g. regeneration, cascading), producing premium products through on-line hydrotreating, demonstrating improved hydrogen utilization for low rank coals using novel heteroatom removal methods, defining and demonstrating two-stage product properties for upgrading; demonstrating efficient and economic solid separation methods, examining the merits of integrated coal cleaning, demonstrating co-processing, studying interactions between the preheater and first and second-stage reactors, improving process operability by testing and incorporating advanced equipment and instrumentation, and demonstrating operation with alternate coal feedstocks. During the past two years major PDU Proof of Concept runs were completed. POC-1 with Illinois No. 6 coal and POC-2 with Black Thunder sub-bituminous coal. Results from these operations are continuing under review and the products are being further refined and upgraded. This paper will update the results from these operations and discuss future plans for the POC program.

  16. Novel bimetallic dispersed catalysts for temperature-programmed coal liquefaction. Technical progress report, October 1995--December 1995

    Energy Technology Data Exchange (ETDEWEB)

    Song, C.; Cooke, W.S.; Schmidt, E.; Schobert, H.H.

    1996-02-01

    Coal liquefaction involves cleavage of methylene, dimethylene and ether bridges connecting polycyclic aromatic units and the reactions of various oxygen functional groups. Here in this quarterly, we report on the catalytic effects of several molybdenum-, cobalt-, and iron-containing compounds in the reactions of dibenzothiophene (DBT) with hydrogen under conditions related to coal liquefaction. The catalytic effects of several molybdenum-, cobalt-, and iron-containing compounds have been examined in the hydrogenation and hydrodesulfurization reactions of dibenzothiophene (DBT) under conditions related to coal liquefaction. The metal compounds are candidate catalyst precursors for direct coal liquefaction. The reactions were carried out in batch microautoclave reactors at 400{degrees}C for 30 minutes with 6.9 MPa (cold) hydrogen pressure, and tridecane solvent. A metal loading of 0.5 mol% resulted in low conversion and only hydrogenation. Addition of sulfur in 4:1 molar ratio led only to a minor increase in conversion and hydrodesulfurization. The use of a higher boiling solvent (octadecane vs. tridecane) was beneficial in providing increased conversion, hydrodesulfurization, and hydrogenation. An increase in metal compound loading to 36.2 mol% led to a dramatic increase in conversion, hydrodesulfurization, and hydrocracking. Molybdenum hexacarbonyl at 36 mol% loading, with added sulfur at 6:1 ratio and octadecane solvent, gave 100% conversion of dibenzothiophene to other products with 100% hydrodesulfurization. Ammonium tetrathiomolybdate and molybdenum(III) chloride are less active under similar conditions. A cobalt-molybdenum thiocubane complex gave unexpectedly low conversions. Iron and cobalt carbonyls also provided very low conversions, even with added sulfur.

  17. FEM analysis of mechanical behaviour of coil support connections in Wendelstein 7-X fusion reactor

    International Nuclear Information System (INIS)

    Krzesinski, G.; Zagrajek, T.; Marek, P.; Dobosz, R.; Czarkowski, P.; Kurzydlowski, K.J.

    2006-01-01

    The objective of Wendelstein 7-X project is the stellarator-type fusion reactor. In this device plasma channel is under control of magnetic field coming from magnet system of very complicated shape, made of 70 superconducting coils symmetrically arranged in 5 identical sections. Every coil is connected to central ring with two extensions which transfer loads resulting from electromagnetic field and gravity. The aim of this work was to analyse mechanical behaviour of the bolted connections using detailed 3D finite element models. All simulations were performed assuming elasto-plastic behaviour of the materials, assembly stresses and friction contacts between different parts of the connections. Stress distributions, displacements, forces acting on the bolts and welds were studied using standard and submodeling routines. The results were subsequently used to optimize the design of critical central support elements. (author)

  18. Studies on liquefaction and pyrolysis of peat and biomass at KTH

    International Nuclear Information System (INIS)

    Bjoernbom, E.; Sjoestrom, K.; Hoernel, C.; Zanzi, R.; Bjoernbom, P.

    1996-01-01

    A brief review of the study on thermochemical conversion of solid fuels is done. The study have been performed in the Royal Institute of Technology, Stockholm, since the outbreak of energy crisis in the seventies. The main problems connected with utilisation of peat for energy are: 90% moisture content in the deposits and 35-40% oxygen content in the dry substance. Simultaneous dewatering and liquefaction of peat have been achieved by the Bjoerbom method. The wet peat has been treated with CO and H 2 O without preliminary drying, using water as a medium agent. After treatment water has been phase-separated from the heavy oil product. Another approach is de-oxygenation of peat prior to liquefaction. A significant part of oxygen in peat and biomass can be removed by thermal decomposition of the fuels prior to liquefaction and removal of carbon dioxide and water from the organic matter in them. The products obtained after de-oxygenation demand low consumption of external hydrogenation agent because they are rich in hydrogen. Some criteria for selection of peat as a raw material for liquefaction are given. The equipment and experimental procedure for pyrolysis of peat and biomass are described. A free fall tubular reactor with max operating pressure of 5 MPa and temperature of 1100 o C has been used. The effect of treatment conditions under the rapid pyrolysis in the free fall reactor on the yield and the reactivity of char obtained after the final pyrolysis is shown. Peat and wood are transformed into pyrolysis products for less than 1 second; 35-50% of the moisture- and ash-free peat and 70% of the wood have been converted into gaseous products.The char obtained in the rapid pyrolysis contains a fraction which can be further de-volatilized by slow pyrolysis for a few minutes - time much longer than the time for formation of primary products. High reactivity of char is favoured by lower pyrolysis temperature, shorter residence time and larger particle size of the fuel

  19. Non-catalytic transfer hydrogenation in supercritical CO2 for coal liquefaction

    Science.gov (United States)

    Elhussien, Hussien

    This thesis presents the results of the investigation on developing and evaluating a low temperature (coal dissolution in supercritical CO2. The main idea behind the thesis was that one hydrogen atom from water and one hydrogen atom from the hydrogen transfer agent (HTA) were used to hydrogenate the coal. The products of coal dissolution were non-polar and polar while the supercritical CO2, which enhanced the rates of hydrogenation and dissolution of the non-polar molecules and removal from the reaction site, was non-polar. The polar modifier (PM) for CO2 was added to the freed to aid in the dissolution and removal of the polar components. The addition of a phase transfer agent (PTA) allowed a seamless transport of the ions and by-product between the aqueous and organic phases. DDAB, used as the PTA, is an effective phase transfer catalyst and showed enhancement to the coal dissolution process. COAL + DH- +H 2O → COAL.H2 + DHO-- This process has a great feature due to the fact that the chemicals were obtained without requir-ing to first convert coal to CO and H2 units as in indirect coal liquefaction. The experiments were conducted in a unique reactor set up that can be connected through two lines. one line to feed the reactor with supercritical CO 2 and the other connected to gas chromatograph. The use of the supercritical CO2 enhanced the solvent option due to the chemical extraction, in addition to the low environmental impact and energy cost. In this thesis the experiment were conducted at five different temperatures from atmos-pheric to 140°C, 3000 - 6000 psi with five component of feed mixture, namely water, HTA, PTA, coal, and PM in semi batch vessels reactor system with a volume of 100 mL. The results show that the chemicals were obtained without requiring to first convert coal to CO and H2 units as in indirect coal liquefaction. The results show that the conversion was found to be 91.8% at opti-mum feed mixtures values of 3, 1.0 and 5.4 for water: PM

  20. A new method to evaluate the sealing reliability of the flanged connections for Molten Salt Reactors

    Energy Technology Data Exchange (ETDEWEB)

    Li, Qiming, E-mail: liqiming@sinap.ac.cn [Shanghai Institute of Applied Physics, Chinese Academy of Sciences, Shanghai 201800 (China); Key Laboratory of Nuclear Radiation and Nuclear Energy Technology, Chinese Academy of Sciences, Shanghai 201800 (China); Tian, Jian; Zhou, Chong [Shanghai Institute of Applied Physics, Chinese Academy of Sciences, Shanghai 201800 (China); Key Laboratory of Nuclear Radiation and Nuclear Energy Technology, Chinese Academy of Sciences, Shanghai 201800 (China); Wang, Naxiu, E-mail: wangnaxiu@sinap.ac.cn [Shanghai Institute of Applied Physics, Chinese Academy of Sciences, Shanghai 201800 (China); Key Laboratory of Nuclear Radiation and Nuclear Energy Technology, Chinese Academy of Sciences, Shanghai 201800 (China)

    2015-06-15

    Highlights: • We novelly valuate the sealing reliability of the flanged connections for MSRs. • We focus on the passive decrease of the leak impetus in flanged connections. • The modified flanged connections are acquired a sealing ability of self-adjustment. • Effects of redesigned flange configurations on molten salt leakage are discussed. - Abstract: The Thorium based Molten Salt Reactor (TMSR) project is a future Generation IV nuclear reactor system proposed by the Chinese Academy of Sciences with the strategic goal of meeting the growing energy needs in the Chinese economic development and social progress. It is based on liquid salts served as both fuel and primary coolant and consequently great challenges are brought into the sealing of the flanged connections. In this study, an improved prototype flange assembly is performed on the strength of the Freeze-Flange initially developed by Oak Ridge National Laboratory (ORNL). The calculation results of the finite element model established to analyze the temperature profile of the Freeze-Flange agree well with the experimental data, which indicates that the numerical simulation method is credible. For further consideration, the ideal-gas thermodynamic model, together with the mathematical approximation, is novelly borrowed to theoretically evaluate the sealing performance of the modified Freeze-Flange and the traditional double gaskets bolted flange joint. This study focuses on the passive decrease of the leak driving force due to multiple gaskets introduced in flanged connections for MSR. The effects of the redesigned flange configuration on molten salt leakage resistance are discussed in detail.

  1. A new method to evaluate the sealing reliability of the flanged connections for Molten Salt Reactors

    International Nuclear Information System (INIS)

    Li, Qiming; Tian, Jian; Zhou, Chong; Wang, Naxiu

    2015-01-01

    Highlights: • We novelly valuate the sealing reliability of the flanged connections for MSRs. • We focus on the passive decrease of the leak impetus in flanged connections. • The modified flanged connections are acquired a sealing ability of self-adjustment. • Effects of redesigned flange configurations on molten salt leakage are discussed. - Abstract: The Thorium based Molten Salt Reactor (TMSR) project is a future Generation IV nuclear reactor system proposed by the Chinese Academy of Sciences with the strategic goal of meeting the growing energy needs in the Chinese economic development and social progress. It is based on liquid salts served as both fuel and primary coolant and consequently great challenges are brought into the sealing of the flanged connections. In this study, an improved prototype flange assembly is performed on the strength of the Freeze-Flange initially developed by Oak Ridge National Laboratory (ORNL). The calculation results of the finite element model established to analyze the temperature profile of the Freeze-Flange agree well with the experimental data, which indicates that the numerical simulation method is credible. For further consideration, the ideal-gas thermodynamic model, together with the mathematical approximation, is novelly borrowed to theoretically evaluate the sealing performance of the modified Freeze-Flange and the traditional double gaskets bolted flange joint. This study focuses on the passive decrease of the leak driving force due to multiple gaskets introduced in flanged connections for MSR. The effects of the redesigned flange configuration on molten salt leakage resistance are discussed in detail

  2. Secondary liquefaction in ethanol production

    DEFF Research Database (Denmark)

    2007-01-01

    The invention relates to a method of producing ethanol by fermentation, said method comprising a secondary liquefaction step in the presence of a themostable acid alpha-amylase or, a themostable maltogenic acid alpha-amylase.......The invention relates to a method of producing ethanol by fermentation, said method comprising a secondary liquefaction step in the presence of a themostable acid alpha-amylase or, a themostable maltogenic acid alpha-amylase....

  3. Magnetic refrigerator for hydrogen liquefaction

    Energy Technology Data Exchange (ETDEWEB)

    Numazawa, T [National Institute for Materials Science, Tsukuba (Japan); Kamlya, K. [Japan Atomic Energy Agency, Naka (Japan); Utaki, T. [Osaka University, Osaka (Japan); Matsumoto, K. [Kanazawa University, Kanazawa (Japan)

    2013-06-15

    This paper reviews the development status of magnetic refrigeration system for hydrogen liquefaction. There is no doubt that hydrogen is one of most important energy sources in the near future. In particular, liquid hydrogen can be utilized for infrastructure construction consisting of storage and transportation. Liquid hydrogen is in cryogenic temperatures and therefore high efficient liquefaction method must be studied. Magnetic refrigeration which uses the magneto-caloric effect has potential to realize not only the higher liquefaction efficiency > 50 %, but also to be environmentally friendly and cost effective. Our hydrogen magnetic refrigeration system consists of Carnot cycle for liquefaction stage and AMR (active magnetic regenerator) cycle for precooling stages. For the Carnot cycle, we develop the high efficient system > 80 % liquefaction efficiency by using the heat pipe. For the AMR cycle, we studied two kinds of displacer systems, which transferred the working fluid. We confirmed the AMR effect with the cooling temperature span of 12 K for 1.8 T of the magnetic field and 6 second of the cycle. By using the simulation, we estimate the total efficiency of the hydrogen liquefaction plant for 10 kg/day. A FOM of 0.47 is obtained in the magnetic refrigeration system operation temperature between 20 K and 77 K including LN2 work input.

  4. Direct liquefaction proof-of-concept facility

    Energy Technology Data Exchange (ETDEWEB)

    Alfred G. Comolli; Peizheng Zhou; HTI Staff

    2000-01-01

    The main objective of the U.S. DOE, Office of Fossil Energy, is to ensure the US a secure energy supply at an affordable price. An integral part of this program was the demonstration of fully developed coal liquefaction processes that could be implemented if market and supply considerations so required, Demonstration of the technology, even if not commercialized, provides a security factor for the country if it is known that the coal to liquid processes are proven and readily available. Direct liquefaction breaks down and rearranges complex hydrocarbon molecules from coal, adds hydrogen, and cracks the large molecules to those in the fuel range, removes hetero-atoms and gives the liquids characteristics comparable to petroleum derived fuels. The current processes being scaled and demonstrated are based on two reactor stages that increase conversion efficiency and improve quality by providing the flexibility to adjust process conditions to accommodate favorable reactions. The first stage conditions promote hydrogenation and some oxygen, sulfur and nitrogen removal. The second stage hydrocracks and speeds the conversion to liquids while removing the remaining sulfur and nitrogen. A third hydrotreatment stage can be used to upgrade the liquids to clean specification fuels.

  5. Survey on development of brown coal liquefaction techniques; Kattan ekika gijutsu ni kansuru chosa

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1980-09-01

    Described herein are results of literature survey on brown coal liquefaction reactions and elementary techniques. Liquefaction of brown coal in the presence of CO and steam, or CO, H{sub 2} and steam has been investigated. It is not clear by the literature survey whether it is superior to the normal process which uses hydrogen. Brown coal contains moisture at high contents, and the drying techniques are necessary to be developed for its liquefaction. The future coal liquefaction plant will be much larger than the past one, and there are a number of problems to be solved, such as those involved in the designs of large-sized high-pressure slurry pumps, heat exchangers and preheaters. It is also necessary to develop the materials of and production techniques for large reactors which are serviceable under severe conditions. The solid-liquid separation for liquefaction products involves a number of the elementary techniques characteristic of coal liquefaction processes, and needs many technological developments. The one-stage brown coal liquefaction process is compared with the two-stage process for the secondary hydrogenation of SCR, but no clear conclusions are reached. (NEDO)

  6. Plasma electrolytic liquefaction of cellulosic biomass

    Science.gov (United States)

    Dingliang, TANG; Xianhui, ZHANG; Si-ze, YANG

    2018-04-01

    In this paper, the rapid liquefaction of a corncob was achieved by plasma electrolysis, providing a new method for cellulosic biomass liquefaction. The liquefaction rate of the corncob was 95% after 5 min with polyethylene glycol and glycerol as the liquefying agent. The experiments not only showed that H+ ions catalyzed the liquefaction of the corncob, but also that using accelerated H+ ions, which were accelerated by an electric field, could effectively improve the liquefaction efficiency. There was an obvious discharge phenomenon, in which the generated radicals efficiently heated the solution and liquefied the biomass, in the process of plasma electrolytic liquefaction. Finally, the optimum parameters of the corncob liquefaction were obtained by experimentation, and the liquefaction products were analyzed.

  7. Hydrothermal liquefaction of biomass: Developments from batch to continuous process

    OpenAIRE

    Elliott, DC; Biller, P; Ross, AB; Schmidt, AJ; Jones, SB

    2015-01-01

    This review describes the recent results in hydrothermal liquefaction (HTL) of biomass in continuous-flow processing systems. Although much has been published about batch reactor tests of biomass HTL, there is only limited information yet available on continuous-flow tests, which can provide a more reasonable basis for process design and scale-up for commercialization. High-moisture biomass feedstocks are the most likely to be used in HTL. These materials are described and results of their pr...

  8. Liquefaction resistance of calcareous sands

    International Nuclear Information System (INIS)

    Sandoval Vallejo, Eimar

    2012-01-01

    Calcareous sands are unique in terms of their origin, mineralogy, shape, fragility and intra particle porosity. This article presents results from an experimental program carried out to study the liquefaction resistance of a calcareous sand retrieved from Cabo Rojo at Puerto Rico. The experimental program included mineralogical characterization, index properties, and undrained cyclic triaxial tests on isotropically consolidated reconstituted samples. Due to the large variation in the calcareous sand properties, results are compared with previous researches carried out on other calcareous sands around the world. Results showed a wide range in the liquefaction resistance of the studied calcareous sands. Cabo Rojo sand experienced greater liquefaction resistance than most of the calcareous sands used for comparison. Important differences in the excess pore pressure generation characteristics were also found.

  9. Development of an extruder-feeder biomass direct liquefaction process

    Energy Technology Data Exchange (ETDEWEB)

    White, D.H.; Wolf, D. (Arizona Univ., Tucson, AZ (United States). Dept. of Chemical Engineering)

    1991-10-01

    As an abundant, renewable, domestic energy resource, biomass could help the United States reduce its dependence on imported oil. Biomass is the only renewable energy technology capable of addressing the national need for liquid transportation fuels. Thus, there is an incentive to develop economic conversion processes for converting biomass, including wood, into liquid fuels. Through research sponsored by the US DOE's Biomass Thermochemical Conversion Program, the University of Arizona has developed a unique biomass direct liquefaction system. The system features a modified single-screw extruder capable of pumping solid slurries containing as high as 60 wt% wood flour in wood oil derived vacuum bottoms at pressures up to 3000 psi. The extruder-feeder has been integrated with a unique reactor by the University to form a system which offers potential for improving high pressure biomass direct liquefaction technology. The extruder-feeder acts simultaneously as both a feed preheater and a pumping device for injecting wood slurries into a high pressure reactor in the biomass liquefaction process. An experimental facility was constructed and following shakedown operations, wood crude oil was produced by mid-1985. By July 1988, a total of 57 experimental continuous biomass liquefaction runs were made using White Birch wood feedstock. Good operability was achieved at slurry feed rates up to 30 lb/hr, reactor pressures from 800 to 3000 psi and temperatures from 350{degree}C to 430{degree}C under conditions covering a range of carbon monoxide feed rates and sodium carbonate catalyst addition. Crude wood oils containing as little as 6--10 wt% residual oxygen were produced. 38 refs., 82 figs., 26 tabs.

  10. Development of liquefaction process of coal and biomass in supercritical water; Chorinkaisui wo mochiita sekitan biomass doji ekika process no kaihatsu

    Energy Technology Data Exchange (ETDEWEB)

    Nonaka, H.; Matsumura, Y.; Tsutsumi, A.; Yoshida, K. [The University of Tokyo, Tokyo (Japan). Faculty of Engineering; Masuno, Y.; Inaba, A. [National Institute for Resources and Environment, Tsukuba (Japan)

    1996-10-28

    Liquefaction of coal and biomass in supercritical water has been investigated, in which strong solubilization force of supercritical water against hydrocarbons is utilized. Free radicals are formed through the cleavage of covalent bonds in coal under the heating condition at around 400{degree}C during coal liquefaction. It is important to stabilize these unstable intermediate products by hydrogen transfer. On the other hand, hydrogen is not required for the liquefaction of biomass having higher H/C atomic ratio and oxygen content than those of coal. Co-liquefaction of coal and biomass was conducted using supercritical water, in which excess hydrogen from the liquefaction of biomass would be transferred to coal, resulting in the effective liquefaction of coal. Mixture of coal and cellulose was liquefied in supercritical water at 390{degree}C under the pressure of 25 MPa using a semi-continuous reactor, and the results were compared with those from the separate liquefaction of them. The co-liquefaction of coal and cellulose did not show any difference in the residue yield from the separate liquefaction of these, but led to the increased production of compounds with lower molecular weight. The liquefaction was completed in 15 minutes. 5 refs., 3 figs., 3 tabs.

  11. Outline of research achievement of fiscal 1983. Development of coal liquefaction technologies; Sekitan ekika gijutsu kaihatsu. 1983 nendo kenkyu seika no gaiyo

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1983-07-01

    Reported are the results of (1) the development of bituminous coal liquefaction technology, (2) development of brown coal liquefaction technology, (3) experimental fabrication and development of plant equipment and materials therefor, and (4) a survey on coal type selection. The goals of the development are mentioned below. Under Item (1), an optimum liquefaction process and a solid/liquid separation process are to be defined, the effect of iron-based catalysts upon liquefaction reaction is to be elucidated, a technology for constructing a direct hydroliquefaction unit is to be established, and a plant using such a unit is to be developed. Under Item (2), an optimum liquefaction technology is to be established, high in economic efficiency and reliability, by subjecting Australia's Victoria brown coal to the direct liquefaction process. In particular, a new brown coal liquefaction technology is to be established, which will be an organic combination of a novel, raw brown coal slurry dehydration technology, a solvent deashing technology, and the secondary hydrogenation technology, all centering on the basic technology of primary hydrogenation. Under Item (3), reactor materials, accessory materials, slurry pumps, etc., are to be experimentally manufactured and developed further. Under Item (4), data are to be collected on coal resources, coal quality, liquefaction characteristics, etc., during the process of technology development for liquefaction, etc. Furthermore, methods are to be established for the effective utilization of liquefaction products and for their optimum refining. (NEDO)

  12. Cooling system for the connecting rings of a fast neutron reactor vessel

    International Nuclear Information System (INIS)

    Martin, J.-P.; Malaval, Claude

    1974-01-01

    A description is given of a cooling system for the vessel connecting rings of a fast neutron nuclear reactor, particularly of a main vessel containing the core of the reactor and a volume of liquid metal coolant at high temperature and a safety vessel around the main vessel, both vessels being suspended to a rigid upper slab kept at a lower temperature. It is mounted in the annular space between the two vessels and includes a neutral gas circuit set up between the wall of the main vessel to be cooled and that of the safety vessel itself cooled from outer. The neutral gas system comprises a plurality of ventilators fitted in holes made through the thickness of the upper slab and opening on to the space between the two vessels. It also includes two envelopes lining the walls of these vessels, establishing with them small section channels for the circulation of the neutral gas cooled against the safety vessel and heated against the main vessel [fr

  13. EARTHQUAKE INDUCED LIQUEFACTION ANALYSIS OF

    African Journals Online (AJOL)

    liquefaction analysis of Tendaho earth-fill dam, which is part ... sugar cane plantation in an area of 60,000 hectares. The project .... The model is prepared using the QUAKE/W program for the ..... Geo-slope International, Ltd., Canada. Dynamic ...

  14. Process for the liquefaction of solid carbonaceous materials wherein nitrogen is separated from hydrogen via ammonia synthesis

    Science.gov (United States)

    Stetka, Steven S.; Nazario, Francisco N.

    1982-01-01

    In a process for the liquefaction of solid carbonaceous materials wherein bottoms residues are upgraded with a process wherein air is employed, the improvement wherein nitrogen buildup in the system is avoided by ammonia synthesis. In a preferred embodiment hydrogen from other portions of the liquefaction process will be combined with hydrogen produced as a result of the bottoms upgrading to increase the H.sub.2 :N.sub.2 ratio in the ammonia reactor.

  15. Pressurized water reactor fuel performance problems connected with fuel cladding corrosion processes

    International Nuclear Information System (INIS)

    Dobrevski, I.; Zaharieva, N.

    2008-01-01

    Generally, Pressurized Water Reactor (WWER, PWR) Fuel Element Performance is connected with fuel cladding corrosion and crud deposition processes. By transient to extended fuel cycles in nuclear power reactors, aiming to achieve higher burnup and better fuel utilization, the role of these processes increases significantly. This evolution modifies the chemical and electrochemical conditions in the reactor primary system, including change of fuel claddings' environment. The higher duty cores are always attended with increased boiling (sub-cooled nucleate boiling) mainly on the feed fuel assemblies. This boiling process on fuel cladding surfaces can cause different consequences on fuel element cladding's environment characteristics. In the case of boiling at the cladding surfaces without or with some cover of corrosion product deposition, the behavior of gases dissolved in water phase is strongly influenced by the vapor generation. The increase of vapor partial pressure will reduce the partial pressures of dissolved gases and will cause their stripping out. By these circumstances the concentrations of dissolved gases in cladding wall water layer can dramatically decrease, including also the case by which all dissolved gases to be stripped out. On the other hand it is known that the hydrogen is added to primary coolant in order to avoid the production of oxidants by radiolysis of water. It is clear that if boiling strips out dissolved hydrogen, the creation of oxidizing conditions at the cladding surfaces will be favored. In this case the local production of oxidants will be a result from local processes of water radiolysis, by which not only both oxygen (O 2 ) and hydrogen (H 2 ) but also hydrogen peroxide (H 2 O 2 ) will be produced. While these hydrogen and oxygen will be stripped out preferentially by boiling, the bigger part of hydrogen peroxide will remain in wall water phase and will act as the most important factor for creation of oxidizing conditions in fuel

  16. Advances in Seabed Liquefaction and its Implications for Marine Structures

    DEFF Research Database (Denmark)

    Sumer, B. Mutlu

    2013-01-01

    A review is presented of recent advances in seabed liquefaction and its implications for marine structures. The review is organized in seven sections: Residual liquefaction, including the sequence of liquefaction, mathematical modelling, centrifuge modelling and comparison with standard wave-flum......-flume results; Momentary liquefaction; Floatation of buried pipelines; Sinking of pipelines and marine objects; Liquefaction at gravity structures; Stability of rock berms in liquefied soils; and Impact of seismic-induced liquefaction....

  17. Coal liquefaction still a dream

    Energy Technology Data Exchange (ETDEWEB)

    Overberg, H

    1982-03-19

    Liquefaction of coal is not profitable in West Germany and will not be so far some time to coal. This is true for West German and imported coal. The result may be improved but not changed by combined conversion of coal and top residues of distilleries. These are the main statements of a study carried out by Messrs. Veba Oel AG, Gelsenkirchen, on behalf of the Federal Minister for Research and Technology. The results of the study are presented in 20 volumes.

  18. Process Water Recycle in Hydrothermal Liquefaction of Microalgae To Enhance Bio-oil Yield

    NARCIS (Netherlands)

    Ramos-Tercero, E.A.; Bertucco, A.; Brilman, Derk Willem Frederik

    2015-01-01

    In this work, the effect of recycling the process water (PW) of hydrothermal liquefaction (HTL) to the HTL reactor was investigated, with the objective being to recover carbon from the organic content of the PW and to develop a solvent-free process. When recycling twice the PW at 220, 240, and 265

  19. Liquefaction technology assessment. Final report

    Energy Technology Data Exchange (ETDEWEB)

    1979-05-01

    A survey of coal liquefaction technology and analysis of projected relative performance of high potential candidates has been completed and the results are reported here. The key objectives of the study included preparation of a broad survey of the status of liquefaction processes under development, selection of a limited number of high potential process candidates for further study, and an analysis of the relative commercial potential of these candidates. Procedures which contributed to the achievement of the above key goals included definition of the characteristics and development status of known major liquefaction process candidates, development of standardized procedures for assessing technical, environmental, economic and product characteristics for the separate candidates, and development of procedures for selecting and comparing high potential processes. The comparisons were made for three production areas and four marketing areas of the US. In view of the broad scope of the objectives the survey was a limited effort. It used the experience gained during preparation of seven comprehensive conceptual designs/economic evaluations plus comprehensive reviews of the designs, construction and operation of several pilot plants. Results and conclusions must be viewed in the perspective of the information available, how this information was treated, and the full context of the economic comparison results. Comparative economics are presented as ratios; they are not intended to be predictors of absolute values. Because the true cost of constructing and operating large coal conversion facilities will be known only after commercialization, relative values are considered more appropriate. (LTN)

  20. Report for fiscal 1981 of Sunshine Program coal group. Basic research on Solvolysis liquefaction technology; 1981 nendo solvolysis ekika gijutsu no kiso kenkyu hokokusho

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1982-03-01

    Basic research is conducted on the Solvolysis liquefaction process for the purpose of producing from coal an ashless, low-sulfur, pollution-free liquid fuel. In the research on the Solvolysis liquefaction (1st stage liquefaction) of coal using a hydrogenation solvent, the Solvolysis liquefaction of coal is studied, for which a refined Solvolysis pitch containing coal substances and a hydride of solvent refined coal are used as Solvolysis liquefaction solvents for the 1st stage. In the research on the 1st stage liquefaction reaction conditions using a high-temperature closed process, two methods are employed. One is a method that uses a mini-pump type reactor in which a small hermetic container is submerged in a high-temperature solvent for rapid heating and the other is a method that uses a pipe type reactor in which coal slurry is caused to travel through a pipe heated to a high temperature. For the analysis of the 2nd stage liquefaction (hydrogenation) reaction conditions, the properties of the 2nd coal liquid, and the constitution of the 2nd coal liquid, and the for the research on the 1st stage liquefaction capacity, the hydrogenation of anthracene oil and solvent refined coal as recyclable solvent models is studied. (NEDO)

  1. Decommissioning of the research nuclear reactor IRT-M and problems connected with radioactive waste

    International Nuclear Information System (INIS)

    Abramidze, S.P.; Katamadze, N.M.; Kiknadze, G.G.; Saralidze, Z.K.

    2000-01-01

    The nuclear research reactor IRT-2000 is described, along with modifications and upgrades made over the past three decades. Considerations are outlined which followed a decision to shut-down the reactor and to dismantle it. (author)

  2. Co-Liquefaction of Elbistan Lignite with Manure Biomass; Part 3 - Effect of Reaction Time and Temperature

    Science.gov (United States)

    Koyunoglu, Cemil; Karaca, Hüseyin

    2017-12-01

    Most of the liquefaction process were carried out in a batch reactor, in which the residence time of the liquefaction products is long enough to favour the retrogressive reactions. To minimize retrogressive reactions, the liquefaction of coal was carried out in a flowing solvent reactor in which a fixed bed of coal is continuously permeated by hot solvent. Solvent flowing through the coal bed carries the liquefaction products out of the reactor. Unlike experiments carried out under similar conditions in a batch reactor no increase in solid residue is observed during long time high temperature runs in the flowing solvent reactor. There is a greater appreciation of the importance of retrograde, or polymerization, reactions. If the free radicals formed when coal breaks down are not quickly capped with hydrogen, they react with each other to form large molecules that are much harder to break down than the original coal. Reaction time impacts both the co-liquefaction cost and the product yield. So as to study this idea, the experiments of Elbistan Lignite (EL) with manure co-liquefaction carried out by changing the reaction time from 30 to 120 minutes. As a result, the greatest oil products yields obtained at 60 minutes. Therefore, by thinking about the oil products yield values acquired, the optimal reaction time was obtained to be 60 minutes for Elbistan lignite (EL) with manure liquefied with the temperature of 350°C and 400°C. Above 425°C did not examine because solvent (tetraline) loses its function after 425 °C. The obtained optimum temperature found 400°C due to higher total conversion of liquefaction products and also oil+gas yields.

  3. Liquefaction macrophenomena in the great Wenchuan earthquake

    Science.gov (United States)

    Chen, Longwei; Yuan, Xiaoming; Cao, Zhenzhong; Hou, Longqing; Sun, Rui; Dong, Lin; Wang, Weiming; Meng, Fanchao; Chen, Hongjuan

    2009-06-01

    On May 12, 2008 at 14:28, a catastrophic magnitude M s 8.0 earthquake struck the Sichuan Province of China. The epicenter was located at Wenchuan (31.00°N, 103.40°E). Liquefaction macrophenomena and corresponding destruction was observed throughout a vast area of 500 km long and 200 km wide following the earthquake. This paper illustrates the geographic distribution of the liquefaction and the relationship between liquefaction behavior and seismic intensity, and summarizes the liquefaction macrophenomena, including sandboils and waterspouts, ground subsidence, ground fissures etc., and relevant liquefaction features. A brief summary of the structural damage caused by liquefaction is presented and discussed. Based on comparisons with liquefaction phenomena observed in the 1976 Tangshan and 1975 Haicheng earthquakes, preliminary analyses were performed, which revealed some new features of liquefaction behavior and associated issues arising from this event. The site investigation indicated that the spatial non-uniformity of liquefaction distribution was obvious and most of the liquefied sites were located in regions of seismic intensity VIII. However, liquefaction phenomena at ten different sites in regions of seismic intensity VI were also observed for the first time in China mainland. Sandboils and waterspouts ranged from centimeters to tens of meters, with most between 1 m to 3 m. Dramatically high water/sand ejections, e.g., more than 10 m, were observed at four different sites. The sand ejections included silty sand, fine sand, medium sand, course sand and gravel, but the ejected sand amount was less than that in the 1976 Tangshan earthquake. Possible liquefaction of natural gravel soils was observed for the first time in China mainland.

  4. The probable types, sizes, positions and orientations of the defects which may appear in connection with manufacture of reactor vessels

    International Nuclear Information System (INIS)

    Bergh, S.

    1980-02-01

    An review of welding technology in manufacture of reactor vessels is made. An inventory of principal defects appearing in connection with manual ARC-welding and coated electrodes is presented. Some important welded joints of BWR reactor vessels are scrutinized. Reheating cracks may appear during stress relief annealing beneath the cladding, and this problem is discussed in the third part. The interest is focussed towards the defects which depend on the conditions during the welding. Slag and incomplete fusion might be found. The review can serve for the guidance of nondestructive testing. The defects are estimated to have the size of a few MM with a maximum to approx. 10 MM right across the weld, possibly with exception for the electroslag welds of the OKG-1 reactor vessel. (GBn)

  5. Whole Algae Hydrothermal Liquefaction Technology Pathway

    Energy Technology Data Exchange (ETDEWEB)

    Biddy, M.; Davis, R.; Jones, S.

    2013-03-01

    This technology pathway case investigates the feasibility of using whole wet microalgae as a feedstock for conversion via hydrothermal liquefaction. Technical barriers and key research needs have been assessed in order for the hydrothermal liquefaction of microalgae to be competitive with petroleum-derived gasoline-, diesel-, and jet-range hydrocarbon blendstocks.

  6. Wave liquefaction in soils with clay content

    DEFF Research Database (Denmark)

    Kirca, Özgür; Sumer, B. Mutlu; Fredsøe, Jørgen

    2012-01-01

    The paper presents the results of an experimental study of the influence of clay content (in silt-clay and sand-clay mixtures) on liquefaction beneath progressive waves. The experiments showed that the influence of clay content is very significant. Susceptibility of silt to liquefaction is increa...

  7. The Texts of the Instruments connected with the Agency's Assistance to Finland in Establishing a Research Reactor Project

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1961-01-24

    The texts of the Supply Agreement between the Agency, the Government of Finland and the Government of the United States of America, and of the Project Agreement between the Agency and the Government of Finland, in connection with the Agency's assistance to the Government of Finland in establishing a research reactor project, are reproduced in this document for the information of all Members of the Agency. These agreements entered into force on 30 December 1960.

  8. The Texts of the Instruments connected with the Agency's Assistance to Pakistan in Establishing a Research Reactor Project

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1962-03-22

    The texts of the Supply Agreement between the Agency, the Government of Pakistan and the Government of the United States of America, and of the Project Agreement between the Agency and the Government of Pakistan, in connection with the Agency's assistance to the Government of Pakistan-in establishing a research reactor project, are reproduced in this document for the information of all Members of the Agency. These Agreements entered into force on 5 March 1962.

  9. The Texts of the Instruments connected with the Agency's Assistance to Yugoslavia in Establishing a Research Reactor Project

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1961-11-24

    The texts of the Supply Agreement between the Agency, the Government of Yugoslavia and the Government of the United States of America, and of the Project Agreement between the Agency and the Government of Yugoslavia, in connection with the Agency's assistance to the Government of Yugoslavia in establishing a research reactor project, are reproduced in this document for the information of all Members of the Agency. These Agreements entered into force on 4 October 1961.

  10. The Texts of the Instruments connected with the Agency's Assistance to Mexico in Establishing a Research Reactor Project

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1964-01-30

    The texts of the Supply Agreement between the Agency and the Governments of Mexico and the United States of America, and of the Project Agreement between the Agency and the Government of Mexico, in connection with the Agency's assistance to that Government in establishing a research reactor project, are reproduced in this document for the information of all Members. These Agreements entered into force on 18 December 1963.

  11. The Texts of the Instruments connected with the Agency's Assistance to Iran in Establishing a Research Reactor Project

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1967-08-31

    The texts of the Supply Agreement between the Agency and the Governments of Iran and the United States of America, and of the Project Agreement between the Agency and the Government of Iran, connected with the Agency's assistance to the latter Government in establishing a research reactor project, are reproduced in this document for the information of all Members. The Agreements entered into force on 7 June and 10 May 1967 respectively.

  12. The Texts of the Instruments connected with the Agency's assistance to Uruguay in Establishing a Research Reactor Project

    International Nuclear Information System (INIS)

    1965-01-01

    The texts of the Supply Agreement between the Agency and the Governments of the United States of America and Uruguay, and of the Project Agreement between the Agency and the Government of Uruguay, in connection with the Agency's assistance to the latter Government in establishing a research reactor project, are reproduced in this document for the information of all Members. These Agreements entered into force on 24 September 1965

  13. The Texts of the Instruments connected with the Agency's assistance to Uruguay in Establishing a Research Reactor Project

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1965-12-09

    The texts of the Supply Agreement between the Agency and the Governments of the United States of America and Uruguay, and of the Project Agreement between the Agency and the Government of Uruguay, in connection with the Agency's assistance to the latter Government in establishing a research reactor project, are reproduced in this document for the information of all Members. These Agreements entered into force on 24 September 1965.

  14. The Texts of the Instruments connected with the Agency's Assistance to Pakistan in Establishing a Research Reactor Project

    International Nuclear Information System (INIS)

    1962-01-01

    The texts of the Supply Agreement between the Agency, the Government of Pakistan and the Government of the United States of America, and of the Project Agreement between the Agency and the Government of Pakistan, in connection with the Agency's assistance to the Government of Pakistan-in establishing a research reactor project, are reproduced in this document for the information of all Members of the Agency. These Agreements entered into force on 5 March 1962

  15. The Texts of the Instruments connected with the Agency's Assistance to Finland in Establishing a Research Reactor Project

    International Nuclear Information System (INIS)

    1961-01-01

    The texts of the Supply Agreement between the Agency, the Government of Finland and the Government of the United States of America, and of the Project Agreement between the Agency and the Government of Finland, in connection with the Agency's assistance to the Government of Finland in establishing a research reactor project, are reproduced in this document for the information of all Members of the Agency. These agreements entered into force on 30 December 1960

  16. The Texts of the Instruments connected with the Agency's Assistance to Iran in Establishing a Research Reactor Project

    International Nuclear Information System (INIS)

    1967-01-01

    The texts of the Supply Agreement between the Agency and the Governments of Iran and the United States of America, and of the Project Agreement between the Agency and the Government of Iran, connected with the Agency's assistance to the latter Government in establishing a research reactor project, are reproduced in this document for the information of all Members. The Agreements entered into force on 7 June and 10 May 1967 respectively

  17. The Texts of the Instruments connected with the Agency's Assistance to Yugoslavia in Establishing a Research Reactor Project

    International Nuclear Information System (INIS)

    1961-01-01

    The texts of the Supply Agreement between the Agency, the Government of Yugoslavia and the Government of the United States of America, and of the Project Agreement between the Agency and the Government of Yugoslavia, in connection with the Agency's assistance to the Government of Yugoslavia in establishing a research reactor project, are reproduced in this document for the information of all Members of the Agency. These Agreements entered into force on 4 October 1961

  18. The Texts of the Instruments connected with the Agency's Assistance to Mexico in Establishing a Research Reactor Project

    International Nuclear Information System (INIS)

    1964-01-01

    The texts of the Supply Agreement between the Agency and the Governments of Mexico and the United States of America, and of the Project Agreement between the Agency and the Government of Mexico, in connection with the Agency's assistance to that Government in establishing a research reactor project, are reproduced in this document for the information of all Members. These Agreements entered into force on 18 December 1963

  19. Coal liquefaction with preasphaltene recycle

    Science.gov (United States)

    Weimer, Robert F.; Miller, Robert N.

    1986-01-01

    A coal liquefaction system is disclosed with a novel preasphaltene recycle from a supercritical extraction unit to the slurry mix tank wherein the recycle stream contains at least 90% preasphaltenes (benzene insoluble, pyridine soluble organics) with other residual materials such as unconverted coal and ash. This subject process results in the production of asphaltene materials which can be subjected to hydrotreating to acquire a substitute for No. 6 fuel oil. The preasphaltene-predominant recycle reduces the hydrogen consumption for a process where asphaltene material is being sought.

  20. Helium refrigeration system for hydrogen liquefaction applications

    Science.gov (United States)

    Nair, J. Kumar, Sr.; Menon, RS; Goyal, M.; Ansari, NA; Chakravarty, A.; Joemon, V.

    2017-02-01

    Liquid hydrogen around 20 K is used as cold moderator for generating “cold neutron beam” in nuclear research reactors. A cryogenic helium refrigeration system is the core upon which such hydrogen liquefaction applications are built. A thermodynamic process based on reversed Brayton cycle with two stage expansion using high speed cryogenic turboexpanders (TEX) along with a pair of compact high effectiveness process heat exchangers (HX), is well suited for such applications. An existing helium refrigeration system, which had earlier demonstrated a refrigeration capacity of 470 W at around 20 K, is modified based on past operational experiences and newer application requirements. Modifications include addition of a new heat exchanger to simulate cryogenic process load and two other heat exchangers for controlling the temperatures of helium streams leading out to the application system. To incorporate these changes, cryogenic piping inside the cold box is suitably modified. This paper presents process simulation, sizing of new heat exchangers as well as fabrication aspects of the modified cryogenic process piping.

  1. A study on the hydrotreating of coal hydro liquefaction residue and its kinetics

    Energy Technology Data Exchange (ETDEWEB)

    Huang, J.; Lu, X.; Zhang, D.; Gao, J. [Department of Chemical Engineering for Energy Resources, East China University of Science and Technology, Shanghai (China)

    2010-09-15

    Hydro-conversion of coal hydro liquefaction residue obtained from a 6 t/day pilot plant of Shenhua Group in Shanghai was carried out under the hydrotreating condition. The coal hydro liquefaction residue and its product were extracted in sequence with n-hexane, toluene and tetrahydrofuran in a Soxhlet apparatus. The n-hexane soluble fractions increased with the increase of reaction temperature and time. Its amount increased from 14.14% to a maximum of 40.86% under the conditions of 470 {sup o}C and 30 min, which meant that moderate extension of coal residence time in the coal hydro liquefaction reactor is beneficial to the increase of oil yield. A 4-lumped kinetic model of coal hydro liquefaction residue hydro-conversion was performed using solubility-based lumped fractions. In the model, the tetrahydrofuran insoluble fractions were classified into two parts: easily reactive part and unreactive part. The kinetic parameters were estimated by a fourth-order Runge-Kutta method and a nonlinear least squares method, and the apparent activation energies were calculated according to the Arrhenius Equation. A large quantity of total catalyst consisting of remained liquefaction catalyst, part of the mineral from raw coal and additive Fe-based catalyst could considerably reduce the apparent activation energy of hydro-conversion for the toluene insoluble/tetrahydrofuran insoluble fractions to 36.79 kJ-mol{sup -1}. The calculated values of the model coincided well with the experimental values. (authors)

  2. Earthquake-induced liquefaction in Ferland, Quebec

    International Nuclear Information System (INIS)

    Tuttle, M.; Seeber, L.

    1991-02-01

    Detailed geological investigations are under way at a number of liquefaction sites in the Ferland-Boilleau valley, Quebec, where sand boils, ground cracks and liquefaction-related damages to homes were documented immediately following the Ms=6.0, Mblg=6.5 Saguenay earthquake of November 25, 1988. To date, results obtained from these subsurface investigations of sand boils at two sites in Ferland, located about 26 km from the epicentre, indicate that: the Saguenay earthquake induced liquefaction in late-Pleistocene and Holocene sediments which was recorded as sand dikes, sills and vents in near-surface sediments and soils; earthquake-induced liquefaction and ground failure have occurred in this area at least three times in the past 10,000 years; and, the size and morphology of liquefaction features and the liquefaction susceptibility of source layers of the features may be indicative of the intensity of ground shaking. These preliminary results are very promising and suggest that with continued research liquefaction features will become a useful tool in glaciated terrains, such as northeastern North America, for determining not only the timing and location but also the size of past earthquakes

  3. Status of October 1, 2004 of the repartition of nuclear reactors connected to the grid and under construction in the world

    International Nuclear Information System (INIS)

    2004-01-01

    This document is a table giving the number of nuclear reactors connected to the grid and under construction in the European countries and in the rest of the world. The percentage of electricity produced by these reactors in 2003 is indicated. (J.S.)

  4. Histotripsy Liquefaction of Large Hematomas.

    Science.gov (United States)

    Khokhlova, Tatiana D; Monsky, Wayne L; Haider, Yasser A; Maxwell, Adam D; Wang, Yak-Nam; Matula, Thomas J

    2016-07-01

    Intra- and extra-muscular hematomas result from repetitive injury as well as sharp and blunt limb trauma. The clinical consequences can be serious, including debilitating pain and functional deficit. There are currently no short-term treatment options for large hematomas, only lengthy conservative treatment. The goal of this work was to evaluate the feasibility of a high intensity focused ultrasound (HIFU)-based technique, termed histotripsy, for rapid (within a clinically relevant timeframe of 15-20 min) liquefaction of large volume (up to 20 mL) extra-vascular hematomas for subsequent fine-needle aspiration. Experiments were performed using in vitro extravascular hematoma phantoms-fresh bovine blood poured into 50 mL molds and allowed to clot. The resulting phantoms were treated by boiling histotripsy (BH), cavitation histotripsy (CH) or a combination in a degassed water tank under ultrasound guidance. Two different transducers operating at 1 MHz and 1.5 MHz with f-number = 1 were used. The liquefied lysate was aspirated and analyzed by histology and sized in a Coulter Counter. The peak instantaneous power to achieve BH was lower than (at 1.5 MHz) or equal to (at 1 MHz) that which was required to initiate CH. Under the same exposure duration, BH-induced cavities were one and a half to two times larger than the CH-induced cavities, but the CH-induced cavities were more regularly shaped, facilitating easier aspiration. The lysates contained a small amount of debris larger than 70 μm, and 99% of particulates were smaller than 10 μm. A combination treatment of BH (for initial debulking) and CH (for liquefaction of small residual fragments) yielded 20 mL of lysate within 17.5 minutes of treatment and was found to be most optimal for liquefaction of large extravascular hematomas. Copyright © 2016 World Federation for Ultrasound in Medicine & Biology. Published by Elsevier Inc. All rights reserved.

  5. Report on results of R and D of coal liquefaction technology in fiscal 1981; 1981 nendo sekitan ekika gijutsu no kenkyu kaihatsu seika setsumeisho

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1982-03-01

    This paper explains the results of development of coal liquefaction technology under the Sunshine Project in fiscal 1981. In connection with solvent extraction and liquefaction, an 1 t/day experimental plant was completed for bituminous coals and operated continuously for 153 hours. An examination also started for the development of a 250 t/day pilot plant. As the element studies, R and D is in progress on the solvent extraction and liquefaction process, solid-liquid separation, secondary hydrogenation, and plant materials. In brown coals, the construction work of a 50 t/day pilot plant started for the purpose of establishing liquefaction technology for brown coal in Victoria State, Australia, with a part of the equipment manufactured. As the element studies, research was conducted on primary hydrogenation, deliming, secondary hydrogenation, dehydration and catalysts. In solvolysis liquefaction, a short-time concluding liquefaction reaction was continuously performed by a plant of 1 t/day scale. In direct hydro-liquefaction, a 2.4 t/day experimental plant was constructed, with the element studies conducted successively. In other words, researches were carried out by the bench scale plant on liquefaction, solid-liquid separation, iron-based catalysts, catalyst and reutilization, motive force recovery system by hydrohoist, and effect of preheating and deaeration. (NEDO)

  6. Assessment and mitigation of liquefaction

    International Nuclear Information System (INIS)

    Czelada, J. A.; Melentijevic, S.

    2014-01-01

    The simplified empirical procedure in its original form presented in Youd et al (2001) and some further developments given in Idriss and Boulanger (2006) for evaluating liquefaction resistance of soils is presented in this paper only for the criteria based on standard penetration test (SPT). Methods for estimating the ground improvement techniques by stone columns and dynamics compaction are presented. For stone columns Priebe method (1995) and homogenized method (equivalent parameters) are present. for dynamic compaction methods proposed by Recomendacion Geotecnica para las Obras Maritimas y/o Porturaria - ROM 0.5-05 (2005) and Nashed et al. (2009) are described. These analysis methods for each ground improvement technique are compared in two different case histories showing similar results in each one. (Author)

  7. Coal liquefaction process streams characterization and evaluation

    Energy Technology Data Exchange (ETDEWEB)

    Robbins, G.A.; Brandes, S.D.; Winschel, R.A.; Burke, F.P.

    1992-03-01

    CONSOL R D is conducting a three-year program to characterize process and product streams from direct coal liquefaction process development projects. The program objectives are two-fold: (1) to obtain and provide appropriate samples of coal liquids for the evaluation of analytical methodology, and (2) to support ongoing DOE-sponsored coal liquefaction process development efforts. The two broad objectives have considerable overlap and together serve to provide a bridge between process development and analytical chemistry.

  8. Two design aspects connected with the safety of the PIK reactor presently under construction

    International Nuclear Information System (INIS)

    Gostev, V.V.; Zakharov, A.S.; Konoplev, K.A.; Levandovskii, N.V.; Ploshchanskii, L.M.; Smolsky, S.L.

    1993-01-01

    The PIK reactor is designed for physical research with neutron beams and sample irradiation. In the central trap the thermal neutrons flux is 4x10 15 n/cm 2 s. The reactor power is 100 MW, the thermal neutron flux in the reflector at the maximum of distribution is 1x10 15 n/cm 2 s. The core with a high uranium concentration of 600 g/l is light water-cooled, heavy water being used in the reflector. The Chernobyl disaster happened at the time of equipment installation at the PIK. The code revision, a change of the authors ideas about the safety, and a change of public attitude towards nuclear installations resulted in a stopping of construction and project revision. Reconstruction project has led to a change of all safety systems and involved in various degrees all essential reactor systems. The construction is presently resumed in spite of economic difficulties in Russia. The reactor was inspected by experts from a number of European countries, USA, and European Commission delegated by their governments to prepare a report on whether supporting the construction to its completion would be reasonable. In the course of inspection the experts from USA and EU expressed doubts concerning two systems, namely, the containment and scram. These two points are discussed in the present paper. Three type of containments are proposed and an analysis of their efficiency is presented. The PIK reactor is controlled by eight rods in the heavy-water reflector -and an absorbing cylinder at the boundary between the core and the central light-water neutron trap. The rods are used for emergency protection and reactor start-up. The central control cylinder called here the shutter serves several functions, namely, as scram, automatic control, and burnup compensation. The delay time before the onset of negative reactivity is 1.05 sec for rods and 0.25 sec for the shutter

  9. FY 1980 Report on results of Sunshine Project. Development of coal liquefaction techniques (Development of materials for the coal liquefaction plant); 1980 nendo sekitan ekika gijutsu no kaihatsu seika hokokusho. Sekitan ekika plant zairyo no kaihatsu

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1981-03-01

    A 1 T/D solvent-extraction type coal liquefaction test plant was constructed and operated to obtain the technical data for the design of, and establish the techniques for, an efficient coal liquefaction plant. The FY 1980 program includes surveys on the materials for coal liquefaction plants, covering those already developed and under development, to clarify the problematical points; drafting the test schedules; and conceptual designs of the material testing facilities. The major problems involved in the materials for coal liquefaction plants include erosion by fluidizing coal slurry, hydrogen embrittlement of the reactor materials, and corrosion by the liquefaction products (e.g., stress-corrosion cracking of austenitic steel, and corrosion by organic acids). The surveys on materials research trends suggest that USA seems to concentrate their research efforts on the reactor materials. The corrosion tests are mostly of in-plant tests, but the stress corrosion and slurry erosion tests are conducted on a laboratory scale. The conceptual designs are drawn for some testing units, e.g., the loop type material testing unit and basic testing unit for jet-spray type slurry erosion. (NEDO)

  10. Basic studies on coal liquefaction reaction, reforming and utilization of liquefaction products

    Energy Technology Data Exchange (ETDEWEB)

    Shiraishi, M. (National Institute for Resources and Environment, Tsukuba (Japan))

    1993-09-01

    This report describes the achievement of research and development of coal liquefaction technologies in the Sunshine Project for FY 1992, regarding the coal liquefaction reaction, reforming and utilization of liquefaction products. For the fundamental study on coal liquefaction reaction, were investigated effect of asphaltene in petroleum residue on coprocessing, pretreatment effect in coprocessing of Taiheiyo coal and tarsand bitumen using oil soluble catalyst, solubilization and liquefaction of Taiheiyo coal at mild conditions with the aid of super acid, and flash hydropyrolysis of finely pulverized swollen coal under high hydrogen pressure. On the other hand, for the study on hydrotreatment of coal derived liquid, were investigated catalytic hydroprocessing of Wandoan coal liquids, production of gasoline from coal liquids by fluid catalytic cracking, solvent extraction of phenolic compounds from coal liquids, and separation of hetero compounds in coal liquid by means of high pressure crystallization. Further progress in these studies has been confirmed. 9 figs., 6 tabs.

  11. Operating characteristic analysis of a 400 mH class HTS DC reactor in connection with a laboratory scale LCC type HVDC system

    Energy Technology Data Exchange (ETDEWEB)

    Kim, Sung-Kyu, E-mail: power@changwon.ac.kr [Changwon National University, 55306 Sarim-dong, Changwon 641-773 (Korea, Republic of); Kim, Kwangmin; Park, Minwon [Changwon National University, 55306 Sarim-dong, Changwon 641-773 (Korea, Republic of); Yu, In-Keun, E-mail: yuik@changwon.ac.kr [Changwon National University, 55306 Sarim-dong, Changwon 641-773 (Korea, Republic of); Lee, Sangjin [Uiduk University, Gyeongju 780-713 (Korea, Republic of)

    2015-11-15

    Highlights: • A 400 mH class HTS DC reactor and a laboratory scale test-bed for line-commutated converter type HVDC transmission system. • The 400 mH class HTS DC reactor was connected to real power network via the HVDC system. • The DC current flowed in HTS DC reactor has several harmonic components and it was analyzed using FFT. - Abstract: High temperature superconducting (HTS) devices are being developed due to their advantages. Most line commutated converter based high voltage direct current (HVDC) transmission systems for long-distance transmission require large inductance of DC reactor; however, generally, copper-based reactors cause a lot of electrical losses during the system operation. This is driving researchers to develop a new type of DC reactor using HTS wire. The authors have developed a 400 mH class HTS DC reactor and a laboratory scale test-bed for line-commutated converter type HVDC system and applied the HTS DC reactor to the HVDC system to investigate their operating characteristics. The 400 mH class HTS DC reactor is designed using a toroid type magnet. The HVDC system is designed in the form of a mono-pole system with thyristor-based 12-pulse power converters. In this paper, the investigation results of the HTS DC reactor in connection with the HVDC system are described. The operating characteristics of the HTS DC reactor are analyzed under various operating conditions of the system. Through the results, applicability of an HTS DC reactor in an HVDC system is discussed in detail.

  12. Operating characteristic analysis of a 400 mH class HTS DC reactor in connection with a laboratory scale LCC type HVDC system

    International Nuclear Information System (INIS)

    Kim, Sung-Kyu; Kim, Kwangmin; Park, Minwon; Yu, In-Keun; Lee, Sangjin

    2015-01-01

    Highlights: • A 400 mH class HTS DC reactor and a laboratory scale test-bed for line-commutated converter type HVDC transmission system. • The 400 mH class HTS DC reactor was connected to real power network via the HVDC system. • The DC current flowed in HTS DC reactor has several harmonic components and it was analyzed using FFT. - Abstract: High temperature superconducting (HTS) devices are being developed due to their advantages. Most line commutated converter based high voltage direct current (HVDC) transmission systems for long-distance transmission require large inductance of DC reactor; however, generally, copper-based reactors cause a lot of electrical losses during the system operation. This is driving researchers to develop a new type of DC reactor using HTS wire. The authors have developed a 400 mH class HTS DC reactor and a laboratory scale test-bed for line-commutated converter type HVDC system and applied the HTS DC reactor to the HVDC system to investigate their operating characteristics. The 400 mH class HTS DC reactor is designed using a toroid type magnet. The HVDC system is designed in the form of a mono-pole system with thyristor-based 12-pulse power converters. In this paper, the investigation results of the HTS DC reactor in connection with the HVDC system are described. The operating characteristics of the HTS DC reactor are analyzed under various operating conditions of the system. Through the results, applicability of an HTS DC reactor in an HVDC system is discussed in detail.

  13. A nuclear reactor core fuel reload optimization using Artificial-Ant-Colony Connective Networks

    International Nuclear Information System (INIS)

    Lima, Alan M.M. de; Schirru, Roberto

    2005-01-01

    A Pressurized Water Reactor core must be reloaded every time the fuel burnup reaches a level when it is not possible to sustain nominal power operation. The nuclear core fuel reload optimization consists in finding a burned-up and fresh-fuel-assembly pattern that maximizes the number of full operational days. This problem is NP-hard, meaning that complexity grows exponentially with the number of fuel assemblies in the core. Besides that, the problem is non-linear and its search space is highly discontinual and multimodal. In this work a parallel computational system based on Ant Colony System (ACS) called Artificial-Ant-Colony Networks is introduced to solve the nuclear reactor core fuel reload optimization problem. ACS is a system based on artificial agents that uses the reinforcement learning technique and was originally developed to solve the Traveling Salesman Problem, which is conceptually similar to the nuclear fuel reload problem. (author)

  14. Achievement report for fiscal 1981 on Sunshine Program-assisted project. Research and development of materials for coal liquefaction plant (Research on materials); 1981 nendo sekitan ekika plant zairyo no kenkyu kaihatsu (zairyo no kenkyu) seika hokokusho

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1982-03-01

    Research and development is started of materials for constituting a liquefaction reactor which is the primary apparatus in the coal liquefaction process. Tested in the basic research on the designing of alloys for the reactor are Cr-Mo-V-Ti based alloys prepared by adding V, Ti, and B to Cr-Mo based alloys presently in use as materials for pressure vessels. They are melted and 50kg test ingots of steel are prepared, and an alloy with a constitution of Low Si-3%Cr-1%Mo-0.25%V-0.02%Ti-0.002%B is selected. In the designing of alloys to serve as stainless steel overlay welding materials and in the development of basic welding technologies, studies are conducted in search for materials that exhibit excellent durability under the conditions of liquefaction reaction and for technologies in this connection. These are accomplished using a test device installed this fiscal year, which is capable of reproducing high-temperature high-pressure hydrogen atmosphere. As the result, basic technologies are acquired, which will enable the achievement of the goal. In the study of on-site production technologies using medium-size ingots as the materials, an 85-ton medium size steel ingot of a new chemical constitution of Low Si-3Cr-1Mo-1/4V-Ti-B is melted, and a shell which is 400mm in thickness and 2m in internal diameter is forged, and the shell is subjected to a property and performance qualification test. (NEDO)

  15. Thermostable endoglucanases in the liquefaction of hydrothermally pretreated wheat straw

    Directory of Open Access Journals (Sweden)

    Siika-aho Matti

    2011-01-01

    Full Text Available Abstract Background Thermostable enzymes have several benefits in lignocellulose processing. In particular, they potentially allow the use of increased substrate concentrations (because the substrate viscosity decreases as the temperature increases, resulting in improved product yields and reduced capital and processing costs. A short pre-hydrolysis step at an elevated temperature using thermostable enzymes aimed at rapid liquefaction of the feedstock is seen as an attractive way to overcome the technical problems (such as poor mixing and mass transfer properties connected with high initial solid loadings in the lignocellulose to ethanol process. Results The capability of novel thermostable enzymes to reduce the viscosity of high-solid biomass suspensions using a real-time viscometric measurement method was investigated. Heterologously expressed enzymes from various thermophilic organisms were compared for their ability to liquefy the lignocellulosic substrate, hydrothermally pretreated wheat straw. Once the best enzymes were identified, the optimal temperatures for these enzymes to decrease substrate viscosity were compared. The combined hydrolytic properties of the thermostable preparations were tested in hydrolysis experiments. The studied mixtures were primarily designed to have good liquefaction potential, and therefore contained an enhanced proportion of the key liquefying enzyme, EGII/Cel5A. Conclusions Endoglucanases were shown to have a superior ability to rapidly reduce the viscosity of the 15% (w/w; dry matter hydrothermally pretreated wheat straw. Based on temperature profiling studies, Thermoascus aurantiacus EGII/Cel5A was the most promising enzyme for biomass liquefaction. Even though they were not optimized for saccharification, many of the thermostable enzyme mixtures had superior hydrolytic properties compared with the commercial reference enzymes at 55°C.

  16. Coal liquefaction and gas conversion: Proceedings. Volume 1

    Energy Technology Data Exchange (ETDEWEB)

    1993-12-31

    Volume I contains papers presented at the following sessions: AR-Coal Liquefaction; Gas to Liquids; and Direct Liquefaction. Selected papers have been processed separately for inclusion in the Energy Science and Technology Database.

  17. Development of continuous bench scale unit for direct liquefaction

    Energy Technology Data Exchange (ETDEWEB)

    Yoon, Wang Lai [Korea Inst. of Energy and Resources, Daeduk (Korea, Republic of)

    1996-12-31

    Batch coal liquefaction experiments using tubing bombs and continuous experiments by cell liquefaction test facility were carried out. The main purpose was to maximize the coal liquefaction yields by improving the activity of coal dissolution catalysts which are oil soluble transition metal naphthenate and to supplement the incomplete research results. In the meantime, the study on the reaction characteristics of coal liquefaction and coal liquid upgrading catalyst upon sulfiding conditions and phosphorous addition have been conducted (author). 102 refs., 35 figs.

  18. Development of continuous bench scale unit for direct liquefaction

    Energy Technology Data Exchange (ETDEWEB)

    Yoon, Wang Lai [Korea Inst. of Energy and Resources, Daeduk (Korea, Republic of)

    1995-12-31

    Batch coal liquefaction experiments using tubing bombs and continuous experiments by cell liquefaction test facility were carried out. The main purpose was to maximize the coal liquefaction yields by improving the activity of coal dissolution catalysts which are oil soluble transition metal naphthenate and to supplement the incomplete research results. In the meantime, the study on the reaction characteristics of coal liquefaction and coal liquid upgrading catalyst upon sulfiding conditions and phosphorous addition have been conducted (author). 102 refs., 35 figs.

  19. Parallel connecting poloidal coil system for a doublet tokamak fusion reactor

    International Nuclear Information System (INIS)

    Toffolo, W.E.; Chen, W.Y.; Purcell, J.R.; Wesley, J.C.

    1977-09-01

    A method has been developed for parallel connection of the ohmic heating (OH) coil. The method involves subdividing the OH-coil into a number of parallel connected subcoils, with each subcoil having about 20 turns. Each of the field shaping coils (F-coils) also contains 20 turns, so that when connected to a common power supply, the OH and F-coils are decoupled. The advantages resulting from the scheme are numerous: (1) each F-coil contains a much smaller number of turns compared with the previous design concept, thus the construction and maintenance will be easier; (2) the parallel connected OH-coils form a constant flux envelope, resulting in an inherently lower error field at the plasma and the TF coil region, and this low error field is not sensitive to the variation in location of the OH-coils; (3) the voltage and current ratings of the individual OH coil conductors are reduced; and (4) the low impedance of the OH-coil system greatly improves the possibility of using a homopolar motor generator as a means of achieving flux reversal during startup and plasma current control during the burn cycle

  20. Conceptual study of hydrogen donor solvent in the NEDOL coal liquefaction process

    Energy Technology Data Exchange (ETDEWEB)

    Kouzu, M.; Onozaki, M.; Oi, S. [Mitsui SRC Co Ltd, Tokyo (Japan)

    2002-03-01

    A 150 ton/day coal liquefaction pilot plant (PP) of the NEDOL process, supported by New Energy and Industrial Technology Development Organization (NEDO), was operated successfully for a total of 269 days at Kashima, Japan. With a great number of data obtained through the operation, the design procedure for the NEDOL process was studied. Middle and heavy oils from the coal employed were recycled as a hydrogen-donor solvent after hydrotreatment over Ni Mo/gamma-Al2O{sub 3} in a trickle bed reactor. The hydrogen donating ability of the solvent was high enough to obtain higher oil yield (50-58 wt%) at the aromaticity of ca. 0.45. Life expectancy of solvent hydrotreatment catalyst, requisite to the hydrotreater design, was estimated under PP operating conditions. In addition, physical properties of the solvent required for process design were determined, and hydrodynamics in the liquefaction bubble column reactors were examined. Taking the obtained hydrodynamics and thermal behavior into consideration, a design procedure of the liquefaction bubble column reactors was establsihed using a process simulator (CARD) validated by the product yields of PP. The simulation including distillation and solvent hydrotreatment showed that the content of heavy oil fraction (b.p. 350 - 538{degree} C) in the solvent was a determinant factor in the design of a large scale plant based on the NEDOL process.

  1. Prospect of coal liquefaction in Indonesia

    International Nuclear Information System (INIS)

    Hartiniati; Dasuki, A.S.; Artanto, Yu.; Sulaksono, D.; Gunanjar

    1997-01-01

    With the current known oil reserves of about 11 billion barrel and annual production of approximately 500 million barrel, the country's oil reserves will be depleted by 2010, and Indonesia would have become net oil importer if no major oil fields be found somewhere in the archipelago. Under such circumstances the development of new sources of liquid fuel becomes a must, and coal liquefaction can be one possible solution for the future energy problem in Indonesia, particularly in the transportation sector due to the availability of coal in huge amount. This paper present the prospect of coal liquefaction in Indonesia and look at the possibility of integrating the process with HTR as a heat supplier. Evaluation of liquidability of several low grade Indonesian coals will also be presented. Coal from South Banko-Tanjung Enim is found to be one of the most suitable coal for liquefaction. Several studies show that an advanced coal liquefaction technology recently developed has the potential to reduce not only the environmental impact but also the production cost. The price of oil produced in the year 2000 is expected to reach US $ 17.5 ∼ 19.2/barrel and this will compete with the current oil price. Not much conclusion can be drawn from the idea of integrating HTR with coal liquefaction plant due to limited information available. (author). 7 figs, 3 tabs

  2. Coal liquefaction and gas conversion contractors review conference: Proceedings

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1995-11-01

    This volume contains 55 papers presented at the conference. They are divided into the following topical sections: Direct liquefaction; Indirect liquefaction; Gas conversion (methane conversion); and Advanced research liquefaction. Papers in this last section deal mostly with coprocessing of coal with petroleum, plastics, and waste tires, and catalyst studies. Selected papers are indexed separately for inclusion in the Energy Science and Technology Database.

  3. Experimental Study of Thermal Crisis in Connection with Tokamak Reactor High Heat Flux Components

    International Nuclear Information System (INIS)

    Gallo, D.; Giardina, M.; Castiglia, F.; Celata, G.P.; Mariani, A.; Zummo, G.; Cumo, M.

    2000-01-01

    The results of an experimental research on high heat flux thermal crisis in forced convective subcooled water flow, under operative conditions of interest to the thermal-hydraulic design of TOKAMAK fusion reactors, are here reported. These experiments, carried out in the framework of a collaboration between the Nuclear Engineering Department of Palermo University and the National Institute of Thermal - Fluid Dynamics of the ENEA - Casaccia (Rome), were performed on the STAF (Scambio Termico Alti Flussi) water loop and consisted, essentially, in a high speed photographic study which enabled focusing several information on bubble characteristics and flow patterns taking place during the burnout phenomenology

  4. A nuclear reactor core fuel reload optimization using artificial ant colony connective networks

    International Nuclear Information System (INIS)

    Lima, Alan M.M. de; Schirru, Roberto; Carvalho da Silva, Fernando; Medeiros, Jose Antonio Carlos Canedo

    2008-01-01

    The core of a nuclear Pressurized Water Reactor (PWR) may be reloaded every time the fuel burn-up is such that it is not more possible to maintain the reactor operating at nominal power. The nuclear core fuel reload optimization problem consists in finding a pattern of burned-up and fresh-fuel assemblies that maximize the number of full operational days. This is an NP-Hard problem, meaning that complexity grows exponentially with the number of fuel assemblies in the core. Moreover, the problem is non-linear and its search space is highly discontinuous and multi-modal. Ant Colony System (ACS) is an optimization algorithm based on artificial ants that uses the reinforcement learning technique. The ACS was originally developed to solve the Traveling Salesman Problem (TSP), which is conceptually similar to the nuclear core fuel reload problem. In this work a parallel computational system based on the ACS, called Artificial Ant Colony Networks is introduced to solve the core fuel reload optimization problem

  5. A nuclear reactor core fuel reload optimization using artificial ant colony connective networks

    Energy Technology Data Exchange (ETDEWEB)

    Lima, Alan M.M. de [Universidade Federal do Rio de Janeiro, PEN/COPPE - UFRJ, Ilha do Fundao s/n, CEP 21945-970 Rio de Janeiro (Brazil)], E-mail: alanmmlima@yahoo.com.br; Schirru, Roberto [Universidade Federal do Rio de Janeiro, PEN/COPPE - UFRJ, Ilha do Fundao s/n, CEP 21945-970 Rio de Janeiro (Brazil)], E-mail: schirru@lmp.ufrj.br; Carvalho da Silva, Fernando [Universidade Federal do Rio de Janeiro, PEN/COPPE - UFRJ, Ilha do Fundao s/n, CEP 21945-970 Rio de Janeiro (Brazil)], E-mail: fernando@con.ufrj.br; Medeiros, Jose Antonio Carlos Canedo [Universidade Federal do Rio de Janeiro, PEN/COPPE - UFRJ, Ilha do Fundao s/n, CEP 21945-970 Rio de Janeiro (Brazil)], E-mail: canedo@lmp.ufrj.br

    2008-09-15

    The core of a nuclear Pressurized Water Reactor (PWR) may be reloaded every time the fuel burn-up is such that it is not more possible to maintain the reactor operating at nominal power. The nuclear core fuel reload optimization problem consists in finding a pattern of burned-up and fresh-fuel assemblies that maximize the number of full operational days. This is an NP-Hard problem, meaning that complexity grows exponentially with the number of fuel assemblies in the core. Moreover, the problem is non-linear and its search space is highly discontinuous and multi-modal. Ant Colony System (ACS) is an optimization algorithm based on artificial ants that uses the reinforcement learning technique. The ACS was originally developed to solve the Traveling Salesman Problem (TSP), which is conceptually similar to the nuclear core fuel reload problem. In this work a parallel computational system based on the ACS, called Artificial Ant Colony Networks is introduced to solve the core fuel reload optimization problem.

  6. Reactor

    International Nuclear Information System (INIS)

    Ikeda, Masaomi; Kashimura, Kazuo; Inoue, Kazuyuki; Nishioka, Kazuya.

    1979-01-01

    Purpose: To facilitate the construction of a reactor containment building, whereby the inspections of the outer wall of a reactor container after the completion of the construction of the reactor building can be easily carried out. Constitution: In a reactor accommodated in a container encircled by a building wall, a space is provided between the container and the building wall encircling the container, and a metal wall is provided in the space so that it is fitted in the building wall in an attachable or detatchable manner. (Aizawa, K.)

  7. Novel bimetallic dispersed catalysts for temperature-programmed coal liquefaction

    Energy Technology Data Exchange (ETDEWEB)

    Chunshan, Song; Kirby, S.; Schmidt, E. [Pennsylvania State Univ., University Park, PA (United States)] [and others

    1995-12-31

    The objective of this project is to explore bimetallic dispersed catalysts for more efficient coal liquefaction. Coal liquefaction involves cleavage of methylene, dimethylene and ether bridges connecting various aromatic units and the reactions of various oxygen functional groups. This paper describes recent results on (1) hydrodeoxygenation of O-containing polycyclic model compounds using novel organometallic catalyst precursors; and (2) activity and selectivity of dispersed Fe catalysts from organometallic and inorganic precursors for hydrocracking of 4-(1-naphthylmethyl) bibenzyl. The results showed that some iron containing catalysts have higher activity in the sulfur-free form, contrary to conventional wisdom. Adding sulfur to Fe precursors with Cp-ligands decreased the activity of the resulting catalyst. This is in distinct contrast to the cases with iron pentacarbonyl and superfine Fe{sub 2}O{sub 3}, where S addition increased their catalytic activity substantially. A positive correlation between sulfur addition and increased activity can be seen, but a reversed trend between Fe cluster size and hydrocracking conversion could be observed, for carbonyl-type Fe precursors. It is apparent that the activity and selectivity of Fe catalysts for NMBB conversion depends strongly on both the type of ligand environment, the oxidation state and the number of intermetal bonds in the molecular precursor.

  8. Residual liquefaction of seabed under standing waves

    DEFF Research Database (Denmark)

    Kirca, V.S. Ozgur; Sumer, B. Mutlu; Fredsøe, Jørgen

    2013-01-01

    This paper presents the results of an experimental study of the seabed liquefaction beneath standing waves. Silt (with d50 =0.070mm) was used in the experiments. Two kinds of measurements were carried out: pore water pressure measurements and water surface elevation measurements. These measurements...... were synchronized with video recording of the liquefaction process from the side. The ranges of the various quantities in the experiments were wave height H= 5.9-12.0 cm, wave period T= 1.09s, and water depth h=30 cm. The experiments show that the seabed liquefaction under standing waves, although...... qualitatively similar, show features different from that caused by progressive waves. The pore water pressure builds up (or accumulated) in the areas around the node and subsequently spreads out toward the antinodes. The experimental results imply that this transport is caused by a diffusion mechanism...

  9. Operating characteristic analysis of a 400 mH class HTS DC reactor in connection with a laboratory scale LCC type HVDC system

    Science.gov (United States)

    Kim, Sung-Kyu; Kim, Kwangmin; Park, Minwon; Yu, In-Keun; Lee, Sangjin

    2015-11-01

    High temperature superconducting (HTS) devices are being developed due to their advantages. Most line commutated converter based high voltage direct current (HVDC) transmission systems for long-distance transmission require large inductance of DC reactor; however, generally, copper-based reactors cause a lot of electrical losses during the system operation. This is driving researchers to develop a new type of DC reactor using HTS wire. The authors have developed a 400 mH class HTS DC reactor and a laboratory scale test-bed for line-commutated converter type HVDC system and applied the HTS DC reactor to the HVDC system to investigate their operating characteristics. The 400 mH class HTS DC reactor is designed using a toroid type magnet. The HVDC system is designed in the form of a mono-pole system with thyristor-based 12-pulse power converters. In this paper, the investigation results of the HTS DC reactor in connection with the HVDC system are described. The operating characteristics of the HTS DC reactor are analyzed under various operating conditions of the system. Through the results, applicability of an HTS DC reactor in an HVDC system is discussed in detail.

  10. Behavior of catalyst and mineral matter in coal liquefaction; Sekitan ekika hannochu no kobusshitsu to shokubai no kyodo

    Energy Technology Data Exchange (ETDEWEB)

    Iwasaki, K.; Wang, J.; Tomita, A. [Tohoku University, Sendai (Japan). Institute for Chemical Reaction Science

    1996-10-28

    Mineral matter in coals is important in various senses for coal liquefaction. It is possible that the catalytic activity is affected by the interaction between catalyst and mineral matter. Iron-based catalyst forms pyrrhotite in the process of liquefaction, but the interaction between it and mineral matter is not known in detail. In this study, the interaction between mineral matter and catalyst and the selective reaction between them were investigated. Tanito Harum coal was used for this study. This coal contains a slight amount of siderite and jarosite besides pyrite as iron compounds. Liquefaction samples were obtained from the 1 t/d NEDOL process PSU. The solid deposits in the reactor mainly contained pyrrhotite and quartz. A slight amount of kaolinite was observed, and pyrite was little remained. It was found that the catalyst (pyrrhotite) often coexisted with quartz, clay and calcite. 8 figs., 2 tabs.

  11. Biomass Indirect Liquefaction Strategy Workshop Summary Report

    Energy Technology Data Exchange (ETDEWEB)

    none,

    2014-07-01

    This report is based on the proceedings of the U.S. Department of Energy Bioenergy Technologies Office Biomass Indirect Liquefaction Strategy Workshop. The workshop, held March 20–21, 2014, in Golden, Colorado, discussed and detailed the research and development needs for biomass indirect liquefaction. Discussions focused on pathways that convert biomass-based syngas (or any carbon monoxide, hydrogen gaseous stream) to liquid intermediates (alcohols or acids) and further synthesize those intermediates to liquid hydrocarbons that are compatible as either a refinery feed or neat fuel.

  12. Liquefaction chemistry and kinetics: Hydrogen utilization studies

    Energy Technology Data Exchange (ETDEWEB)

    Rothenberger, K.S.; Warzinski, R.P.; Cugini, A.V. [Pittsburgh Energy Technology Center, PA (United States)] [and others

    1995-12-31

    The objectives of this project are to investigate the chemistry and kinetics that occur in the initial stages of coal liquefaction and to determine the effects of hydrogen pressure, catalyst activity, and solvent type on the quantity and quality of the products produced. The project comprises three tasks: (1) preconversion chemistry and kinetics, (2) hydrogen utilization studies, and (3) assessment of kinetic models for liquefaction. The hydrogen utilization studies work will be the main topic of this report. However, the other tasks are briefly described.

  13. Fundamental studies of coal liquefaction

    Energy Technology Data Exchange (ETDEWEB)

    1995-01-01

    The authors have examined the pyrolysis of Argonne samples of Wyodak and Illinois No. 6 coal in argon, undecane, Tetralin, and water. The effects of the pyrolysis on individual particles of coal were monitored visually in a cell with diamond windows capable of operation to temperature and pressures in excess of 500{degrees}C and 3000 psi. The changes in the particles from ambient to 460{degrees}C were recorded in real time on video tape, and images were then taken from the tape record and analyzed. The study showed that in argon both coals developed tars at 350{degrees}-370{degrees}C. The tars then quickly evaporated, leaving core particles remarkably similar in size and shape to the initial particles. These observations suggest that coal does not melt nor become fully liquid when heated. Nor does the softened coal undergo crosslinking to generate coke. Rather the simple loss of volatiles leaves behind the core residue as coke. Contrary to the common view, there appears to be no link between the bond-breaking processes yielding tar and the interaction of the coal with H-donors leading to liquefaction. Water as a medium was surprising in its effect. Both coals began to shrink at 300{degrees}-350{degrees}C, with the effect appearing to be more of an erosion rather than a uniform loss of substance as seen in Tetralin. The Wyodak continued to shrink to 460{degrees}C to about half its initial size. With the Illinois No. 6 coal, however, the process reversed at around 420{degrees}C, and the particles appeared to grow with the evolution of a tar, continuing to 460{degrees}C. The authors submit that this final observation is evidence for hydrothermal synthesis of hydrocarbons at these conditions.

  14. Methods of natural gas liquefaction and natural gas liquefaction plants utilizing multiple and varying gas streams

    Science.gov (United States)

    Wilding, Bruce M; Turner, Terry D

    2014-12-02

    A method of natural gas liquefaction may include cooling a gaseous NG process stream to form a liquid NG process stream. The method may further include directing the first tail gas stream out of a plant at a first pressure and directing a second tail gas stream out of the plant at a second pressure. An additional method of natural gas liquefaction may include separating CO.sub.2 from a liquid NG process stream and processing the CO.sub.2 to provide a CO.sub.2 product stream. Another method of natural gas liquefaction may include combining a marginal gaseous NG process stream with a secondary substantially pure NG stream to provide an improved gaseous NG process stream. Additionally, a NG liquefaction plant may include a first tail gas outlet, and at least a second tail gas outlet, the at least a second tail gas outlet separate from the first tail gas outlet.

  15. Catalytic subcritical water liquefaction of flax straw for high yield of furfural

    International Nuclear Information System (INIS)

    Harry, Inibehe; Ibrahim, Hussameldin; Thring, Ron; Idem, Raphael

    2014-01-01

    There is substantial interest in the application of biomass as a renewable fuel or for production of chemicals. Flax straw can be converted into valuable chemicals and biofuels via liquefaction in sub-critical water. In this study, the yield of furfural and the kinetics of flax straw liquefaction under sub-critical water conditions were investigated using a high-pressure autoclave reactor. The liquefaction was conducted in the temperature range of 175–325 °C, pressure of 0.1 MPa–8 MPa, retention time in the range of 0 min–120 min, and flax straw mass fraction (w F ) of 5–20 %. Also, the effect of acid catalysts on furfural yield was studied. The kinetic parameters of flax straw liquefaction were determined using nonlinear regression of the experimental data, assuming second-order kinetics. The apparent activation energy was found to be 27.97 kJ mol −1 while the reaction order was 2.0. The optimum condition for furfural yield was at 250 °C, 6.0 MPa, w F of 5% and 0 retention time after reaching set conditions. An acid catalyst was found to selectively favour furfural yield with 40% flax straw conversion. - Highlights: • Flax straw liquefaction in subcritical water. • Creation of a reaction pathway that can be used to optimized furfural production. • Acid catalyst selectively favoured furfural yield with respect to other liquid products. • At the highest process temperature of 325 °C, a carbon conversion of 40% was achieved. • Activation energy and reaction order was 28 kJ/mol and 2.0 respectively

  16. Direct hydrothermal liquefaction of undried macroalgae Enteromorpha prolifera using acid catalysts

    International Nuclear Information System (INIS)

    Yang, Wenchao; Li, Xianguo; Liu, Shishi; Feng, Lijuan

    2014-01-01

    Highlights: • Bio-oil from liquefaction of wet E. prolifera was as feasible as dry powder. • Adding acid catalysts could improve the flow property of bio-oil. • Alkenes in the bio-oil converted to ketones in the presence of acid catalysts. • Content of 5-methyl furfural increased in the bio-oil obtained with acid catalysts. • Esters were formed in the bio-oil when adding sulfuric acid as a catalyst. - Abstract: Direct liquefaction of macroalgae Enteromorpha prolifera without predrying treatment was performed in a batch reactor. Effects of temperature, reaction time, biomass-to-water ratio and acid catalysts (sulfuric acid and acetic acid) on liquefaction products were investigated. Raw material and liquefaction products were analyzed by elemental analysis, Fourier transform infrared (FT-IR) and gas chromatography–mass spectrometry (GC–MS). Results showed that liquefaction at 290 °C for 20 min with 1:3 biomass-to-water ratio produced the highest bio-oil yield of 28.4 wt%, and high heating value (HHV) was 29.5 MJ/kg. Main components of bio-oil were fatty acids, ketones, alkenes and 5-methyl furfural, and main components of water soluble organics (WSOs) were pyridines, carboxylic acids and glycerol. In the bio-oil obtained with acid catalysts, content of ketones significantly increased while alkenes disappeared. Content of 5-methyl furfural also increased. Flow property of bio-oils was improved in the presence of acid catalysts. Moreover, esters were formed when adding sulfuric acid

  17. Improvements on mapping soil liquefaction at a regional scale

    Science.gov (United States)

    Zhu, Jing

    Earthquake induced soil liquefaction is an important secondary hazard during earthquakes and can lead to significant damage to infrastructure. Mapping liquefaction hazard is important in both planning for earthquake events and guiding relief efforts by positioning resources once the events have occurred. This dissertation addresses two aspects of liquefaction hazard mapping at a regional scale including 1) predictive liquefaction hazard mapping and 2) post-liquefaction cataloging. First, current predictive hazard liquefaction mapping relies on detailed geologic maps and geotechnical data, which are not always available in at-risk regions. This dissertation improves the predictive liquefaction hazard mapping by the development and validation of geospatial liquefaction models (Chapter 2 and 3) that predict liquefaction extent and are appropriate for global application. The geospatial liquefaction models are developed using logistic regression from a liquefaction database consisting of the data from 27 earthquake events from six countries. The model that performs best over the entire dataset includes peak ground velocity (PGV), VS30, distance to river, distance to coast, and precipitation. The model that performs best over the noncoastal dataset includes PGV, VS30, water table depth, distance to water body, and precipitation. Second, post-earthquake liquefaction cataloging historically relies on field investigation that is often limited by time and expense, and therefore results in limited and incomplete liquefaction inventories. This dissertation improves the post-earthquake cataloging by the development and validation of a remote sensing-based method that can be quickly applied over a broad region after an earthquake and provide a detailed map of liquefaction surface effects (Chapter 4). Our method uses the optical satellite images before and after an earthquake event from the WorldView-2 satellite with 2 m spatial resolution and eight spectral bands. Our method

  18. The Texts of the Instruments connected with the Agency's Assistance to the Democratic Republic of the Congo in Continuing a Research Reactor Project Project. Extension Agreement

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1966-11-18

    The text of the Project Extension Agreement between the Agency and the Government of the Democratic Republic of the Congo in connection with the Agency's additional assistance to that Government in continuing a research reactor project is reproduced in this document for the information of all Members. This Agreement entered into force on 27 September 1966.

  19. The Texts of the Instruments connected with the Agency's Assistance to Finland in relation to a Research Reactor Project. A Fourth Supply Agreement

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1970-02-05

    As a sequel to the assistance which the Agency provided to the Government of Finland in connection with a research reactor project, a fourth Supply Agreement has been concluded between the Agency and the Governments of Finland and the United States of America. This Agreement entered into force on 27 November 1969, and the text is reproduced herein for the information of all Members.

  20. The Texts of the Instruments connected with the Agency's Assistance to Finland in relation to a Research Reactor Project. A Third Supply Agreement

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1968-01-12

    As a sequel to the assistance which the Agency provided to the Government of Finland in connection with a research reactor project), a third Supply Agreement has been concluded between the Agency and the Governments of Finland and the United States of America. This Agreement entered into force on 5 November 1967, and the text) is reproduced herein for the information of all Members.

  1. The Texts of the Instruments connected with the Agency's Assistance to Yugoslavia in Establishing a Research Reactor Project. Third Supply Agreement

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1971-03-11

    As a sequel to the assistance which the Agency provided to the Government of Yugoslavia in connection with a research reactor project, a third Supply Agreement has been concluded between the Agency and the Governments of the United States of America and Yugoslavia. This Agreement entered into force on 30 December 1970, and the text is reproduced herein for the information of all Members.

  2. The Texts of the Instruments connected with the Agency's Assistance to Finland in relation to a Research Reactor Project. A Third Supply Agreement

    International Nuclear Information System (INIS)

    1968-01-01

    As a sequel to the assistance which the Agency provided to the Government of Finland in connection with a research reactor project), a third Supply Agreement has been concluded between the Agency and the Governments of Finland and the United States of America. This Agreement entered into force on 5 November 1967, and the text) is reproduced herein for the information of all Members

  3. The Texts of the Instruments connected with the Agency's Assistance to Yugoslavia in Establishing a Research Reactor Project. Third Supply Agreement

    International Nuclear Information System (INIS)

    1971-01-01

    As a sequel to the assistance which the Agency provided to the Government of Yugoslavia in connection with a research reactor project, a third Supply Agreement has been concluded between the Agency and the Governments of the United States of America and Yugoslavia. This Agreement entered into force on 30 December 1970, and the text is reproduced herein for the information of all Members

  4. The Texts of the Instruments connected with the Agency's Assistance to Finland in relation to a Research Reactor Project. A Fourth Supply Agreement

    International Nuclear Information System (INIS)

    1970-01-01

    As a sequel to the assistance which the Agency provided to the Government of Finland in connection with a research reactor project, a fourth Supply Agreement has been concluded between the Agency and the Governments of Finland and the United States of America. This Agreement entered into force on 27 November 1969, and the text is reproduced herein for the information of all Members

  5. Dispersed-phase catalysis in coal liquefaction

    International Nuclear Information System (INIS)

    Utz, B.R.; Cugini, A.V.; Frommell, E.A.

    1990-01-01

    This paper reports that the specific reaction (activation) conditions for the conversion of catalyst precursors to unsupported catalyst have a direct effect on the catalytic activity and dispersion. The importance of reaction intermediates in decomposition of ammonium heptamolybdate and ammonium tetrathiomolybdate, and the sensitivity of these intermediates to reaction conditions, were studied in coal liquefaction systems. Recent results indicate that optimization of activation conditions facilitates the formation of a highly dispersed and active form of molybdenum disulfide for coal liquefaction. The use of the catalyst precursors ammonium heptamolybdate, ammonium tetrathiomolybdate, and molybdenum trisulfide for the conversion of coal to soluble products will be discussed. The use of an unsupported dispersed-phase catalyst for direct coal liquefaction is not a novel concept and has been employed in may studies with varying success. Dispersed-phase catalysts soluble and oil-soluble salts, and as finely divided powders. While some methods of catalyst introduction give higher dispersion of the catalyst and greater activity for the liquefaction of coal, all of the techniques allow the formation of a finely dispersed inorganic phase

  6. Hydrothermal Liquefaction of the Microalgae Phaeodactylum tricornutum

    DEFF Research Database (Denmark)

    Sigaard Christensen, Per; Peng, Gaël; Vogel, Frédéric

    2014-01-01

    The microalgae Phaeodactylum tricornutum was processed by hydrothermal liquefaction in order to assess the influence of reaction temperature and reaction time on the product and elemental distribution. The experiments were carried out at different reaction times (5 and 15 min) and over a wide range...

  7. Evaluating liquefaction potential. A case history

    International Nuclear Information System (INIS)

    Blystra, A.R.

    1991-01-01

    Several earthen hydropower embankment dams in the midwestern United States were constructed using hydraulic fill methods and are liable to liquefaction during an earthquake due to the use of very loose, saturated sand in the embankment or foundations. A case history is presented describing the methodology used in evaluating the liquefaction potential of the largest earthfill dam in Michigan. The methodology includes the use of standard penetration and cone penetration test data in the formulation of a simplified procedure. Field investigations, laboratory testing, and analyses used are described. In addition to the drilling program, field work included an extensive ground penetrating radar survey, acoustic emission testing, and an electrical resistivity survey. It was found that the lowest calculated factor of safety against liquefaction is 0.63 for a loose zone ca 140 feet below the top of the embankment, and the factor of safety against slope failure, should the zone liquefy, is 1.49. It was concluded that while liquefaction is possible, post earthquake stability is adequate. 6 refs., 3 figs., 1 tab

  8. Liquefaction of torrefied wood using microwave irradiation

    Science.gov (United States)

    Mengchao Zhou; Thomas Eberhardt; Pingping Xin; Chung-Yun Hse; Hui Pan

    2016-01-01

    Torrefaction is an effective pretreatment method to improve the uniformity and quality of lignocellulosic biomass before further thermal processing (e.g., gasification, combustion). The objective of this study was to determine the impacts of torrefaction as a pretreatment before liquefaction. Wood chips were torrefied for 2 h at three different temperatures (230, 260,...

  9. Fiscal 1997 achievement report. Coal liquefaction technology development - Bituminous coal liquefaction technology development - Study for supporting pilot plant - Study using 1t/d PSU (Study of operation using PSU); 1997 nendo seika hokokusho. Sekitan ekika gijutsu kaihatsu - Rekiseitan ekika gijutsu no kaihatsu - Pilot plant no shien kenkyu - 1t/d process support unit (PSU) ni yoru kenkyu (PSU ni yoru unten kenkyu)

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1998-03-01

    The operation of a 1t/d PSU (process support unit) was studied for the NEDOL coal liquefaction process. In the modification of facilities, equipment and devices were procured for the product oil reforming facilities and their installation was partly accomplished. In the coal injection operation, a 60-day slurry operation was conducted, using coal types of the upper limit and lower limit qualities, for expanding the scope of coal types applicable to the NEDOL process and for exploring optimum conditions, and another operation of 37 days was conducted using Chinese coal and Chinese-prepared liquefaction catalysts, and the two operations were studied for difference in yields and in operationality. Characteristics of the liquefaction reactors were investigated and basic studies were made relative to the physical property of the yielded coal oil. In the operation for maintenance, the 1st liquefaction reactor was singly operated for an 8-day slurry operation, which was to check the progress of liquefaction in a 1-reactor setup. Concerning the reforming of the product oil, the hydrogenation reactors were checked for their response to temperature control. Moreover, hydrogenation solvents were produced for the PSU and for China. (NEDO)

  10. OLIGOMERIZATION AND LIQUEFACTION OF ETHYLENE

    African Journals Online (AJOL)

    oligomerize ethylene gas in a packed bed reactor operated at 100-300°C under apressure of 500psi and ... The gas flow was then switched back to N, gas and temperature controller was simultaneously set to the desired reaction temperature. Once the desired .... be considered non-ideal for ethylene oligomerization.

  11. A method for emergency flooding of the gland in the main circulating pump of pressurized water reactors and the connection therefor

    International Nuclear Information System (INIS)

    Skalicky, A.

    1978-01-01

    A method is described for the emergency flooding of the main circulating pumps of a pressurized water reactor such that in pressure drop in the flooded gland owing to pump suction, the pump head is connected by the pressure difference action to the flooding gland pipe, this via the heat sink and the filter of the emergency flooding circuit connected to the pump head. The emergency flooding circuit consisting of a pressure reducing valve, a check valve and a stop valve is connected to the pump head, behind the heat sink and the filter. The pressure reducing valve separates two pressure spaces. The former is connected to the pump head via the check valve and to the flooding pipe via the stop valve and the check valve. The latter is connected to the suction pump. (B.S.)

  12. Coal liquefaction in early stage of NEDOL process 1t/d PSU; 1t/d PSU ni okeru ekika shoki hanno ni kansuru kento

    Energy Technology Data Exchange (ETDEWEB)

    Ikeda, K.; Kawabata, M.; Mochizuki, M.; Imada, K. [Nippon Steel Corp., Tokyo (Japan); Nogami, Y.; Inokuchi, K. [Mitsui SRC Development Co. Ltd., Tokyo (Japan)

    1996-10-28

    To investigate the behavior of coal liquefaction reaction in early stage as a part of studies on the coal liquefaction characteristics using NEDOL process 1 t/d process supporting unit (PSU), coal slurry sample was taken from the outlet of slurry preheater located in the upflow of liquefaction reactors, and was tested. Tanito Harum coal was used for liquefaction. Preheater was operated under the condition of pressure of 170 kg/cm{sup 2}, gas flow rate of 64 Nm{sup 3}/hr, and at temperature up to 410{degree}C at the outlet, in response to the standard test condition. The slurry sample was discharged into a high temperature separator with temperature of 250{degree}C. Liquefaction was not proceeded at the outlet of preheater. Solid residue yielded around 80%, and liquid yielded around 15%. Gases, CO and CO2, and water yielded also small amount around 3%. The solid sample contained much IOM fraction (tetrahydrofuran-insoluble and ash), and the liquid contained much heavy oil fraction. Hydrogenation was not proceeded, and the hydrogen consumption was very low showing below one-tenth of that at the usual operation. Hydrogen sulfide gas was formed at early stage, which suggested that the change of iron sulfide catalyst occur at early stage of liquefaction. 1 ref., 5 figs., 2 tabs.

  13. Bio-crude production from secondary pulp/paper-mill sludge and waste newspaper via co-liquefaction in hot-compressed water

    International Nuclear Information System (INIS)

    Zhang, Linghong; Champagne, Pascale; Xu, Chunbao

    2011-01-01

    Co-liquefaction of secondary pulp/paper-mill sludge (solids concentration: 1.6 wt%) and waste newspaper with a total solids concentration of 11.3 wt% was investigated with and without the addition of catalysts in a 75 ml Parr High-Pressure reactor at temperatures of 250-380 o C for 20 min. The yield of heavy oil (HO) without catalyst was between 16.7 and 28.0 wt% within this temperature range, and peaked at 350 o C. The addition of HCO 2 H, FeS, or KOH at 5 wt% of the total solids (on a dry basis) was found to enhance the HO yield at 300 o C, particularly HCO 2 H, which increased the yield of HO from 24.9 to 34.4 wt%. More interestingly, synergistic effects between secondary pulp/paper-mill sludge and waste newspaper were observed in the co-liquefaction operations. For example, the HO yield attained was 26.9 wt% at 300 o C in the co-liquefaction of the mixture of 33 wt% sludge and 67 wt% waste newspaper, and was noted to be 9 wt% and 6 wt% higher than the yields obtained from liquefaction of sludge and waste newspaper alone, respectively. The HOs from liquefaction or co-liquefaction at 300 o C for 20 min exhibited significantly higher energy contents (HHV ≥ 30 MJ/kg), almost doubled those (-tilde 16 MJ/kg) of the original feedstocks.

  14. Effect of process parameters on hydrothermal liquefaction of oil palm biomass for bio-oil production and its life cycle assessment

    International Nuclear Information System (INIS)

    Chan, Yi Herng; Yusup, Suzana; Quitain, Armando T.; Tan, Raymond R.; Sasaki, Mitsuru; Lam, Hon Loong; Uemura, Yoshimitsu

    2015-01-01

    Highlights: • Water is used as a clean solvent to liquefy palm biomass to bio-oil. • The optimum liquefaction condition of oil palm biomass is 390 °C and 25 MPa. • Optimum reaction time for liquefaction of empty fruit bunch and palm mesocarp fiber is 120 min. • Optimum reaction time for liquefaction of palm kernel shell is 240 min. • From the life cycle assessment, a net 2.29 kg CO 2 equivalent is generated per kg of bio-oil produced. - Abstract: This paper presents the studies on the effect of three process parameters; temperature, pressure and reaction time on the subcritical and supercritical hydrothermal liquefaction of oil palm empty fruit bunch, palm mesocarp fiber and palm kernel shell. The effect of temperature (330–390 °C), pressure (25–35 MPa) and reaction time (30–240 min) on bio-oil yields were investigated using a Inconel batch reactor. The optimum liquefaction condition for empty fruit bunch, palm mesocarp fiber and palm kernel shell was at supercritical condition of water; 390 °C and 25 MPa. For the effect of reaction time, bio-oil from empty fruit bunch and palm mesocarp fiber attained maximum yields at 120 min, whereas bio-oil yield from palm kernel shell continued to increase at reaction time of 240 min. Lastly, a life cycle assessment based on a conceptual biomass hydrothermal liquefaction process for bio-oil production was constructed and presented

  15. Direct catalytic hydrothermal liquefaction of spirulina to biofuels with hydrogen

    Science.gov (United States)

    Zeng, Qin; Liao, Hansheng; Zhou, Shiqin; Li, Qiuping; Wang, Lu; Yu, Zhihao; Jing, Li

    2018-01-01

    We report herein on acquiring biofuels from direct catalytic hydrothermal liquefaction of spirulina. The component of bio-oil from direct catalytic hydrothermal liquefaction was similar to that from two independent processes (including liquefaction and upgrading of biocrude). However, one step process has higher carbon recovery, due to the less loss of carbons. It was demonstrated that the yield and HHV of bio-oil from direct catalytic algae with hydrothermal condition is higher than that from two independent processes.

  16. Whole Algae Hydrothermal Liquefaction Technology Pathway

    Energy Technology Data Exchange (ETDEWEB)

    Biddy, Mary J.; Davis, Ryan; Jones, Susanne B.; Zhu, Yunhua

    2013-03-31

    In support of the Bioenergy Technologies Office, the National Renewable Energy Laboratory (NREL) and the Pacific Northwest National Laboratory (PNNL) are undertaking studies of biomass conversion technologies to hydrocarbon fuels to identify barriers and target research toward reducing conversion costs. Process designs and preliminary economic estimates for each of these pathway cases were developed using rigorous modeling tools (Aspen Plus and Chemcad). These analyses incorporated the best information available at the time of development, including data from recent pilot and bench-scale demonstrations, collaborative industrial and academic partners, and published literature and patents. This pathway case investigates the feasibility of using whole wet microalgae as a feedstock for conversion via hydrothermal liquefaction. Technical barriers and key research needs have been assessed in order for the hydrothermal liquefaction of microalgae to be competitive with petroleum-derived gasoline, diesel and jet range blendstocks.

  17. Experimental study on the liquefaction of cellulose in supercritical ethanol

    Science.gov (United States)

    Peng, Jinxing; Liu, Xinyuan; Bao, Zhenbo

    2018-03-01

    Cellulose is the major composition of solid waste for producing biofuel; cellulose liquefaction is helpful for realizing biomass supercritical liquefaction process. This paper is taking supercritical ethanol as the medium, liquefied cellulose with the intermittence installation of high press cauldron. Experiments have studied technical condition and the technology parameter of cellulose liquefaction in supercritical ethanol, and the pyrolysis mechanism was analysed based on the pyrolysis product. Results show that cellulose can be liquefied, can get good effect through appropriate technology condition. Under not catalyst, highest liquefaction rate of cellulose can reach 73.5%. The composition of the pyrolysis product was determined by GC-MS.

  18. Reactors

    DEFF Research Database (Denmark)

    Shah, Vivek; Vaz Salles, Marcos António

    2018-01-01

    The requirements for OLTP database systems are becoming ever more demanding. Domains such as finance and computer games increasingly mandate that developers be able to encode complex application logic and control transaction latencies in in-memory databases. At the same time, infrastructure...... engineers in these domains need to experiment with and deploy OLTP database architectures that ensure application scalability and maximize resource utilization in modern machines. In this paper, we propose a relational actor programming model for in-memory databases as a novel, holistic approach towards......-level function calls. In contrast to classic transactional models, however, reactors allow developers to take advantage of intra-transaction parallelism and state encapsulation in their applications to reduce latency and improve locality. Moreover, reactors enable a new degree of flexibility in database...

  19. EXPLORATORY RESEARCH ON NOVEL COAL LIQUEFACTION CONCEPT

    Energy Technology Data Exchange (ETDEWEB)

    Brandes, S.D.; Winschel, R.A.

    1998-11-30

    The report presents a summary the work performed under DOE Contract No. DE-AC22-95PC95050. Investigations performed under Task 4--Integrated Flow Sheet Testing are detailed. In this program, a novel direct coal liquefaction technology was investigated by CONSOL Inc. with the University of Kentucky Center for Applied Energy Research and LDP Associates. The process concept explored consists of a first-stage coal dissolution step in which the coal is solubilized by hydride ion donation. In the second stage, the products are catalytically upgraded to refinery feedstocks. Integrated first-stage and solids-separation steps were used to prepare feedstocks for second-stage catalytic upgrading. An engineering and economic evaluation was conducted concurrently with experimental work throughout the program. Approaches to reduce costs for a conceptual commercial plant were recommended at the conclusion of Task 3. These approaches were investigated in Task 4. The economic analysis of the process as it was defined at the conclusion of Task 4, indicates that the production of refined product (gasoline) via this novel direct liquefaction technology is higher than the cost associated with conventional two-stage liquefaction technologies.

  20. Design optimization of single mixed refrigerant natural gas liquefaction process using the particle swarm paradigm with nonlinear constraints

    International Nuclear Information System (INIS)

    Khan, Mohd Shariq; Lee, Moonyong

    2013-01-01

    The particle swarm paradigm is employed to optimize single mixed refrigerant natural gas liquefaction process. Liquefaction design involves multivariable problem solving and non-optimal execution of these variables can waste energy and contribute to process irreversibilities. Design optimization requires these variables to be optimized simultaneously; minimizing the compression energy requirement is selected as the optimization objective. Liquefaction is modeled using Honeywell UniSim Design ™ and the resulting rigorous model is connected with the particle swarm paradigm coded in MATLAB. Design constraints are folded into the objective function using the penalty function method. Optimization successfully improved efficiency by reducing the compression energy requirement by ca. 10% compared with the base case. -- Highlights: ► The particle swarm paradigm (PSP) is employed for design optimization of SMR NG liquefaction process. ► Rigorous SMR process model based on UniSim is connected with PSP coded in MATLAB. ► Stochastic features of PSP give more confidence in the optimality of complex nonlinear problems. ► Optimization with PSP notably improves energy efficiency of the SMR process.

  1. Characteristics of the products of hydrothermal liquefaction combined with cellulosic bio-ethanol process

    International Nuclear Information System (INIS)

    Li, Rundong; Xie, Yinghui; Yang, Tianhua; Li, Bingshuo; Zhang, Yang; Kai, Xingping

    2016-01-01

    The integration utilization of fermentation residues from cellulosic bio-ethanol has attracted a great deal of attention to balance the total cost of bio-ethanol production while simultaneously dealing with bio-ethanol wastewater. A process of hydrothermal liquefaction (HTL) of intact materials from cellulosic bio-ethanol in a batch reactor was proposed. The effects of the reaction temperature and time on the liquefaction characteristics were examined. The optimum condition for liquefaction fermentation residues was 370 °C (21.25 MPa) and 30 min with a bio-oil yield of 40.79 wt%. GC-MS results indicated that the major chemical species in the bio-oil were phenols, ketones, long-chain hydrocarbons and fatty acids. Supercritical conditions (375 °C, 23.50 MPa) was favored for the low-molecular-weight species formation compared to subcritical conditions (370 °C, 21.25 MPa), as some long-chain species decreased. This work thus can provide a novel idea for bio-oil production from HTL of cellulosic bio-ethanol fermentation residues. - Highlights: • Bio-oil production via HTL combined with cellulosic bio-ethanol process was proposed. • Optimum condition for HTL of materials from cellulosic bio-ethanol was 370 °C and 30 min. • Bio-oil contained higher content of hydrocarbons and lower contents of organic acids.

  2. A novel vortex tube-based N2-expander liquefaction process for enhancing the energy efficiency of natural gas liquefaction

    Directory of Open Access Journals (Sweden)

    Qyyum Muhammad Abdul

    2017-01-01

    Full Text Available This research work unfolds a simple, safe, and environment-friendly energy efficient novel vortex tube-based natural gas liquefaction process (LNG. A vortex tube was introduced to the popular N2-expander liquefaction process to enhance the liquefaction efficiency. The process structure and condition were modified and optimized to take a potential advantage of the vortex tube on the natural gas liquefaction cycle. Two commercial simulators ANSYS® and Aspen HYSYS® were used to investigate the application of vortex tube in the refrigeration cycle of LNG process. The Computational fluid dynamics (CFD model was used to simulate the vortex tube with nitrogen (N2 as a working fluid. Subsequently, the results of the CFD model were embedded in the Aspen HYSYS® to validate the proposed LNG liquefaction process. The proposed natural gas liquefaction process was optimized using the knowledge-based optimization (KBO approach. The overall energy consumption was chosen as an objective function for optimization. The performance of the proposed liquefaction process was compared with the conventional N2-expander liquefaction process. The vortex tube-based LNG process showed a significant improvement of energy efficiency by 20% in comparison with the conventional N2-expander liquefaction process. This high energy efficiency was mainly due to the isentropic expansion of the vortex tube. It turned out that the high energy efficiency of vortex tube-based process is totally dependent on the refrigerant cold fraction, operating conditions as well as refrigerant cycle configurations.

  3. A novel vortex tube-based N2-expander liquefaction process for enhancing the energy efficiency of natural gas liquefaction

    Science.gov (United States)

    Qyyum, Muhammad Abdul; Wei, Feng; Hussain, Arif; Ali, Wahid; Sehee, Oh; Lee, Moonyong

    2017-11-01

    This research work unfolds a simple, safe, and environment-friendly energy efficient novel vortex tube-based natural gas liquefaction process (LNG). A vortex tube was introduced to the popular N2-expander liquefaction process to enhance the liquefaction efficiency. The process structure and condition were modified and optimized to take a potential advantage of the vortex tube on the natural gas liquefaction cycle. Two commercial simulators ANSYS® and Aspen HYSYS® were used to investigate the application of vortex tube in the refrigeration cycle of LNG process. The Computational fluid dynamics (CFD) model was used to simulate the vortex tube with nitrogen (N2) as a working fluid. Subsequently, the results of the CFD model were embedded in the Aspen HYSYS® to validate the proposed LNG liquefaction process. The proposed natural gas liquefaction process was optimized using the knowledge-based optimization (KBO) approach. The overall energy consumption was chosen as an objective function for optimization. The performance of the proposed liquefaction process was compared with the conventional N2-expander liquefaction process. The vortex tube-based LNG process showed a significant improvement of energy efficiency by 20% in comparison with the conventional N2-expander liquefaction process. This high energy efficiency was mainly due to the isentropic expansion of the vortex tube. It turned out that the high energy efficiency of vortex tube-based process is totally dependent on the refrigerant cold fraction, operating conditions as well as refrigerant cycle configurations.

  4. Liquefaction of aspen poplar wood

    Energy Technology Data Exchange (ETDEWEB)

    Eager, R L; Mathews, J F; Pepper, J M

    1982-01-01

    Dried and green aspen poplar wood suspended in water containing alkali catalysts was converted completely to an oil, water-soluble chemical, and gases by heating for 1 hour in the presence of CO in a rocking batch reactor. Within the ranges of parameters studied: temperature of 593-633 K; nominal reaction times of less than or equal to 1 hour; water-to-wood ratio of 0.5:1-5:1; Na/sub 2/CO/sub 3/, K/sub 2/CO/sub 3/, and NaOH catalysts; amount of catalyst 7.0-12.5%; and initial H-CO ratios of 2:1-0:1, the water-to-wood ratio was most important. Oil yields of approximately 50% with a C plus H content of approximately 80% and representing a C recovery of approximately 66% were obtained. The higher heats of combustion were 32.2-36.0 MJ/kg.

  5. The Texts of the Instruments Concerning the Agency's Assistance to Pakistan in connection with the Establishment of a Nuclear Power Reactor Project

    International Nuclear Information System (INIS)

    1968-01-01

    The terms of the Supply Agreement between the Agency and the Governments of Pakistan and the United States of America, and of the Project Agreement between the Agency and the Government of Pakistan concerning the Agency's assistance to that Government in connection with the establishment of a nuclear power reactor project, are reproduced herein for the information of all Members. Both Agreements entered into force on 17 June 1968

  6. The Texts of the Instruments concerning the Agency's Assistance to Pakistan in connection with the Establishment of a Nuclear Power Reactor Project. A Second Supply Agreement

    International Nuclear Information System (INIS)

    1971-01-01

    As a sequel to the assistance which the Agency provided to the Government of Pakistan in connection with a nuclear power reactor project, a Second Supply Agreement has been concluded between the Agency and the Governments of Pakistan and the United States of America. This Agreement entered into force on 22 June 1971, and the text is reproduced herein for the information of all Members

  7. The Texts of the Instruments Concerning the Agency's Assistance to Pakistan in connection with the Establishment of a Nuclear Power Reactor Project

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1968-09-06

    The terms of the Supply Agreement between the Agency and the Governments of Pakistan and the United States of America, and of the Project Agreement between the Agency and the Government of Pakistan concerning the Agency's assistance to that Government in connection with the establishment of a nuclear power reactor project, are reproduced herein for the information of all Members. Both Agreements entered into force on 17 June 1968.

  8. The Texts of the Instruments connected with the Agency's Assistance to Argentina in Establishing a Research and Isotope Production Reactor Project

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1965-11-04

    The texts of the Title Transfer Agreement between the Agency and the Governments of Argentina and the United States of America, and of the Project Agreement between the Agency and the Government of Argentina, in connection with the Agency's assistance to that Government in establishing a research and isotope production reactor project, are reproduced in this document for the information of all Members. These Agreements entered into force on 2 December 1964.

  9. The Texts of the Instruments connected with the Agency's Assistance to the Democratic Republic of the Congo in Continuing a Research Reactor Project. A Second Supply Agreement

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1971-10-04

    As a sequel to the assistance which the Agency provided to the Government of the Democratic Republic of the Congo in connection with a research reactor project, a Second Supply Agreement has been concluded between the Agency and the Governments of the Congo and the United States of America. This Agreement entered into force on 15 April 1971, and the text is reproduced herein for the information of all Members.

  10. The Texts of the Instruments concerning the Agency's Assistance to Pakistan in connection with the Establishment of a Nuclear Power Reactor Project. A Second Supply Agreement

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1971-10-08

    As a sequel to the assistance which the Agency provided to the Government of Pakistan in connection with a nuclear power reactor project, a Second Supply Agreement has been concluded between the Agency and the Governments of Pakistan and the United States of America. This Agreement entered into force on 22 June 1971, and the text is reproduced herein for the information of all Members.

  11. The Texts of the Instruments connected with the Agency's Assistance to the Democratic Republic of the Congo in Continuing a Research Reactor Project. A Second Supply Agreement

    International Nuclear Information System (INIS)

    1971-01-01

    As a sequel to the assistance which the Agency provided to the Government of the Democratic Republic of the Congo in connection with a research reactor project, a Second Supply Agreement has been concluded between the Agency and the Governments of the Congo and the United States of America. This Agreement entered into force on 15 April 1971, and the text is reproduced herein for the information of all Members

  12. The Texts of the Instruments connected with the Agency's Assistance to Mexico in Establishing a Research Reactor Project. A Second Supply Agreement

    International Nuclear Information System (INIS)

    1972-01-01

    As a sequel to the assistance which the Agency has provided to the Government of Mexico in connection with a research reactor project, a Second Supply Agreement has been concluded between the Agency and the Governments of Mexico and the United States of America. This Agreement entered into force on 4 October 1972, and the text is reproduced herein for the information of all Members

  13. The Texts of the Instruments connected with the Agency's Assistance to Mexico in Establishing a Research Reactor Project. A Second Supply Agreement

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1972-11-17

    As a sequel to the assistance which the Agency has provided to the Government of Mexico in connection with a research reactor project, a Second Supply Agreement has been concluded between the Agency and the Governments of Mexico and the United States of America. This Agreement entered into force on 4 October 1972, and the text is reproduced herein for the information of all Members.

  14. The Texts of the Instruments connected with the Agency's Assistance to Argentina in Establishing a Research and Isotope Production Reactor Project

    International Nuclear Information System (INIS)

    1965-01-01

    The texts of the Title Transfer Agreement between the Agency and the Governments of Argentina and the United States of America, and of the Project Agreement between the Agency and the Government of Argentina, in connection with the Agency's assistance to that Government in establishing a research and isotope production reactor project, are reproduced in this document for the information of all Members. These Agreements entered into force on 2 December 1964

  15. The Texts of the Instruments connected with the Agency's Assistance to Pakistan in Establishing a Research Reactor Project. A Third Supply Agreement

    International Nuclear Information System (INIS)

    1974-01-01

    As a sequel to the assistance which the Agency has provided to the Government of Pakistan in connection with a research reactor project, a Third Supply Agreement has been concluded between the Agency and the Governments of Pakistan and the United States of America. The Agreement entered into force on 14 June 1974 pursuant to Article V, and the text is reproduced herein for the information of all Members

  16. Design of generic coal conversion facilities: Indirect coal liquefaction, Fischer-Tropsch synthesis

    Energy Technology Data Exchange (ETDEWEB)

    1991-10-01

    A comprehensive review of Fischer-Tropsch (F-T) technology, including fixed, fluidized, and bubble column reactors, was undertaken in order to develop an information base before initiating the design of the Fischer-Tropsch indirect liquefaction PDU as a part of the Generic Coal Conversion Facilities to be built at the Pittsburgh Energy Technology Center (PETC). The pilot plant will include a fixed bed and slurry bubble column reactor for the F-T mode of operation. The review encompasses current status of both these technologies, their key variables, catalyst development, future directions, and potential improvement areas. However, more emphasis has been placed on the slurry bubble column reactor since this route is likely to be the preferred technology for commercialization, offering process advantages and, therefore, better economics than fixed and fluidized bed approaches.

  17. Fiscal 1996 achievement report. Coal liquefaction technology development - Bituminous coal liquefaction technology development - Study for supporting pilot plant - Study using 1t/d PSU (Study of operation using PSU); 1996 nendo seika hokokusho. Sekitan ekika gijutsu kaihatsu - Rekiseitan ekika gijutsu no kaihatsu - Pilot plant no shien kenkyu - 1t/d process support unit (PSU) ni yoru kenkyu (PSU ni yoru unten kenkyu)

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1997-03-01

    The operation of a 1t/d PSU (process support unit) was studied for the NEDOL coal liquefaction process. In the modification of facilities, detailed designs were prepared for product oil reforming facilities and some equipment and devices were procured. In addition, the 3rd liquefaction reactor cone section and the neutron attenuation-aided measuring device were refurbished. In the injection of coal, a 62-day and 23-day slurry injection operations were accomplished using Tanito Harum coal, when the impact imposed on the yield of the product, etc., by the change of liquefaction catalysts and by gas phase hydrogen concentration enriching conditions was investigated, and the unit was examined for operationality. During a 42-day operation for maintenance, the unit was operated using only the slurry heater for the investigation of the initial reaction in liquefaction, and studies were conducted about the heater exit temperature, G/L (gas-liquid ratio), and the effect to ensue from the use of a different solvent. In the effort to develop and evaluate new materials, implantation tests were conducted for metallic materials and the 3rd liquefaction reactor was subjected to a non-destructive inspection. Wastewater from the process was examined for quality, and environment-related measurements were performed for the atmosphere. (NEDO)

  18. Liquefaction Microzonation of Babol City Using Artificial Neural Network

    DEFF Research Database (Denmark)

    Farrokhzad, F.; Choobbasti, A.J.; Barari, Amin

    2012-01-01

    that will be less susceptible to damage during earthquakes. The scope of present study is to prepare the liquefaction microzonation map for the Babol city based on Seed and Idriss (1983) method using artificial neural network. Artificial neural network (ANN) is one of the artificial intelligence (AI) approaches...... microzonation map is produced for research area. Based on the obtained results, it can be stated that the trained neural network is capable in prediction of liquefaction potential with an acceptable level of confidence. At the end, zoning of the city is carried out based on the prediction of liquefaction...... that can be classified as machine learning. Simplified methods have been practiced by researchers to assess nonlinear liquefaction potential of soil. In order to address the collective knowledge built-up in conventional liquefaction engineering, an alternative general regression neural network model...

  19. Reactor

    International Nuclear Information System (INIS)

    Fujibayashi, Toru.

    1976-01-01

    Object: To provide a boiling water reactor which can enhance a quake resisting strength and flatten power distribution. Structure: At least more than four fuel bundles, in which a plurality of fuel rods are arranged in lattice fashion which upper and lower portions are supported by tie-plates, are bundled and then covered by a square channel box. The control rod is movably arranged within a space formed by adjoining channel boxes. A spacer of trapezoidal section is disposed in the central portion on the side of the channel box over substantially full length in height direction, and a neutron instrumented tube is disposed in the central portion inside the channel box. Thus, where a horizontal load is exerted due to earthquake or the like, the spacers come into contact with each other to support the channel box and prevent it from abnormal vibrations. (Furukawa, Y.)

  20. The text of the Agreement of 25 September 1980 between Cuba and the Agency for the application of safeguards in connection with the supply of a nuclear research reactor from the Union of Soviet Socialist Republics

    International Nuclear Information System (INIS)

    1982-08-01

    The full text of the agreement between Cuba and the International Atomic Energy Agency for the application of safeguards in connection with the supply of a nuclear research reactor from the USSR is presented

  1. The text of the Agreement of 12 June 1981 between Viet Nam and the Agency relating to the application of safeguards in connection with the supply of nuclear fuel for the Da Lat research reactor

    International Nuclear Information System (INIS)

    1982-02-01

    The full text of the agreement between Viet Nam and the International Atomic Energy Agency relating to the application of safeguards in connection with the supply of nuclear fuel for the DA LAT Research Reactor is presented

  2. Development of an extruder-feeder biomass direct liquefaction process. Volume 2, Parts 4--8: Final report

    Energy Technology Data Exchange (ETDEWEB)

    White, D.H.; Wolf, D. [Arizona Univ., Tucson, AZ (United States). Dept. of Chemical Engineering

    1991-10-01

    As an abundant, renewable, domestic energy resource, biomass could help the United States reduce its dependence on imported oil. Biomass is the only renewable energy technology capable of addressing the national need for liquid transportation fuels. Thus, there is an incentive to develop economic conversion processes for converting biomass, including wood, into liquid fuels. Through research sponsored by the US DOE`s Biomass Thermochemical Conversion Program, the University of Arizona has developed a unique biomass direct liquefaction system. The system features a modified single-screw extruder capable of pumping solid slurries containing as high as 60 wt% wood flour in wood oil derived vacuum bottoms at pressures up to 3000 psi. The extruder-feeder has been integrated with a unique reactor by the University to form a system which offers potential for improving high pressure biomass direct liquefaction technology. The extruder-feeder acts simultaneously as both a feed preheater and a pumping device for injecting wood slurries into a high pressure reactor in the biomass liquefaction process. An experimental facility was constructed and following shakedown operations, wood crude oil was produced by mid-1985. By July 1988, a total of 57 experimental continuous biomass liquefaction runs were made using White Birch wood feedstock. Good operability was achieved at slurry feed rates up to 30 lb/hr, reactor pressures from 800 to 3000 psi and temperatures from 350{degree}C to 430{degree}C under conditions covering a range of carbon monoxide feed rates and sodium carbonate catalyst addition. Crude wood oils containing as little as 6--10 wt% residual oxygen were produced. 38 refs., 82 figs., 26 tabs.

  3. Hydrothermal Liquefaction Treatment Preliminary Hazard Analysis Report

    Energy Technology Data Exchange (ETDEWEB)

    Lowry, Peter P.; Wagner, Katie A.

    2015-08-31

    A preliminary hazard assessment was completed during February 2015 to evaluate the conceptual design of the modular hydrothermal liquefaction treatment system. The hazard assessment was performed in 2 stages. An initial assessment utilizing Hazard Identification and Preliminary Hazards Analysis (PHA) techniques identified areas with significant or unique hazards (process safety-related hazards) that fall outside of the normal operating envelope of PNNL and warranted additional analysis. The subsequent assessment was based on a qualitative What-If analysis. This analysis was augmented, as necessary, by additional quantitative analysis for scenarios involving a release of hazardous material or energy with the potential for affecting the public.

  4. Hydrotreating of heavy distillate derived from Wandoan coal liquefaction

    Energy Technology Data Exchange (ETDEWEB)

    Sato, Y. [National Institute for Resources and Environment, Osaka (Japan). Hydrocarbon Research Lab.

    1997-12-03

    The paper reports how the hydrotreatment of coal-derived heavy distillate, obtained from the liquefaction of Wandoan coal using a 1 t/day bench unit, was performed to clarify the effects of catalyst species, reaction temperature and hydrogen pressure on the chemical composition of the product. Experimental runs were carried out over alumina-supported Go-Mo and Ni-Mo catalysts in a fixed bed reactor of 20 ml in volume at 350-390{degree}C under hydrogen pressure of 50-150 kg/cm{sup 2}G with liquid hourly space velocity (LHSV) of 0.5-2 h{sup -1}. The product, as analyzed by gas chromatography, indicated that larger amounts of alkylbenzenes such as toluene or xylenes were produced at the elevated temperature of 390{degree}C, but the concentrations of condensed aromatics such as naphthalene, biphenyl, fluorene and phenanthrene decreased with the severity of reaction conditions. Pyrene and methylpyrene decreased in amount with a shorter LHSV and higher hydrogen pressure, but increased at higher temperature of 390{degree}C. Shorter LHSV and higher hydrogen pressure are much more effective in hydrogenation, hydrodnitrogenation and hydrodeoxygenation than the higher reaction temperature up to 390{degree}C.

  5. Mars Propellant Liquefaction Modeling in Thermal Desktop

    Science.gov (United States)

    Desai, Pooja; Hauser, Dan; Sutherlin, Steven

    2017-01-01

    NASAs current Mars architectures are assuming the production and storage of 23 tons of liquid oxygen on the surface of Mars over a duration of 500+ days. In order to do this in a mass efficient manner, an energy efficient refrigeration system will be required. Based on previous analysis NASA has decided to do all liquefaction in the propulsion vehicle storage tanks. In order to allow for transient Martian environmental effects, a propellant liquefaction and storage system for a Mars Ascent Vehicle (MAV) was modeled using Thermal Desktop. The model consisted of a propellant tank containing a broad area cooling loop heat exchanger integrated with a reverse turbo Brayton cryocooler. Cryocooler sizing and performance modeling was conducted using MAV diurnal heat loads and radiator rejection temperatures predicted from a previous thermal model of the MAV. A system was also sized and modeled using an alternative heat rejection system that relies on a forced convection heat exchanger. Cryocooler mass, input power, and heat rejection for both systems were estimated and compared against sizing based on non-transient sizing estimates.

  6. Economically viable large-scale hydrogen liquefaction

    Science.gov (United States)

    Cardella, U.; Decker, L.; Klein, H.

    2017-02-01

    The liquid hydrogen demand, particularly driven by clean energy applications, will rise in the near future. As industrial large scale liquefiers will play a major role within the hydrogen supply chain, production capacity will have to increase by a multiple of today’s typical sizes. The main goal is to reduce the total cost of ownership for these plants by increasing energy efficiency with innovative and simple process designs, optimized in capital expenditure. New concepts must ensure a manageable plant complexity and flexible operability. In the phase of process development and selection, a dimensioning of key equipment for large scale liquefiers, such as turbines and compressors as well as heat exchangers, must be performed iteratively to ensure technological feasibility and maturity. Further critical aspects related to hydrogen liquefaction, e.g. fluid properties, ortho-para hydrogen conversion, and coldbox configuration, must be analysed in detail. This paper provides an overview on the approach, challenges and preliminary results in the development of efficient as well as economically viable concepts for large-scale hydrogen liquefaction.

  7. The text of the instruments connected with the Agency's assistance to Argentina in establishing a research and isotope production reactor project

    International Nuclear Information System (INIS)

    1995-01-01

    The Agreement between the Republic of Argentina, the Federative Republic of Brazil, the Brazilian-Argentine Agency for Accounting and Control of Nuclear Materials and the International Atomic Energy Agency for the Application of Safeguards came into force on 4 March 1994. As a result of the coming into force of the aforesaid Agreement for Argentina, the application of safeguards under the Project Agreement of 2 December 1964 between Argentina and the IAEA in connection with the Agency's assistance to Argentina in establishing a research and isotope production reactor project has been suspended

  8. Coal liquefaction technologies for producing ultra clean fuel

    International Nuclear Information System (INIS)

    Tahir, M.S.; Haq, N.U.; Nasir, H.; Islam, N.

    2011-01-01

    The expanding demand for petroleum, accompanied by the diminishing petroleum reserves and the energy security, has intensified the significance in coal liquefaction technologies (CTL) globally and specially in Pakistan. Pakistan is rich in coal resources, but short of petroleum. The Geological Survey of Pakistan based on wide spread drilling over an area of 9000 sq. km, a total of 175 billion tons of coal resource potential has been assessed. This paper overviews a general introduction on the mechanisms and processes of CLT such as direct coal liquefaction (DCL) and indirect coal liquefaction (ICL) technologies. (author)

  9. Influence of clay content on wave-induced liquefaction

    DEFF Research Database (Denmark)

    Kirca, V.S. Ozgur; Sumer, B. Mutlu; Fredsøe, Jørgen

    2014-01-01

    of measurements were carried out: (1) pore-water pressure measurements across the soil depth and (2) water-surface elevation measurements. These measurements were synchronized with video recordings of the liquefaction process from the side. The ranges of the various quantities in the experiments were wave height...... of silt and clay was not liquefied. Sand may become prone to liquefaction with the introduction of clay, contrary to the general perception that this type of sediment is normally liquefaction-resistant under waves. For instance, sand with d50 50:4 mmwas liquefied with CC510:8%, whereas sand with d50 50...

  10. Hydrothermal Liquefaction of Dried Distillers Grains with solubles: A reaction temperature study

    DEFF Research Database (Denmark)

    Mørup, Anders; Christensen, Per Runge; Aarup, David Friis

    2012-01-01

    provides rapid heating of biomass feeds and the option of performing multiple sequential repetitions. This bypasses long, uncontrollable temperature gradients and unintended changes in the reaction chemistry. The product, a crude bio-oil, was characterized in terms of yield, elemental composition......The effect of the reaction temperature on hydrothermal liquefaction of dried distillers grains with solubles (DDGS) was investigated using a novel stop-flow reactor system at varying temperatures (300–400 °C), fixed pressure (250 bar), and fixed reaction time (15 min). The stop-flow reactor......, and chemical composition. Higher reaction temperatures resulted in improved bio-oil yields, less char formation, and higher heating values of the bio-oil. A supercritical reaction temperature of 400 °C was found to produce bio-oil in the highest yields and of the best quality....

  11. Numerical simulation of liquefaction behaviour of granular materials ...

    Indian Academy of Sciences (India)

    R. Narasimhan (Krishtel eMaging) 1461 1996 Oct 15 13:05:22

    cles using Discrete Element Method (DEM) is used to study the liquefaction behaviour of ... studies have focussed on the stress-strain relation- ... experimentation still remains quite problematic. ... distorting the periodic cell and changing its vol-.

  12. On the risk of liquefaction of buffer and backfill

    Energy Technology Data Exchange (ETDEWEB)

    Pusch, R. [Geodevelopment AB, Lund (Sweden)

    2000-10-01

    The necessary prerequisites for liquefaction of buffers and backfills in a KBS-3 repository exist but the stress conditions and intended densities practically eliminate the risk of liquefaction for single earthquakes with magnitudes up to M=8 and normal duration. For buffers rich in expandable minerals it would be possible to reduce the density at water saturation to 1,700 - 1,800 kg/m{sup 3} or even less without any significant risk of liquefaction, while the density at saturation of backfills with 10 - 15% expandable clay should not be reduced to less than about 1,900 kg/m{sup 3}. Since the proposed densities of both buffers and backfills will significantly exceed these minimum values it is concluded that there is no risk of liquefaction of the engineered soil barriers in a KBS-3 repository even for very significant earthquakes.

  13. On the risk of liquefaction of buffer and backfill

    International Nuclear Information System (INIS)

    Pusch, R.

    2000-10-01

    The necessary prerequisites for liquefaction of buffers and backfills in a KBS-3 repository exist but the stress conditions and intended densities practically eliminate the risk of liquefaction for single earthquakes with magnitudes up to M=8 and normal duration. For buffers rich in expandable minerals it would be possible to reduce the density at water saturation to 1,700 - 1,800 kg/m 3 or even less without any significant risk of liquefaction, while the density at saturation of backfills with 10 - 15% expandable clay should not be reduced to less than about 1,900 kg/m 3 . Since the proposed densities of both buffers and backfills will significantly exceed these minimum values it is concluded that there is no risk of liquefaction of the engineered soil barriers in a KBS-3 repository even for very significant earthquakes

  14. Initial Earthquake Centrifuge Model Experiments for the Study of Liquefaction

    National Research Council Canada - National Science Library

    Steedman, R

    1998-01-01

    .... These are intended to gather data suitable for the development of improved design approaches for the prediction of liquefaction under earthquake loading using the new centrifuge facility at the WES...

  15. Whole Algae Hydrothermal Liquefaction: 2014 State of Technology

    Energy Technology Data Exchange (ETDEWEB)

    Jones, Susanne B.; Zhu, Yunhua; Snowden-Swan, Lesley J.; Anderson, Daniel; Hallen, Richard T.; Schmidt, Andrew J.; Albrecht, Karl O.; Elliott, Douglas C.

    2014-07-30

    This report describes the base case yields and operating conditions for converting whole microalgae via hydrothermal liquefaction and upgrading to liquid fuels. This serves as the basis against which future technical improvements will be measured.

  16. An Advanced Wet Expansion Turbine for Hydrogen Liquefaction, Phase I

    Data.gov (United States)

    National Aeronautics and Space Administration — This proposal is responsive to NASA SBIR Topic X10.01, specifically, the need for efficient small- to medium-scale hydrogen liquefaction technologies including...

  17. Technical and economic aspects of brown coal gasification and liquefaction

    International Nuclear Information System (INIS)

    Speich, P.

    1980-01-01

    A number of gasification and liquefaction processes for Rhenish brown coal are investigated along with the technical and economic aspects of coal beneficiation. The status of coal beneficiation and the major R + D activities are reviewed. (orig.) [de

  18. Assessment of Soil Liquefaction Potential Based on Numerical Method

    DEFF Research Database (Denmark)

    Choobasti, A. Janalizadeh; Vahdatirad, Mohammad Javad; Torabi, M.

    2012-01-01

    Paying special attention to geotechnical hazards such as liquefaction in huge civil projects like urban railways especially in susceptible regions to liquefaction is of great importance. A number of approaches to evaluate the potential for initiation of liquefaction, such as Seed and Idriss...... simplified method have been developed over the years. Although simplified methods are available in calculating the liquefaction potential of a soil deposit and shear stresses induced at any point in the ground due to earthquake loading, these methods cannot be applied to all earthquakes with the same...... accuracy, also they lack the potential to predict the pore pressure developed in the soil. Therefore, it is necessary to carry out a ground response analysis to obtain pore pressures and shear stresses in the soil due to earthquake loading. Using soil historical, geological and compositional criteria...

  19. Advanced direct liquefaction concepts for PETC generic units

    Energy Technology Data Exchange (ETDEWEB)

    1992-04-01

    In the Advance Coal Liquefaction Concept Proposal (ACLCP) carbon monoxide (CO) and water have been proposed as the primary reagents in the pretreatment process. The main objective of this project is to develop a methodology for pretreating coal under mild conditions based on a combination of existing processes which have shown great promise in liquefaction, extraction and pyrolysis studies. The aim of this pretreatment process is to partially depolymerise the coal, eliminate oxygen and diminish the propensity for retograde reactions during subsequent liquefaction. The desirable outcome of the CO pretreatment step should be: (1) enhanced liquefaction activity and/or selectivity toward products of higher quality due to chemical modification of the coal structure; (2) cleaner downstream products; (3) overall improvement in operability and process economics.

  20. New method for evaluating liquefaction potential

    Energy Technology Data Exchange (ETDEWEB)

    Arulmoli, K.; Arulanandan, K.; Seed, H.B.

    1985-01-01

    A new method of indexing the grain and aggregate properties of sand using electrical parameters is described. Correlations are established between these parameters and relative density, D /sub r/ , cyclic stress ratio, /tau//sigma'/sub 0/, and K2 /sub max/ . An electrical probe, used to predict these parameters from in-situ electrical measurements, is described. Evaluations are made of D /sub r/ and /tau//sigma/sub 0/, which are compared with values measured independently from controlled laboratory tests. Reasonable agreement is found between predicted and measured values. The potential applicability of the electrical probe in the field is shown by evaluation of liquefaction and nonliquefaction at sites affected by the 1906 San Francisco, Niigata and Tangshan earthquakes.

  1. Potential of soil liquefaction at Perlis, northern region of Malalysia

    Science.gov (United States)

    Ghazaly, Zuhayr Md; Rahim, Mustaqqim Abdul; Nasir, Mohamad Amzar Bin Mhd; Isa, Nur Fitriah; Zaki, Mohd Faiz Mohammad; Hassan, Zulkarnain Bin; Ismail, Zul-Atfi Bin

    2017-09-01

    Soil liquefaction is earthquake's secondary effect which could cause fatal damages and structures instability. Despite Malaysia been located in stable zone of Pacific Ring of Fire, few significant surrounded quakes like Sumatra-Andaman earthquake had prompted Malaysian's public concern, especially in Perlis area, on local seismic resistant. Hence, this research presents the analysis result of liquefaction potential of the soils, as the secondary effect of earthquake, within Perlis, northern region of Malaysia; the next strong and sustainable metropolis by using semi-empirical procedures introduced by Seed and Idriss. The study consists of two stages which were determination of the local geological and geotechnical site conditions within Perlis and analysis of soil liquefaction susceptibility by using various methods and liquefaction potential by using Simplified Procedure developed by Seed and Idriss on stress approach. There were consist of four phases implemented in order to achieve the objectives targeted for the study after problem being identified. Firstly, a comprehensive review of literature on liquefaction at Perlis was carried out. Second phase was data collection process that includes collection of Site Investigation (SI) report. Thirdly, data analysis was carried out by utilizing suitable method. The final phase was to draw conclusion and recommendation for this study. It can be concluded that the overall Perlis due to earthquake moment magnitude below 7.5 has no potential to soil liquefaction. However, with the range of liquefaction potential of 1.60 to 5.64 in Kuala Perlis area, it is liquefiable. The development of liquefaction severity map of Perlis, Malaysia in this research, may be used by others as a reference for seismic design and standard safety measures as well as for further research work.

  2. Liquefaction Potential for Soil Deposits in Muscat, Oman

    Science.gov (United States)

    El Hussain, I. W.; Deif, A.; Girgis, M.; Al-Rawas, G.; Mohamed, A.; Al-Jabri, K.; Al-Habsi, Z.

    2015-12-01

    Muscat is located in the northeastern part of Oman on a narrow strip between Oman coast and Oman Mountains, which is the place for at least four earthquakes of order of 5.2 magnitude in the last 1300 years. The near surface geology of Muscat varies from hard rocks in the eastern, southern and western parts to dense and lose sediments in the middle and northern parts. Liquefaction occurs in saturated cohesionless soils when its shear strength decreased to zero due to the increase of pore pressure. More than 500 boreholes in Muscat area were examined for their liquefaction susceptibility based on the soil characteristics data. Only soils susceptible to liquefaction are further considered for liquefaction hazard assessment. Liquefaction occurs if the cyclic stress ratio (CSR) caused by the earthquake is higher than the cyclic resistance ratio (CRR) of the soil. CSR values were evaluated using PGA values at the surface obtained from previously conducted seismic hazard and microzonation studies. CRR for Muscat region is conducted using N values of SPT tests from numerous borehole data and the shear wave velocity results from 99 MASW surveys over the entire region. All the required corrections are conducted to get standardized (N1) 60 values, to correct shear-wave velocity, and scale the results for Mw 6.0 instead of the proposed 7.5 (magnitude scaling factor). Liquefaction hazard maps are generated using the minimum factor of safety (FS) at each site as a representative of the FS against liquefaction at that location. Results indicate that under the current level of seismic hazard, liquefaction potential is possible at few sites along the northern coast where alluvial soils and shallow ground water table are present. The expected soft soil settlement is also evaluated at each liquefiable site.

  3. The Liquefaction of Hydrogen and Helium Using Small Coolers

    International Nuclear Information System (INIS)

    Green, Michael A.

    2006-01-01

    This report discusses the history of the liquefaction of hydrogen and helium using small coolers. This history dates form the 1960's when two stage GM coolers capable of reaching 7 K were used to liquefy helium and hydrogen by suing an added compressor and J-T circuit. Liquefaction using the added circuit failed to become mainstream because the J-T valve and heat exchanger clogged because of impurities in the gas being liquefied. Liquefaction using a GM cooler without an added J-T circuit proved to be difficult because the first stage was not used to pre-cool the gas coming to the second stage of the cooler. Once the gas being liquefied was pre-cooled using the cooler first stage, improvements in the liquefaction rates were noted. The advent of low temperature pulse tube cooler (down to 2.5 K) permitted one to achieve dramatic improvement is the liquefactions rates for helium. Similar but less dramatic improvements are expected for hydrogen as well. Using the PT-415 cooler, one can expect liquefaction rates of 15 to 20 liters per day for helium or hydrogen provided the heat leak into the cooler and the storage vessel is low. A hydrogen liquefier for MICE is presented at the end of this report

  4. Two-stage liquefaction of a Spanish subbituminous coal

    Energy Technology Data Exchange (ETDEWEB)

    Martinez, M.T.; Fernandez, I.; Benito, A.M.; Cebolla, V.; Miranda, J.L.; Oelert, H.H. (Instituto de Carboquimica, Zaragoza (Spain))

    1993-05-01

    A Spanish subbituminous coal has been processed in two-stage liquefaction in a non-integrated process. The first-stage coal liquefaction has been carried out in a continuous pilot plant in Germany at Clausthal Technical University at 400[degree]C, 20 MPa hydrogen pressure and anthracene oil as solvent. The second-stage coal liquefaction has been performed in continuous operation in a hydroprocessing unit at the Instituto de Carboquimica at 450[degree]C and 10 MPa hydrogen pressure, with two commercial catalysts: Harshaw HT-400E (Co-Mo/Al[sub 2]O[sub 3]) and HT-500E (Ni-Mo/Al[sub 2]O[sub 3]). The total conversion for the first-stage coal liquefaction was 75.41 wt% (coal d.a.f.), being 3.79 wt% gases, 2.58 wt% primary condensate and 69.04 wt% heavy liquids. The heteroatoms removal for the second-stage liquefaction was 97-99 wt% of S, 85-87 wt% of N and 93-100 wt% of O. The hydroprocessed liquids have about 70% of compounds with boiling point below 350[degree]C, and meet the sulphur and nitrogen specifications for refinery feedstocks. Liquids from two-stage coal liquefaction have been distilled, and the naphtha, kerosene and diesel fractions obtained have been characterized. 39 refs., 3 figs., 8 tabs.

  5. Switching overvoltage when disconnecting a combined 400 kVcable/overhead line with permanently connected shunt reactor

    DEFF Research Database (Denmark)

    Bak, Claus Leth; Søgaard, Kim

    2008-01-01

    consisting of overhead lines, crossbonded cable sections and shunt reactor has been created in PSCAD/EMTDC and verified against measurements with good results. Main focus has been put on the generation of switching overvoltages. It is shown that the generation of switching overvoltages is caused by slightly...... different resonant frequencies of the three phases which are reflected between the phases by mutual couplings in such a way that a low-frequent modulation appears in the phase voltages....

  6. Connected analysis nuclear-thermo-hydraulic of parallel channels of a BWR reactor using distributed computation; Analisis acoplado nuclear-termohidraulico de canales paralelos de un reactor BWR empleando computacion distribuida

    Energy Technology Data Exchange (ETDEWEB)

    Campos Gonzalez, Rina Margarita

    2007-07-15

    This work consists of the integration of three models previously developed which are described widely in Literature: model of the thermo-hydraulic channel, model of the modal neutronic and the model of the recirculation bows. The tool used for this connection of models is the PVM system, Parallel Virtual Machine that allowed paralleling the model by means of the concept of distributed computation. The purpose of making this connection of models is the one of obtaining a more complete tool than better represents the real configuration and the phenomenology of the nucleus of a BWR reactor, thus obtaining better results. In addition to maintaining the flexibility to improve the resulting model at any time, since the very complex or sophisticated models are difficult to improve being impossible to modify the equations they use and can include variables that are not of primary importance in the tackled problem or that mask relations among variables due to the excess of results. Also maintaining the flexibility for adding component of models or systems of the BWR reactor, all of this following the modeling needs. The Swedish Ringhals power plant was chosen to characterize the resulting connected model for counting on a Stability Benchmark that offers the opportunity to count on real plant data. Besides that in case 9 of cycle 14 of this Benchamark oscillations outside phase appeared, which are from great interest because the detection systems that register the average of the power of the nucleus do not detect them. Additionally in this work the model of the recirculation bows as an independent module is obtained in an individual way, since this model belongs to another work and works connected to the reactor vessel. The model of the recirculation bows is able to model several transients of interest, as it is shown in the Appendix A of this work, among which are found the tripping of recirculation pumps or the transference at low or high velocity of them. The scope of the

  7. Effects of Long-Duration Ground Motions on Liquefaction Hazards

    Science.gov (United States)

    Greenfield, Michael W.

    Soil liquefaction during past earthquakes has caused extensive damage to buildings, bridges, dam, pipelines and other elements of infrastructure. Geotechnical engineers use empirical observations from earthquake case histories in conjunction with soil mechanics to predict the behavior of liquefiable soils. However, current empirical databases are insufficient to evaluate the behavior of soils subject to long-duration earthquakes, such as a possible Mw = 9.0 Cascadia Subduction Zone earthquake. The objective of this research is to develop insight into the triggering and effects of liquefaction due to long-duration ground motions and to provide recommendations for analysis and design. Recorded ground motions from 21 case histories with surficial evidence of liquefaction showed marked differences in soil behavior before and after liquefaction was triggered. In some cases, strong shaking continued for several minutes after the soil liquefied, and a variety of behaviors were observed including dilation pulses, continued softening due to soil fabric degradation, and soil stiffening due to pore pressure dissipation and drainage. Supplemental field and laboratory investigations were performed at three sites that liquefied during the 2011 Mw = 9.0 Tohoku earthquake. The recorded ground motions and field investigation data were used in conjunction with laboratory observations, analytical models, and numerical models to evaluate the behavior of liquefiable soils subjected to long-duration ground motions. Observations from the case histories inspired a framework to predict ground deformations based on the differences in soil behavior before and after liquefaction has triggered. This framework decouples the intensity of shaking necessary to trigger liquefaction from the intensity of shaking that drives deformation by identifying the time when liquefaction triggers. The timing-based framework promises to dramatically reduce the uncertainty in deformation estimates compared to

  8. Sinking during earthquakes: Critical acceleration criteria control drained soil liquefaction

    Science.gov (United States)

    Clément, C.; Toussaint, R.; Stojanova, M.; Aharonov, E.

    2018-02-01

    This article focuses on liquefaction of saturated granular soils, triggered by earthquakes. Liquefaction is defined here as the transition from a rigid state, in which the granular soil layer supports structures placed on its surface, to a fluidlike state, in which structures placed initially on the surface sink to their isostatic depth within the granular layer. We suggest a simple theoretical model for soil liquefaction and show that buoyancy caused by the presence of water inside a granular medium has a dramatic influence on the stability of an intruder resting at the surface of the medium. We confirm this hypothesis by comparison with laboratory experiments and discrete-element numerical simulations. The external excitation representing ground motion during earthquakes is simulated via horizontal sinusoidal oscillations of controlled frequency and amplitude. In the experiments, we use particles only slightly denser than water, which as predicted theoretically increases the effect of liquefaction and allows clear depth-of-sinking measurements. In the simulations, a micromechanical model simulates grains using molecular dynamics with friction between neighbors. The effect of the fluid is captured by taking into account buoyancy effects on the grains when they are immersed. We show that the motion of an intruder inside a granular medium is mainly dependent on the peak acceleration of the ground motion and establish a phase diagram for the conditions under which liquefaction happens, depending on the soil bulk density, friction properties, presence of water, and peak acceleration of the imposed large-scale soil vibrations. We establish that in liquefaction conditions, most cases relax toward an equilibrium position following an exponential in time. We also show that the equilibrium position itself, for most liquefaction regimes, corresponds to the isostatic equilibrium of the intruder inside a medium of effective density. The characteristic time to relaxation is

  9. The Texts of the Instruments connected with the Agency's Assistance to Yugoslavia in Establishing a Research Reactor Project. The Third Supply Agreement. Amendments

    International Nuclear Information System (INIS)

    1975-01-01

    On 29 December 1972 the Agency and the Governments of the United States of America and Yugoslavia amended by letter of agreement Sections l(i), 4 and 5 of the Third Supply Agreement, concluded in connection with the Agency's assistance to Yugoslavia for the continuation of a research reactor project and reproduced in document INFCIRC/32/Add. 3, to provide for the transfer to Yugoslavia of up to a total net amount of 4800 grams of uranium-23 5 contained in uranium enriched up to approximately 70 per cent in the isotope uranium-235, and for payment by Yugoslavia within 20 days from the date of the invoice received from the Agency and by the Agency within 30 days from the date of the invoice received from the United States Atomic Energy Commission

  10. Numerical analysis of performance of steam reformer of methane reforming hydrogen production system connected with high-temperature gas-cooled reactor

    International Nuclear Information System (INIS)

    Yin Huaqiang; Jiang Shengyao; Zhang Youjie

    2007-01-01

    Methane conversion rate and hydrogen output are important performance indexes of the steam reformer. The paper presents numerical analysis of performance of the reformer connected with high-temperature gas-cooled reactor HTR-10. Setting helium inlet flow rate fixed, performance of the reformer was examined with different helium inlet temperature, pressure, different process gas temperature, pressure, flow rate, and different steam to carbon ratio. As the range concerned, helium inlet temperature has remarkable influence on the performance, and helium inlet temperature, process gas temperature and pressure have little influence on the performance, and improving process gas flow rate, methane conversion rate decreases and hydrogen output increases, however improving steam to carbon ratio has reverse influence on the performance. (authors)

  11. A study concerning tritium concentration evolution in the moderator of a CANDU reactor connected on-line to a detritiation facility

    International Nuclear Information System (INIS)

    Bidica, Nicolae; Bornea, Anisia

    2005-01-01

    The present work is a theoretical study on the tritium concentration evolution in the CANDU reactor moderator connected on-line with a detritiation facility. This study is based on a calculation model which takes into account the evolution curve of the tritium concentration in the absence of detritiation process in both the moderator and SPTC of the Unit 1 CANDU reactor at Cernavoda NPP. This study leads to determination of the tritium concentration evolution in the moderator in the presence of the detritiation process for both a range of intake flows and initial concentration. Also, the intake flow change will be analyzed for a detritiation facility as a function of tritium initial concentration existing in the moderator in the case of a survey of the detritiation over a given period of time. The conclusions of this study were the following: - an optimum of the detritiation factor can be determined; - detritiation starts at a lower value for the tritium concentration in moderator which reduces the strain upon the detritiation facility and therefore the costs of its building, maintenance and operation. (authors)

  12. Small scale demand type neon liquefaction plant

    International Nuclear Information System (INIS)

    Dube, W.P.; Slifka, A.J.; Bitsy, R.M.; Sparks, L.L.; Johnson, K.B.

    1990-01-01

    Low-temperature measurement of the thermal conductivity of insulating materials is generally made using a boil-off calorimetry technique involving liquid hydrogen (LH2). Liquid neon (LNe) has nearly the same normal boiling point as LH2, but has a much larger heat of vaporization, allowing extended run times. The main drawback of using LNe has been its excessive cost; $170.00 versus $1.50/l for LH2 (1989 prices). A neon liquefaction plant has been designed and constructed to capture, purify, and refrigerate the neon boil-off from calorimetry experiments. Recycling the neon reduces operating costs to approximately $20/l. The system consists of a purification section, a heat exchanger, LNe and LH2 storage dewars, and a fully automated control system. After purification, neon is liquified in the heat exchanger by LH2 flowing countercurrently through stainless steel cooling coils. Hydrogen flow is automatically adjusted to keep the neon at its normal saturation temperature, 27 K. The liquid neon is then stored in a dewar placed directly below the heat exchanger

  13. Catalytic multi-stage liquefaction (CMSL)

    Energy Technology Data Exchange (ETDEWEB)

    Comolli, A.G.; Ganguli, P.; Karolkiewicz, W.F.; Lee, T.L.K.; Pradhan, V.R.; Popper, G.; Smith, T.; Stalzer, R.H.

    1996-11-01

    Reported herein are the details and the results of laboratory and bench scale experiments that were conducted at Hydrocarbon Technologies, Inc. under DOE Contract No. DE-AC22-93PC92147 during the period of October 1, 1992, to December 31, 1995. The program results described herein build on the previous technology base and investigating additional methods to improve the economics of producing transportation fuels from coal. This included purely physical parameters, coal treatment and variation in solvent to coal ratio, the use of syngas to replace part of the hydrogen as the reducing gas, the use of dispersed catalyst in addition to and replacing the supported catalyst, and the co-processing of coal with plastic waste material. The overall objective of this program is to produce liquid fuels from direct coal liquefaction at a cost that is competitive with conventional fuels. The report includes the results of an economic assessment of the various process strategies that were evaluated during this program. A summary of the technical/economic evaluations is given in Volume I, Section II of this report. The experimental details of the eleven run of the program are given in Volume I, Section III and Volume II of this report. The details of the technical evaluations are given in the Volume III of the report.

  14. Hydrothermal Liquefaction Treatment Hazard Analysis Report

    Energy Technology Data Exchange (ETDEWEB)

    Lowry, Peter P. [Pacific Northwest National Lab. (PNNL), Richland, WA (United States); Wagner, Katie A. [Pacific Northwest National Lab. (PNNL), Richland, WA (United States)

    2016-09-12

    Hazard analyses were performed to evaluate the modular hydrothermal liquefaction treatment system. The hazard assessment process was performed in 2 stages. An initial assessment utilizing Hazard Identification and Preliminary Hazards Analysis (PHA) techniques identified areas with significant or unique hazards (process safety-related hazards) that fall outside of the normal operating envelope of PNNL and warranted additional analysis. The subsequent assessment was based on a qualitative What-If analysis. The analysis was augmented, as necessary, by additional quantitative analysis for scenarios involving a release of hazardous material or energy with the potential for affecting the public. The following selected hazardous scenarios received increased attention: •Scenarios involving a release of hazardous material or energy, controls were identified in the What-If analysis table that prevent the occurrence or mitigate the effects of the release. •Scenarios with significant consequences that could impact personnel outside the immediate operations area, quantitative analyses were performed to determine the potential magnitude of the scenario. The set of “critical controls” were identified for these scenarios (see Section 4) which prevent the occurrence or mitigate the effects of the release of events with significant consequences.

  15. Hydrothermal Liquefaction of Wastewater Treatment Plant Solids

    Energy Technology Data Exchange (ETDEWEB)

    Billing, Justin M.

    2016-10-16

    Feedstock cost is the greatest barrier to the commercial production of biofuels. The merits of any thermochemical or biological conversion process are constrained by their applicability to the lowest cost feedstocks. At PNNL, a recent resource assessment of wet waste feedstocks led to the identification of waste water treatment plant (WWTP) solids as a cost-negative source of biomass. WWTP solids disposal is a growing environmental concern [1, 2] and can account for up to half of WWTP operating costs. The high moisture content is well-suited for hydrothermal liquefaction (HTL), avoiding the costs and parasitic energy losses associated with drying the feedstock for incineration. The yield and quality of biocrude and upgraded biocrude from WWTP solids is comparable to that obtained from algae feedstocks but the feedstock cost is $500-1200 less per dry ton. A collaborative project was initiated and directed by the Water Environment & Reuse Foundation (WERF) and included feedstock identification, dewatering, shipping to PNNL, conversion to biocrude by HTL, and catalytic hydrothermal gasification of the aqueous byproduct. Additional testing at PNNL included biocrude upgrading by catalytic hydrotreatment, characterization of the hydrotreated product, and a preliminary techno-economic analysis (TEA) based on empirical results. This short article will cover HTL conversion and biocrude upgrading. The WERF project report with complete HTL results is now available through the WERF website [3]. The preliminary TEA is available as a PNNL report [4].

  16. Assessment of liquefaction potential during earthquakes by arias intensity

    Science.gov (United States)

    Kayen, R.E.; Mitchell, J.K.

    1997-01-01

    An Arias intensity approach to assess the liquefaction potential of soil deposits during earthquakes is proposed, using an energy-based measure of the severity of earthquake-shaking recorded on seismograms of the two horizontal components of ground motion. Values representing the severity of strong motion at depth in the soil column are associated with the liquefaction resistance of that layer, as measured by in situ penetration testing (SPT, CPT). This association results in a magnitude-independent boundary that envelopes initial liquefaction of soil in Arias intensity-normalized penetration resistance space. The Arias intensity approach is simple to apply and has proven to be highly reliable in assessing liquefaction potential. The advantages of using Arias intensity as a measure of earthquake-shaking severity in liquefaction assessment are: Arias intensity is derived from integration of the entire seismogram wave form, incorporating both the amplitude and duration elements of ground motion; all frequencies of recorded motion are considered; and Arias intensity is an appropriate measure to use when evaluating field penetration test methodologies that are inherently energy-based. Predictor equations describing the attenuation of Arias intensity as a function of earthquake magnitude and source distance are presented for rock, deep-stiff alluvium, and soft soil sites.

  17. Energy-based numerical models for assessment of soil liquefaction

    Directory of Open Access Journals (Sweden)

    Amir Hossein Alavi

    2012-07-01

    Full Text Available This study presents promising variants of genetic programming (GP, namely linear genetic programming (LGP and multi expression programming (MEP to evaluate the liquefaction resistance of sandy soils. Generalized LGP and MEP-based relationships were developed between the strain energy density required to trigger liquefaction (capacity energy and the factors affecting the liquefaction characteristics of sands. The correlations were established based on well established and widely dispersed experimental results obtained from the literature. To verify the applicability of the derived models, they were employed to estimate the capacity energy values of parts of the test results that were not included in the analysis. The external validation of the models was verified using statistical criteria recommended by researchers. Sensitivity and parametric analyses were performed for further verification of the correlations. The results indicate that the proposed correlations are effectively capable of capturing the liquefaction resistance of a number of sandy soils. The developed correlations provide a significantly better prediction performance than the models found in the literature. Furthermore, the best LGP and MEP models perform superior than the optimal traditional GP model. The verification phases confirm the efficiency of the derived correlations for their general application to the assessment of the strain energy at the onset of liquefaction.

  18. Seismic behavior of breakwaters on complex ground by numerical tests: Liquefaction and post liquefaction ground settlements

    Science.gov (United States)

    Gu, Linlin; Zhang, Feng; Bao, Xiaohua; Shi, Zhenming; Ye, Guanlin; Ling, Xianzhang

    2018-04-01

    A large number of breakwaters have been constructed along coasts to protect humans and infrastructures from tsunamis. There is a risk that foundation soils of these structures may liquefy, or partially liquefy during the earthquake preceding a tsunami, which would greatly reduce the structures' capacity to resist the tsunami. It is necessary to consider not only the soil's liquefaction behavior due to earthquake motions but also its post-liquefaction behavior because this behavior will affect the breakwater's capacity to resist an incoming tsunami. In this study, numerical tests based on a sophisticated constitutive model and a soil-water coupled finite element method are used to predict the mechanical behavior of breakwaters and the surrounding soils. Two real breakwaters subjected to two different seismic excitations are examined through numerical simulation. The simulation results show that, earthquakes affect not only the immediate behavior of breakwaters and the surrounding soils but also their long-term settlements due to post-earthquake consolidation. A soil profile with thick clayey layers beneath liquefied soil is more vulnerable to tsunami than a soil profile with only sandy layers. Therefore, quantitatively evaluating the seismic behavior of breakwaters and surrounding soils is important for the design of breakwater structures to resist tsunamis.

  19. Optimization for microwave-assisted direct liquefaction of bamboo residue in glycerol/methanol mixtures

    Science.gov (United States)

    Jiulong Xie; Jinqiu Qi; Chungyun Hse; Todd F. Shupe

    2015-01-01

    Bamboo residues were liquefied in a mixture of glycerol and methanol in the presence of sulfuric acid using microwave energy. We investigated the effects of liquefaction conditions, including glycerol/methanol ratio, liquefaction temperature, and reaction time on the conversion yield. The optimal liquefaction conditions were under the temperature of 120

  20. FY 1994 report on the Coal Liquefaction Committee; 1994 nendo sekitan ekika iinkai hokokusho

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1995-03-01

    The paper reported the FY 1994 activities of the Coal Liquefaction Committee. The Coal Liquefaction Committee in this fiscal year was held on November 29, 1994 (1st) and March 22, 1995 (2nd), and report was made on the bituminous coal liquefaction study and state of the R and D of liquefaction base technology. Report was also made on the state of construction of bituminous coal liquefaction PP, outline of the results of the PSU operation, outline of the 11th Japan-U.S. JTM, etc. In the liquefaction base study, report/discussion were made about the improvement/rationalization of liquefaction process, study of innovative technology of coal liquefaction, study of coal liquefaction conditions, study for higher liquefaction element technology, project on the internationalization of coal liquefaction technology, etc. As to the relation of the entrained bed coal gasification power plant, report/discussion were made about survey/study on the processing of coal for coal gasification use (survey of coal kind selection, development of information processing system for coal conversion technology). Besides, as a topic, report was made on the economical evaluation/calculation of a commercial plant for brown coal liquefaction. (NEDO)

  1. Liquefaction behaviors of bamboo residues in a glycerol-based solvent using microwave energy

    Science.gov (United States)

    Jiulong Xie; Chung-Yun Hse; Todd F. Shupe; Jinqiu Qi; Hui Pan

    2014-01-01

    Liquefaction of bamboo was performed in glycerol–methanol as co-solvent using microwave energy and was evaluated by characterizing the liquefied residues. High efficiency conversion of bamboo was achieved under mild reaction conditions. Liquefaction temperature and time interacted to affect the liquefaction reaction. Fourier transform infrared analyzes of the residues...

  2. Exploratory research on solvent refined coal liquefaction. Annual technical progress report, January 1-December 31, 1979

    Energy Technology Data Exchange (ETDEWEB)

    None

    1980-09-01

    This report summarizes the progress of the Exploratory Research on Solvent Refined Coal Liquefaction project by The Pittsburg and Midway Coal Mining Co.'s Merriam Laboratory during 1979. In a series of experiments with varying feed gas composition, low levels (5 to 10 mole %) of carbon monoxide had little effect on the SRC II processing of Pittsburgh Seam coal (Powhatan No. 5 Mine) while higher levels (20 to 40 mole %) resulted in a general degradation of operability and reduced oil yields. Addition of finely divided (approx. 1 ..mu..m) pyrite to the reactive Powhatan coal had little effect on oil yields although the molecular weight of the distillation residue was apparently decreased. When finely divided pyrite and magnetite were added to the less reactive coals from the Loveridge and Blacksville No. 1 Mines (also Pittsburgh Seam), however, substantial increases in oil yields and product quality were obtained. In a comparison of upflow and downflow dissolver configurations with Powhatan coal in the SRC II mode, there was no difference in yields or product quality. A study characterizing specific reactors revealed a significantly higher conversion in the SRC I mode with a reactor approximating plug flow conditions compared to a completely backmixed reactor. In the SRC II mode there was only a slightly higher oil yield with the plug flow reactor.

  3. Assessment of stone columns as a mitigation technique of liquefaction-induced effects during Italian earthquakes (May 2012).

    Science.gov (United States)

    Forcellini, Davide; Tarantino, Angelo Marcello

    2014-01-01

    Soil liquefaction has been observed worldwide during recent major earthquakes with induced effects responsible for much of the damage, disruption of function, and considerable replacement expenses for structures. The phenomenon has not been documented in recent time with such damage in Italian context before the recent Emilia-Romagna Earthquake (May 2012). The main lateral spreading and vertical deformations affected the stability of many buildings and impacted social life inducing valuable lessons on liquefaction risk assessment and remediation. This paper aims first of all to reproduce soil response to liquefaction-induced lateral effects and thus to evaluate stone column mitigation technique effectiveness by gradually increasing the extension of remediation, in order to achieve a satisfactory lower level of permanent deformations. The study is based on the use of a FE computational interface able to analyse the earthquake-induced three-dimensional pore pressure generation adopting one of the most credited nonlinear theories in order to assess realistically the displacements connected to lateral spreading.

  4. Co, Fe and Ni catalysts supported on coke for direct coal liquefaction

    International Nuclear Information System (INIS)

    Jimenez, Jose A; Villalba, Oscar A; Rodriguez, Luis I; Hernandez, Orlando; Agamez, Yasmin Y; Dias Jose de Jesus

    2008-01-01

    Transition metal catalysts supported on coke were prepared by impregnation with a solution of complex of metal-thiourea, that is produced from salt precursors of cobalt chloride, Nickel chloride or iron sulfate and ammonium. sulphide formation on the support surface was generated by decomposition of the metal complex. The catalysts obtained were used in direct coal liquefaction of a medium volatile bituminous coal (Yerbabuena N 1) from Cundinamarca using a 250 Ml, Parr reactor at 723 K and a hydrogen-donor solvent. The catalytic results show, for all samples, both a good coal conversion and an enhancement of the yield of oils, this indicates that the proposed preparation method of catalyst is effective and that eventually the H 2 S sulphidation conventional process could be replaced

  5. Liquefaction under drained condition, from the lab to reality ?

    Science.gov (United States)

    Clément, Cécile; Aharonov, Einat; Stojanova, Menka; Toussaint, Renaud

    2015-04-01

    Liquefaction constitutes a significant natural hazard in relation to earthquakes and landslides. This effect can cause buildings to tilt or sink into the soil, mud-volcanoes, floatation of buried objects, long-runout landslides, etc. In this work we present a new understanding regarding the mechanism by which buildings sink and tilt during liquefaction caused by earthquakes. Conventional understanding of liquefaction explains most observed cases as occurring in an undrained, under-compacted, layer of sandy soil saturated with water [1]: According to that understanding, the under compacted sandy layer has the tendency to compact when a load is applied. In our case the load comes from ground shaking during an earthquake. When the soil compacts, the fluid pore pressure rises. Because in undrained conditions the fluid cannot flow out, the pore pressure builds up. The weight of buildings is in this case transferred from the grains of the soil to the pore water. The soil loses its rigidity and it flows like a liquid. From this model scientists made theoretical and empirical laws for geotechnical use and buildings construction. Despite the success of this conventional model in many cases, liquefied soils were also observed under drained conditions, and in previously compacted soils, which doesn't agree with the assumption of the model quoted above. One of the famous liquefaction events is the Kobe port destruction during the 1995 earthquake. A simple calculation of the Deborah number following Goren et al ([2][3]) shows that the undrained constraint was not met below the Kobe port during the 1995 earthquake. We propose another model, of liquefaction in drained granular media. According to our model the mere presence of water in granular media is enough to cause liquefaction during an earthquake, provided that the water reaches close to the surface. Our computations are based on the buoyancy force, and we take into account the static fluid pressure only. For small

  6. The sequence of sediment behaviour during wave-induced liquefaction

    DEFF Research Database (Denmark)

    Sumer, B. Mutlu; Hatipoglu, Figen; Fredsøe, Jørgen

    2006-01-01

    to be in agreement with recent centrifuge wave-tank experiments. As for the final stage of the sequence of processes (formation of ripples), the ripple steepness (normalized with the angle of repose) for sediment with liquefaction history is found to be the same as that in sediment with no liquefaction history.......This paper presents the results of an experimental investigation of the complete sequence of sediment behaviour beneath progressive waves. The sediment was silty with d(50) = 0.060 mm. Two kinds of measurements were carried out: pore-water pressure measurements (across the sediment depth...... of liquefaction and compaction fronts in the sediment and (iii) the characteristics of the orbital motion of the liquefied sediment including the motion of the interface between the water body and the sediment. The ranges of the various quantities in the tests were: wave height, H = 9-17 cm, wave period, T = 1...

  7. Ground motions estimates for a cascadia earthquake from liquefaction evidence

    Science.gov (United States)

    Dickenson, S.E.; Obermeier, S.F.

    1998-01-01

    Paleoseismic studies conducted in the coastal regions of the Pacific Northwest in the past decade have revealed evidence of crustal downdropping and subsequent tsunami inundation, attributable to a large earthquake along the Cascadia subduction zone which occurred approximately 300 years ago, and most likely in 1700 AD. In order to characterize the severity of ground motions from this earthquake, we report on results of a field search for seismically induced liquefaction features. The search was made chiefly along the coastal portions of several river valleys in Washington, rivers along the central Oregon coast, as well as on islands in the Columbia River of Oregon and Washington. In this paper we focus only on the results of the Columbia River investigation. Numerous liquefaction features were found in some regions, but not in others. The regional distribution of liquefaction features is evaluated as a function of geologic and geotechnical factors at each site in order to estimate the intensity of ground shaking.

  8. Transport fuels from two-stage coal liquefaction

    Energy Technology Data Exchange (ETDEWEB)

    Benito, A.; Cebolla, V.; Fernandez, I.; Martinez, M.T.; Miranda, J.L.; Oelert, H.; Prado, J.G. (Instituto de Carboquimica CSIC, Zaragoza (Spain))

    1994-03-01

    Four Spanish lignites and their vitrinite concentrates were evaluated for coal liquefaction. Correlationships between the content of vitrinite and conversion in direct liquefaction were observed for the lignites but not for the vitrinite concentrates. The most reactive of the four coals was processed in two-stage liquefaction at a higher scale. First-stage coal liquefaction was carried out in a continuous unit at Clausthal University at a temperature of 400[degree]C at 20 MPa hydrogen pressure and with anthracene oil as a solvent. The coal conversion obtained was 75.41% being 3.79% gases, 2.58% primary condensate and 69.04% heavy liquids. A hydroprocessing unit was built at the Instituto de Carboquimica for the second-stage coal liquefaction. Whole and deasphalted liquids from the first-stage liquefaction were processed at 450[degree]C and 10 MPa hydrogen pressure, with two commercial catalysts: Harshaw HT-400E (Co-Mo/Al[sub 2]O[sub 3]) and HT-500E (Ni-Mo/Al[sub 2]O[sub 3]). The effects of liquid hourly space velocity (LHSV), temperature, gas/liquid ratio and catalyst on the heteroatom liquids, and levels of 5 ppm of nitrogen and 52 ppm of sulphur were reached at 450[degree]C, 10 MPa hydrogen pressure, 0.08 kg H[sub 2]/kg feedstock and with Harshaw HT-500E catalyst. The liquids obtained were hydroprocessed again at 420[degree]C, 10 MPa hydrogen pressure and 0.06 kg H[sub 2]/kg feedstock to hydrogenate the aromatic structures. In these conditions, the aromaticity was reduced considerably, and 39% of naphthas and 35% of kerosene fractions were obtained. 18 refs., 4 figs., 4 tabs.

  9. Liquefaction of solid carbonaceous material with catalyst recycle

    Science.gov (United States)

    Gupta, Avinash; Greene, Marvin I.

    1992-01-01

    In the two stage liquefaction of a carbonaceous solid such as coal wherein coal is liquefied in a first stage in the presence of a liquefaction solvent and the first stage effluent is hydrogenated in the presence of a supported hydrogenation catalyst in a second stage, catalyst which has been previously employed in the second stage and comminuted to a particle size distribution equivalent to 100% passing through U.S. 100 Mesh, is passed to the first stage to improve the overall operation.

  10. Hydrothermal liquefaction of microalgae's for bio oil production

    DEFF Research Database (Denmark)

    Toor, Saqib; Reddy, Harvind; Deng, Shuguang

    process water for algae cultivation. GC-MS, elemental analyzer, calorimeter and nutrient analysis were used to analyze bio-crude, lipid-extracted algae and water samples produced in the hydrothermal liquefaction process. The highest bio-oil yield of 46% was obtained on Nannochloropsis salina at 310 °C...... and 107 bar. For Spirulina platensis algae sample, the highest bio-oil yield is 38% at 350 °C and 195 bar. Preliminary data also indicate that a lipid-extracted algae solid residue sample obtained in the hydrothermal liquefaction process contains a high level of proteins...

  11. Cooperative research in coal liquefaction. Final report, May 1, 1990-- April 30, 1991

    Energy Technology Data Exchange (ETDEWEB)

    Huffman, G.P. [ed.

    1992-02-15

    The Consortium for Fossil Fuel Liquefaction Science (CFFLS) is currently engaged in a three year contract with the US Department of Energy investigating a range of research topics dealing with direct coal liquefaction. This report summarizes the results of this program in its second year, from May 1, 1990 to April 30, 1991. Accomplishments for this period are presented for the following tasks: Iron-based catalysts for coal liquefaction, exploratory research on coal conversion, novel coal liquefaction concepts, and novel catalysts for coal liquefaction.

  12. The text of the Agreement of 7 October 1983 between Cuba and the Agency for the application of safeguards in connection with the supply of a zero-power nuclear reactor from the Hungarian People's Republic

    International Nuclear Information System (INIS)

    1984-01-01

    The full text of the agreement of 7 October 1983 between Cuba and the Agency for the application of safeguards in connection with the supply of a zero-power nuclear reactor from the Hungarian People's Republic and to the nuclear material to be used therein to be supplied by the Union of Soviet Socialist Republics is presented

  13. Assessment of liquefaction-induced hazards using Bayesian networks based on standard penetration test data

    Science.gov (United States)

    Tang, Xiao-Wei; Bai, Xu; Hu, Ji-Lei; Qiu, Jiang-Nan

    2018-05-01

    Liquefaction-induced hazards such as sand boils, ground cracks, settlement, and lateral spreading are responsible for considerable damage to engineering structures during major earthquakes. Presently, there is no effective empirical approach that can assess different liquefaction-induced hazards in one model. This is because of the uncertainties and complexity of the factors related to seismic liquefaction and liquefaction-induced hazards. In this study, Bayesian networks (BNs) are used to integrate multiple factors related to seismic liquefaction, sand boils, ground cracks, settlement, and lateral spreading into a model based on standard penetration test data. The constructed BN model can assess four different liquefaction-induced hazards together. In a case study, the BN method outperforms an artificial neural network and Ishihara and Yoshimine's simplified method in terms of accuracy, Brier score, recall, precision, and area under the curve (AUC) of the receiver operating characteristic (ROC). This demonstrates that the BN method is a good alternative tool for the risk assessment of liquefaction-induced hazards. Furthermore, the performance of the BN model in estimating liquefaction-induced hazards in Japan's 2011 Tōhoku earthquake confirms its correctness and reliability compared with the liquefaction potential index approach. The proposed BN model can also predict whether the soil becomes liquefied after an earthquake and can deduce the chain reaction process of liquefaction-induced hazards and perform backward reasoning. The assessment results from the proposed model provide informative guidelines for decision-makers to detect the damage state of a field following liquefaction.

  14. Report on the coal liquefaction committee in fiscal 1992; 1992 nendo sekitan ekika iinkai hokokusho

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1993-03-01

    This paper reports the activities of the coal liquefaction committee in fiscal 1992. The first committee meeting was held on August 21. After having confirmed the minutes of the previous meeting, an explanation was given on the research and development plans in fiscal 1992. The explanation covered the general explanation, bituminous coal liquefaction, brown coal liquefaction, and the common and fundamental aspects. The presented topics included the achievements in the operations using a bituminous coal liquefaction PSU and a small device, the status of compiling the achievements in the brown coal liquefaction project, preparation of the basic policy on developing the common basic technologies, and structuring of a coal liquefaction technology package. The second meeting was held on March 18, 1993. The meeting verified the minutes of the previous meeting, and gave the sub-committee reports for fiscal 1992. The sub-committees include those for bituminous coal liquefaction, brown coal liquefaction, environmental safety evaluation, and separation and refining technologies. As the summary of the achievements in fiscal 1992, descriptions were given on the bituminous coal liquefaction, brown coal liquefaction, and common and basic aspects. The fiscal 1993 plan presented included the budget aspect. A description was given as a topic on the economic performance evaluation and the working scheme (the execution plan) for the brown coal liquefaction process. (NEDO)

  15. Cooperative research in coal liquefaction. Technical progress report, May 1, 1993--April 30, 1994

    Energy Technology Data Exchange (ETDEWEB)

    Huffman, G.P. [ed.

    1994-10-01

    Accomplishments for the past year are presented for the following tasks: coliquefaction of coal with waste materials; catalysts for coal liquefaction to clean transportation fuels; fundamental research in coal liquefaction; and in situ analytical techniques for coal liquefaction and coal liquefaction catalysts some of the highlights are: very promising results have been obtained from the liquefaction of plastics, rubber tires, paper and other wastes, and the coliquefaction of wastes with coal; a number of water soluble coal liquefaction catalysts, iron, cobalt, nickel and molybdenum, have been comparatively tested; mossbauer spectroscopy, XAFS spectroscopy, TEM and XPS have been used to characterize a variety of catalysts and other samples from numerous consortium and DOE liquefaction projects and in situ ESR measurements of the free radical density have been conducted at temperatures from 100 to 600{degrees}C and H{sub 2} pressures up to 600 psi.

  16. Co-liquefaction of Elbistan Lignite with Manure Biomass; Part 2 - Effect of Biomass Type, Waste to Lignite Ratio and Solid to Liquid Ratio

    Science.gov (United States)

    Karaca, Hüseyin; Koyunoglu, Cemil

    2017-12-01

    Most coal hydrogenation processes require a large quantity of hydrogen. In general, a coal derived liquid such as anthracene oil was used as a hydrogen donor solvent. Tetralin, partially hydrogenated pyrene, phenantrene and coal-derived solvents, which contain hydroaromatic compounds, are efficient solvents to donate hydrogen. In an attempt to reduce the high cost of hydrogen, part of the hydrogen was replaced by a low cost hydrogen donor solvent. This must be hydrogenated during or before the process and recycled. To reduce the cost of hydrogen donor vehicles instead of liquids recycled from the liquefaction process or several biomass types, industrial by products, liquid fractions derived from oil sands bitumen were successfully used to solubilize a coal from the past. In an attempt to reduce the high cost of hydrogen, part of the hydrogen was replaced by a low cost hydrogen donor solvent. However, when hydrogen is supplied from the hydroaromatic structures present in the solvent, the activity of coal minerals is too low to rehydrogenate the solvent in-situ. Nevertheless, a decrease of using oxygen, in addition to enhanced usage of the hydrogen supply by using various waste materials might lead to a decrease of the cost of the liquefaction procedure. So instead of using tetralin another feeding material such as biomass is becoming another solution improving hydrogen donor substances. Most of the liquefaction process were carried out in a batch reactor, in which the residence time of the liquefaction products is long enough to favour the retrogressive reactions, early studies which are related to liquefaction of coal with biomass generally focus on the synergetic effects of coal while biomass added. Early studies which are related to liquefaction of coal with biomass generally focus on the synergetic effects of coal while biomass added. Alternatively, to understand the hydrogen transfer from biomass to coal, in this study, Elbistan Lignite (EL) with manure, tea

  17. Hydrothermal liquefaction of barley straw to bio-crude oil

    DEFF Research Database (Denmark)

    Zhu, Zhe; Rosendahl, Lasse; Toor, Saqib

    2015-01-01

    Hydrothermal liquefaction (HTL) of barley straw with K2CO3 at different temperatures (280–400 C) was conducted and compared to optimize its process conditions; the aqueous phase as a co-product from this process was recycled to explore the feasibility of implementing wastewater reuse for bio...

  18. Mineral catalysis of oil producing reactions in coal liquefaction

    Energy Technology Data Exchange (ETDEWEB)

    Shridharani, K.G.

    1983-01-01

    This work was concerned primarily with the development of a relatively inexpensive, readily available, high activity catalyst that can be used as a disposable catalyst in coal liquefaction processes. For a fair evaluation of the developmental mineral catalyst (presulfided iron oxide), it was necessary to determine at different stages of this work, whether catalyst inhibition, deactivation or activity was the limiting factor in coal liquefaction catalysis. First, different routes were explored to prepare a high hydrogenation activity, iron-based catalyst. Naphthalene hydrogenation was used as a model reaction to rate the hydrogenation activities of different additives. Presulfiding of iron oxide with H/sub 2/S, under controlled conditions, rendered the highest hydrogenation activity mineral catalyst, which had a hydrogenation activity even greater than that of commercial CoMo/Al/sub 2/O/sub 3/ catalyst sulfided with creosote oil and hydrogen. Sulfiding of CoMo/Al/sub 2/O/sub 3/ catalyst with H/sub 2/S remarkably improved its initial hydrogenation activity. Second, the catalyst inhibition and deactivation during liquefaction were studied. Liquefaction-process solvents contain a number of compounds that can either deactivate or inhibit the hydrogenation activity of a catalyst. Finally, the hydrocracking activity of the presulfided iron oxide catalyst was compared with that of commercial catalysts, CoMo/Al/sub 2/O/sub 3/ and low alumina FCC catalyst.

  19. Finite Element Modelling of Seismic Liquefaction in Soils

    NARCIS (Netherlands)

    Galavi, V.; Petalas, A.; Brinkgreve, R.B.J.

    2013-01-01

    Numerical aspects of seismic liquefaction in soils as implemented in the finite element code, PLAXIS, is described in this paper. After description of finite element equations of dynamic problems, three practical dynamic boundary conditions, namely viscous boundary tractions, tied degrees of freedom

  20. Biological production of alcohols from coal through indirect liquefaction

    Energy Technology Data Exchange (ETDEWEB)

    Barik, S; Prieto, S; Harrison, S B; Clausen, E C; Gaddy, J L

    1988-08-01

    The purpose of this project is to demonstrate the feasibility of producing liquid fuels from the components of synthesis gas through biological indirect liquefaction. The results of pure culture and natural source screening studies aimed at finding organisms capable of carrying out the conversions are presented and discussed. 17 refs., 2 figs., 8 tabs.

  1. The making of Andersen’s liquefaction chart

    DEFF Research Database (Denmark)

    Sabaliauskas, Tomas; Ibsen, Lars Bo

    Andersen’s chart (Andersen & Berre, 1999) is a graphical method of observing cyclic soil response. It allows observing soil response to various stress amplitudes that can lead to liquefaction, excess plastic deformation stabilizing soil response.The process of obtaining the original chart has been...

  2. Determination of Liquefaction Potential using Artificial Neural Networks

    DEFF Research Database (Denmark)

    Farrokhzad, F; Choobbasti, A.J; Barari, Amin

    2011-01-01

    The authors propose an alternative general regression model based on neural networks, which enables analysis of summary data obtained by liquefaction analysis according to usual methods. For that purpose, the data from some thirty boreholes made during field investigations in Babol, in the Iranian...

  3. Liquefaction of ground tire rubber at low temperature.

    Science.gov (United States)

    Cheng, Xiangyun; Song, Pan; Zhao, Xinyu; Peng, Zonglin; Wang, Shifeng

    2018-01-01

    Low-temperature liquefaction has been investigated as a novel method for recycling ground tire rubber (GTR) into liquid using an environmentally benign process. The liquefaction was carried out at different temperatures (140, 160 and 180 °C) over variable time ranges (2-24 h) by blending the GTR with aromatic oil in a range from 0 to 100 parts per hundred rubber (phr). The liquefied GTR was separated into sol (the soluble fraction of rubber which can be extracted with toluene) and gel fractions (the solid fraction obtained after extraction) to evaluate the reclaiming efficiency. It was discovered that the percentage of the sol fraction increased with time, swelling ratio and temperature. Liquefied rubber was obtained with a high sol fraction (68.34 wt%) at 140 °C. Simultaneously, separation of nano-sized carbon black from the rubber networks occurred. The separation of carbon black from the network is the result of significant damage to the cross-linked-network that occurs throughout the liquefaction process. During liquefaction, a competitive reaction between main chain scission and cross-link bond breakage takes place. Copyright © 2017 Elsevier Ltd. All rights reserved.

  4. Thermochemical liquefaction characteristics of microalgae in sub- and supercritical ethanol

    Energy Technology Data Exchange (ETDEWEB)

    You, Qiao; Chen, Liang [College of Environmental Science and Engineering, Hunan University, Changsha (China); Key Laboratory of Environment Biology and Pollution Control, Ministry of Education, Changsha (China)

    2011-01-15

    Thermochemical liquefaction characteristics of Spirulina, a kind of high-protein microalgae, were investigated with the sub- and supercritical ethanol as solvent in a 1000 mL autoclave. The influences of various liquefaction parameters on the yields of products (bio-oil and residue) from the liquefaction of Spirulina were studied, such as the reaction temperature (T), the S/L ratio (R{sub 1}, solid: Spirulina, liquid: ethanol), the solvent filling ratio (R{sub 2}) and the type and dosage of catalyst. Without catalyst, the bio-oil yields were in the range of 35.4 wt.% and 45.3 wt.% depending on the changes of T, R{sub 1} and R{sub 2}. And the bio-oil yields increased generally with increasing T and R{sub 2}, while the bio-oil yields reduced with increasing R{sub 1}. The FeS catalyst was certified to be an ideal catalyst for the liquefaction of Spirulina microalgae for its advantages on promoting bio-oil production and suppressing the formation of residue. The optimal dosage of catalyst (FeS) was ranging from 5-7 wt.%. The elemental analyses and FT-IR and GC-MS measurements for the bio-oils revealed that the liquid products have much higher heating values than the crude Spirulina sample and fatty acid ethyl ester compounds were dominant in the bio-oils, irrespective of whether catalyst was used. (author)

  5. Direct liquefaction of plastics and coprocessing of coal with plastics

    Energy Technology Data Exchange (ETDEWEB)

    Huffman, G.P.; Feng, Z.; Mahajan, V. [Univ. of Kentucky, Lexington, KY (United States)

    1995-12-31

    The objectives of this work were to optimize reaction conditions for the direct liquefaction of waste plastics and the coprocessing of coal with waste plastics. In previous work, the direct liquefaction of medium and high density polyethylene (PE), polypropylene (PPE), poly(ethylene terephthalate) (PET), and a mixed plastic waste, and the coliquefaction of these plastics with coals of three different ranks was studied. The results established that a solid acid catalyst (HZSM-5 zeolite) was highly active for the liquefaction of the plastics alone, typically giving oil yields of 80-95% and total conversions of 90-100% at temperatures of 430-450 {degrees}C. In the coliquefaction experiments, 50:50 mixtures of plastic and coal were used with a tetralin solvent (tetralin:solid = 3:2). Using approximately 1% of the HZSM-5 catalyst and a nanoscale iron catalyst, oil yields of 50-70% and total conversion of 80-90% were typical. In the current year, further investigations were conducted of the liquefaction of PE, PPE, and a commingled waste plastic obtained from the American Plastics Council (APC), and the coprocessing of PE, PPE and the APC plastic with Black Thunder subbituminous coal. Several different catalysts were used in these studies.

  6. Alkaline hydrothermal liquefaction of swine carcasses to bio-oil

    Energy Technology Data Exchange (ETDEWEB)

    Zheng, Ji-Lu, E-mail: triace@163.com; Zhu, Ming-Qiang; Wu, Hai-tang

    2015-09-15

    Highlights: • Swine carcasses can be converted to bio-oil by alkaline hydrothermal liquefaction. • It seems that the use of the bio-oil for heat or CHP is technically suitable. • Some valuable chemicals were found in the bio-oils. • The bio-oil and the solid residue constituted an energy efficiency of 93.63% for the feedstock. • The solid residue can be used as a soil amendment, to sequester C and for preparing activated carbon. - Abstract: It is imperative that swine carcasses are disposed of safely, practically and economically. Alkaline hydrothermal liquefaction of swine carcasses to bio-oil was performed. Firstly, the effects of temperature, reaction time and pH value on the yield of each liquefaction product were determined. Secondly, liquefaction products, including bio-oil and solid residue, were characterized. Finally, the energy recovery ratio (ERR), which was defined as the energy of the resultant products compared to the energy input of the material, was investigated. Our experiment shows that reaction time had certain influence on the yield of liquefaction products, but temperature and pH value had bigger influence on the yield of liquefaction products. Yields of 62.2 wt% bio-oil, having a high heating value of 32.35 MJ/kg and a viscosity of 305cp, and 22 wt% solid residue were realized at a liquefaction temperature of 250 °C, a reaction time of 60 min and a pH value of 9.0. The bio-oil contained up to hundreds of different chemical components that may be classified according to functional groups. Typical compound classes in the bio-oil were hydrocarbons, organic acids, esters, ketones and heterocyclics. The energy recovery ratio (ERR) reached 93.63%. The bio-oil is expected to contribute to fossil fuel replacement in stationary applications, including boilers and furnaces, and upgrading processes for the bio-oil may be used to obtain liquid transport fuels.

  7. Alkaline hydrothermal liquefaction of swine carcasses to bio-oil

    International Nuclear Information System (INIS)

    Zheng, Ji-Lu; Zhu, Ming-Qiang; Wu, Hai-tang

    2015-01-01

    Highlights: • Swine carcasses can be converted to bio-oil by alkaline hydrothermal liquefaction. • It seems that the use of the bio-oil for heat or CHP is technically suitable. • Some valuable chemicals were found in the bio-oils. • The bio-oil and the solid residue constituted an energy efficiency of 93.63% for the feedstock. • The solid residue can be used as a soil amendment, to sequester C and for preparing activated carbon. - Abstract: It is imperative that swine carcasses are disposed of safely, practically and economically. Alkaline hydrothermal liquefaction of swine carcasses to bio-oil was performed. Firstly, the effects of temperature, reaction time and pH value on the yield of each liquefaction product were determined. Secondly, liquefaction products, including bio-oil and solid residue, were characterized. Finally, the energy recovery ratio (ERR), which was defined as the energy of the resultant products compared to the energy input of the material, was investigated. Our experiment shows that reaction time had certain influence on the yield of liquefaction products, but temperature and pH value had bigger influence on the yield of liquefaction products. Yields of 62.2 wt% bio-oil, having a high heating value of 32.35 MJ/kg and a viscosity of 305cp, and 22 wt% solid residue were realized at a liquefaction temperature of 250 °C, a reaction time of 60 min and a pH value of 9.0. The bio-oil contained up to hundreds of different chemical components that may be classified according to functional groups. Typical compound classes in the bio-oil were hydrocarbons, organic acids, esters, ketones and heterocyclics. The energy recovery ratio (ERR) reached 93.63%. The bio-oil is expected to contribute to fossil fuel replacement in stationary applications, including boilers and furnaces, and upgrading processes for the bio-oil may be used to obtain liquid transport fuels

  8. FBR type reactor

    International Nuclear Information System (INIS)

    Kimura, Kimitaka; Fukuie, Ken; Iijima, Tooru; Shimpo, Masakazu.

    1994-01-01

    In an FBR type reactor for exchanging fuels by pulling up reactor core upper mechanisms, a connection mechanism is disposed for connecting the top of the reactor core and the lower end of the reactor core upper mechanisms. In addition, a cylindrical body is disposed surrounding the reactor core upper mechanisms, and a support member is disposed to the cylindrical body for supporting an intermediate portion of the reactor core upper mechanisms. Then, the lower end of the reactor core upper mechanisms is connected to the top of the reactor core. Same displacements are caused to both of them upon occurrence of earthquakes and, as a result, it is possible to eliminate mutual horizontal displacement between a control rod guide hole of the reactor core upper mechanisms and a control rod insertion hole of the reactor core. In addition, since the intermediate portion of the reactor core upper mechanisms is supported by the support member disposed to the cylindrical body surrounding the reactor core upper mechanisms, deformation caused to the lower end of the reactor core upper mechanisms is reduced, so that the mutual horizontal displacement with respect to the control rod insertion hole of the reactor core can be reduced. As a result, performance of control rod insertion upon occurrence of the earthquakes is improved, so that reactor shutdown is conducted more reliably to improve reactor safety. (N.H.)

  9. Semi-automated landform classification for hazard mapping of soil liquefaction by earthquake

    Science.gov (United States)

    Nakano, Takayuki

    2018-05-01

    Soil liquefaction damages were caused by huge earthquake in Japan, and the similar damages are concerned in near future huge earthquake. On the other hand, a preparation of soil liquefaction risk map (soil liquefaction hazard map) is impeded by the difficulty of evaluation of soil liquefaction risk. Generally, relative soil liquefaction risk should be able to be evaluated from landform classification data by using experimental rule based on the relationship between extent of soil liquefaction damage and landform classification items associated with past earthquake. Therefore, I rearranged the relationship between landform classification items and soil liquefaction risk intelligibly in order to enable the evaluation of soil liquefaction risk based on landform classification data appropriately and efficiently. And I developed a new method of generating landform classification data of 50-m grid size from existing landform classification data of 250-m grid size by using digital elevation model (DEM) data and multi-band satellite image data in order to evaluate soil liquefaction risk in detail spatially. It is expected that the products of this study contribute to efficient producing of soil liquefaction hazard map by local government.

  10. Coal liquefaction committee report for fiscal 1981; 1981 nendo sekitan ekika iinkai hokokusho

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1982-03-01

    For the assurance of smooth progress of coal technology development endeavors, the New Energy and Industrial Technology Development Organization (NEDO) has installed coal technology development committees (general committee on coal technologies, coal liquefaction committee, plant materials committee, coal type survey committee, total system committee, and coal gasification committee). The coal liquefaction committee deliberates and evaluates liquefaction technology and propels forward smoothly the efforts to develop the technology. Under the coal liquefaction committee, there are four subcommittees, which are the 1st subcommittee (primary liquefaction subcommittee), 2nd subcommittee (solid/liquid separation subcommittee), 3rd subcommittee (secondary hydrogenation subcommittee), and the 4th subcommittee (brown coal liquefaction subcommittee). The 2nd and 3rd subcommittees deal with common tasks as they were studied in fiscal 1980. The 1st subcommittee incorporates into itself the old subcommittees that respectively worked on the three liquefaction processes (the direct hydrogenation process, the solvent extraction process, and the Solvolysis process), and is designed to provide a site for information exchange. A brown coal liquefaction committee is incorporated into the coal liquefaction committee as the 4th subcommittee. This report is a compilation of the agendas of the respective subcommittees of the coal liquefaction committee. (NEDO)

  11. Fiscal 1994 achievement report 1/2. Coal liquefaction technology development - Bituminous coal liquefaction technology development - Study for supporting pilot plant - Study using 1t/d PSU (Study of operation using PSU); 1994 nendo seika hokokusho 1/2. Sekitan ekika gijutsu kaihatsu - Rekiseitan ekika gijutsu no kaihatsu - Pilot plant no shien kenkyu - 1t/d process support unit (PSU) ni yoru kenkyu (PSU ni yoru unten kenkyu)

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1995-03-01

    The operation of a 1t/d PSU (process support unit) was studied in the NEDOL coal liquefaction process. Modification was made, which involved the installation of a high-temperature/high-pressure sampling device for observing reaction and fluidity in the liquefaction reactor, a differential pressure measuring device, and a neutron attenuation-aided measuring device. Relative to coal injection, a 49.5-day and 49.3-day slurry injections were carried out using Tanito Harum coal, when impacts on the product yield and the operability of the unit were examined. A verification test was conducted for an improved hydrogenation catalyst, and liquefaction reactor characteristics were investigated. During a 19-day operation for the study of maintenance, newly installed equipment and devices were verified for function, and operating methods were probed into. In the survey of environments, characteristics were examined of the wastewater discharged from the Tanito Harum coal liquefaction process, and wastewater treatment methods were studied. The air, odor, and tar mist were examined with the PSU in operation, and the measured values were found to be below the management limits showing that its operation did not pose any problems relating to working environments. (NEDO)

  12. Role of heat exchangers in helium liquefaction cycles: Simulation studies using Collins cycle

    Energy Technology Data Exchange (ETDEWEB)

    Thomas, Rijo Jacob, E-mail: rijojthomas@gmail.com [Cryogenic Engineering Centre, Indian Institute of Technology, Kharagpur 721302 (India); Ghosh, Parthasarathi; Chowdhury, Kanchan [Cryogenic Engineering Centre, Indian Institute of Technology, Kharagpur 721302 (India)

    2012-01-15

    Highlights: Black-Right-Pointing-Pointer Role of heat exchangers in basic helium liquefier analyzed to design large-scale ones. Black-Right-Pointing-Pointer Heat exchangers that determine inlet temperature to expanders are more significant. Black-Right-Pointing-Pointer Limiting values of nondimensional UA for each heat exchanger have been determined. Black-Right-Pointing-Pointer Extra area distributed such that effectiveness of all heat exchangers increase uniformly. Black-Right-Pointing-Pointer Heat exchanger performance variation have little influence on the optimum expander flow. - Abstract: Energy efficiency of large-scale helium liquefiers generally employed in fusion reactors and accelerators is determined by the performance of their constituting components. Simulation with Aspen HYSYS{sup Registered-Sign} V7.0, a commercial process simulator, helps to understand the effects of heat exchanger parameters on the performance of a helium liquefier. Effective UA (product of overall heat transfer coefficient U, heat transfer surface area A and deterioration factor F) has been taken as an independent parameter, which takes into account all thermal irreversibilities and configuration effects. Nondimensionalization of parameters makes the results applicable to plants of any capacity. Rate of liquefaction is found to increase linearly with the effectiveness of heat exchangers. Performance of those heat exchangers that determine the inlet temperatures to expanders have more influence on the liquid production. Variation of sizes of heat exchangers does not affect the optimum rate of flow through expanders. Increasing UA improves the rate of liquid production; however, the improvement saturates at limiting UA. Maximum benefit in liquefaction is obtained when the available heat transfer surface area is distributed in such a way that the effectiveness remains equal for all heat exchangers. Conclusions from this study may be utilized in analyzing and designing large helium

  13. Role of heat exchangers in helium liquefaction cycles: Simulation studies using Collins cycle

    International Nuclear Information System (INIS)

    Thomas, Rijo Jacob; Ghosh, Parthasarathi; Chowdhury, Kanchan

    2012-01-01

    Highlights: ► Role of heat exchangers in basic helium liquefier analyzed to design large-scale ones. ► Heat exchangers that determine inlet temperature to expanders are more significant. ► Limiting values of nondimensional UA for each heat exchanger have been determined. ► Extra area distributed such that effectiveness of all heat exchangers increase uniformly. ► Heat exchanger performance variation have little influence on the optimum expander flow. - Abstract: Energy efficiency of large-scale helium liquefiers generally employed in fusion reactors and accelerators is determined by the performance of their constituting components. Simulation with Aspen HYSYS ® V7.0, a commercial process simulator, helps to understand the effects of heat exchanger parameters on the performance of a helium liquefier. Effective UA (product of overall heat transfer coefficient U, heat transfer surface area A and deterioration factor F) has been taken as an independent parameter, which takes into account all thermal irreversibilities and configuration effects. Nondimensionalization of parameters makes the results applicable to plants of any capacity. Rate of liquefaction is found to increase linearly with the effectiveness of heat exchangers. Performance of those heat exchangers that determine the inlet temperatures to expanders have more influence on the liquid production. Variation of sizes of heat exchangers does not affect the optimum rate of flow through expanders. Increasing UA improves the rate of liquid production; however, the improvement saturates at limiting UA. Maximum benefit in liquefaction is obtained when the available heat transfer surface area is distributed in such a way that the effectiveness remains equal for all heat exchangers. Conclusions from this study may be utilized in analyzing and designing large helium plants.

  14. STUDY OF SOLVENT AND CATALYST INTERACTIONS IN DIRECT COAL LIQUEFACTION; FINAL

    International Nuclear Information System (INIS)

    Michael T. Klein; William H. Calkins; Jasna Tomic

    2000-01-01

    To provide a better understanding of the roles of a solid catalyst and the solvent in Direct Coal Liquefaction, a small reactor was equipped with a porous-walled basket which was permeable to the solvent but was not permeable to the coal or solid catalyst. With this equipment and a high volatile bituminous coal it was found that direct contact between the catalyst in the basket and the coal outside the basket is not required for catalyzed coal liquefaction. The character of the solvent in this system makes a significant difference in the conversion of the coal, the better solvents being strong donor solvents. Because of the extensive use of thermogravimetric analysis in this laboratory, it was noted that the peak temperature for volatiles evolution from coal was a reliable measure of coal rank. Because of this observation, a variety of coals of a range of ranks was investigated. It was shown in this work that measuring the peak temperature for volatiles evolution was a quite precise indicator of rank and correlated closely with the rank value obtained by measuring vitrinite reflectance, a more difficult measurement to make. This prompted the desire to know the composition of the volatile material evolved as a function of coal rank. This was then measured by coupling a TGA to a mass spectrometer using laser activation and photoionization detection TG-PI-MS. The predominant species in volatiles of low rank coal turned out to be phenols with some alkenes. As the rank increases, the relative amounts of alkene and aromatic hydrocarbons increases and the oxygenated species decrease. It was shown that these volatiles were actually pyrolytic products and not volatilization products of the coal. Solvent extraction experiments coupled with Thermogravimetric-photoionization-mass spectrometry (TG-PI-MS) indicated that the low boiling and more extractable material are essentially similar in chemical types to the non-extractable portions but apparently higher molecular weight

  15. Hydrothermal liquefaction of agricultural and forestry wastes: state-of-the-art review and future prospects.

    Science.gov (United States)

    Cao, Leichang; Zhang, Cheng; Chen, Huihui; Tsang, Daniel C W; Luo, Gang; Zhang, Shicheng; Chen, Jianmin

    2017-12-01

    Hydrothermal liquefaction has been widely applied to obtain bioenergy and high-value chemicals from biomass in the presence of a solvent at moderate to high temperature (200-550°C) and pressure (5-25MPa). This article summarizes and discusses the conversion of agricultural and forestry wastes by hydrothermal liquefaction. The history and development of hydrothermal liquefaction technology for lignocellulosic biomass are briefly introduced. The research status in hydrothermal liquefaction of agricultural and forestry wastes is critically reviewed, particularly for the effects of liquefaction conditions on bio-oil yield and the decomposition mechanisms of main components in biomass. The limitations of hydrothermal liquefaction of agricultural and forestry wastes are discussed, and future research priorities are proposed. Copyright © 2017 Elsevier Ltd. All rights reserved.

  16. Grain boundary sweeping and liquefaction-induced fission product behavior in nuclear fuel under severe-core damage accident conditions

    International Nuclear Information System (INIS)

    Rest, J.

    1984-05-01

    The theoretical FASTGRASS-VFP model has been used in the interpretation of fission gas, iodine, tellurium, and cesium release from: (1) irradiated high-burnup LWR fuel in a flowing steam atmosphere during high-temperature, in-cell heating tests performed at Oak Ridge National Laboratory; and (2) trace-irradiated and high-burnup LWR fuel during severe-fuel-damage (SFD) tests performed in the PBF reactor in Idaho. A theory of grain boundary sweeping of gas bubbles, gas bubble behavior during fuel liquefaction (destruction of grain boundaries due to formation of a U-rich melt phase), and U-Zr eutectic melting has been included within the FASTGRASS-VFP formalism. Results of the analyses demonstrate that intragranular fission product behavior during both types of tests can be interpreted in terms of a grain-growth/grain-boundary-sweeping mechanism that enhances the flow of fission products from within the grains to the grain boundaries. Whereas fuel liquefaction leads to an enhanced release of fission products in trace-irradiated fuel, the occurrence of fuel liquefaction in high-burnup fuel can degrade fission product release. This phenomenon is due in part to reduced gas-bubble mobilities in a viscous medium as compared to vapor transport, and in part to a degradation of grain growth rates and the subsequent decrease in grain-boundary sweeping of intragranular fission products into the liquefied lamina. The analysis shows that total UO 2 dissolution due to eutectic melting leads to increased release for both trace-irradiated and high-burnup fuel. The FASTGRASS-VFP predictions, measured release rates from the above tests, and previously published release rates are compared and differences between fission product behavior in trace-irradiated and in high-burnup fuel are highlighted

  17. Post-liquefaction soil-structure interaction for buried structures: Sensitivity analysis studies

    International Nuclear Information System (INIS)

    Pires, J.A.; Ang, H.S.; Katayama, I.; Satoh, M.

    1993-01-01

    The post liquefaction behavior of buried conduits is analyzed and sensitivity analysis is conducted to investigate the damage potential of the forces induced in the buried lifelines following seismically induced liquefaction of the surrounding soil. Various lifeline configurations and loading conditions are considered. The loading conditions considered are: buoyancy forces and permanent ground displacements parallel to the lifeline axis. Pertinent parameters for the soil-lifeline interaction following liquefaction are identified. (author)

  18. Inhibitors degradation and microbial response during continuous anaerobic conversion of hydrothermal liquefaction wastewater.

    Science.gov (United States)

    Si, Buchun; Li, Jiaming; Zhu, Zhangbing; Shen, Mengmeng; Lu, Jianwen; Duan, Na; Zhang, Yuanhui; Liao, Qiang; Huang, Yun; Liu, Zhidan

    2018-07-15

    One critical challenge of hydrothermal liquefaction (HTL) is its complex aqueous product, which has a high concentration of organic pollutants (up to 100gCOD/L) and diverse fermentation inhibitors, such as furfural, phenolics and N-heterocyclic compounds. Here we report continuous anaerobic digestion of HTL wastewater via an up-flow anaerobic sludge bed reactor (UASB) and packed bed reactor (PBR). Specifically, we investigated the transformation of fermentation inhibitors and microbial response. GC-MS identified the complete degradation of furfural and 5-hydroxymethylfurfural (5-HMF), and partial degradation (54.0-74.6%) of organic nitrogen and phenolic compounds, including 3-hydroxypyridine, phenol and 4-ethyl-phenol. Illumina MiSeq sequencing revealed that the bacteria families related to detoxification increased in response to the HTL aqueous phase. In addition, the increase of acetate-oxidizing bacteria in UASB and acetogens in PBR showed a strengthened acetogenesis. As for the archaeal communities, an increase in hydrogenotrophic methanogens was observed. Based on GC-MS/HPLC and microbial analysis, we speculate that dominant fermentation inhibitors were transformed into intermediates (Acetyl-CoA and acetate), further contributing to biomethane formation. Copyright © 2018 Elsevier B.V. All rights reserved.

  19. Studies on the catalysts for coal liquefaction. ; Kinetic discussion in initial stage of coal liquefaction. Sekitan ekikayo shokubai ni kansuru kenkyu. ; Sekitan ekika shoki dankai no sokudoronteki kosatsu

    Energy Technology Data Exchange (ETDEWEB)

    Muraoka, T; Ikenaga, N; Oda, H; Yokokawa, C [Kansai University, Osaka (Japan). Faculty of Engineering

    1990-11-29

    Discussions were given on features of various kinds of coal liquefaction catalysts exhibited by them in hydrocracking of coal (Taiheiyo coal), and particularly on selectivity of the reaction in its initial stage. Four kinds of catalysts were tested: Adkins catalyst which is an oxide of copper and chromium, Fe2O3+S, Mo-TiO2 and MoS3-Al2O3. Three grams of coal and 0.3 gram each of the catalysts were charged into an autoclave reactor and experiment was conducted under an initial hydrogen pressure of 10 MPa, temperatures from 653 K to 693 K and for durations of 0 to 120 minutes to derive apparent reaction rate constants. The MoS3-Al2O3 catalyst has promoting the reaction apparently in the primary reaction at any temperature, while the other catalysts had the rate constants varied in the initial and the later stages. It was recognized that the temperature dependence of rate constants varies considerably according to the types of catalyst. Particularly the MoO3-TiO3 catalyst has small temperature dependence in the rate constants, and high molecular weight reducing power. 3 refs., 4 figs., 3 tabs.

  20. Reactor container

    International Nuclear Information System (INIS)

    Kato, Masami; Nishio, Masahide.

    1987-01-01

    Purpose: To prevent the rupture of the dry well even when the melted reactor core drops into a reactor pedestal cavity. Constitution: In a reactor container in which a dry well disposed above the reactor pedestal cavity for containing the reactor pressure vessel and a torus type suppression chamber for containing pressure suppression water are connected with each other, the pedestal cavity and the suppression chamber are disposed such that the flow level of the pedestal cavity is lower than the level of the pressure suppression water. Further, a pressure suppression water introduction pipeway for introducing the pressure suppression water into the reactor pedestal cavity is disposed by way of an ON-OFF valve. In case if the melted reactor core should fall into the pedestal cavity, the ON-OFF valve for the pressure suppression water introduction pipeway is opened to introduce the pressure suppression water in the suppression chamber into the pedestal cavity to cool the melted reactor core. (Ikeda, J.)

  1. Nitrogen expander cycles for large capacity liquefaction of natural gas

    Energy Technology Data Exchange (ETDEWEB)

    Chang, Ho-Myung; Park, Jae Hoon; Gwak, Kyung Hyun [Hong Ik University, Department of Mechanical Engineering, Seoul, 121-791 (Korea, Republic of); Choe, Kun Hyung [Korea Gas Corporation, Incheon, 406-130 (Korea, Republic of)

    2014-01-29

    Thermodynamic study is performed on nitrogen expander cycles for large capacity liquefaction of natural gas. In order to substantially increase the capacity, a Brayton refrigeration cycle with nitrogen expander was recently added to the cold end of the reputable propane pre-cooled mixed-refrigerant (C3-MR) process. Similar modifications with a nitrogen expander cycle are extensively investigated on a variety of cycle configurations. The existing and modified cycles are simulated with commercial process software (Aspen HYSYS) based on selected specifications. The results are compared in terms of thermodynamic efficiency, liquefaction capacity, and estimated size of heat exchangers. The combination of C3-MR with partial regeneration and pre-cooling of nitrogen expander cycle is recommended to have a great potential for high efficiency and large capacity.

  2. Nitrogen expander cycles for large capacity liquefaction of natural gas

    Science.gov (United States)

    Chang, Ho-Myung; Park, Jae Hoon; Gwak, Kyung Hyun; Choe, Kun Hyung

    2014-01-01

    Thermodynamic study is performed on nitrogen expander cycles for large capacity liquefaction of natural gas. In order to substantially increase the capacity, a Brayton refrigeration cycle with nitrogen expander was recently added to the cold end of the reputable propane pre-cooled mixed-refrigerant (C3-MR) process. Similar modifications with a nitrogen expander cycle are extensively investigated on a variety of cycle configurations. The existing and modified cycles are simulated with commercial process software (Aspen HYSYS) based on selected specifications. The results are compared in terms of thermodynamic efficiency, liquefaction capacity, and estimated size of heat exchangers. The combination of C3-MR with partial regeneration and pre-cooling of nitrogen expander cycle is recommended to have a great potential for high efficiency and large capacity.

  3. Nitrogen expander cycles for large capacity liquefaction of natural gas

    International Nuclear Information System (INIS)

    Chang, Ho-Myung; Park, Jae Hoon; Gwak, Kyung Hyun; Choe, Kun Hyung

    2014-01-01

    Thermodynamic study is performed on nitrogen expander cycles for large capacity liquefaction of natural gas. In order to substantially increase the capacity, a Brayton refrigeration cycle with nitrogen expander was recently added to the cold end of the reputable propane pre-cooled mixed-refrigerant (C3-MR) process. Similar modifications with a nitrogen expander cycle are extensively investigated on a variety of cycle configurations. The existing and modified cycles are simulated with commercial process software (Aspen HYSYS) based on selected specifications. The results are compared in terms of thermodynamic efficiency, liquefaction capacity, and estimated size of heat exchangers. The combination of C3-MR with partial regeneration and pre-cooling of nitrogen expander cycle is recommended to have a great potential for high efficiency and large capacity

  4. Thermodynamic design of natural gas liquefaction cycles for offshore application

    Science.gov (United States)

    Chang, Ho-Myung; Lim, Hye Su; Choe, Kun Hyung

    2014-09-01

    A thermodynamic study is carried out for natural gas liquefaction cycles applicable to offshore floating plants, as partial efforts of an ongoing governmental project in Korea. For offshore liquefaction, the most suitable cycle may be different from the on-land LNG processes under operation, because compactness and simple operation are important as well as thermodynamic efficiency. As a turbine-based cycle, closed Claude cycle is proposed to use NG (natural gas) itself as refrigerant. The optimal condition for NG Claude cycle is determined with a process simulator (Aspen HYSYS), and the results are compared with fully-developed C3-MR (propane pre-cooled mixed refrigerant) JT cycles and various N2 (nitrogen) Brayton cycles in terms of efficiency and compactness. The newly proposed NG Claude cycle could be a good candidate for offshore LNG processes.

  5. Direct liquefaction of low-rank coals under mild conditions

    Energy Technology Data Exchange (ETDEWEB)

    Braun, N.; Rinaldi, R. [Max-Planck-Institut fuer Kohlenforschung, Muelheim an der Ruhr (Germany)

    2013-11-01

    Due to decreasing of petroleum reserves, direct coal liquefaction is attracting renewed interest as an alternative process to produce liquid fuels. The combination of hydrogen peroxide and coal is not a new one. In the early 1980, Vasilakos and Clinton described a procedure for desulfurization by leaching coal with solutions of sulphuric acid/H{sub 2}O{sub 2}. But so far, H{sub 2}O{sub 2} has never been ascribed a major role in coal liquefaction. Herein, we describe a novel approach for liquefying low-rank coals using a solution of H{sub 2}O{sub 2} in presence of a soluble non-transition metal catalyst. (orig.)

  6. Characteristics estimation of coal liquefaction residue; Sekitan ekika zansa seijo no suisan ni kansuru kento

    Energy Technology Data Exchange (ETDEWEB)

    Itonaga, M.; Imada, K. [Nippon Steel Corp., Tokyo (Japan); Okada, Y.; Inokuchi, K. [Mitsui SRC Development Co. Ltd., Tokyo (Japan)

    1996-10-28

    The paper studied a possibility of estimating characteristics of coal liquefaction residue from liquefaction conditions in the case of fixing coal kind in the NEDOL process coal liquefaction PSU. Wyoming coal was used for the study, and the already proposed simplified liquefaction reaction models were used. Among material balances explained by the models, those of asphaltene, preasphaltene, THF insoluble matters are concerned with residue composition. Ash content is separately calculated from ash balance. Reaction velocity constants of simplified liquefaction reaction models which influence the residue composition were obtained by the multiple regression method from experimental results in the past. The estimation expression of residue viscosity was introduced from residue ash/composition. When the residue composition is estimated by the model from liquefaction conditions, and the residue viscosity is obtained using it, the higher the liquefaction temperature is, the higher the residue viscosity is. The result obtained well agreed the measuring result. The simplified liquefaction model of a certain coal kind has been established, and characteristics of residue can be estimated even at liquefaction conditions which have never been experienced before if there is a certain amount of the accumulated data on residue composition/characteristics. 4 refs., 4 figs., 4 tabs.

  7. Japan's New Sunshine Project. 1994 annual summary of coal liquefaction and gasification

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1995-08-01

    This paper summarizes the report for fiscal 1994 on research and development related to coal liquefaction and gasification. In the research and development of coal liquefaction technologies, reports were given on research of liquefaction characteristics of different coals and liquefaction process thereof, and on research of catalysts for the coal liquefaction. In the research and development of coal gasification technologies, reports were given on fundamental studies on gasification characteristics of different coals. In the research and development of liquefaction technologies for bituminous coal, reports were given on design, construction and operation of a bituminous coal liquefaction pilot plant with a capacity of 150 t/d, and the operation supporting studies on the pilot plant. In the fundamental research on the coal liquefaction process, reports were given on refining technologies and utilization of the refined materials, and studies on environment preservation in applying the coal liquefaction technologies. In the research on hydrogen manufacturing technologies by using the fundamental coal technology, reports were given on design, construction and operational studies of a pilot plant. In the research and development of the coal gasification technologies, reports were given on development of a jet-flow gasified coal electric power plant, selection of coals, and development of a data processing system. (NEDO)

  8. FY 1992 report on the Coal Liquefaction Committee; 1992 nendo sekitan ekika iinkai hokokusho

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1993-03-01

    The paper reported activities of the Coal Liquefaction Committee in FY 1992. In the 1st committee meeting, report/discussion were made of the summary of the FY 1992 R and D plan on the bituminous coal liquefaction, brown coal liquefaction and the common/basic technology. Further, the following were reported as topics: results of the operation by bituminous coal liquefaction PSU and small equipment, state of arrangement of the results of the brown coal liquefaction project, making of the basic policy for development of the common/basic technology, construction of package of coal liquefaction technology. In the 2nd committee meeting, the summary of the results of the FY 1992 R and D was reported/discussed. As to the development of bituminous coal liquefaction technology, study using pilot plant and support study were reported. Concerning the development of brown coal liquefaction technology, study using a 50t/d pilot plant and complementary study of operation. Relating to the development of the common/basic technology, trial manufacture/development of plant equipment/materials, survey of selection of coal kind, etc. The paper also reported a scheme on the evaluation of efficiency of the brown coal liquefaction process. (NEDO)

  9. Japan's New Sunshine Project. 1994 annual summary of coal liquefaction and gasification

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1995-08-01

    This paper summarizes the report for fiscal 1994 on research and development related to coal liquefaction and gasification. In the research and development of coal liquefaction technologies, reports were given on research of liquefaction characteristics of different coals and liquefaction process thereof, and on research of catalysts for the coal liquefaction. In the research and development of coal gasification technologies, reports were given on fundamental studies on gasification characteristics of different coals. In the research and development of liquefaction technologies for bituminous coal, reports were given on design, construction and operation of a bituminous coal liquefaction pilot plant with a capacity of 150 t/d, and the operation supporting studies on the pilot plant. In the fundamental research on the coal liquefaction process, reports were given on refining technologies and utilization of the refined materials, and studies on environment preservation in applying the coal liquefaction technologies. In the research on hydrogen manufacturing technologies by using the fundamental coal technology, reports were given on design, construction and operational studies of a pilot plant. In the research and development of the coal gasification technologies, reports were given on development of a jet-flow gasified coal electric power plant, selection of coals, and development of a data processing system. (NEDO)

  10. The making of Andersen’s liquefaction chart

    OpenAIRE

    Sabaliauskas, Tomas; Ibsen, Lars Bo

    2017-01-01

    Andersen’s chart (Andersen & Berre, 1999) is a graphical method of observing cyclic soil response. It allows observing soil response to various stress amplitudes that can lead to liquefaction, excess plastic deformation stabilizing soil response.The process of obtaining the original chart has been improved. Algorithm based approximation is introduced. Pore pressure dependent ultimate bearing capacity normalization factor is introduced to normalize the chart.

  11. The current status of coal liquefaction technologies - Panorama 2008

    International Nuclear Information System (INIS)

    2008-01-01

    In 2008, a first coal liquefaction unit to produce motor fuel (20,000 BPSD) will come on-stream in Shenhua, China (in the Ercos region of Inner Mongolia). Other, more ambitious projects have been announced in China for between now and 2020. Since oil production is expected to peak in the medium term, this technology may develop regionally in the next 20 years to cover ever-increasing demand for motor fuel

  12. New magnetic refrigeration materials for the liquefaction of hydrogen

    International Nuclear Information System (INIS)

    Gschneidner, K.A.; Takeya, H.; Moorman, J.O.; Pecharsky, V.K.; Malik, S.K.; Zimm, C.B.

    1994-01-01

    Five heavy lanthanide ferromagnetic intermetallic compounds were studied as potential magnetic refrigerants for the liquefaction of hydrogen gas. (Dy 0.5 Er 0.5 )Al 2 and TbNi 2 appear to be better refrigerants than GdPd for a Joule-Brayton cycle refrigerator, while (Gd 0.54 Er 0.46 )AlNi seems to be a suitable refrigerant for an Ericsson cycle refrigerator

  13. A Characterization and Evaluation of Coal Liquefaction Process Streams

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1998-10-01

    An updated assessment of the physico-chemical analytical methodology applicable to coal-liquefaction product streams and a review of the literature dealing with the modeling of fossil-fuel resid conversion to product oils are presented in this document. In addition, a summary is provided for the University of Delaware program conducted under this contract to develop an empirical test to determine relative resid reactivity and to construct a computer model to describe resid structure and predict reactivity.

  14. Machine learning modelling for predicting soil liquefaction susceptibility

    Directory of Open Access Journals (Sweden)

    P. Samui

    2011-01-01

    Full Text Available This study describes two machine learning techniques applied to predict liquefaction susceptibility of soil based on the standard penetration test (SPT data from the 1999 Chi-Chi, Taiwan earthquake. The first machine learning technique which uses Artificial Neural Network (ANN based on multi-layer perceptions (MLP that are trained with Levenberg-Marquardt backpropagation algorithm. The second machine learning technique uses the Support Vector machine (SVM that is firmly based on the theory of statistical learning theory, uses classification technique. ANN and SVM have been developed to predict liquefaction susceptibility using corrected SPT [(N160] and cyclic stress ratio (CSR. Further, an attempt has been made to simplify the models, requiring only the two parameters [(N160 and peck ground acceleration (amax/g], for the prediction of liquefaction susceptibility. The developed ANN and SVM models have also been applied to different case histories available globally. The paper also highlights the capability of the SVM over the ANN models.

  15. Solvent recyclability in a multistep direct liquefaction process

    Energy Technology Data Exchange (ETDEWEB)

    Hetland, M.D.; Rindt, J.R. [Univ. of North Dakota, Grand Forks, ND (United States)

    1995-12-31

    Direct liquefaction research at the Energy & Environmental Research Center (EERC) has, for a number of years, concentrated on developing a direct liquefaction process specifically for low-rank coals (LRCs) through the use of hydrogen-donating solvents and solvents similar to coal-derived liquids, the water/gas shift reaction, and lower-severity reaction conditions. The underlying assumption of all of the research was that advantage could be taken of the reactivity and specific qualities of LRCs to produce a tetrahydrofuran (THF)-soluble material that might be easier to upgrade than the soluble residuum produced during direct liquefaction of high-rank coals. A multistep approach was taken to produce the THF-soluble material, consisting of (1) preconversion treatment to prepare the coal for solubilization, (2) solubilization of the coal in the solvent, and (3) polishing to complete solubilization of the remaining material. The product of these three steps can then be upgraded during a traditional hydrotreatment step. The results of the EERC`s research indicated that additional studies to develop this process more fully were justified. Two areas were targeted for further research: (1) determination of the recyclability of the solvent used during solubilization and (2) determination of the minimum severity required for hydrotreatment of the liquid product. The current project was funded to investigate these two areas.

  16. Technology for advanced liquefaction processes: Coal/waste coprocessing studies

    Energy Technology Data Exchange (ETDEWEB)

    Cugini, A.V.; Rothenberger, K.S.; Ciocco, M.V. [Pittsburgh Energy Technology Center, PA (United States)] [and others

    1995-12-31

    The efforts in this project are directed toward three areas: (1) novel catalyst (supported and unsupported) research and development, (2) study and optimization of major operating parameters (specifically pressure), and (3) coal/waste coprocessing. The novel catalyst research and development activity has involved testing supported catalysts, dispersed catalysts, and use of catalyst testing units to investigate the effects of operating parameters (the second area) with both supported and unsupported catalysts. Several supported catalysts were tested in a simulated first stage coal liquefaction application at 404{degrees}C during this performance period. A Ni-Mo hydrous titanate catalyst on an Amocat support prepared by Sandia National laboratories was tested. Other baseline experiments using AO-60 and Amocat, both Ni-Mo/Al{sub 2}O{sub 3} supported catalysts, were also made. These experiments were short duration (approximately 12 days) and monitored the initial activity of the catalysts. The results of these tests indicate that the Sandia catalyst performed as well as the commercially prepared catalysts. Future tests are planned with other Sandia preparations. The dispersed catalysts tested include sulfated iron oxide, Bayferrox iron oxide (iron oxide from Miles, Inc.), and Bailey iron oxide (micronized iron oxide from Bailey, Inc.). The effects of space velocity, temperature, and solvent-to-coal ratio on coal liquefaction activity with the dispersed catalysts were investigated. A comparison of the coal liquefaction activity of these catalysts relative to iron catalysts tested earlier, including FeOOH-impregnated coal, was made. These studies are discussed.

  17. STUDY OF SOLVENT AND CATALYST INTERACTIONS IN DIRECT COAL LIQUEFACTION; SEMIANNUAL

    International Nuclear Information System (INIS)

    Michael T. Klein

    2000-01-01

    There are several aspects of the Direct Coal Liquefaction process which are not fully understood and which if better understood might lead to improved yields and conversions. Among these questions are the roles of the catalyst and the solvent. While the solvent is known to act by transfer of hydrogen atoms to the free radicals formed by thermal breakdown of the coal in an uncatalyzed system, in the presence of a solid catalyst as is now currently practiced, the yields and conversions are higher than in an uncatalyzed system. The role of the catalyst in this case is not completely understood. DOE has funded many projects to produce ultrafine and more active catalysts in the expectation that better contact between catalyst and coal might result. This approach has met with limited success probably because mass transfer between two solids in a fluid medium i.e. the catalyst and the coal, is very poor. It is to develop an understanding of the role of the catalyst and solvent in Direct Liquefaction that this project was initiated. Specifically it was of interest to know whether direct contact between the coal and the catalyst was important. By separating the solid catalyst in a stainless steel basket permeable to the solvent but not the coal in the liquefaction reactor, it was shown that the catalyst still maintains a catalytic effect on the liquefaction process. There is apparently transfer of hydrogen atoms from the catalyst through the basket wall to the coal via the solvent. Strong hydrogen donor solvents appear to be more effective in this respect than weak hydrogen donors. It therefore appears that intimate contact between catalyst and coal is not a requirement, and that the role of the catalyst may be to restore the hydrogen donor strength to the solvent as the reaction proceeds. A range of solvents of varying hydrogen donor strength was investigated. Because of the extensive use of thermogravimetric analysis in this laboratory in was noted that the peak

  18. Report on the brown coal liquefaction sub-committee in fiscal 1992; 1992 nendo kattan ekika bukai hokokusho

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1993-03-01

    This paper reports the activities of the brown coal liquefaction sub-committee in fiscal 1992. The first sub-committee meeting presented an interim report on the status of progress in complementary researches in fiscal 1992. The report covers the following items: discussions on effects of reaction factors on scale deposition in a preheater and a reactor and the liquefaction oil yield, supplementary experiments to enhance recovery rate of naphtha from under-flow in the de-ashing system and enhance accuracy of expression to estimate the interface precipitation velocity, and discussions on product oil types and catalyst types. The second sub-committee meeting reported fundamental discussions on the primary hydrogenation and hot water treatment of brown coal as an interim report on the achievements, and discussions on de-ashing and catalyst properties, liquefying reaction activity and scaling performance of catalysts. The third meeting reported the support on compiling the achievements by means of collecting complementary data of the pilot plant using PDU. A 7,800-hour life verification test was completed on the fixed bed secondary hydrogenation catalyst. A method was established to recover naphtha from the under-flow in a de-ashing settler. An expression to estimate the interface precipitation velocity was also established. Affirmation was made on the pylite catalyst performance, and reactivity of the category A coal assumed in the demonstration device. (NEDO)

  19. Post-cyclic behavior of low plasticity silt under full and limited liquefaction using triaxial compression testing.

    Science.gov (United States)

    2010-02-01

    During an earthquake, liquefaction does not happen all the time. It depends on the duration and magnitude of the earthquake and the properties (with relationship to resistance of liquefaction) of the low plasticity silt. Under low duration or magnitu...

  20. Comparative study on liquefaction of creosote and chromated copper arsenate (CCA)-treated wood and untreated southern pine wood: effects of acid catalyst content, liquefaction time, temperature, and phenol to wood ratio

    Science.gov (United States)

    Hui Pan; Chung-Yun Hse; Todd F. Shupe

    2009-01-01

    Creosote- and chromated copper arsenate (CCA)-treated wood waste and untreated southern pine wood were liquefied with phenol and sulfuric acid. The effects of sulfuric acid content, liquefaction time, liquefaction temperature, and phenol to wood ratio on liquefaction rate (i.e., wood residue content) were investigated and analyzed by analysis of variance (...

  1. Nuclear reactor shutdown system

    International Nuclear Information System (INIS)

    Mangus, J.D.; Cooper, M.H.

    1982-01-01

    An improved nuclear reactor shutdown system is described comprising a temperature sensitive device connected to control the electric power supply to a magnetic latch holding a body of a neutron absorbing material. The temperature sensitive device is exposed to the reactor coolant so that when the reactor coolant temperature rises above a specific level, the temperature sensitive device will cause deenergization of the magnetic latch to allow the body of neutron absorbing material to enter the reactor core. (author)

  2. BP and NCB to collaborate in coal liquefaction study. [Supercritical gas extraction; dissolution in anthracene oil

    Energy Technology Data Exchange (ETDEWEB)

    1978-02-17

    British Petroleum and NCB are collaborating in a two year study of coal liquefaction which could result in a demonstration plant being built. The two liquefaction techniques which the NCB is developing at present are supercritical extraction, and dissolution in anthracene oil. A disadvantage of the latter process is that high grade coking coals must be used.

  3. Japan`s sunshine project. 17.. 1992 annual summary of coal liquefaction and gasification

    Energy Technology Data Exchange (ETDEWEB)

    1993-09-01

    This report describes the achievement of coal liquefaction and gasification technology development in the Sunshine Project for FY 1992. It presents the research and development of coal liquefaction which includes studies on reaction mechanism of coal liquefaction and catalysts for coal liquefaction, the research and development of coal gasification technologies which includes studies on gasification characteristics of various coals and improvement of coal gasification efficiency, the development of bituminous coal liquefaction which includes engineering, construction and operation of a bituminous coal liquefaction pilot plant and research by a process supporting unit (PSU), the development of brown coal liquefaction which includes research on brown coal liquefaction with a pilot plant and development of techniques for upgrading coal oil from brown coal, the development of common base technologies which includes development of slurry letdown valves and study on upgrading technology of coal-derived distillates, the development of coal-based hydrogen production technology with a pilot plant, the development of technology for entrained flow coal gasification, the assessment of coal hydrogasification, and the international co-operation. 4 refs., 125 figs., 39 tabs.

  4. Renewable chemical feedstocks from integrated liquefaction processing of lingocellulosic materials using microwave energy

    Science.gov (United States)

    Junming Xu; Jianchun Jiang; Chung-Yun Hse; Todd F. Shupe

    2012-01-01

    The objective of this investigation was to find a simple method for the production of phenolic rich products and sugar derivatives (biopolyols) via separation of liquefied lingocellulosic materials. Liquefaction of lignocellulosic materials was conducted in methanol at 180 °C for 15 min with the conversion of raw materials at about 75%. After liquefaction, the...

  5. Design, synthesis, and characterization of novel fine-particle, unsupported catalysts for coal liquefaction

    Energy Technology Data Exchange (ETDEWEB)

    Klein, M.T.

    1991-12-30

    The purpose of this work is to investigate the kinetics-assisted design, synthesis and characterization of fme-pardcle, unsupported catalysts for coal liquefaction. The goal is to develop a fundamental understanding of coal catalysis and catalysts that will, in turn, allow for the specification of a novel optimal catalyst for coal liquefaction.

  6. Influence of solvent type on microwave-assisted liquefaction of bamboo

    Science.gov (United States)

    Jiulong Xie; Chung Hse; Todd F. Shupe; Tingxing Hu

    2016-01-01

    Microwave-assisted liquefaction of bamboo in glycerol, polyethylene glycerol (PEG), methanol, ethanol, and water were comparatively investigated by evaluating the temperature-dependence for conversion and liquefied residue characteristics. The conversion for the liquefaction in methanol, ethanol, and water increased with an increase in reaction temperature, while that...

  7. Dynamic dielectric properties of a wood liquefaction system using polyethylene glycol and glycerol

    Science.gov (United States)

    Mengchao Zhou; Thomas L. Eberhardt; Bo Cai; Chung-Yun Hse; Hui Pan

    2017-01-01

    Microwave-assisted liquefaction has shown potential for rapid thermal processing of lignocellulosic biomass. The efficiency of microwave heating depends largely on the dielectric properties of the materials being heated. The objective of this study was to investigate the dynamic interactions between microwave energy and the reaction system during the liquefaction of a...

  8. Evaluation of soil liquefaction potential for level ground during earthquakes. A summary report

    International Nuclear Information System (INIS)

    Seed, H.B.; Arango, I.; Chan, C.K.

    1975-10-01

    The results of a three-year research program conducted to investigate the settlement and liquefaction of sands under multi-directional shaking are evaluated. The investigation indicated that the behavior of a saturated sand under cyclic loading conditions is a function of its geologic and seismic history and grain structure as well as its placement density. It is concluded that the resistance to liquefaction of a sand deposit can best be estimated by laboratory testing on undisturbed samples. It is shown that cyclic triaxial tests used in conjunction with appropriate correction factors to account for multi-directional shaking, simple shear loading conditions, and overconsolidation effects can provide valid data on cyclic loading characteristics. The concepts of ''limited strain potential'' and acceptable value of the factor of safety against initial liquefaction are introduced. Finally, the two basic methods for evaluating liquefaction potential and the effects of liquefaction are reviewed and updated with the information obtained through this research effort

  9. Kinetics of coal liquefaction during heating-up and isothermal stages

    Energy Technology Data Exchange (ETDEWEB)

    Xian Li; Haoquan Hu; Shengwei Zhu; Shuxun Hu; Bo Wu; Meng Meng [Dalian University of Technology, Dalian (China). Institute of Coal Chemical Engineering

    2008-04-15

    Direct liquefaction of Shenhua bituminous coal was carried out in a 500 ml autoclave with iron catalyst and coal liquefaction cycle-oil as solvent at initial hydrogen of 8.0 MPa, residence time of 0-90 min. To investigate the liquefaction kinetics, a model for heating-up and isothermal stages was developed to estimate the rate constants of both stages. In the model, the coal was divided into three parts, easy reactive part, hard reactive part and unreactive part, and four kinetic constants were used to describe the reaction mechanism. The results showed that the model is valid for both heating-up and isothermal stages of liquefaction perfectly. The rate-controlled process for coal liquefaction is the reaction of preasphaltene plus asphaltene (PAA) to oil plus gas (O + G). The upper-limiting conversion of isothermal stage was estimated by the kinetic calculation. 21 refs., 4 figs., 4 tabs.

  10. Seismic response of nuclear reactors in layered liquefiable soil deposits including nonlinear soil-structure interaction

    International Nuclear Information System (INIS)

    Zaman, M.; Mamoon, S.M.

    1989-01-01

    Analysis of seismic response of structures located at a site with potential for soil liquefaction has drawn attention of many researchers. The topic is particularly important in the design of critical facilities like nuclear reactors and defense installations. This paper presents the results of a study involving evaluation of coupled seismic response of structures (model nuclear reactors) and characteristics of soil liquefaction at a site. The analysis procedure employed is based on the nonlinear finite element (FE) technique and accounts for the interaction effects due to a neighboring structure. Emphasis is given to the following features: prediction of spatial and temporal variation of pore water pressure; identification of the on-set of liquefaction based on the effective stress approach, and tracing the propagation of the liquefied zones with time and resulting response of the structures

  11. Testing the ability of a proposed geotechnical based method to evaluate the liquefaction potential analysis subjected to earthquake vibrations

    Science.gov (United States)

    Abbaszadeh Shahri, A.; Behzadafshar, K.; Esfandiyari, B.; Rajablou, R.

    2010-12-01

    During the earthquakes a number of earth dams have had severe damages or suffered major displacements as a result of liquefaction, thus modeling by computer codes can provide a reliable tool to predict the response of the dam foundation against earthquakes. These modeling can be used in the design of new dams or safety assessments of existing ones. In this paper, on base of the field and laboratory tests and by combination of several software packages a seismic geotechnical based analysis procedure is proposed and verified by comparison with computer model tests, field and laboratory experiences. Verification or validation of the analyses relies to ability of the applied computer codes. By use of Silakhor earthquake (2006, Ms 6.1) and in order to check the efficiency of the proposed framework, the procedure is applied to the Korzan earth dam of Iran which is located in Hamedan Province to analyze and estimate the liquefaction and safety factor. Design and development of a computer code by authors which named as “Abbas Converter” with graphical user interface which operates as logic connecter function that can computes and models the soil profiles is the critical point of this study and the results are confirm and proved the ability of the generated computer code on evaluation of soil behavior under the earthquake excitations. Also this code can make and render facilitate this study more than previous have done, and take over the encountered problem.

  12. Coal liquefaction policy in China: Explaining the policy reversal since 2006

    International Nuclear Information System (INIS)

    Rong Fang; Victor, David G.

    2011-01-01

    China has emerged as a leader in coal liquefaction. While the country's abundant coal resources and acute concerns about oil security help explain China's interest in liquefaction, the driving forces for this industry are complicated and policy has been inconsistent. Since 2006 Beijing has tried to slow down the development of liquefaction; even as China has become more dependent on imported oil, the central government has been wary about the large impact of liquefaction technologies on scarce resources such as water. However, local government officials in coal rich areas have strong incentives to pour investment into the technology, which helps explain the uneven development and policy. The future of coal liquefaction will depend on how these forces unfold along with major Beijing-led reforms in the Chinese coal industry, which is closing smaller mines and favoring the emergence of larger coal producing firms. Those reforms will have mixed effects on liquefaction. They temporarily contribute to higher prices for coal while over the longer term creating coal companies that have much greater financial and technical skills needed to deploy technologies such as coal liquefaction at a scale needed if this energy pathway is to be competitive with conventional sources of liquid fuel. - Highlights: ► We explain swings in Chinese policy on coal liquefaction, a possible substitute for imported oil. ► Since 2006 Beijing's support has waned due to fears about environmental impacts and cost of liquefaction. ► Local governments in some coal rich regions remain strongly supportive. ► Volatile oil prices and rising coal prices make this industry more risky than previously thought. ► Consolidation of the coal industry will have mixed effects on viability of liquefaction projects.

  13. Probabilistic versus deterministic hazard assessment in liquefaction susceptible zones

    Science.gov (United States)

    Daminelli, Rosastella; Gerosa, Daniele; Marcellini, Alberto; Tento, Alberto

    2015-04-01

    Probabilistic seismic hazard assessment (PSHA), usually adopted in the framework of seismic codes redaction, is based on Poissonian description of the temporal occurrence, negative exponential distribution of magnitude and attenuation relationship with log-normal distribution of PGA or response spectrum. The main positive aspect of this approach stems into the fact that is presently a standard for the majority of countries, but there are weak points in particular regarding the physical description of the earthquake phenomenon. Factors like site effects, source characteristics like duration of the strong motion and directivity that could significantly influence the expected motion at the site are not taken into account by PSHA. Deterministic models can better evaluate the ground motion at a site from a physical point of view, but its prediction reliability depends on the degree of knowledge of the source, wave propagation and soil parameters. We compare these two approaches in selected sites affected by the May 2012 Emilia-Romagna and Lombardia earthquake, that caused widespread liquefaction phenomena unusually for magnitude less than 6. We focus on sites liquefiable because of their soil mechanical parameters and water table level. Our analysis shows that the choice between deterministic and probabilistic hazard analysis is strongly dependent on site conditions. The looser the soil and the higher the liquefaction potential, the more suitable is the deterministic approach. Source characteristics, in particular the duration of strong ground motion, have long since recognized as relevant to induce liquefaction; unfortunately a quantitative prediction of these parameters appears very unlikely, dramatically reducing the possibility of their adoption in hazard assessment. Last but not least, the economic factors are relevant in the choice of the approach. The case history of 2012 Emilia-Romagna and Lombardia earthquake, with an officially estimated cost of 6 billions

  14. Latent hazard related to a hydrogen liquefaction installation

    International Nuclear Information System (INIS)

    Spoendlin, R.

    1961-01-01

    In this note, the author reports an attempt of analysis of hazards which could be related to a hydrogen liquefaction installation in order to identify the most appropriate safety measures. In order to do so, experiments have been performed on electrostatic charges born by solid crystals in liquid hydrogen, and explosion tests have been performed on a mixture of solid oxygen and liquid hydrogen. Moreover, the author tried to analyse accidents which occurred in this field by performing a survey among scientists working in laboratories in different countries

  15. Ground Characterization Studies in Canakkale Pilot Site of LIQUEFACT Project

    Science.gov (United States)

    Ozcep, F.; Oztoprak, S.; Aysal, N.; Bozbey, I.; Tezel, O.; Ozer, C.; Sargin, S.; Bekin, E.; Almasraf, M.; Cengiz Cinku, M.; Ozdemir, K.

    2017-12-01

    The our aim is to outline the ground characterisation studies in Canakkale test site. Study is based on the EU H2020 LIQUEFACT project entitled "Liquefact: Assessment and mitigation of liquefaction potential across Europe: a holistic approach to protect structures / infrastructures for improved resilience to earthquake-induced liquefaction disasters". Objectives and extent of ground characterization for Canakkale test site includes pre-existing soil investigation studies and complementary field studies. There were several SPT and geophysical tests carried out in the study area. Within the context of the complementary tests, six (6) study areas in the test site were chosen and complementary tests were carried out in these areas. In these areas, additional boreholes were opened and SPT tests were performed. It was decided that additional CPT (CPTU and SCPT) and Marchetti Dilatometer (DMT) tests should be carried out within the scope of the complementary testing. Seismic refraction, MASW and micro tremor measurements had been carried out in pre-existing studies. Shear wave velocities obtained from MASW measurements were evaluated to the most rigorous level. These tests were downhole seismic, PS-logging, seismic refraction, 2D-ReMi, MASW, micro tremor (H/V Nakamura method), 2D resistivity and resonance acoustic profiling (RAP). RAP is a new technique which will be explained briefly in the relevant section. Dynamic soil properties had not been measured in pre-existing studies, therefore these properties were investigated within the scope of the complementary tests. Selection of specific experimental tests of the complementary campaign was based on cost-benefit considerations Within the context of complementary field studies, dynamic soil properties were measured using resonant column and cyclic direct shear tests. Several sieve analyses and Atterberg Limits tests which were documented in the pre-existing studies were evaluated. In the complementary study carried out

  16. Analysis of engineering cycles power, refrigerating and gas liquefaction plant

    CERN Document Server

    Haywood, R W

    1991-01-01

    Extensively revised, updated and expanded, the fourth edition of this popular text provides a rigorous analytical treatment of modern energy conversion plant. Notable for both its theoretical and practical treatment of conventional and nuclear power plant, and its studies of refrigerating and gas-liquefaction plant. This fourth edition now includes material on topics of increasing concern in the fields of energy 'saving' and reduction of environmental pollution. This increased coverage deals specifically with the following areas: CHP (cogeneration) plant, studies of both gas and coal burning p

  17. Liquefaction of Saturated Soil and the Diffusion Equation

    Science.gov (United States)

    Sawicki, Andrzej; Sławińska, Justyna

    2015-06-01

    The paper deals with the diffusion equation for pore water pressures with the source term, which is widely promoted in the marine engineering literature. It is shown that such an equation cannot be derived in a consistent way from the mass balance and the Darcy law. The shortcomings of the artificial source term are pointed out, including inconsistencies with experimental data. It is concluded that liquefaction and the preceding process of pore pressure generation and the weakening of the soil skeleton should be described by constitutive equations within the well-known framework of applied mechanics. Relevant references are provided

  18. Rationale for continuing R&D in indirect coal liquefaction

    Energy Technology Data Exchange (ETDEWEB)

    Gray, D.; Tomlinson, G. [MITRE Corp., McLean, VA (United States)

    1995-12-31

    The objective of this analysis is to use the world energy demand/supply model developed at MITRE to examine future liquid fuels supply scenarios both for the world and for the United States. This analysis has determined the probable extent of future oil resource shortages and the likely time frame in which the shortages will occur. The role that coal liquefaction could play in helping to alleviate this liquid fuels shortfall is also examined. The importance of continuing R&D to improve process performance and reduce the costs of coal-derived transportation fuel is quantified in terms of reducing the time when coal liquids will become competitive with petroleum.

  19. The Comparative Analysis of the Efficiency of Coal Liquefaction Technologies

    Directory of Open Access Journals (Sweden)

    Rudyka Viktor I.

    2017-12-01

    Full Text Available Organization of production of synthetic liquid fuels (SLF in Ukraine becomes an especially topical and at the same time complex scientific and applied task, taking into consideration criteria of the techno-ecological and economic rationality. The article presents a methodical approach to the comparative analysis of efficiency of the main methods and technologies for the synthetic liquid fuels production and a carried out testing, the results of which allowed to conclude that the most rational is the technology of indirect coal liquefaction based on coal thermal plasma gasification.

  20. Reactor containment

    International Nuclear Information System (INIS)

    Kawabe, Ryuhei; Yamaki, Rika.

    1990-01-01

    A water vessel is disposed and the gas phase portion of the water vessel is connected to a reactor container by a pipeline having a valve disposed at the midway thereof. A pipe in communication with external air is extended upwardly from the liquid phase portion to a considerable height so as to resist against the back pressure by a waterhead in the pipeline. Accordingly, when the pressure in the container is reduced to a negative level, air passes through the pipeline and uprises through the liquid phase portion in the water vessel in the form of bubbles and then flows into the reactor container. When the pressure inside of the reactor goes higher, since the liquid surface in the water vessel is forced down, water is pushed up into the pipeline. Since the waterhead pressure of a column of water in the pipeline and the pressure of the reactor container are well-balanced, gases in the reactor container are not leaked to the outside. Further, in a case if a great positive pressure is formed in the reactor container, the inner pressure overcomes the waterhead of the column of water, so that the gases containing radioactive aerosol uprise in the pipeline. Since water and the gases flow being in contact with each other, this can provide the effect of removing aerosol. (T.M.)

  1. Russian RERTR program as a part of Joint US DOE-RF MINATOM collaboration on elimination of the threat connected to the use of HEU in research reactors

    International Nuclear Information System (INIS)

    Arkhangelsky, N.

    2002-01-01

    The Russian RERTR Program started at the end of 70's, the final goal of the program is to eliminate supplies of HEU in fuel elements and assemblies for foreign research reactors that were designed according to Russian projects. Basic directions of the work include: completion of the development of the fuel elements and assemblies on a basis of uranium dioxide; development of the fuel on a basis of U-Mo alloy; and development of pin type fuel elements. Fuel assemblies of WWR-M2 type with LEU were developed and qualified for using in foreign research reactors that use such type of fuel assemblies. These assemblies are ready for the supplying several operating foreign research reactors. There are more than 20 sites in Eastern European countries, former Soviet republics and another countries that have big amount of Russian origin HEU in fresh and spent fuel. The problem of the shipment of SNF from sites of research reactors is also very important for domestic Russian research reactors. More than ten years from its beginning the Russian RERTR program developed practically independently from the international RERTR program and only at the begin of 90's the Russian specialists started to contact with foreign scientists and the exchange of the scientific information has become more intensive. In September 1994, representatives of Minatom and DOE signed a protocol of intent to reduce an enrichment of uranium in research reactors. The main aspects of collaboration involve: Several domestic Russian research reactors such as WWR-M, IR-8 and others were investigated from the point of view of possibility of reducing of enrichment; financial support of the program from US DOE which is insufficient. The important part of international collaboration is the import of Russian origin spent and fresh fuel of research reactors to Russia. In August 2002 an impressive result of the Russian-American collaboration with support of IAEA and with the help and assistance of Yugoslavian side was

  2. Direct liquefaction of wood through solvolysis and catalytic hydrodeoxygenation: an engineering assessment

    Energy Technology Data Exchange (ETDEWEB)

    Moffat, J.M.; Overend, J.P.

    1985-01-01

    Liquefaction of wood to produce fuel and chemical intermediates has been intensively studied over the last decade. The results of Canadian research into process feasibility are presented on the basis of two studies, the first in 1980 utilizing data of the mid-70s and the other on the basis of research conducted up to 1982. The earlier study was for a single reactor concept in which catalyst, wood and hydrogen were reacted to produce a proto-oil, while the later study embodies a two-stage concept involving dissolution of the polymer matrix followed by fractionation and catalytic upgrading using hydrodeoxygenation. Increased knowledge of the characteristics of the first stage products show that there are many component mixtures containing between 10 and 20% oxygen. Most of the oxygen is in aromatic phenol-type structures with some ether linkages, and low severity processes to deoxygenate the product while increasing the hydrogen to carbon ratio are called for. The economic prospects for a two-stage process are described on the basis of a hydrocarbon process proposed by HRI International for Kraft process lignin. These show that a mix of BTX products and fuel oil could generate a profitable rate of return. 62 references.

  3. Probabilistic liquefaction hazard analysis at liquefied sites of 1956 Dunaharaszti earthquake, in Hungary

    Science.gov (United States)

    Győri, Erzsébet; Gráczer, Zoltán; Tóth, László; Bán, Zoltán; Horváth, Tibor

    2017-04-01

    Liquefaction potential evaluations are generally made to assess the hazard from specific scenario earthquakes. These evaluations may estimate the potential in a binary fashion (yes/no), define a factor of safety or predict the probability of liquefaction given a scenario event. Usually the level of ground shaking is obtained from the results of PSHA. Although it is determined probabilistically, a single level of ground shaking is selected and used within the liquefaction potential evaluation. In contrary, the fully probabilistic liquefaction potential assessment methods provide a complete picture of liquefaction hazard, namely taking into account the joint probability distribution of PGA and magnitude of earthquake scenarios; both of which are key inputs in the stress-based simplified methods. Kramer and Mayfield (2007) has developed a fully probabilistic liquefaction potential evaluation method using a performance-based earthquake engineering (PBEE) framework. The results of the procedure are the direct estimate of the return period of liquefaction and the liquefaction hazard curves in function of depth. The method combines the disaggregation matrices computed for different exceedance frequencies during probabilistic seismic hazard analysis with one of the recent models for the conditional probability of liquefaction. We have developed a software for the assessment of performance-based liquefaction triggering on the basis of Kramer and Mayfield method. Originally the SPT based probabilistic method of Cetin et al. (2004) was built-in into the procedure of Kramer and Mayfield to compute the conditional probability however there is no professional consensus about its applicability. Therefore we have included not only Cetin's method but Idriss and Boulanger (2012) SPT based moreover Boulanger and Idriss (2014) CPT based procedures into our computer program. In 1956, a damaging earthquake of magnitude 5.6 occurred in Dunaharaszti, in Hungary. Its epicenter was located

  4. Study on thermochemical liquefaction of biomass feedstocks; Biomass genryo no yuka hanno tokusei ni kansuru kisoteki kenkyu

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1997-02-10

    Liquefaction is applied to various biomass wastes and unused biomass to study characteristics of the liquefaction in each case. The paper described the system of the conversion and use of biomass into energy, conducted the positioning of the liquefaction, and outlined a history of the liquefaction chemistry and the study. To obtain basic data of characteristics of the liquefaction of various biomass raw materials, the liquefaction was conducted changing operational factors for the purpose of clarifying the product distribution of oil and by-products and oil properties. A comprehensive consideration was made of the liquefaction based on basic data and literature reports on the liquefaction of various biomass. From the above-mentioned studies, it was concluded that the energy can be recovered in a form of oil by applying the liquefaction to various biomass materials. A series of the study clarified effects of various operational factors on characteristics of the liquefaction as well as effects of classification of biomass materials and composition of the materials on characteristics of the liquefaction. 141 refs., 78 figs., 56 tabs.

  5. Cooperative research in coal liquefaction infratechnology and generic technology development: Final report, October 1, 1985 to December 31, 1986

    Energy Technology Data Exchange (ETDEWEB)

    Sendlein, L.V.A.

    1987-06-29

    During the first year of its research program, the Consortium for Fossil Fuel Liquefaction Science has made significant progress in many areas of coal liquefaction and coal structure research. Research topics for which substantial progress has been made include integrated coal structure and liquefaction studies, investigation of differential liquefaction processes, development and application of sophisticated techniques for structural analysis, computer analysis of multivariate data, biodesulfurization of coal, catalysis studies, co-processing of coal and crude oil, coal dissolution and extraction processes, coal depolymerization, determination of the liquefaction characteristics of many US coals for use in a liquefaction database, and completion of a retrospective technology assessment for direct coal liquefaction. These and related topics are discussed in considerably more detail in the remainder of this report. Individual projects are processed separately for the data base.

  6. Review and experimental study on pyrolysis and hydrothermal liquefaction of microalgae for biofuel production

    International Nuclear Information System (INIS)

    Chiaramonti, David; Prussi, Matteo; Buffi, Marco; Rizzo, Andrea Maria; Pari, Luigi

    2017-01-01

    Highlights: • A review of microalgae thermochemical conversion to bioliquids was carried out. • We focused on pyrolysis and hydrothermal liquefaction for biocrude/biofuels. • Original experimental research on microalgae pyrolysis was also carried out. • Starvation does not impact significant on the energy content of the biocrude. • This result is relevant for designing full scale microalgae production plants. - Abstract: Advanced Biofuels steadily developed during recent year, with several highly innovative processes and technologies explored at various scales: among these, lignocellulosic ethanol and CTO (Crude Tall Oil)-biofuel technologies already achieved early-commercial status, while hydrotreating of vegetable oils is today fully commercial, with almost 3.5 Mt/y installed capacity worldwide. In this context, microalgae grown in salt-water and arid areas represent a promising sustainable chain for advanced biofuel production but, at the same time, they also represent a considerable challenge. Processing microalgae in an economic way into a viable and sustainable liquid biofuel (a low-cost mass-product) is not trivial. So far, the most studied microalgae-based biofuel chain is composed by microorganism cultivation, lipid accumulation, oil extraction, co-product valorization, and algae oil conversion through conventional esterification into Fatty Acids Methyl Esters (FAME), i.e. Biodiesel, or Hydrotreated Esters and Fatty Acids (HEFA), the latter representing a very high quality drop-in biofuel (suitable either for road transport or for aviation). However, extracting the algae oil at low cost and industrial scale is not yet a mature process, and there is not yet industrial production of algae-biofuel from these two lipid-based chains. Another option can however be considered: processing the algae through dedicated thermochemical reactors into advanced biofuels, thus approaching the downstream processing of algae in a completely different way than

  7. Hydrothermal liquefaction of cellulose to bio-oil under acidic, neutral and alkaline conditions

    International Nuclear Information System (INIS)

    Yin, Sudong; Tan, Zhongchao

    2012-01-01

    Highlights: ► Hydrothermal liquefaction (HTL) at acidic, neutral and alkaline conditions. ► Bio-oil compositions varied with acidic, neutral and alkaline conditions. ► Reaction mechanisms varied with acidic, neutral and alkaline conditions. ► HTL should be classified to acidic, neutral and alkaline processes. -- Abstract: Hydrothermal liquefaction (HTL) of biomass to bio-oil under alkaline or neutral conditions has been widely reported in literature. However, there has been limited data available in literature on comparing HTL of biomass to bio-oil under acidic, neutral, and alkaline in terms of chemical compositions and yields by using the same reaction conditions and reactor. Using cellulose as a feedstock we conducted the comparative studies for pH = 3, 7 and 14 at temperatures of 275–320 °C with reaction residence times of 0–30 min. Results showed that the chemical compositions of the bio-oils were different for acidic, neutral and alkaline conditions. Under acidic and neutral conditions, the main composition of HTL bio-oil was 5-(Hydroxymethyl)furfural (HMF). Under alkaline conditions, the main compounds became C 2–5 carboxylic acids. For bio-oil yields, it was observed that high temperatures and long residence times had negative effects, regardless of the pH levels. However, the corresponding reaction mechanisms are different. Under acidic conditions, the decrease in the bio-oil yields was mainly caused by polymerization of 5-HMF to solids. Under neutral conditions, the bio-oil yields decreased because 5-HMF was converted to both solid and gaseous products. Under alkaline conditions, the bio-oil decomposed to gases through the formation of short chain acids and aldehydes. Therefore, although they were all referred to as HTL bio-oil in literature, they were formed by different reaction pathways and had different properties due to their different chemical compositions. Given these differences, different strategies are recommended in this study to

  8. Subtask 3.9 - Direct Coal Liquefaction Process Development

    Energy Technology Data Exchange (ETDEWEB)

    Aulich, Ted; Sharma, Ramesh

    2012-07-01

    The Energy and Environmental Research Center (EERC), in partnership with the U.S. Department of Energy (DOE) and Accelergy Corporation, an advanced fuels developer with technologies exclusively licensed from ExxonMobil, undertook Subtask 3.9 to design, build, and preliminarily operate a bench-scale direct coal liquefaction (DCL) system capable of converting 45 pounds/hour of pulverized, dried coal to a liquid suitable for upgrading to fuels and/or chemicals. Fabrication and installation of the DCL system and an accompanying distillation system for off-line fractionation of raw coal liquids into 1) a naphtha middle distillate stream for upgrading and 2) a recycle stream was completed in May 2012. Shakedown of the system was initiated in July 2012. In addition to completing fabrication of the DCL system, the project also produced a 500-milliliter sample of jet fuel derived in part from direct liquefaction of Illinois No. 6 coal, and submitted the sample to the Air Force Research Laboratory (AFRL) at Wright Patterson Air Force Base, Dayton, Ohio, for evaluation. The sample was confirmed by AFRL to be in compliance with all U.S. Air Force-prescribed alternative aviation fuel initial screening criteria.

  9. Novel use of residue from direct coal liquefaction process

    Energy Technology Data Exchange (ETDEWEB)

    Jianli Yang; Zhaixia Wang; Zhenyu Liu; Yuzhen Zhang [Chinese Academy of Sciences, Taiyuan (China). State Key Laboratory of Coal Conversion

    2009-09-15

    Direct coal liquefaction residue (DCLR) is, commonly, designed to be used as a feed stock for gasification or combustion. Use of DCLR as a value added product is very important for improving overall economy of direct coal liquefaction processes. This study shows that the DCLR may be used as a pavement asphalt modifier. The modification ability is similar to that of Trinidad Lake Asphalt (TLA), a superior commercial modifier. Asphalts modified by two DCLRs meet the specifications of ASTM D5710 and BSI BS-3690 designated for the TLA-modified asphalts. The required addition amount for the DCLRs tested is less than that for TLA due possibly to the high content of asphaltene in DCLRs. Different compatibility was observed for the asphalts with the same penetration grade but from the different origin. Different components in the DCLR play different roles in the modification. Positive synergetic effects among the fractions were observed, which may due to the formation of the stable colloid structure. Unlike polymer-type modifier, the structure of asphalt-type modifier has a similarity with petroleum asphalts which favors the formation of a stable dispersed polar fluid (DPF) colloid structure and improves the performance of pavement asphalt. 12 refs., 1 fig., 6 tabs.

  10. Efficient Air Desulfurization Catalysts Derived from Pig Manure Liquefaction Char

    Directory of Open Access Journals (Sweden)

    Rajiv Wallace

    2017-11-01

    Full Text Available Biochar from the liquefaction of pig manure was used as a precursor of H2S desulfurization adsorbents. In its inorganic matter, it contains marked quantities of calcium, magnesium and iron, which are known as hydrogen sulfide oxidation catalysts. The char was used either as-received or mixed with 10% nanographite. The latter was added to increase both the content of the carbon phase and conductivity. ZnCl2 in two different ratios of char to an activation agent (1:1 and 1:2 was used to create the porosity in the carbon phase. The content of the later was between 18–45%. The activated samples adsorbed 144 mg/g H2S. Sulfur was the predominant product of reactive adsorption. Its deposition in the pore system and blockage of the most active pores ceased the materials’ activity. The presence of the catalytic phase was necessary but not sufficient to guarantee good performance. The developed porosity, which can store oxidation products in the resulting composite, is essential for the good performance of the desulfurization process. The surface of the composite with nanographite showed the highest catalytic activity, similar to that of the commercial Midas® carbon catalyst. The results obtained indicate that a high quality reactive adsorbent/catalyst for H2S removal can be obtained from pig manure liquefaction wastes.

  11. Report for fiscal 1995 by basic liquefaction technology subcommittee; 1995 nendo ekika kiban gijutsu bukai hokokusho

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1996-03-01

    Delivered at the 1st meeting are a report on the fiscal 1995 research plan and an interim report, involving the use of coal-derived oils, research on refining technology using a PDU (process developing unit), reforming technology and petroleum blending technology for coal-derived oils, development of new reforming catalysts, technology of heterocompound separation, and the development of applications. Reported in relation with the development of environmentally friendly coal liquefaction technology are the study of coal liquefaction conditions, study of the upgrading of basic liquefaction techniques for the improvement and rationalization of the liquefaction process, and a project of liquefaction technology internationalization. A report is also given on a liquefaction catalyst study meeting. At the 2nd meeting, reports are delivered on the development of environmentally friendly coal liquefaction technology, including a briefing on the situation in general, designing of highly active catalysts, elucidation of the mechanism of emergence of activity, achievement of the marginal yield of coal-derived oils, and the properties of catalyst attached to coal. Delivered in relation with the use of coal-derived oils and technology for their refining are a briefing on the situation in general and reports on the blockup to occur in the naphtha fraction process and measures to counter the problem, control of the metamorphosis of active metals in reaction, heterocompound separation technology, and the development of applications. (NEDO)

  12. Post Hoc Analysis of Passive Cavitation Imaging for Classification of Histotripsy-Induced Liquefaction in Vitro.

    Science.gov (United States)

    Bader, Kenneth B; Haworth, Kevin J; Maxwell, Adam D; Holland, Christy K

    2018-01-01

    Histotripsy utilizes focused ultrasound to generate bubble clouds for transcutaneous tissue liquefaction. Bubble activity maps are under development to provide image guidance and monitor treatment progress. The aim of this paper was to investigate the feasibility of using plane wave B-mode and passive cavitation images to be used as binary classifiers of histotripsy-induced liquefaction. Prostate tissue phantoms were exposed to histotripsy pulses over a range of pulse durations (5- ) and peak negative pressures (12-23 MPa). Acoustic emissions were recorded during the insonation and beamformed to form passive cavitation images. Plane wave B-mode images were acquired following the insonation to detect the hyperechoic bubble cloud. Phantom samples were sectioned and stained to delineate the liquefaction zone. Correlation between passive cavitation and plane wave B-mode images and the liquefaction zone was assessed using receiver operating characteristic (ROC) curve analysis. Liquefaction of the phantom was observed for all the insonation conditions. The area under the ROC (0.94 versus 0.82), accuracy (0.90 versus 0.83), and sensitivity (0.81 versus 0.49) was greater for passive cavitation images relative to B-mode images ( ) along the azimuth of the liquefaction zone. The specificity was greater than 0.9 for both imaging modalities. These results demonstrate a stronger correlation between histotripsy-induced liquefaction and passive cavitation imaging compared with the plane wave B-mode imaging, albeit with limited passive cavitation image range resolution.

  13. Fiscal 1991 report. Coal liquefaction committee; 1991 nendo sekitan ekika iinkai hokokusho

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1992-03-01

    The committee in this fiscal year had the 1st meeting in July 1991, the 2nd in August 1991, and the 3rd in March 1992, when fiscal 1990 research and development results, fiscal 1991 research and development programs, fiscal 1991 research and development results, etc., were reported and deliberated. At the 2nd meeting, the meaning of coal liquefaction technology development and how to go ahead with the task were described, which topic for discussion was entitled 'How coal liquefaction technology should be for the 21st century.' After discussion, it was agreed upon that a coal liquefaction technology package be completed in fiscal 2000 based on the absorption of each other's findings and on the utilization of basic studies common to both to be realized through the exchange of technologies between the brown coal liquefaction project and the bituminous coal liquefaction project. Under the brown coal liquefaction project, a 50 ton/day pilot plant was built and operated in Victoria, Australia, and the operation was completed in October 1990. The results of research and development under the coal brown liquefaction project will be compiled by fiscal 1993. (NEDO)

  14. Effect of pre-swelling of coal on its liquefaction properties

    Energy Technology Data Exchange (ETDEWEB)

    Hengfu Shui; Zhicai Wang; Meixia Cao [Anhui University of Technology, Ma' anshan (China). School of Chemistry & Chemical Engineering

    2007-07-01

    The effects of pre-swelling of Shenhua coal on its liquefaction property were studied in this paper. It was found that pre-swelling treatments of Shenhua coal in three solvents, i.e toluene (TOL), N-methyl-2-pyrrolidinone (NMP) and tetralin (THN) increased its liquefaction conversion, and the liquefied product distributions were also quite different. Removal of the pre-swelling solvent from the swollen coals further increased the liquefaction conversion compared to that of the swollen coals with the swelling solvent existed in them. It was found that oil and gas yields for the liquefaction of swollen coals in NMP and TOL with swelling solvent existed dramatically decreased. Pre-swelling in THN at 120{sup o}C gave the highest liquefaction conversion, however the liquefaction conversion decreased with the increase of pre-swelling temperature in the case of NMP. TG and FTIR analyses of raw coal, the swollen coals and liquefied products were carried out and the mechanism of the effects of pre-swelling of coal on its extraction and liquefaction behaviors were probed in the paper. 12 refs., 6 figs., 3 tabs.

  15. Novel bimetallic dispersed catalysts for temperature-programmed coal liquefaction. Final report

    Energy Technology Data Exchange (ETDEWEB)

    Chunshan Song; Schobert, H.H.; Parfitt, D.P. [and others

    1997-11-01

    Development of new catalysts is a promising approach to more efficient coal liquefaction. It has been recognized that dispersed catalysts are superior to supported catalysts for primary liquefaction of coals, because the control of initial coal dissolution or depolymerization requires intimate contact between the catalyst and coal. This research is a fundamental and exploratory study on catalytic coal liquefaction, with the emphasis on exploring novel bimetallic dispersed catalysts for coal liquefaction and the effectiveness of temperature-programmed liquefaction using dispersed catalysts. The primary objective of this research was to explore novel bimetallic dispersed catalysts from organometallic molecular precursors, that could be used in low concentrations but exhibit relatively high activity for efficient hydroliquefaction of coals under temperature-programmed conditions. We have synthesized and tested various catalyst precursors in liquefaction of subbituminous and bituminous coals and in model compound studies to examine how do the composition and structure of the catalytic precursors affect their effectiveness for coal liquefaction under different reaction conditions, and how do these factors affect their catalytic functions for hydrogenation of polyaromatic hydrocarbons, for cleavage of C-C bonds in polycyclic systems such as 4-(1-naphthylmethyl)bibenzyl, for hydrogenolysis of C-O bond such as that in dinaphthylether, for hydrodeoxygenation of phenolic compounds and other oxygen-containing compounds such as xanthene, and for hydrodesulfurization of polycyclic sulfur compounds such as dibenzothiophene. The novel bimetallic and monometallic precursors synthesized and tested in this project include various Mo- and Fe-based compounds.

  16. Liquefaction induced by earthquakes in Japan. Jiban no ekijoka/ekijoka saigai chosa kenkyu no seika

    Energy Technology Data Exchange (ETDEWEB)

    Tono, I [Nation Inst. for Enviromental Studies, Tsukuba (Japan)

    1992-09-01

    Disaster caused by liquefaction is an important problem for the development of water-front because most of the places suffered from liquefaction disasters recently are located on sandy grounds. The damaged cases in the past due to liquefaction induced by earthquakes are grouped into: subsidence and inclination caused by the loss of supporting force of the ground, coming to the surface of buried structures due to excess pore hydrostatic pressure, destruction of lifeline accompanying the fluidization of ground, breakdown of bulkhead, retaining wall, etc. by increased earth pressure, sinking of soil structures, ground fissure, sliding, and immersion in floods and submergence of farms due to spouting of underground water. As regards prediction of liquefaction, description is made on the prediction of the occurrence of liquefaction and liquefaction prediction for which sedimentation environment is taken into consideration. Open-cut investigation can be said as the most effective means for accurate learning of the depth, thickness and sedimentation structure of liquefied layers. Liquefaction layers found in remains are also introduced. 16 refs., 6 figs.

  17. FY 1991 report on the bituminous coal liquefaction section; 1991 nendo rekiseitan ekikabukai hokokusho

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1992-03-01

    The paper reported activities of the bituminous coal liquefaction section in FY 1991. In the 1st bituminous coal liquefaction section meeting, report/discussion were made on the outline of the plan on the FY 1991 research using pilot plant and the support study of pilot plant. In the 2nd section meeting, report was made on 'How the development of coal liquefaction technology should be in the 21st century,' a report made by the joint section of bituminous coal/brown coal liquefaction. In the 3rd section meeting, report/discussion were made on the state of progress of the FY 1991 R and D and results. In the study using the bituminous coal liquefaction pilot plant, report was made on the outline of construction of a 150t/d pilot plant, study on the acquisition of material balance, analytical study of the data on liquefaction tower, testing survey on properties of coal slurry, and testing survey on slurry preheating furnace. In the support study of pilot plant, report was made on the study using 1t/d PUS, study on the development of the optimum coal refining technology and improvement in the distillate distribution, study of conditions for coal liquefaction and study of solvent hydrogenation catalyst. (NEDO)

  18. An experimental and theoretical investigation of the liquefaction dynamics of a phase change material in a normal gravity environment

    Science.gov (United States)

    Bain, R. L.; Stermole, F. J.; Golden, J. O.

    1972-01-01

    Experimental and theoretical investigations were undertaken to determine the role of gravity-induced free convection upon the liquefaction dynamics of a cylindrical paraffin slab under normal gravity conditions. The experimental equipment consisted of a test cell, a fluid-loop heating system, and a multipoint recorder. The test chamber was annular in shape with an effective radius of 1.585 cm and a length of 5.08 cm. The heating chamber was a 1.906 cm diameter tube going through the center of the test chamber, and connected to the fluid loop heating system. All experimental runs were made with the longitudinal axis of the test cell in the vertical direction to insure that convection was not a function of the angular axis of the cell. Ten melting runs were made at various hot wall temperatures. Also, two pure conduction solidification runs were made to determine an experimental latent heat of fusion.

  19. Single-phase AutoReClosure ARC failure on 400 kV combinedcable/overhead line with permanently connected shunt reactor

    DEFF Research Database (Denmark)

    Bak, Claus Leth; Søgaard, Kim

    2008-01-01

    consisting of overhead lines, crossbonded cable sections and shunt reactor has been created in PSCAD/EMTDC and verified against measurements with good results. Main focus has been put on the likelihood of having a successful single-phase autoreclosure ARC in such a combined cable/OHL line....

  20. The Texts of the Instruments connected with the Agency's Assistance to Pakistan in Establishing a Research Reactor Project. A Second Supply Agreement

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1968-01-12

    As a sequel to the assistance which the Agency provided to the Government of Pakistan in establishing a research reactor project, a second Supply Agreement has been concluded between the Agency and the Governments of Pakistan and the United States of America. This Agreement entered into force on 19 October 1967, and the text is reproduced herein for the information of all Members.

  1. The Texts of the Instruments connected with the Agency's Assistance to Yugoslavia in Establishing a Research Reactor Project. Second Supply Agreement

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1968-08-28

    As a sequel to the assistance which the Agency provided to the Government of Yugoslavia in establishing a research reactor project, a second Supply Agreement has been concluded between the Agency and the Governments of the United States of America and Yugoslavia. The Agreement entered into force on 20 February 1968, and the text is reproduced herein for the information of all Members.

  2. The Texts of the Instruments connected with the Agency's Assistance to Finland in relation to a Research Reactor Project. Second Supply Agreement

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1966-07-25

    As a sequel to the assistance which the Agency provided to the Government of Finland in establishing a research reactor project, a second Supply Agreement has been concluded between the Agency and the Government of Finland and the United States of America. This Agreement entered into force on 8 July 1966, and the text is reproduced herein for the information of all Members.

  3. The Texts of the Instruments connected with the Agency's Assistance to Pakistan in Establishing a Research Reactor Project. A Second Supply Agreement. An Amendment

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1971-10-04

    The text of an Amendment to the Contract for the Transfer of Enriched Uranium for a Research Reactor (the Second Supply Agreement) between the Agency and the Governments of Pakistan and the United States of America is reproduced herein for the information of all Members. The Amendment entered into force on 16 June 1971.

  4. The Texts of the Instruments connected with the Agency's Assistance to Pakistan in Establishing a Research Reactor Project. A Second Supply Agreement

    International Nuclear Information System (INIS)

    1968-01-01

    As a sequel to the assistance which the Agency provided to the Government of Pakistan in establishing a research reactor project, a second Supply Agreement has been concluded between the Agency and the Governments of Pakistan and the United States of America. This Agreement entered into force on 19 October 1967, and the text is reproduced herein for the information of all Members

  5. The Texts of the Instruments connected with the Agency's Assistance to Yugoslavia in Establishing a Research Reactor Project. Second Supply Agreement

    International Nuclear Information System (INIS)

    1968-01-01

    As a sequel to the assistance which the Agency provided to the Government of Yugoslavia in establishing a research reactor project, a second Supply Agreement has been concluded between the Agency and the Governments of the United States of America and Yugoslavia. The Agreement entered into force on 20 February 1968, and the text is reproduced herein for the information of all Members

  6. The Texts of the Instruments connected with the Agency's Assistance to Finland in relation to a Research Reactor Project. Second Supply Agreement

    International Nuclear Information System (INIS)

    1966-01-01

    As a sequel to the assistance which the Agency provided to the Government of Finland in establishing a research reactor project, a second Supply Agreement has been concluded between the Agency and the Government of Finland and the United States of America. This Agreement entered into force on 8 July 1966, and the text is reproduced herein for the information of all Members

  7. Reactor System Design

    International Nuclear Information System (INIS)

    Chi, S. K.; Kim, G. K.; Yeo, J. W.

    2006-08-01

    SMART NPP(Nuclear Power Plant) has been developed for duel purpose, electricity generation and energy supply for seawater desalination. The objective of this project IS to design the reactor system of SMART pilot plant(SMART-P) which will be built and operated for the integrated technology verification of SMART. SMART-P is an integral reactor in which primary components of reactor coolant system are enclosed in single pressure vessel without connecting pipes. The major components installed within a vessel includes a core, twelve steam generator cassettes, a low-temperature self pressurizer, twelve control rod drives, and two main coolant pumps. SMART-P reactor system design was categorized to the reactor coe design, fluid system design, reactor mechanical design, major component design and MMIS design. Reactor safety -analysis and performance analysis were performed for developed SMART=P reactor system. Also, the preparation of safety analysis report, and the technical support for licensing acquisition are performed

  8. Hydrogen Transfer during Liquefaction of Elbistan Lignite to Biomass; Total Reaction Transformation Approach

    Science.gov (United States)

    Koyunoglu, Cemil; Karaca, Hüseyin

    2017-12-01

    Given the high cost of the tetraline solvent commonly used in liquefaction, the use of manure with EL is an important factor when considering the high cost of using tetraline as a hydrogen transfer source. In addition, due to the another cost factor which is the catalyst prices, red mud (commonly used, produced as a byproduct in the production of aluminium) is reduced cost in the work of liquefaction of coal, biomass, even coal combined biomass, corresponding that making the EL liquefaction an agenda for our country is another important factor. Conditions for liquefaction experiments conducted for hydrogen transfer from manure to coal; Catalyst concentration of 9%, liquid/solid ratio of 3/1, reaction time of 60 min, fertilizer/lignite ratio of 1/3, and the reaction temperature of 400 °C, the stirred speed of 400 rpm and the initial nitrogen pressure of 20 bar was fixed. In order to demonstrate the hydrogen, transfer from manure to coal, coal is used solely, by using tetraline (also known as a hydrogen carrier) and distilled water which is not hydrogen donor as a solvent in the co-liquefaction of experiments, and also the liquefaction conditions are carried out under an inert (N2) gas atmosphere. According to the results of the obtained liquefaction test; using tetraline solvent the total liquid product conversion percentage of the oil + gas conversion was 38.3 %, however, the results of oil+gas conversion obtained using distilled water and EL combined with manure the total liquid product conversion percentage was 7.4 %. According to the results of calorific value and elemental analysis, only the ratio of (H/C)atomic of coal obtained by using tetraline increased with the liquefaction of manure and distilled water. The reason of the increase in the amount of hydrogen due to hydrogen transfer from the manure on the solid surface of the coal, and also on the surface of the inner pore of the coal during the liquefaction, brings about the evaluation of the coal as a

  9. Cooperative research program in coal liquefaction. Quarterly report, May 1, 1993--October 31, 1993

    Energy Technology Data Exchange (ETDEWEB)

    Hoffman, G.P. [ed.

    1994-07-01

    This report summarizes progress in four areas of research under the general heading of Coal Liquefaction. Results of studies concerning the coliquefaction of coal with waste organic polymers or chemical products of these polymers were reported. Secondly, studies of catalytic systems for the production of clean transportation fuels from coal were discussed. Thirdly, investigations of the chemical composition of coals and their dehydrogenated counterparts were presented. These studies were directed toward elucidation of coal liquefaction processes on the chemical level. Finally, analytical methodologies developed for in situ monitoring of coal liquefaction were reported. Techniques utilizing model reactions and methods based on XAFS, ESR, and GC/MS are discussed.

  10. Experimental validation of a mathematical model for seabed liquefaction in waves

    DEFF Research Database (Denmark)

    Sumer, B. Mutlu; Kirca, Özgür; Fredsøe, Jørgen

    2011-01-01

    This paper summarizes the results of an experimental study directed towards the validation of a mathematical model for the buildup of pore water pressure and resulting liquefaction of marine soils under progressive waves. Experiments were conducted under controlled conditions with silt ( d50 = 0.......070 mm) in a wave flume with a soil pit. Waves with wave heights in the range 7.7-18 cm with the water depth 55 cm and the wave period 1.6 s enabled us to study both the liquefaction and no-liquefaction regime pore water pressure buildup. The experimental data was used to validate the model. A numerical...

  11. Reactors 2000: consultation on the technical and economical requirements connected with the possible realization of nuclear installations in Switzerland after the year 2000

    International Nuclear Information System (INIS)

    Haldi, P.A.

    1992-07-01

    In 1989 the OECD started a consultation on the development of nuclear reactors of small and medium size (SMR). The present study is part of the Swiss contribution to this international work. Beyond this primary goal, without being limited solely to SMRs, but exclusively in the Swiss framework, the study attempts to determine a profile for reactors which could be built in Switzerland after the year 2000. The study ''Reactors 2000'' is based on two polls which were conducted among about 70 persons from concerned professional circles (industry, utilities, scientific groups, energy policy makers, safety authorities, public organizations) in June 1990 and February 1991. A large majority of the persons interviewed think that - Switzerland should not jeopardize its energetic future by phasing out all activity in the nuclear field, based on circumstances which could be only temporary, - Switzerland should continue its activities in the nuclear field in order to maintain the necessary know-how and a sufficient number of highly qualified specialists both for the safe operation of the existing plants and for the continuation of the development of nuclear technology, - for future plants the goal of an even higher safety level should be aimed for, although, according to the explicit comments of many interviews, today's reactors are considered to be sufficiently safe, - future nuclear power plants should be designed in such a way that the possibility of a severe accident necessitating an evacuation of the Swiss population could be excluded, - Switzerland should participate in international projects, in order to maintain contact to the international development of nuclear technology; on the other hand, it should avoid any single-handed effort (including in the domain of small heating reactors). (author)

  12. Study of short-lived fission products with the aid of an isotope separator connected to reactor R2-0

    International Nuclear Information System (INIS)

    Rudstam, G.

    1976-01-01

    This report constitutes a final report on project 74-3289 together with a preliminary report for project 75-3332. These projects have been included in the budget years 1974/75 and 1975/76 as a contribution to the operating costs of reactor R2-0 at Studsvik. The reactor was used for experimental studies on short-lived fission products with OSIRIS isotope-separator equipment. The scientific programme is very broad. It comprises, in the first place, characterisation of fission products (a study of their excitation levels, measurement of decay properties such as half-life and emission of delayed neutrons, determination of neutron energy spectrum, determination of total decay energy, etc.). An important application of this field of research is the determination of decay heat in nuclear fuel. The programme thus comprises research of a fundamental character and applied research. (H.E.G.)

  13. A nuclear reactor core fuel reload optimization using Artificial-Ant-Colony Connective Networks; Recarga de reatores nucleares utilizando redes conectivas de colonias de formigas artificiais

    Energy Technology Data Exchange (ETDEWEB)

    Lima, Alan M.M. de; Schirru, Roberto [Universidade Federal, Rio de Janeiro, RJ (Brazil). Coordenacao dos Programas de Pos-graduacao de Engenharia. Programa de Engenharia Nuclear]. E-mail: alan@lmp.ufrj.br; schirru@lmp.ufrj.br

    2005-07-01

    A Pressurized Water Reactor core must be reloaded every time the fuel burnup reaches a level when it is not possible to sustain nominal power operation. The nuclear core fuel reload optimization consists in finding a burned-up and fresh-fuel-assembly pattern that maximizes the number of full operational days. This problem is NP-hard, meaning that complexity grows exponentially with the number of fuel assemblies in the core. Besides that, the problem is non-linear and its search space is highly discontinual and multimodal. In this work a parallel computational system based on Ant Colony System (ACS) called Artificial-Ant-Colony Networks is introduced to solve the nuclear reactor core fuel reload optimization problem. ACS is a system based on artificial agents that uses the reinforcement learning technique and was originally developed to solve the Traveling Salesman Problem, which is conceptually similar to the nuclear fuel reload problem. (author)

  14. Problems and prospects connected with development of high-temperature filtration technology at nuclear power plants equipped with VVER-1000 reactors

    Science.gov (United States)

    Shchelik, S. V.; Pavlov, A. S.

    2013-07-01

    Results of work on restoring the service properties of filtering material used in the high-temperature reactor coolant purification system of a VVER-1000 reactor are presented. A quantitative assessment is given to the effect from subjecting a high-temperature sorbent to backwashing operations carried out with the use of regular capacities available in the design process circuit in the first years of operation of Unit 3 at the Kalinin nuclear power plant. Approaches to optimizing this process are suggested. A conceptual idea about comprehensively solving the problem of achieving more efficient and safe operation of the high-temperature active water treatment system (AWT-1) on a nuclear power industry-wide scale is outlined.

  15. Analysis of materials in connection with corium melt retention in WWER reactor vessels. Final report for the period 15 October 1995 - 14 October 1996

    International Nuclear Information System (INIS)

    Efanov, A.D.

    1997-02-01

    Analysis of the state of severe accident codes being developed in Russia describing processes of corium - reactor pressure vessel interaction during severe accidents showed that at present there is no reliable validated and verified code. This study considered some of the most advanced severe accident codes which include models of heat generating liquid convections and RPV tolerance capacity however the possibility of physico-chemical interactions is not being considered. The final report demonstrates one of the examples for the settlement modelling of processes of reactor core debris cooling and corium pool mirror cooling with the use of the KOSTER 2 Code developed at IPPE. It was shown that cooling by water spray within some definite region of drop dimensions (0.5 / 4 mm in diameter) could provide the opportunity of the WWER type RPV integrity preservation under the accepted conditions. Due to some uncertainties in calculation modules obtained results are recommended to be treated as preliminary. (author). 26 refs, figs, tabs

  16. Connecting numeric models

    International Nuclear Information System (INIS)

    Caremoli, C.; Erhard, P.

    1996-01-01

    Computerized simulation uses calculation codes whose validation is reliable. Reactor simulators should take greater advantage of latest computer technology impact, in particular in the field of parallel processing. Instead of creating more global simulation codes whose validation might be a problem, connecting several existing codes should be a promising solution. (D.L.). 3 figs

  17. Dosimetry work and calculations in connection with the irradiation of large devices in the high flux materials testing reactor BR2

    International Nuclear Information System (INIS)

    De Raedt, C.; Leenders, L.; Tourwe, H.; Farrar, H. IV.

    1982-01-01

    For about fifteen years the high flux reactor BR2 has been involved in the testing of fast reactor fuel pins. In order to simulate the fast reactor neutron environment most devices are irradiated under cadmium screen, cutting off the thermal flux component. Extensive neutronic calculations are performed to help the optimization of the fuel bundle design. The actual experiments are preceded by irradiations of their mock-ups in BR02, the zero power model of BR2. The mock-up irradiations, supported by supplementary calculations, are performed for the determination of the main neutronic characteristics of the irradiation proper in BR2 and for the determination of the corresponding operation data. At the end of the BR2 irradiation, the experimental results, such as burn-ups, neutron fluences, helium production in the fuel pin claddings, etc. are correlated by neutronic calculations in order to examine the consistency of the post-irradiation results and to validate the routine calculation procedure and cross-section data employed. A comparison is made in this paper between neutronic calculation results and some post-irradiation data for MOL 7D, a cadmium screened sodium cooled loop containing a nineteen fuel pin bundle

  18. Coal liquefaction: A research and development needs assessment: Final report, Volume II

    Energy Technology Data Exchange (ETDEWEB)

    Schindler, H.D.; Burke, F.P.; Chao, K.C.; Davis, B.H.; Gorbaty, M.L.; Klier, K.; Kruse, C.W.; Larsen, J.W.; Lumpkin, R.E.; McIlwain, M.E.; Wender, I.; Stewart, N.

    1989-03-01

    Volume II of this report on an assessment of research needs for coal liquefaction contains reviews of the five liquefaction technologies---direct, indirect, pyrolysis, coprocessing, and bioconversion. These reviews are not meant to be encyclopedic; several outstanding reviews of liquefaction have appeared in recent years and the reader is referred to these whenever applicable. Instead, these chapters contain reviews of selected topics that serve to support the panel's recommendations or to illustrate recent accomplishments, work in progress, or areas of major research interest. At the beginning of each of these chapters is a brief introduction and a summary of the most important research recommendations brought out during the panel discussions and supported by the material presented in the review. A review of liquefaction developments outside the US is included. 594 refs., 100 figs., 60 tabs.

  19. Exergy analysis of helium liquefaction systems based on modified Claude cycle with two-expanders

    Science.gov (United States)

    Thomas, Rijo Jacob; Ghosh, Parthasarathi; Chowdhury, Kanchan

    2011-06-01

    Large-scale helium liquefaction systems, being energy-intensive, demand judicious selection of process parameters. An effective tool for design and analysis of thermodynamic cycles for these systems is exergy analysis, which is used to study the behavior of a helium liquefaction system based on modified Claude cycle. Parametric evaluation using process simulator Aspen HYSYS® helps to identify the effects of cycle pressure ratio and expander flow fraction on the exergetic efficiency of the liquefaction cycle. The study computes the distribution of losses at different refrigeration stages of the cycle and helps in selecting optimum cycle pressures, operating temperature levels of expanders and mass flow rates through them. Results from the analysis may help evolving guidelines for designing appropriate thermodynamic cycles for practical helium liquefaction systems.

  20. Applied research and evaluation of process concepts for liquefaction and gasification of western coals. Final report

    Energy Technology Data Exchange (ETDEWEB)

    Wiser, W. H.

    1980-09-01

    Fourteen sections, including five subsections, of the final report covering work done between June 1, 1975 to July 31, 1980 on research programs in coal gasification and liquefaction have been entered individually into EDB and ERA. (LTN)

  1. Subtask 3.3 - Feasibility of Direct Coal Liquefaction in the Modern Economic Climate

    Energy Technology Data Exchange (ETDEWEB)

    Benjamin Oster; Joshua Strege; Marc Kurz; Anthony Snyder; Melanie Jensen

    2009-06-15

    Coal liquefaction provides an alternative to petroleum for the production of liquid hydrocarbon-based fuels. There are two main processes to liquefy coal: direct coal liquefaction (DCL) and indirect coal liquefaction (ICL). Because ICL has been demonstrated to a greater extent than DCL, ICL may be viewed as the lower-risk option when it comes to building a coal liquefaction facility. However, a closer look, based on conversion efficiencies and economics, is necessary to determine the optimal technology. This report summarizes historical DCL efforts in the United States, describes the technical challenges facing DCL, overviews Shenhua's current DCL project in China, provides a DCL conceptual cost estimate based on a literature review, and compares the carbon dioxide emissions from a DCL facility to those from an ICL facility.

  2. Advanced direct liquefaction concepts for PETC generic units. Quarterly technical progress report, January--March 1992

    Energy Technology Data Exchange (ETDEWEB)

    1992-04-01

    In the Advance Coal Liquefaction Concept Proposal (ACLCP) carbon monoxide (CO) and water have been proposed as the primary reagents in the pretreatment process. The main objective of this project is to develop a methodology for pretreating coal under mild conditions based on a combination of existing processes which have shown great promise in liquefaction, extraction and pyrolysis studies. The aim of this pretreatment process is to partially depolymerise the coal, eliminate oxygen and diminish the propensity for retograde reactions during subsequent liquefaction. The desirable outcome of the CO pretreatment step should be: (1) enhanced liquefaction activity and/or selectivity toward products of higher quality due to chemical modification of the coal structure; (2) cleaner downstream products; (3) overall improvement in operability and process economics.

  3. Report on results for fiscal 1997 on development of coal liquefaction technology . Development of liquefaction base technology (studies on development and internationalization of environmentally benign coal liquefaction technology); 1997 nendo sekitan ekika gijutsu seika hokokusho. Ekika kiban gijutsu no kaihatsu (kankyo chowagata sekitan ekika gijutsu no kaihatsu oyobi kokusaika kenkyu)

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1998-03-01

    The research objective is the development of environmentally benign coal liquefaction technology and the studies on internationalization of coal liquefaction technology. Implemented for the former are (1) research on improvement and rationalization of liquefaction process and (2) research on advancement of liquefaction base technology. In (1), studies were made on in-oil preprocessing technology and scale suppressing measures for the purpose of obtaining reform/high grade of coal, and on improvement of liquefied oil collecting ratio, sophistication of coal slurry and attainment of light oil/high grade from liquefied crude oil for the purpose of optimizing liquefaction reactive conditions and improving a solvent. In (2), in developing high activity/high dispersion type new catalysts, catalytic sufurization behavior and activity manifestation mechanism were explored, as were iron hydroxide based iron ore properties and liquefaction reactive characteristics. The initial reactive characteristics of liquefaction for example were investigated for the purpose of collecting basic data for expanding kinds of coal. In order to attain the latter objective of the research, a feasibility study of liquefaction location was conducted, as were the investigation including sampling of iron ore for catalytic material and the investigation of coal gasification technology. After the completion of the Australian brown coal liquefaction project, the development of the coal liquefaction technology commenced in fiscal 1994 produced a number of useful records and ended in 1997. (NEDO)

  4. Pressure swing adsorption cycle for natural gas pretreatment for liquefaction

    Energy Technology Data Exchange (ETDEWEB)

    Mann, R.E.

    1984-01-10

    An improved apparatus and method for a regeneration of a solid adsorbent used to pretreat a gas before liquefaction. The spent adsorbent is subjected to a two-step regenerative process, in the first of which the adsorbent is subjected to a low pressure produced by the use of mechanical vacuum pumps. When the pressure of the atmosphere in contact with the adsorbent has been reduced to a level sufficiently low to insure that the gas will flow under laminar rather than viscous conditions, the adsorbent is exposed to the action of a cryoplate condenser maintained at a sufficiently low temperature to cause any molecules of water which impinge thereon to condense and freeze, thereby reducing the partial pressure of water vapor within the chamber. The reduced partial pressure of the water vapor in turn causes adsorbed water on the adsorbent to be desorbed, thereby effectively removing the water from the adsorbent and depositing it as solid ice on the cryoplate condenser.

  5. Experimental Study of Subcritical Water Liquefaction of Biomass

    DEFF Research Database (Denmark)

    Zhu, Zhe; Toor, Saqib; Rosendahl, Lasse

    2014-01-01

    In this work, hydrothermal liquefaction (HTL) of wood industry residues (wood, bark, sawdust) and macroalgae for producing biofuels has been investigated under subcritical water conditions (at temperature of 300 C), with and without the presence of catalyst. The effects of catalyst and biomass type...... bio-crudes were analyzed. The results showed that the higher heating values (HHVs) were in the range of 24.15 to 31.79 MJ/kg, and they were enhanced in the presence of catalyst, except for that of the macroalgae. The solid residues were characterized by heating value, SEM and FTIR. It was found...... that the addition of K2CO3 lowered the solids quality in terms of the heating values, while it did not have apparent effect on the functional groups of solid residues. SEM analysis of the raw biomass and solid residues revealed that the char formation for wood, sawdust and macroalgae had initially finished when...

  6. An optimum cold end configuration for helium liquefaction cycles

    International Nuclear Information System (INIS)

    Minta, M.; Smith, J.L.

    1984-01-01

    This chapter examines the effect of the non-ideal behavior of helium at low temperature on the performance of helium liquefaction cycles. The effect is isolated by means of a continuum model for the precooling stage. The cold end losses are due primarily to the composite effect of the non-ideality of helium at low temperatures and the heat exchanger losses, in addition to the component losses fixed by the expander/compressor efficiencies. Topics considered include continuously distributed full-pressure ratio expanders, continuously distributed full-flow expanders, the heat exchange effect (ideal gas working fluid, real gas working fluid), and cold end configuration. The cold end configuration minimizes the cycle cold end losses

  7. Characterization of solid residues from coal liquefaction processes. Phase I

    Energy Technology Data Exchange (ETDEWEB)

    Potter, J.; McDougall, W.M.; Kybett, B.D.; Neufeld, C.

    1981-01-01

    Various coal liquefaction and beneficiation processes are being investigated by independent research groups sponsored by the Canadian Federal Government. These processes include the co-processing of heavy oils and bitumen with coal, oxygen removal and hydrogenation of coal and supercritical gas extraction of coal. The end products, gaseous and liquid fuels and insoluble organic residues, vary with the experimental conditions. The physical properties and origin of the insoluble residue may influence such factors as degree of conversion, efficiency of the process, and ultimately, gaseous and liquid yields. One of the most suitable methods of assessing the nature of the insoluble residues is the use of petrography. This report deals with petrographic assessment of the coals and residues from various coal conversion processes; attempts were made to characterize the solid phases in the residues; to assess them in a quantitative manner and where possible; to correlate the results with experimental data; and to assess their effects on conversion. (30 refs.)

  8. System evaluation of offshore platforms with gas liquefaction processes

    DEFF Research Database (Denmark)

    Nguyen, Tuong-Van; de Oliveira Júnior, Silvio

    2018-01-01

    Abstract Floating, production, storage and offloading plants are facilities used for offshore processing of hydrocarbons in remote locations. At present, the produced gas is injected back into the reservoir instead of being exported. The implementation of refrigeration processes offshore for liqu......Abstract Floating, production, storage and offloading plants are facilities used for offshore processing of hydrocarbons in remote locations. At present, the produced gas is injected back into the reservoir instead of being exported. The implementation of refrigeration processes offshore...... improvements are discussed based on an energy and exergy analysis. Compared to a standard platform where gas is directly injected into the reservoir, the total power consumption increases by up to 50%, and the exergy destruction within the processing plant doubles when a liquefaction system is installed....... It is therefore essential to conduct a careful analysis of the trade-off between the capital costs and operating revenues for such options....

  9. Zeolites as Catalysts for Fuels Refining after Indirect Liquefaction Processes

    Directory of Open Access Journals (Sweden)

    Arno de Klerk

    2018-01-01

    Full Text Available The use of zeolite catalysts for the refining of products from methanol synthesis and Fisher–Tropsch synthesis was reviewed. The focus was on fuels refining processes and differences in the application to indirect liquefaction products was compared to petroleum, which is often a case of managing different molecules. Processes covered were skeletal isomerisation of n-butenes, hydroisomerisation of n-butane, aliphatic alkylation, alkene oligomerisation, methanol to hydrocarbons, ethanol and heavier alcohols to hydrocarbons, carbonyls to hydrocarbons, etherification of alkenes with alcohols, light naphtha hydroisomerisation, catalytic naphtha reforming, hydroisomerisation of distillate, hydrocracking and fluid catalytic cracking. The zeolite types that are already industrially used were pointed out, as well as zeolite types that have future promise for specific conversion processes.

  10. Low-Cost Methane Liquefaction Plant and Vehicle Refueling Station

    International Nuclear Information System (INIS)

    Wilding, B.; Bramwell, D.

    1999-01-01

    The Idaho National Engineering and Environmental Laboratory (INEEL) is currently negotiating a collaborative effort with Pacific Gas and Electric (PG and E) that will advance the use of liquefied natural gas (LNG) as a vehicle fuel. We plan to develop and demonstrate a small-scale methane liquefaction plant (production of 5,000 to 10,000 gallons per day) and a low-cost ($150,000) LNG refueling station to supply fuel to LNG-powered transit buses and other heavy-duty vehicles. INEEL will perform the research and development work. PG and E will deploy the new facilities commercially in two demonstration projects, one in northern California, and one in southern California

  11. GIS-based soil liquefaction susceptibility map of Mumbai city for earthquake events

    Science.gov (United States)

    Mhaske, Sumedh Yamaji; Choudhury, Deepankar

    2010-03-01

    The problem of liquefaction of soil during seismic event is one of the important topics in the field of Geotechnical Earthquake Engineering. Liquefaction of soil is generally occurs in loose cohesionless saturated soil when pore water pressure increases suddenly due to induced ground motion and shear strength of soil decreases to zero and leading the structure situated above to undergo a large settlement, or failure. The failures took place due to liquefaction induced soil movement spread over few square km area continuously. Hence this is a problem where spatial variation involves and to represent this spatial variation Geographic Information System (GIS) is very useful in decision making about the area subjected to liquefaction. In this paper, GIS software GRAM++ is used to prepare soil liquefaction susceptibility map for entire Mumbai city in India by marking three zones viz. critically liquefiable soil, moderately liquefiable soil and non liquefiable soil. Extensive field borehole test data for groundwater depth, standard penetration test (SPT) blow counts, dry density, wet density and specific gravity, etc. have been collected from different parts of Mumbai. Simplified procedure of Youd et al. (2001) is used for calculation of factor of safety against soil liquefaction potential. Mumbai city and suburban area are formed by reclaiming lands around seven islands since 1865 till current date and still it is progressing in the area such as Navi Mumbai and beyond Borivali to Mira road suburban area. The factors of safety against soil liquefaction were determined for earthquake moment magnitude ranging from Mw = 5.0 to 7.5. It is found that the areas like Borivali, Malad, Dahisar, Bhandup may prone to liquefaction for earthquake moment magnitude ranging from Mw = 5.0 to 7.5. The liquefaction susceptibility maps were created by using GRAM++ by showing the areas where the factor of safety against the soil liquefaction is less than one. Proposed liquefaction

  12. Combined Reverse-Brayton Joule Thompson Hydrogen Liquefaction Cycle

    Energy Technology Data Exchange (ETDEWEB)

    Shimko, Martin A. [Gas Equipment Engineering Corporation, Milford, CT (United States); Dunn, Paul M. [Gas Equipment Engineering Corporation, Milford, CT (United States)

    2011-12-31

    The following is a compilation of Annual Progress Reports submitted to the DOE’s Fuel Cell Technologies Office by Gas Equipment Engineering Corp. for contract DE-FG36-05GO15021. The reports cover the project activities from August 2005 through June 2010. The purpose of this project is to produce a pilot-scale liquefaction plant that demonstrates GEECO’s ability to meet or exceed the efficiency targets set by the DOE. This plant will be used as a model to commercialize this technology for use in the distribution infrastructure of hydrogen fuel. It could also be applied to markets distributing hydrogen for industrial gas applications. Extensive modeling of plant performance will be used in the early part of the project to identify the liquefaction cycle architecture that optimizes the twin goals of increased efficiency and reduced cost. The major challenge of the project is to optimize/balance the performance (efficiency) of the plant against the cost of the plant so that the fully amortized cost of liquefying hydrogen meets the aggressive goals set by DOE. This project will design and build a small-scale pilot plant (several hundred kg/day) that will be both a hardware demonstration and a model for scaling to larger plant sizes (>50,000 kg/day). Though an effort will be made to use commercial or near-commercial components, key components that will need development for either a pilot- or full-scale plant will be identified. Prior to starting pilot plant fabrication, these components will be demonstrated at the appropriate scale to demonstrate sufficient performance for use in the pilot plant and the potential to achieve the performance used in modeling the full-scale plant.

  13. Microbial liquefaction of peat for the production of synthetic fuels

    Energy Technology Data Exchange (ETDEWEB)

    Gunasekaran, M.

    1988-01-01

    Objectives of this study were: to evaluate the potential of using various microorganisms to hydrolyse and liquify peat; to determine the optimal conditions for peat hydrolysis and liquefaction; to study the co-metabolizable substances; to separate the compounds present in liquified peat by alumina and silica acid chromatography and capillary gas chromatography; and to identify the compounds in liquified peat by capillary GC-Mass spectrometry. Organisms used in the study include: Coprinus comatus, Coriolus hirsutus, Ganoderma lucidum, Lentinus edodes, Lenzites trabea, Phanerochaete chrysosporium, Pleurotus ostreatus, P. sapidus, Polyporus adjustus, Neurospora sitophila, Rhizophus arrhizus, Bacillus subtilis, Acinetobacter sp. and Alcaligenes sp. The fungi were maintained and cultivated in potato dextrose agar at 30 C. The bacteria were maintained in nutrient agar at 30 C. We have also initiated work on coal solubilization in addition to the studies on peat liquefaction. A relatively new substratum or semi-solid base for culture media called Pluronic F-127, or Polyol (BASF, New Jersey). Objectives of this study were: (1) to study the growth patterns of Candida ML 13 on pluronic as substratum; (2) to determine the rate of microbial coal solubilization on pluronic F-127 amended in different growth media; (3) to separate the mycelial mat of Candida ML 13 from unsolubilized coal particles and solubilized coal products from pluronic F-127; (4) to determine the effects of pH on microbial coal solubilization in pluronic F-127 media; (5) the effect of concentration of pluronic F-127 in media on coal solubilization; and, (6) to study the role of extracellular factors secreted by Candida ML 13 on coal solubilization in pluronic F-127 media. Results are discussed. 4 refs.

  14. Coal liquefaction process streams characterization and evaluation. Quarterly technical progress report, October 1--December 31, 1991

    Energy Technology Data Exchange (ETDEWEB)

    Robbins, G.A.; Brandes, S.D.; Winschel, R.A.; Burke, F.P.

    1992-03-01

    CONSOL R&D is conducting a three-year program to characterize process and product streams from direct coal liquefaction process development projects. The program objectives are two-fold: (1) to obtain and provide appropriate samples of coal liquids for the evaluation of analytical methodology, and (2) to support ongoing DOE-sponsored coal liquefaction process development efforts. The two broad objectives have considerable overlap and together serve to provide a bridge between process development and analytical chemistry.

  15. Report on the achievements in the Sunshine Project in fiscal 1988. Development of a coal liquefaction technology (Liquefaction performance test on Chinese coals); 1988 nendo sekitan ekika gijutsu kaihatsu, Chugokutan ekika seino shiken seika hokokusho

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1989-03-01

    Development has been carried out on a Chinese coal liquefaction technology jointly by Japan and China. The Japanese side fabricated and built a small continuous testing equipment. Shenbei coal produced in Liaoning Province, Tienju coal produced in Gansu Province and Shenmu coal produced in Shaanxi Province were used as test sample coals. These coals were crushed, washed with water, sorted, dried, pulverized below 100 mesh, and used as the test samples. For catalysts, a reagent Fe{sub 2}O{sub 3} and S as an auxiliary catalyst made in China were used. Anthracene oil freed from crystal was used as a starting solvent when making one-through operation and recycling operation. Hydrogen used had purity of 99.5% or higher. The current fiscal year has performed smoothly to the end either of the one-through operation or the solvent circulating operation on RUN-2200, 2300 (Chenbei coal) and 2,400, 2500 (Tienju coal). Operation of 2600, 2700 (Shenmu coal) experienced noise in the stirrer of the reactor, and leakage of the circulating gas from the recycled gas compressor. In addition, the differential pressure during operating the last run has increased to 50 k, when the temperature and pressure were reduced, and substances clogging the reactor inlet line were removed. Three kinds of the liquefied oils were brought back to Japan for detailed analyses. (NEDO)

  16. Nuclear reactor

    International Nuclear Information System (INIS)

    Shirakawa, Toshihisa.

    1979-01-01

    Purpose: To prevent cladding tube injuries due to thermal expansion of each of the pellets by successively extracting each of the control rods loaded in the reactor core from those having less number of notches, as well as facilitate the handling work for the control rods. Constitution: A recycle flow control device is provided to a circulation pump for forcibly circulating coolants in the reactor container and an operational device is provided for receiving each of the signals concerning number of notches for each of the control rods and flow control depending on the xenon poisoning effect obtained from the signals derived from the in-core instrument system connected to the reactor core. The operational device is connected with a control rod drive for moving each of the control rods up and down and a recycle flow control device. The operational device is set with a pattern for the aimed control rod power and the sequence of extraction. Upon extraction of the control rods, they are extracted successively from those having less notch numbers. (Moriyama, K.)

  17. Thermal properties of biopolyol from oil palm fruit fibre (OPFF) using solvolysis liquefaction technique

    Science.gov (United States)

    Kormin, Shaharuddin; Rus, Anika Zafiah M.; Azahari, M. Shafiq M.

    2017-09-01

    Liquefaction is known to be an effective method for converting biomass into a biopolyol. The biomass liquefaction of oil palm fruit waste (PFW) in the presence of liquefaction solvent/polyhydric alcohol (PA): polyethylene glycol 400 (PEG400) using sulfuric acid as catalyst was studied. For all experiments, the liquefaction was conducted at 150°C and atmospheric pressure. The mass ratio of OPFW to liquefaction solvents used in all the experiments was, 1/3. Thermogravimetric analyses (TGA) were used to analyze their biopolyol and residue behaviors. It was found that thermal stability of oil palm mesocarp fibre (PM), oil palm shell (PS) and oil palm kernel (PK) fibre exhibited the first degradation of hard segment at (232, 104, 230°C) and the second degradation of soft segment at (314, 226, 412°C) as compared to PM, PS and PK residue which (229, 102, 227°C) of hard segment and (310, 219, 299°C) of segment, respectively. This behavior of thermal degradation of the hard segment and soft segment of biopolyol was changes after undergo solvolysis liquefaction process. The result analysis showed that the resulting biopolyol and its residue was suitable monomer for polyurethane (PU) synthesis for the production of PU foams.

  18. Prediction of strain energy-based liquefaction resistance of sand-silt mixtures: An evolutionary approach

    Science.gov (United States)

    Baziar, Mohammad H.; Jafarian, Yaser; Shahnazari, Habib; Movahed, Vahid; Amin Tutunchian, Mohammad

    2011-11-01

    Liquefaction is a catastrophic type of ground failure, which usually occurs in loose saturated soil deposits under earthquake excitations. A new predictive model is presented in this study to estimate the amount of strain energy density, which is required for the liquefaction triggering of sand-silt mixtures. A wide-ranging database containing the results of cyclic tests on sand-silt mixtures was first gathered from previously published studies. Input variables of the model were chosen from the available understandings evolved from the previous studies on the strain energy-based liquefaction potential assessment. In order to avoid overtraining, two sets of validation data were employed and a particular monitoring was made on the behavior of the evolved models. Results of a comprehensive parametric study on the proposed model are in accord with the previously published experimental observations. Accordingly, the amount of strain energy required for liquefaction onset increases with increase in initial effective overburden pressure, relative density, and mean grain size. The effect of nonplastic fines on strain energy-based liquefaction resistance shows a more complicated behavior. Accordingly, liquefaction resistance increases with increase in fines up to about 10-15% and then starts to decline for a higher increase in fines content. Further verifications of the model were carried out using the valuable results of some downhole array data as well as centrifuge model tests. These verifications confirm that the proposed model, which was derived from laboratory data, can be successfully utilized under field conditions.

  19. Effect of pre-swelling of coal on its solvent extraction and liquefaction properties

    Energy Technology Data Exchange (ETDEWEB)

    Hengfu Shui; Zhicai Wang; Meixia Cao [Anhui University of Technology, Ma' anshan (China). School of Chemistry and Chemical Engineering

    2008-10-15

    Effects of pre-swelling of coal on solvent extraction and liquefaction properties were studied with Shenhua coal. It was found that pre-swelling treatments of the coal in three solvents, i.e., toluene (TOL), N-methyl-2-pyrrolidinone (NMP) and tetralin (THN) increased its extraction yield and liquefaction conversion, and differed the liquefied product distributions. The pre-swollen coals after removing the swelling solvents showed increased conversion in liquefaction compared with that of the swollen coals in the presence of swelling solvents. It was also found that the yields of (oil + gas) in liquefaction of the pre-swollen coals with NMP and TOL dramatically decreased in the presence of swelling solvent. TG and FTIR analyses of the raw coal, the swollen coals and the liquefied products were carried out in order to investigate the mechanism governing the effects of pre-swelling treatment on coal extraction and liquefaction. The results showed that the swelling pre-treatment could disrupt some non-covalent interactions of the coal molecules, relax its network structure and loosened the coal structure. It would thus benefit diffusion of a hydrogen donor solvent into the coal structure during liquefaction, and also enhance the hydrogen donating ability of the hydrogen-rich species derived from the coal. 21 refs., 4 figs., 3 tabs.

  20. Preliminary study of soil liquefaction hazard at Terengganu shoreline, Peninsular Malaysia

    Science.gov (United States)

    Hashim, H.; Suhatril, M.; Hashim, R.

    2017-06-01

    Terengganu is a shoreline state located in Peninsular Malaysia which is a growing hub for port industries and tourism centre. The northern part offers pristine settings of a relax beach areas whereas the southern part are observed to be a growing centre for development. The serious erosion on soil deposit along the beach line presents vulnerable soil condition to soil liquefaction consists of sandy with low plasticity and shallow ground water. Moreover, local earthquake from nearby fault have present significant tremors over the past few years which need to be considered in the land usage or future development in catering the seismic loading. Liquefaction analysis based on field standard penetration of soil is applied on 546 boreholes scattered along the shoreline areas ranging 244 km of shoreline stretch. Based on simplified approach, it is found that more than 70% of the studied areas pose high liquefaction potential since there are saturated loose sand and silt deposits layer ranges at depth 3 m and up to 20 m. The presence of clay deposits and hard stratum at the remaining 30% of the studied areas shows good resistance to soil liquefaction hence making the area less significant to liquefaction hazard. Result indicates that liquefaction improving technique is advisable in future development of shoreline areas of Terengganu state.

  1. Japan`s New Sunshine Project. 20. 1995 annual summary of coal liquefaction and gasification

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1996-10-01

    The paper described a summary of the 1995 study on coal liquefaction and gasification under the New Sunshine Project. As for coal liquefaction, a study was made of liquefaction characteristics and catalysts of various coals. Also studied were liquefaction conditions for quality improvement of liquefaction products, an evaluation method of quality of coal liquid, and a utilization method of coal liquid. In order to prevent carbonization and realize effective liquefaction, a study was conducted for elucidation of the reaction mechanism of high pressure hydrogenation. In a 150t/d pilot plant using hydrogen transfer hydrogenation solvents, the NEDOL method was studied using various catalysts and kinds of coals. This is a step prior to data acquisition for engineering, actual construction of equipment and operation. A 1t/d process supporting unit is a unit to support it. The unit conducts studies on slurry letdown valves and synthetic iron sulfide catalysts, screening of Chinese coals, etc. As to coal gasification, the paper added to the basic research the combined cycle power generation using entrained flow coal gasification for improvement of thermal efficiency and environmental acceptability and the HYCOL method for hydrogen production. 68 refs., 40 figs.

  2. Effect of Recycle Solvent Hydrotreatment on Oil Yield of Direct Coal Liquefaction

    Directory of Open Access Journals (Sweden)

    Shansong Gao

    2015-07-01

    Full Text Available Effects of the recycle solvent hydrotreatment on oil yield of direct coal liquefaction were carried out in the 0.18 t/day direct coal liquefaction bench support unit of National Engineering Laboratory for Direct Coal Liquefaction (China. Results showed that the hydrogen-donating ability of the hydrogenated recycle solvent improved and the hydrogen consumption of solvent hydrotreatment was increased by decreasing liquid hourly space velocity (LHSV from 1.5 to 1.0 h−1 and increasing reaction pressure from 13.7 to 19.0 MPa. The hydrogen-donating ability of the hydrogenated recycle solvent was enhanced, thus promoting the oil yield and coal conversion of the liquefaction reaction. The coal conversion and distillates yield of coal liquefaction were increased from 88.74% to 88.82% and from 47.41% to 49.10%, respectively, with the increase in the solvent hydrotreatment pressure from 13.7 to 19.0 MPa. The coal conversion and distillates of coal liquefaction were increased from 88.82% to 89.27% and from 49.10% to 54.49%, respectively, when the LHSV decreased from 1.5 to 1.0 h−1 under the solvent hydrotreatment pressure of 19.0 MPa.

  3. A novel process for small-scale pipeline natural gas liquefaction

    International Nuclear Information System (INIS)

    He, T.B.; Ju, Y.L.

    2014-01-01

    Highlights: • A novel process was proposed to liquefy natural gas by utilizing the pressure exergy. • The process is zero energy consumption. • The maximum liquefaction rate of the process is 12.61%. • The maximum exergy utilization rate is 0.1961. • The economic analysis showed that the payback period of the process is quit short. - Abstract: A novel process for small-scale pipeline natural gas liquefaction is designed and presented. The novel process can utilize the pressure exergy of the pipeline to liquefy a part of natural gas without any energy consumption. The thermodynamic analysis including mass, energy balance and exergy analysis are adopted in this paper. The liquefaction rate and exergy utilization rate are chosen as the objective functions. Several key parameters are optimized to approach the maximum liquefaction rate and exergy utilization rate. The optimization results showed that the maximum liquefaction rate is 12.61% and the maximum exergy utilization rate is 0.1961. What is more, the economic performances of the process are also discussed and compared by using the maximum liquefaction rate and exergy utilization rate as indexes. In conclusion, the novel process is suitable for pressure exergy utilization due to its simplicity, zero energy consumption and short payback period

  4. Motor fuels made by direct liquefaction of coal, peat and biomass. Drivmedel genom direktfoervaetskning av kol, torv och biomassa

    Energy Technology Data Exchange (ETDEWEB)

    Granath, L; Karlsson, G; Karlsson, G; Nilsson, T

    1981-01-01

    The Department of Chemical Technology at the Royal Institute of Technology has completed a system study concerning direct liquefaction of peat and biomass to produce transportation fuel. A comprehensive survey of coal liquefaction is included. Gasoline produced in Sweden from direct liquefaction of imported coal may compete with regular gasoline at the earliest around 1985. Biomass can become a competitive alternative to black coal at the beginning of the 21st century. Methanol can be produced from wood with a higher efficiency than the transportation fuels which are produced by direct liquefaction. The peat is not good source for liquefaction as wood chips. A continuously working liquefaction plant designed also for peat among other substances is under construction at the Royal Institute of Technology, Stockholm.

  5. Safety device for nuclear reactor

    International Nuclear Information System (INIS)

    Jacquelin, Roland.

    1977-01-01

    This invention relates to a safety device for a nuclear reactor, particularly a liquid metal (generally sodium) cooled fast reactor. This safety device includes an absorbing element with a support head connected by a disconnectable connector formed by the armature of an electromagnet at the end of an axially mobile vertical control rod. This connection is so designed that in the event of it becoming disconnected, the absorbing element gravity slides in a passage through the reactor core into an open container [fr

  6. Nuclear reactor

    International Nuclear Information System (INIS)

    Hattori, Sadao; Sekine, Katsuhisa.

    1987-01-01

    Purpose: To decrease the thickness of a reactor container and reduce the height and the height and plate thickness of a roof slab without using mechanical vibration stoppers. Constitution: Earthquake proofness is improved by filling fluids such as liquid metal between a reactor container and a secondary container and connecting the outer surface of the reactor container with the inner surface of the secondary container by means of bellows. That is, for the horizontal seismic vibrations, horizontal loads can be supported by the secondary container without providing mechanical vibration stoppers to the reactor container and the wall thickness can be reduced thereby enabling to simplify thermal insulation structure for the reduction of thermal stresses. Further, for the vertical seismic vibrations, verical loads can be transmitted to the secondary container thereby enabling to reduce the wall thickness in the same manner as for the horizontal load. By the effect of transferring the point of action of the container load applied to the roof slab to the outer circumferential portion, the intended purpose can be attained and, in addition, the radiation dose rate at the upper surface of the roof slab can be decreased. (Kamimura, M.)

  7. Reactor system

    International Nuclear Information System (INIS)

    Miyano, Hiroshi; Narabayashi, Naoshi.

    1990-01-01

    The represent invention concerns a reactor system with improved water injection means to a pressure vessel of a BWR type reactor. A steam pump is connected to a heat removing system pipeline, a high pressure water injection system pipeline and a low pressure water injection system pipeline for injecting water into the pressure vessel. A pump actuation pipeline is disposed being branched from a main steam pump or a steam relieaf pipeline system, through which steams are supplied to actuate the steam pump and supply cooling water into the pressure vessel thereby cooling the reactor core. The steam pump converts the heat energy into the kinetic energy and elevates the pressure of water to a level higher than the pressure of the steams supplied by way of a pressure-elevating diffuser. Cooling water can be supplied to the pressure vessel by the pressure elevation. This can surely inject cooling water into the pressure vessel upon loss of coolant accident or in a case if reactor scram is necessary, without using an additional power source. (I.N.)

  8. Nuclear reactors

    International Nuclear Information System (INIS)

    Matheson, J.E.

    1983-01-01

    A nuclear reactor has an upper and a lower grid plate. Protrusions project from the upper grid plate. Fuel assemblies having end fittings fit between the grid plates. An arrangement is provided for accepting axial forces generated during the operation of the nuclear reactor by the flow of the cooling medium and thermal expansion and irradiation-induced growth of the fuel assembly, which comprises rods. Each fuel assembly rests on the lower grid plate and its upper end is elastically supported against the upper grid plate by the above-mentioned arrangement. The arrangement comprises four (for example) torsion springs each having a torsion tube and a torsion bar nested within the torsion tube and connected at one end thereto. The other end of the torsion bar is connected to an associated one of four lever arms. The torsion tube is rigidly connected to the other end fitting and the springs are disposed such that the lever arms are biassed against the protrusions. (author)

  9. Demineralization of Sargassum spp. Macroalgae Biomass: Selective Hydrothermal Liquefaction Process for Bio-Oil Production

    Energy Technology Data Exchange (ETDEWEB)

    Díaz-Vázquez, Liz M., E-mail: limdiaz@uprrp.edu; Rojas-Pérez, Arnulfo; Fuentes-Caraballo, Mariela; Robles, Isis V. [Department of Chemistry, University of Puerto Rico Río Piedras Campus, San Juan, PR (United States); Jena, Umakanta [Bioenergy Laboratory, Desert Research Institute, Reno, NV (United States); Das, K. C. [College of Engineering, University of Georgia, Athens, GA (United States)

    2015-02-11

    Algae biomasses are considered a viable option for the production of biofuel because of their high yields of oil produced per dry weight. Brown macroalgae Sargassum spp. are one of the most abundant species of algae in the shores of Puerto Rico. Its availability in large quantity presents a great opportunity for use as a source of renewable energy. However, high ash content of macroalgae affects the conversion processes and the quality of resulting fuel products. This research studied the effect of different demineralization treatments of Sargassum spp. biomass, subsequent hydrothermal liquefaction (HTL), and bio-oil characterization. Demineralization constituted five different treatments: nanopure water, nitric acid, citric acid, sulfuric acid, and acetic acid. Performance of demineralization was evaluated by analyzing both demineralized biomass and HTL products by the following analyses: total carbohydrates, proteins, lipids, ash content, caloric content, metals analysis, Fourier transform infrared-attenuated total reflectance spectroscopy, energy dispersive spectroscopy, scanning electron microscopy, and GCMS analysis. HTL of Sargassum spp. before and after citric acid treatment was performed in a 1.8 L batch reactor system at 350°C with a holding time of 60 min and high pressures (5–21 MPa). Demineralization treatment with nitric acid was found the most effective in reducing the ash content of the macroalgae biomass from 27.46 to 0.99% followed by citric acid treatment that could reduce the ash content to 7%. Citric acid did not show significant leaching of organic components such as carbohydrates and proteins, and represented a less toxic and hazardous option for demineralization. HTL of untreated and citric acid treated Sargassum spp. resulted in bio-oil yields of 18.4 ± 0.1 and 22.2 ± 0.1% (ash-free dry basis), respectively.

  10. Demineralization of Sargassum spp. Macroalgae Biomass: Selective Hydrothermal Liquefaction Process for Bio-Oil Production

    International Nuclear Information System (INIS)

    Díaz-Vázquez, Liz M.; Rojas-Pérez, Arnulfo; Fuentes-Caraballo, Mariela; Robles, Isis V.; Jena, Umakanta; Das, K. C.

    2015-01-01

    Algae biomasses are considered a viable option for the production of biofuel because of their high yields of oil produced per dry weight. Brown macroalgae Sargassum spp. are one of the most abundant species of algae in the shores of Puerto Rico. Its availability in large quantity presents a great opportunity for use as a source of renewable energy. However, high ash content of macroalgae affects the conversion processes and the quality of resulting fuel products. This research studied the effect of different demineralization treatments of Sargassum spp. biomass, subsequent hydrothermal liquefaction (HTL), and bio-oil characterization. Demineralization constituted five different treatments: nanopure water, nitric acid, citric acid, sulfuric acid, and acetic acid. Performance of demineralization was evaluated by analyzing both demineralized biomass and HTL products by the following analyses: total carbohydrates, proteins, lipids, ash content, caloric content, metals analysis, Fourier transform infrared-attenuated total reflectance spectroscopy, energy dispersive spectroscopy, scanning electron microscopy, and GCMS analysis. HTL of Sargassum spp. before and after citric acid treatment was performed in a 1.8 L batch reactor system at 350°C with a holding time of 60 min and high pressures (5–21 MPa). Demineralization treatment with nitric acid was found the most effective in reducing the ash content of the macroalgae biomass from 27.46 to 0.99% followed by citric acid treatment that could reduce the ash content to 7%. Citric acid did not show significant leaching of organic components such as carbohydrates and proteins, and represented a less toxic and hazardous option for demineralization. HTL of untreated and citric acid treated Sargassum spp. resulted in bio-oil yields of 18.4 ± 0.1 and 22.2 ± 0.1% (ash-free dry basis), respectively.

  11. Demineralization of Sargassum spp. macroalgae biomass: selective hydrothermal liquefaction process for bio-oil production

    Directory of Open Access Journals (Sweden)

    Liz M Díaz-Vázquez

    2015-02-01

    Full Text Available Algae biomasses are considered a viable option for the production of biofuel because of their high yields of oil produced per dry weight. Brown macroalgae Sargassum spp. are one of the most abundant species of algae in the shores of Puerto Rico. Its availability in large quantity presents a great opportunity for use as a source of renewable energy. However, high ash content of macroalgae affects the conversion processes and the quality of resulting fuel products. This research studied the effect of different demineralization treatments of Sargassum spp. biomass, subsequent hydrothermal liquefaction (HTL and bio-oil characterization. Demineralization constituted five different treatments: nanopure water, nitric acid, citric acid, sulfuric acid, and acetic acid. Performance of demineralization was evaluated by analyzing both demineralized biomass and HTL products by the following analyses: total carbohydrates, proteins, lipids, ash content, caloric content, metals analysis, Fourier Transform Infrared - Attenuated Total Reflectance (FTIR-ATR Spectroscopy, Energy Dispersive Spectroscopy (EDS, Scanning Electron Microscopy (SEM, and GCMS analysis. HTL of Sargassum spp. before and after citric acid treatment, was performed in a 1.8 L batch reactor system at 350°C with a holding time of 60 min and high pressures (5-21 MPa. Demineralization treatment with nitric acid was found the most effective in reducing the ash content of the macroalgae biomass from 27.46% to 0.99% followed by citric acid treatment that could reduce the ash content to 7%. Citric acid did not show significant leaching of organic components such as carbohydrates and proteins, and represented a less toxic and hazardous option for demineralization. HTL of untreated and citric acid treated Sargassum spp. resulted in bio-oil yields of 18.4±0.1 % and 22.2±0.1 % (ash free dry basis, respectively.

  12. Reactor container

    International Nuclear Information System (INIS)

    Ichiki, Tadaharu; Saba, Kazuhisa.

    1979-01-01

    Purpose: To improve the earthquake resistance as well as reduce the size of a container for a nuclear reactor with no adverse effects on the decrease of impact shock to the container and shortening of construction step. Constitution: Reinforcing profile steel materials are welded longitudinally and transversely to the inner surface of a container, and inner steel plates are secured to the above profile steel materials while keeping a gap between the materials and the container. Reactor shielding wall planted to the base concrete of the container is mounted to the pressure vessel, and main steam pipeways secured by the transverse beams and led to the outside of container is connected. This can improve the rigidity earthquake strength and the safetiness against the increase in the inside pressure upon failures of the container. (Yoshino, Y.)

  13. Co-liquefaction of micro algae with coal. 2; Bisai sorui to sekitan no kyoekika hanno. 2

    Energy Technology Data Exchange (ETDEWEB)

    Ueda, C.; Matsui, T.; Otsuki, M.; Ikenaga, N.; Suzuki, T. [Kansai University, Osaka (Japan). Faculty of Engineering

    1996-10-28

    For the removal and recycle of CO2, a global warming gas, utilization of photosynthesis by micro algae is investigated. Formed micro algae are decomposed into CO2, H2O and CH4 again, which does not result in the permanent fixation. For the effective utilization of these micro algae, creation of petroleum alternate energy was tried through the co-liquefaction of micro algae with coal. Were investigated influences of the reaction temperature during the co-liquefaction and influences of catalysts, such as Fe(CO)5-S, Ru(CO)12, and Mo(CO)6-S, which are effective for the coal liquefaction. Micro algae, such as chlorella, spirulina, and littorale, and Yallourn brown coal were tested. It was found that co-liquefaction of micro algae with coal can be successfully proceeded under the same conditions as the liquefaction of coal. The oil yield obtained from the co-liquefaction in the presence of Fe(CO)5-S, an effective catalyst for coal liquefaction, agreed appropriately with the arithmetical mean value from separate liquefaction of coal and micro algae. It was suggested that pyrrhotite, an active species for coal liquefaction, was sufficiently formed by increasing the addition of sulfur. 2 refs., 7 figs., 1 tab.

  14. Nuclear reactor safety systems

    International Nuclear Information System (INIS)

    Ball, R.M.; Roberts, R.C.

    1980-01-01

    A safety system for shutting down a nuclear reactor under overload conditions is described. The system includes a series of parallel-connected computer memory type look-up tables each of which receives data on a particular reactor parameter and in each of which a precalculated functional value for that parameter is stored indicative of the percentage of maximum reactor load that the parameter contributes. The various functional values corresponding to the actual measured parameters are added together to provide a control signal used to shut down the reactor under overload conditions. (U.K.)

  15. Experimental assessment of the liquefaction resistance of calcareous biogenous sands

    Directory of Open Access Journals (Sweden)

    Sandoval Eimar

    2012-10-01

    Full Text Available

    ABSTRACT

    Liquefaction is a phenomenon in which soils, typically sands, suddenly loose a substantial amount of their shear strength and stiffness, this often triggered by large-magnitude earthquakes. Most liquefaction research has focused on silicate-based sands and not on other sand types, such as calcareous biogenous sands Calcareous sands are usually composed of skeletal or non-skeletal remains of marine organisms, with unique characteristics in terms of their mineralogy surface roughness, particle shape, crushability, and intraparticle porosity. The unique characteristics of calcareous sands suggest that their geotechnical engineering behaviour can be substantially different compared to that of terrigenous sands, including their behaviour under seismic loading, which have not been very well studied

    This paper presents the results of an experimental programme aimed at studying the cyclic liquefaction resistance of uncemented calcareous biogenous sands retrieved from south-western Puerto Rico Evaluation of liquefaction potential involved a comprehensive set of isotropically consolidated undrained cyclic triaxial tests on reconstituted samples of this calcareous sand. The programme also included tests on Ottawa terrigenous silica sand samples prepared and tested in similar conditions for comparison purposes.

    In general, the experimental results showed that Cabo Rojo calcareous sands had higher liquefaction resistance compared to Ottawa silica sands tested under similar conditions. Important differences between calcareous and silica sands regarding pore pressure generation characteristics and axial strain accumulation were also observed


  16. Refueling of nuclear reactor

    International Nuclear Information System (INIS)

    Kaufmann, J.W.; Swidwa, K.J.; Hornak, L.P.

    1989-01-01

    This patent describes an apparatus for refueling a nuclear reactor, the reactor being disposed for refueling under water in a pit in a containment, the apparatus including a bridge to be mounted moveably over the pit on the containment, first means connected to the bridge, for moving the bridge forward and backward on the containment over the pit along a first path, a first pulse generator, connected to the moving means, responsive to the movement of the bridge, for producing pulses, means, connected to the generator,for counting the pulses, the count of the pulses being dependent on the distance of the movement of the bridge

  17. Liquefaction susceptibility of fine-grained soils: preliminary study report. Final report, September 1985-March 1986

    Energy Technology Data Exchange (ETDEWEB)

    Chang, N.Y.

    1987-09-01

    Soil liquefaction, a hazardous ground failure induced by strong motion earthquakes, can cause catastrophic damage to structures such as dams, bridges, power plants, and water-front structures and may involve great losses of life. Examples of liquefaction and resulting damage were observed during the Alaska (1964), Niigata, Japan (1964), and Tangshan, China (1976), earthquakes. Ground failure due to earthquake-induced soil liquefaction may manifest itself as excessive settlement, loss of bearing capacity, sand boiling, and flow slides. The liquefaction potential of clean sands has been studied extensively for the last two decades. However, case histories revealed that liquefied sands were seldom clean. They may contain various percentages of silt or clay or both. In fact, the Chinese observation in the Tansghan earthquake indicated that some cohesive soils may have liquefied. If this indeed had happened, then structures underlain by fine-grained soils, with a marginal safety factor based on the liquefaction criteria normally applied to sands, may actually be unsafe. Thus there is an urgent need for establishing new criteria for the liquefaction susceptibility of soils to include those identified as fine-grained. The author, Professor N.Y. Chang of the University of Colorado at Denver, visited several Chinese agencies and and universities in and near Beijing, China, in the summer of 1985 in an attempt to investigate and verify reported data on the liquefaction of cohesive soils during the Tangshan earthquake of 1976 and to negotiate cooperative research into the problem. This report presents the result of supportive literature review and the findings of the China trip.

  18. Design of a Natural Gas Liquefaction System with Minimum Components

    International Nuclear Information System (INIS)

    Bergese, Franco

    2004-01-01

    In this work an economic method for liquefying natural gas by diminishing its temperature by means of the Joule-Thomson effect is presented.The pressures from and to which the gas must be expanded arose from a thermodynamic calculation optimizing the cost per unit mass of Liquefied Natural Gas LNG).It was determined that the gas should be expanded from 200 atm to 4 atm.This expansion ratio can be used in different scales.Large Scale: liquefaction of gas at well.It takes advantage of the fact that the gas inside the well is stored at high pressure.The gas is expanded in a valve / nozzle and then compressed to the pressure of the local pipeline system.The objective of this project is to export natural gas as LNG, which is transported by ships to the markets of consumption.Using this method of liquefaction, the LNG production levels are limited to a fraction of the production of the well, due to the injection of the un condensed gas into the local pipelines system.Medium Scale: A high pressure pipeline is the source of the gas.The expansion is performed and then the gas is again compressed to the pressure of a lower pressure pipeline into which the gas is injected.The pressure reductions of natural gas are performed nearby big cities.The aim of this project scale is the storage of fuel for gas thermal power plants during periods of low energy consumption for later burning when the resource is limited. Another possibility that offers this size of plant is the transportation of gas to regions where the resource is unavailable.This transportation would be carried out by means of cistern trucks, in the same way that conventional liquid fuels are transported.Small scale: the place of production would be a CNG refueling station. The source of gas is in this case a gas pipeline of urban distribution and the gas should be compressed with the compressor of the refueling station.Compressors have generally low loading factor and the periods of time when they are not producing

  19. Characterisation of Liquefaction Effects for Beyond-Design Basis Safety Assessment of Nuclear Power Plants

    Science.gov (United States)

    Bán, Zoltán; Győri, Erzsébet; János Katona, Tamás; Tóth, László

    2015-04-01

    Preparedness of nuclear power plants to beyond design base external effects became high importance after 11th of March 2011 Great Tohoku Earthquakes. In case of some nuclear power plants constructed at the soft soil sites, liquefaction should be considered as a beyond design basis hazard. The consequences of liquefaction have to be analysed with the aim of definition of post-event plant condition, identification of plant vulnerabilities and planning the necessary measures for accident management. In the paper, the methodology of the analysis of liquefaction effects for nuclear power plants is outlined. The case of Nuclear Power Plant at Paks, Hungary is used as an example for demonstration of practical importance of the presented results and considerations. Contrary to the design, conservatism of the methodology for the evaluation of beyond design basis liquefaction effects for an operating plant has to be limited to a reasonable level. Consequently, applicability of all existing methods has to be considered for the best estimation. The adequacy and conclusiveness of the results is mainly limited by the epistemic uncertainty of the methods used for liquefaction hazard definition and definition of engineering parameters characterizing the consequences of liquefaction. The methods have to comply with controversial requirements. They have to be consistent and widely accepted and used in the practice. They have to be based on the comprehensive database. They have to provide basis for the evaluation of dominating engineering parameters that control the post-liquefaction response of the plant structures. Experience of Kashiwazaki-Kariwa plant hit by Niigata-ken Chuetsu-oki earthquake of 16 July 2007 and analysis of site conditions and plant layout at Paks plant have shown that the differential settlement is found to be the dominating effect in case considered. They have to be based on the probabilistic seismic hazard assessment and allow the integration into logic

  20. Experiments on graphite block gaps connected with leak flow in bottom-core structure of experimental very high-temperature gas-cooled reactor

    International Nuclear Information System (INIS)

    Kikuchi, Kenji; Futakawa, Masatoshi; Takizuka, Takakazu; Kaburaki, Hideo; Sanokawa, Konomo

    1984-01-01

    In order to minimize the leak flow rate of an experimental VHTR (a multi-purpose very high-temperature gas-cooled reactor), the graphite blocks are tightened to reduce the gap distance between blocks by core restrainers surrounded outside of the fixed reflectors of the bottom-core structure and seal elements are placed in the gaps. By using a 1/2.75-scale model of the bottom-core structure, the experiments on the following items have been carried out: a relationship between core restraint force and block gap, a relationship between core restraint force and inclined angle of the model, leak flow characteristics of seal elements etc. The conclusions derived from the experiments are as follows: (1) Core restraint force is significantly effective for decreasing the gap distance between hot plenum blocks, but ineffective for the gap between hot plenum block and fixed reflector. (2) Graphite seal element reduces the leak flow rate from the top surface of hot plenum block into plenum region to one-third. (author)

  1. Properties of Direct Coal Liquefaction Residue Modified Asphalt Mixture

    Directory of Open Access Journals (Sweden)

    Jie Ji

    2017-01-01

    Full Text Available The objectives of this paper are to use Direct Coal Liquefaction Residue (DLCR to modify the asphalt binders and mixtures and to evaluate the performance of modified asphalt mixtures. The dynamic modulus and phase angle of DCLR and DCLR-composite modified asphalt mixture were analyzed, and the viscoelastic properties of these modified asphalt mixtures were compared to the base asphalt binder SK-90 and Styrene-Butadiene-Styrene (SBS modified asphalt mixtures. The master curves of the asphalt mixtures were shown, and dynamic and viscoelastic behaviors of asphalt mixtures were described using the Christensen-Anderson-Marasteanu (CAM model. The test results show that the dynamic moduli of DCLR and DCLR-composite asphalt mixtures are higher than those of the SK-90 and SBS modified asphalt mixtures. Based on the viscoelastic parameters of CAM models of the asphalt mixtures, the high- and low-temperature performance of DLCR and DCLR-composite modified asphalt mixtures are obviously better than the SK-90 and SBS modified asphalt mixtures. In addition, the DCLR and DCLR-composite modified asphalt mixtures are more insensitive to the frequency compared to SK-90 and SBS modified asphalt mixtures.

  2. Air liquefaction and enrichment system propulsion in reusable launch vehicles

    Science.gov (United States)

    Bond, W. H.; Yi, A. C.

    1994-07-01

    A concept is shown for a fully reusable, Earth-to-orbit launch vehicle with horizontal takeoff and landing, employing an air-turborocket for low speed and a rocket for high-speed acceleration, both using liquid hydrogen for fuel. The turborocket employs a modified liquid air cycle to supply the oxidizer. The rocket uses 90% pure liquid oxygen as its oxidizer that is collected from the atmosphere, separated, and stored during operation of the turborocket from about Mach 2 to 5 or 6. The takeoff weight and the thrust required at takeoff are markedly reduced by collecting the rocket oxidizer in-flight. This article shows an approach and the corresponding technology needs for using air liquefaction and enrichment system propulsion in a single-stage-to-orbit (SSTO) vehicle. Reducing the trajectory altitude at the end of collection reduces the wing area and increases payload. The use of state-of-the-art materials, such as graphite polyimide, in a direct substitution for aluminum or aluminum-lithium alloy, is critical to meet the structure weight objective for SSTO. Configurations that utilize 'waverider' aerodynamics show great promise to reduce the vehicle weight.

  3. An entropy flow optimization technique for helium liquefaction cycles

    International Nuclear Information System (INIS)

    Minta, M.; Smith, J.L.

    1984-01-01

    This chapter proposes a new method of analyzing thermodynamic cycles based on a continuous distribution of precooling over the temperature range of the cycle. The method gives the optimum distribution of precooling over the temperature range of the cycle by specifying the mass flow to be expanded at each temperature. The result is used to select a cycle configuration with discrete expansions and to initialize the independent variables for final optimization. Topics considered include the continuous precooling model, the results for ideal gas, the results for real gas, and the application to the design of a saturated vapor compression (SVC) cycle. The optimization technique for helium liquefaction cycles starts with the minimization of the generated entropy in a cycle model with continuous precooling. The pressure ratio, the pressure level and the distribution of the heat exchange are selected based on the results of the continuous precooling analysis. It is concluded that the technique incorporates the non-ideal behavior of helium in the procedure and allows the trade-off between heat exchange area and losses to be determined

  4. [Longjintonglin Capsules for type IIIA prostatitis accompanied by abnormal semen liquefaction: A clinical observation].

    Science.gov (United States)

    Cai, Hong-cai; Wan, Chang-chun; Geng, Qiang; Liu, Wei; Zhang, Guo-wei; Shang, Xue-jun; Huang, Yu-feng

    2016-01-01

    To evaluate the therapeutic effect of Longjintonglin Capsules on type IIIA prostatitis accompanied by abnormal semen liquefaction. We selected 140 patients with type IIIA prostatitis accompanied by abnormal semen liquefaction according to the diagnostic standards of the American Institutes of Health (NIH) and treated them with Longjintonglin Capsules orally 3 capsules once tid for 12 weeks. We obtained the NIH Chronic Prostatitis Symptom Indexes (NIH-CPSI), traditional Chinese medicine (TCM) syndrome scores, leukocyte count in the expressed prostatic secretion (EPS), semen liquefaction time, and the results of semen analysis and compared these indicators before and after the treatment. Of the 140 cases, 132 were included in this study, excluding 8 due to their incomplete case histories. Before and after 4, 8 and 12 weeks of medication, the total NIH-CPSI scores were 24.52 ± 5.43, 21.28 ± 4.85, 18.01 ± 4.28, and 14.49 ± 3.65 (P prostatitis were cured and another 72 well responded, with an overall response rate of 78.0%. Of those with abnormal semen liquefaction, 61 were cured, 39 well responded, and 32 failed to respond, with an overall effectiveness rate of 75.8%. Semen analysis showed significantly increased percentage of progressively motile sperm after 4, 8 and 12 weeks of medication as compared with the baseline (P prostatitis accompanied by abnormal semen liquefaction.

  5. A spotlight on liquefaction: evidence from clinical settings and experimental models in tuberculosis.

    Science.gov (United States)

    Cardona, Pere-Joan

    2011-01-01

    Liquefaction is one of the most intriguing aspects of human tuberculosis. It is a major cause of the transition from the infection to active disease (tuberculosis, TB) as well as the transmission of M. tuberculosis to other persons. This paper reviews the natural history of liquefaction in humans from a pathological and radiological point of view and discusses how the experimental models available can be used to address the topic of liquefaction and cavity formation. Different concepts that have been related to liquefaction, from the influence of immune response to mechanical factors, are reviewed. Synchronic necrosis or apoptosis of infected macrophages in a close area, together with an ineffective fibrosis, appears to be clue in this process, in which macrophages, the immune response, and bacillary load interact usually in a particular scenario: the upper lobes of the lung. The summary would be that even if being a stochastic effect, liquefaction would result if the organization of the intragranulomatous necrosis (by means of fibrosis) would be disturbed.

  6. A Spotlight on Liquefaction: Evidence from Clinical Settings and Experimental Models in Tuberculosis

    Directory of Open Access Journals (Sweden)

    Pere-Joan Cardona

    2011-01-01

    Full Text Available Liquefaction is one of the most intriguing aspects of human tuberculosis. It is a major cause of the transition from the infection to active disease (tuberculosis, TB as well as the transmission of M. tuberculosis to other persons. This paper reviews the natural history of liquefaction in humans from a pathological and radiological point of view and discusses how the experimental models available can be used to address the topic of liquefaction and cavity formation. Different concepts that have been related to liquefaction, from the influence of immune response to mechanical factors, are reviewed. Synchronic necrosis or apoptosis of infected macrophages in a close area, together with an ineffective fibrosis, appears to be clue in this process, in which macrophages, the immune response, and bacillary load interact usually in a particular scenario: the upper lobes of the lung. The summary would be that even if being a stochastic effect, liquefaction would result if the organization of the intragranulomatous necrosis (by means of fibrosis would be disturbed.

  7. Catalytic activity of pyrite for coal liquefaction reaction; Tennen pyrite no shokubai seino ni kansuru kento

    Energy Technology Data Exchange (ETDEWEB)

    Hirano, K.; Kozu, M.; Okada, T.; Kobayashi, M. [Nippon Coal Oil Co. Ltd., Tokyo (Japan)

    1996-10-28

    Since natural pyrite is easy to obtain and cheap as coal liquefaction catalyst, it is to be used for the 150 t/d scale NEDOL process bituminous coal liquefaction pilot plant. NEDO and NCOL have investigated the improvement of catalytic activity of pulverized natural pyrite for enhancing performance and economy of the NEDOL process. In this study, coal liquefaction tests were conducted using natural pyrite catalyst pulverized by dry-type bowl mill under nitrogen atmosphere. Mechanism of catalytic reaction of the natural pyrite was discussed from relations between properties of the catalyst and liquefaction product. The natural pyrite provided an activity to transfer gaseous hydrogen into the liquefaction product. It was considered that pulverized pyrite promotes the hydrogenation reaction of asphaltene because pulverization increases its contact rate with reactant and the amount of active points on its surface. It was inferred that catalytic activity of pyrite is affected greatly by the chemical state of Fe and S on its surface. 3 refs., 4 figs., 1 tab.

  8. Retesting of liquefaction and nonliquefaction case histories from the 1976 Tangshan earthquake

    Science.gov (United States)

    Moss, R.E.S.; Kayen, R.E.; Tong, L.-Y.; Liu, S.-Y.; Cai, G.-J.; Wu, J.

    2011-01-01

    A field investigation was performed to retest liquefaction and nonliquefaction sites from the 1976 Tangshan earthquake in China. These sites were carefully investigated in 1978 and 1979 by using standard penetration test (SPT) and cone penetration test (CPT) equipment; however, the CPT measurements are obsolete because of the now nonstandard cone that was used at the time. In 2007, a modern cone was mobilized to retest 18 selected sites that are particularly important because of the intense ground shaking they sustained despite their high fines content and/or because the site did not liquefy. Of the sites reinvestigated and carefully reprocessed, 13 were considered accurate representative case histories. Two of the sites that were originally investigated for liquefaction have been reinvestigated for cyclic failure of fine-grained soil and removed from consideration for liquefaction triggering. The most important outcome of these field investigations was the collection of more accurate data for three nonliquefaction sites that experienced intense ground shaking. Data for these three case histories is now included in an area of the liquefaction triggering database that was poorly populated and will help constrain the upper bound of future liquefaction triggering curves. ?? 2011 American Society of Civil Engineers.

  9. Fiscal 1991 report on the brown coal liquefaction section meeting; 1991 nendo kattan ekika bukai hokokusho

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1992-03-01

    At the 1st through 5th brown coal liquefaction group meetings held for the fiscal year, reports are delivered and discussions are made about the progress of research and development. At the 1st meeting, a fiscal 1991 brown coal liquefaction research plan is introduced, and discussed. At the 2nd meeting, an interim report on the brown coal liquefaction technology development project is discussed. At the 3rd meeting (a joint meeting of the brown coal and bituminous coal liquefaction groups), an agendum entitled 'what the development of brown/bituminous coal liquefaction technologies for the 21st century should be' is reported, and discussed. At the 4th meeting, reports are made on the results of deliberation at the Industrial Technology Council, progress of the follow-up study, progress of the collection of achievements, and so forth. At the 5th meeting, the outline of the follow-up study, the collection of achievements in the pilot plant study (a project report preparation schedule and materials evaluation), the progress of pilot plant dismantling work, etc., are reported and discussed. (NEDO)

  10. Fiscal 1989 report. Coal liquefaction committee; 1989 nendo sekitan ekika iinkai hokokusho

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1990-03-01

    The committee in this fiscal year had its 1st meeting in June 1989 and 2nd meeting in March 1990, when fiscal 1989 research and development programs and fiscal 1989 research and development results, etc., were reported and discussed. The operating status of the 1 ton/day PSU (process supporting unit) for bituminous coal liquefaction was reported and discussed. The report included its 1st operation for the demonstration of a long-term stable run under standard conditions that continued for trouble-free 50 days, the 2nd operation for the investigation of the effect of liquefaction reaction temperature in which the liquefaction yield recorded the maximum at 450 degrees C with the collection of coal oils of 55 wt.% on the average, and the 3rd operation for the investigation of the effects of liquefaction reaction pressure and catalyst injection size whose details were being analyzed. Reported in relation with the brown coal liquefaction pilot plant was a comprehensive operation of a series of 1st hydrogenation, solvent deashing, and 2nd hydrogenation processes completed after a continuous operation of 460 hours establishing a total operating time of 1050 hours. (NEDO)

  11. Assessment of Soil Liquefaction Potential in Defence Housing Authority, Karachi, Pakistan

    Directory of Open Access Journals (Sweden)

    Sumaira Asif Khan

    2017-04-01

    Full Text Available The occurrence of liquefaction phenomenon may be induced in the event of a large magnitude earthquake but sometimes loose, saturated and poorly graded sand may be subjected to liquefaction due to the vibration produced by other sources. Liquefaction could cause damage to building and infrastructure due to sudden increase of pore pressure in the loose layers of saturated sand causing the loss of bearing capacity and shear strength. Defence Housing Authority (DHA is the well planned residential scheme established by Pakistan Army along the coastal belt of Karachi. The soil occurring in DHA is fine grained, poorly graded and mainly comprises of sandy silt and silty sand of Recent age, where water table is encountered at very shallow depth. Hence, it is important to assess the geotechnical behavior of the soil in DHA area, where most of the high rise buildings and mega civil structures are being constructed. In present study, seismic soil liquefaction was evaluated at 15 sites (30 bore holes in DHA by using simplified empirical method in terms of Factor of Safety (FS. The Relative Density (RD was determined with the help of Standard Penetration Test (SPT data. Grain size analysis was also carried out on each borehole samples. The results revealed that the DHA area is vulnerable to liquefaction during severe seismic event of magnitude between 6.5 and 7.5 in Karachi.

  12. Fiscal 1991 report on the brown coal liquefaction section meeting; 1991 nendo kattan ekika bukai hokokusho

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1992-03-01

    At the 1st through 5th brown coal liquefaction group meetings held for the fiscal year, reports are delivered and discussions are made about the progress of research and development. At the 1st meeting, a fiscal 1991 brown coal liquefaction research plan is introduced, and discussed. At the 2nd meeting, an interim report on the brown coal liquefaction technology development project is discussed. At the 3rd meeting (a joint meeting of the brown coal and bituminous coal liquefaction groups), an agendum entitled 'what the development of brown/bituminous coal liquefaction technologies for the 21st century should be' is reported, and discussed. At the 4th meeting, reports are made on the results of deliberation at the Industrial Technology Council, progress of the follow-up study, progress of the collection of achievements, and so forth. At the 5th meeting, the outline of the follow-up study, the collection of achievements in the pilot plant study (a project report preparation schedule and materials evaluation), the progress of pilot plant dismantling work, etc., are reported and discussed. (NEDO)

  13. Nuclear reactors

    International Nuclear Information System (INIS)

    Prescott, R.F.; George, B.V.; Baglin, C.J.

    1979-01-01

    In a nuclear reactor (e.g. one having coolant down-flow through a core to a hearth below) thermal insulation (e.g. of a floor of the hearth) comprises a layer of bricks and a layer of tiles thereon, with smaller clearances between the tiles than between the bricks but with the bricks being of reduced cross-section immediately adjacent the tiles so as to be surrounded by interconnected passages, of relatively large dimensions, constituting a continuous chamber extending behind the layer of tiles. By this arrangement, lateral coolant flow in the inter-brick clearances is much reduced. The reactor core is preferably formed of hexagonal columns, supported on diamond-shaped plates each supported on a pillar resting on one of the hearth-floor tiles. Each plate has an internal duct, four upper channels connecting the duct with coolant ducts in four core columns supported by the plate, and lower channels connecting the duct to a downwardly-open recess common to three plates, grouped to form a hexagon, at their mutually-adjacent corners. This provides mixing, and temperature-averaging, of coolant from twelve columns

  14. Agreement of 27 February 1992 between the Government of the People's Democratic Republic of Algeria and the International Atomic Energy Agency for the application of safeguards in connection with the supply of a research reactor from the People's Republic of China

    International Nuclear Information System (INIS)

    1992-04-01

    The document reproduces the text of the Agreement of 27 February 1992 between the Government of the People's Democratic Republic of Algeria and the IAEA for the application of safeguards in connection with the supply of a 15 MW (thermal) research reactor from the People's Republic of China. The Agreement was approved by the Agency's Board of Governors on 25 February 1992

  15. Agreement of 27 February 1992 between the government of the People's Democratic Republic of Algeria and the International Atomic Energy Agency for the application of safeguards in connection with the supply of a research reactor from the People's Republic of China

    International Nuclear Information System (INIS)

    1992-07-01

    The document informs that the Agreement between the Government of the People's Democratic Republic of Algeria and the International Atomic Energy Agency for the Application of Safeguards in connection with the Supply of a Research Reactor from the People's Republic of China, which has been applied provisionally as from 27 February 1992, entered into force on 2 June 1992

  16. Water cooled nuclear reactor

    International Nuclear Information System (INIS)

    1975-01-01

    A description is given of a cooling water intake collector for a nuclear reactor. It includes multiple sub-collectors extending out in a generally parallel manner to each other, each one having a first end and a second one separated along their length, and multiple water outlets for connecting each one to a corresponding pressure tube of the reactor. A first end tube and a second one connect the sub-collector tubes together to their first and second ends respectively. It also includes multiple collector tubes extending transversely by crossing over the sub-collector tubes and separated from each other in the direction of these tubes. Each collector tubes has a water intake for connecting to a water pump and multiple connecting tubes separated over its length and connecting each one to the corresponding sub-collector [fr

  17. Nuclear reactor

    International Nuclear Information System (INIS)

    Jungmann, A.

    1975-01-01

    Between a PWR's reactor pressure vessel made of steel and the biological shield made of concrete there is a gap. This gap is filled up with a heat insulation facting the reactor pressure vessel, for example with insulating concrete segments jacketed with sheet steel and with an additional layer. This layer serves for smooth absorption of compressive forces originating in radial direction from the reactor pressure vessel. It consists of cylinder-segment shaped bricks made of on situ concrete, for instance. The bricks have cooling agent ports in one or several rows which run parallel to the wall of the pressure vessel and in alignment with superposed bricks. Between the layer of bricks and the biological shield or rather the heat insulation, there are joints which are filled, however, with injected mortar. That guarantees a smooth series of connected components resistant tom compression. Besides, a slip foil can be set between the heat insulation and the joining joint filled with mortar for the reduction of the friction at thermal expansions. (TK) [de

  18. Reactor container

    International Nuclear Information System (INIS)

    Hidaka, Masataka; Hatamiya, Shigeo; Kawasaki, Terufumi; Fukui, Toru; Suzuki, Hiroaki; Kataoka, Yoshiyuki; Kawabe, Ryuhei; Murase, Michio; Naito, Masanori.

    1990-01-01

    In order to suppress the pressure elevation in a reactor container due to high temperature and high pressure steams jetted out upon pipeway rupture accidents in the reactor container, the steams are introduced to a pressure suppression chamber for condensating them in stored coolants. However, the ability for suppressing the pressure elevation and steam coagulation are deteriorated due to the presence of inactive incondensible gases. Then, there are disposed a vent channel for introducing the steams in a dry well to a pressure suppression chamber in the reactor pressure vessel, a closed space disposed at the position lower than a usual liquid level, a first channel having an inlet in the pressure suppression chamber and an exit in the closed space and a second means connected by way of a backflow checking means for preventing the flow directing to the closed space. The first paths are present by plurality, a portion of which constitutes a syphon. The incondensible gases and the steams are discharged to the dry well at high pressure by using the difference of the water head for a long cooling time after the pipeway rupture accident. Then, safety can be improved without using dynamic equipments as driving source. (N.H.)

  19. Isolation and characterization of cellulose nanofibers from bamboo using microwave liquefaction combined with chemical treatment and ultrasonication

    Science.gov (United States)

    Jiulong Xie; Chung Hse; Cornelis F. De Hoop; Tingxing Hu; Jinqiu Qi; Todd F. Shupe

    2016-01-01

    Cellulose nanofibers were successfully isolated from bamboo using microwave liquefaction combinedwith chemical treatment and ultrasonic nanofibrillation processes. The microwave liquefaction couldeliminate almost all the lignin in bamboo, resulting in high cellulose content residues within 7 min, andthe cellulose enriched residues could be readily purified by...

  20. Microwave-assisted liquefaction of wood with polyhydric alcohols and its application in preparation of polyurethane (PU) foams

    Science.gov (United States)

    Hui Pan; Zhifeng Zheng; Chung Y. Hse

    2011-01-01

    Microwave radiation was used as the heating source in southern pine wood liquefaction with PEG/glycerin binary solvent. It was found that microwave heating was more efficient than conventional oil bath heating for wood liquefaction. The wood residue content of the H2SO4 catalyzed liquefied wood dropped to zero within 5 min with microwave heating. The resulting...

  1. Report for fiscal 1994 by subcommittee on coal liquefaction basic technology; 1994 nendo ekika kiban gijutsu bukai hokokusho

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1995-03-01

    This report covers the proceedings of subcommittee meetings. Using PDUs (process development unit), comparison is made between bituminous coal-derived oils (150t/d plant for the Indonesian coal) and brown coal-derived oils (50t/d plant for the Yallourn coal), product quality is improved by a 2-stage refining process, engines are tested, etc., all these demonstration and research efforts intended to win social recognition for coal liquefaction products. Among basic studies, there are the development of technologies for reforming coal-derived oils and for mixing them will petroleum, development of new catalysts for reforming, development of a technology for separating heterocompounds and the like, and the development of their applications. Furthermore, technologies are developed for environmentally friendly coal liquefaction, feasibility of coal liquefaction technology internationalization is deliberated, and technical researches and joint researches are conducted. At the second meeting of the subcommittee, achievements relative to the refining and applications of liquefaction products are presented, including the hydrorefining of naphtha, heating oil, and light oil; development of new catalysts; heterocompound separation technology; and the development of new applications. In relation with the development of environmentally friendly coal liquefaction technologies, studies are presented on liquefaction conditions and on the upgrading of basic technologies of liquefaction. Also referred to are the reports delivered at a meeting on liquefaction catalysts (January 1995). (NEDO)

  2. Investigation of bio-composites using Novolac type liquefied wood resin: effects of liquefaction and fabrication conditions

    Science.gov (United States)

    Hui Pan; Chung-Yun Hse; Todd F. Shupe

    2009-01-01

    Wood liquefaction using an organic solvent and an acid catalyst has long been studied as a novel technique to utilize biomass as an alternative to petroleum-based products. Oxalic acid is a weaker organic acid than a mineral acid and wood liquefaction with oxalic acid as a catalyst will result in a higher amount of wood residue than that with a mineral acid....

  3. Two-stage alkaline hydrothermal liquefaction of wood to biocrude in a continuous bench-scale system

    DEFF Research Database (Denmark)

    Sintamarean, Iulia-Maria; Grigoras, Ionela; Jensen, Claus Uhrenholt

    2017-01-01

    unit. In total, 100 kg of wood paste with 25% dry matter is processed at 400 °C and 30 MPa, demonstrating the usefulness of this two-stage liquefaction strategy. An additional advantage liquefaction of such pretreated wood shows increased biocrude yields with approximately 10% compared to the case...

  4. Biomass Direct Liquefaction Options. TechnoEconomic and Life Cycle Assessment

    Energy Technology Data Exchange (ETDEWEB)

    Tews, Iva J.; Zhu, Yunhua; Drennan, Corinne; Elliott, Douglas C.; Snowden-Swan, Lesley J.; Onarheim, Kristin; Solantausta, Yrjo; Beckman, David

    2014-07-31

    The purpose of this work was to assess the competitiveness of two biomass to transportation fuel processing routes, which were under development in Finland, the U.S. and elsewhere. Concepts included fast pyrolysis (FP), and hydrothermal liquefaction (HTL), both followed by hydrodeoxygenation, and final product refining. This work was carried out as a collaboration between VTT (Finland), and PNNL (USA). The public funding agents for the work were Tekes in Finland and the Bioenergy Technologies Office of the U.S. Department of Energy. The effort was proposed as an update of the earlier comparative technoeconomic assessment performed by the IEA Bioenergy Direct Biomass Liquefaction Task in the 1980s. New developments in HTL and the upgrading of the HTL biocrude product triggered the interest in reinvestigating this comparison of these biomass liquefaction processes. In addition, developments in FP bio-oil upgrading had provided additional definition of this process option, which could provide an interesting comparison.

  5. Activity and selectivity of three molybdenum catalysts for coal liquefaction reactions

    Energy Technology Data Exchange (ETDEWEB)

    Curtis, C.W.; Pellegrino, J.L.

    The activity and selectivity of three different molybdenum catalysts for reactions occurring in coal liquefaction, specifically for hydrogenation (HYD), hydrodeoxygenation (HDO), hydrodenitrogenation (HDN), hydrodesulfurization (HDS), and hydrocracking (HYC), have been examined. The three molybdenum catalysts used were molybdenum napthenate, molybdenum on ..gamma..-alumina, and a precipitated, disordered MoS/sub 2/. Molybdenum naphthenate was most selective for HYD and HDN. All three catalysts exhibited approximately equal activity for HDS and HDO and little selectivity for HYC of alkyl bridge structures. The activity and selectivity of the three molybdenum catalysts for producing hydrocarbons and removing heteroatoms from coal during liquefaction were determined and compared. Molybdenum naphthenate was the most active catalyst for hydrocarbon production and removal of nitrogen- and oxygen-containing species during coal liquefaction. 31 refs., 4 figs., 7 tabs.

  6. Numerical analysis of stone columns in mitigating liquefaction effects in embankment fills

    Energy Technology Data Exchange (ETDEWEB)

    Borghei, Z.; Soroush, A. [Amirkabir University of Technology, Tehran, (Iran, Islamic Republic of); Noorzad, A. [Power and Water University of Technology, Tehran, (Iran, Islamic Republic of)

    2010-07-01

    The traditional approach to liquefaction in embankment fills is to use in-situ densification. The use of stone columns offers the possibility of preventing liquefaction and associated settlements while reducing the cost and time required for treatment. This paper investigated the behaviour of stone columns using a numerical method. The study focused on a case study, a sand layer beneath two wall tanks, butane and propane NGL, located on Siri Island, Persian Gulf, Iran. Numerical analyses were carried out to evaluate the rate of excess pore pressure build-up in the improved ground. The numerical model results were compared to the simulation results from a centrifuge test for a uniform 19m-thick liquefiable sand layer. The numerical methodology was verified. The results showed that the stone columns can significantly increase the rate of pore pressure dissipation and reduce the settlement. It was found that the installation process densifies the surrounding soil, decreasing the liquefaction potential.

  7. Efficient direct coal liquefaction of a premium brown coal catalyzed by cobalt-promoted fumed oxides

    Energy Technology Data Exchange (ETDEWEB)

    Trautmann, M.; Loewe, A.; Traa, Y. [Stuttgart Univ. (Germany). Inst. of Chemical Technology

    2013-11-01

    The search for alternatives in the fuel sector is an important technological challenge. An interim solution could be provided by direct coal liquefaction. Hydrogen economy and the lack of an efficient catalyst are the main obstacles for this process. We used a premium German brown coal with a high H/C molar ratio of 1.25 and nanostructured cobalt catalysts to improve the efficiency of direct coal liquefaction. We were able to recover and recycle the catalyst efficiently and reached good brown coal conversions and oil yields with single-stage coal liquefaction. The oil quality observed almost reached that of a conventional crude oil considering higher heating value (HHV), H/C molar ratio and aliphatic content. (orig.)

  8. Subcritical hydrothermal liquefaction of barley straw in fresh water and recycled aqueous phase

    DEFF Research Database (Denmark)

    Zhu, Zhe; Toor, Saqib; Rosendahl, Lasse

    2014-01-01

    This project focuses on the investigation of addition of aqueous phase in the production of biofuel from biomass through hydrothermal liquefaction (HTL) technology. Hydrothermal liquefaction is a wet thermal conversion process, which can convert all kinds of biomass to fuels. In this study, barley...... straw was first liquefied in fresh distilled water with the presence of K2CO3 catalyst at 300 C as the reference run. Afterwards, the aqueous phase which is obtained from liquefaction process in the previous run was recycled and used as the reaction medium from the second to the fourth run....... With the addition of recycling aqueous phase in HTL process, it is expected that the amount of the waste water and energy consumption can be reduced. The effect of water recirculation on product yield and properties was investigated in this study. The results showed that bio-oil yield was 34.85 wt% when the barley...

  9. Assessment of materials selection and performance for direct-coal- liquefaction plants in the United States

    Energy Technology Data Exchange (ETDEWEB)

    Olsen, A.R.; Judkins, R.R.; Keiser, J.R.

    1996-09-01

    Several direct coal liquefaction processes have been demonstrated at the pilot plant level in the United States. Presently only one plant remains operational, namely, the Hydrocarbon Technologies, Inc., 4.0- ton-per-day process development unit in Lawrenceville, New Jersey. The period from 1974 to 1982 saw the greatest amount of development of direct coal liquefaction in the United States with four major pilot plants being devoted to variants of this technology. The plants included the SRC-I plant at Wilsonville, Alabama, which operated from 1974 to 1992; the SRC-I/II plant at Fort Lewis, Washington, which operated from 1974 to 1981; the H-Coal plant at Catlettsburg, Kentucky, which operated from 1980 to 1982; and the Exxon Coal Liquefaction Pilot Plant at Baytown, Texas, which operated from 1980 to 1982. Oak Ridge National Laboratory scientists and engineers were actively involved in many phases and technical disciplines at all four of these plants, especially in materials testing, evaluation, and failure analyses. In addition, ORNL materials scientists and engineers conducted reviews of the demonstration and commercial plant designs for materials selections. The ORNL staff members worked closely with materials engineers at the pilot plants in identifying causes of materials degradation and failures, and in identifying solutions to these problems. This report provides a comprehensive summary of those materials activities. Materials performance data from laboratory and coal liquefaction pilot plant tests, failure analyses, and analyses of components after use in pilot plants were reviewed and assessed to determine the extent and causes of materials degradation in direct coal liquefaction process environments. Reviews of demonstration and commercial plant design documents for materials selections were conducted. These reviews and assessments are presented to capture the knowledge base on the most likely materials of construction for direct coal liquefaction plants.

  10. Quaternary Geology and Liquefaction Susceptibility, Napa, California 1:100,000 Quadrangle: A Digital Database

    Science.gov (United States)

    Sowers, Janet M.; Noller, Jay S.; Lettis, William R.

    1998-01-01

    Earthquake-induced ground failures such as liquefaction have historically brought loss of life and damage to property and infrastructure. Observations of the effects of historical large-magnitude earthquakes show that the distribution of liquefaction phenomena is not random. Liquefaction is restricted to areas underlain by loose, cohesionless sands and silts that are saturated with water. These areas can be delineated on the basis of thorough geologic, geomorphic, and hydrologic mapping and map analysis (Tinsley and Holzer, 1990; Youd and Perkins, 1987). Once potential liquefaction zones are delineated, appropriate public and private agencies can prepare for and mitigate seismic hazard in these zones. In this study, we create a liquefaction susceptibility map of the Napa 1:100,000 quadrangle using Quaternary geologic mapping, analysis of historical liquefaction information, groundwater data, and data from other studies. The study is atterned after state-of-the-art studies by Youd (1973) Dupre and Tinsley (1980) and Dupre (1990) in the Monterey-Santa Cruz area, Tinsley and others (1985) in the Los Angeles area, and Youd and Perkins (1987) in San Mateo County, California. The study area comprises the northern San Francisco Metropolitan Area, including the cities of Santa Rosa, Vallejo, Napa, Novato, Martinez, and Fairfield (Figure 1). Holocene estuarine deposits, Holocene stream deposits, eolian sands, and artificial fill are widely present in the region (Helley and Lajoie, 1979) and are the geologic materials of greatest concern. Six major faults capable of producing large earthquakes cross the study area, including the San Andreas, Rodgers Creek, Hayward, West Napa, Concord, and Green Valley faults (Figure 1).

  11. SUMMARY REPORT OF THE DOE DIRECT LIQUEFACTION PROCESS DEVELOPMENT CAMPAIGN OF THE LATE TWENTIETH CENTURY; FINAL

    International Nuclear Information System (INIS)

    F.P. Burke; S.D. Brandes; D.C. McCoy; R.A. Winschel; D. Gray; G. Tomlinson

    2001-01-01

    Following the petroleum price and supply disruptions of 1973, the U.S. government began a substantial program to fund the development of alternative fuels. Direct coal liquefaction was one of the potential routes to alternative fuels. The direct coal liquefaction program was funded at substantial levels through 1982, and at much lower levels thereafter. Those processes that were of most interest during this period were designed to produce primarily distillate fuels. By 1999, U.S. government funding for the development of direct coal liquefaction ended. Now that the end of this campaign has arrived, it is appropriate to summarize the process learnings derived from it. This report is a summary of the process learnings derived from the DOE direct coal liquefaction process development campaign of the late twentieth century. The report concentrates on those process development programs that were designed to produce primarily distillate fuels and were largely funded by DOE and its predecessors in response to the petroleum supply and price disruptions of the 1970s. The report is structured as chapters written by different authors on most of the major individual DOE-funded process development programs. The focus of the report is process learnings, as opposed to, say, fundamental coal liquefaction science or equipment design. As detailed in the overview (Chapter 2), DOE's direct coal liquefaction campaign made substantial progress in improving the process yields and the quality of the distillate product. Much of the progress was made after termination by 1983 of the major demonstration programs of the ''first generation'' (SRC-II, H-Coal, EDS) processes

  12. Emergency reactor shutdown device

    International Nuclear Information System (INIS)

    Ikehara, Morihiko.

    1982-01-01

    Purpose: To smoothen the emergency operation of the control rod in a BWR type reactor and to eliminate the external discharge of radioactively contaminated water. Constitution: A drain receiving tank is connected through a scram valve to the top of a cylinder which is containing a hydraulic piston connected to a trombone-shaped control rod and an accumulator is connected through another scram valve to the bottom of the cylinder. The respective scram valves are constructed to be opened by the reactor emergency shutdown signal from a reactor control system in such a manner that drain valve and a vent valve of the tank normally opened at the standby time are closed after approx. 10 seconds from the opening of the scram valves. In this manner, back pressure is not applied to the hydraulic piston at the emergency time, thereby smoothly operating the control rod. (Sikiya, K.)

  13. Connecting Grammaticalisation

    DEFF Research Database (Denmark)

    Nørgård-Sørensen, Jens; Heltoft, Lars; Schøsler, Lene

    morphological, topological and constructional paradigms often connect to form complex paradigms. The book introduces the concept of connecting grammaticalisation to describe the formation, restructuring and dismantling of such complex paradigms. Drawing primarily on data from Germanic, Romance and Slavic...

  14. Application of Algae as Cosubstrate To Enhance the Processability of Willow Wood for Continuous Hydrothermal Liquefaction

    DEFF Research Database (Denmark)

    Sintamarean, Iulia-Maria; Pedersen, Thomas Helmer; Zhao, Xueli

    2017-01-01

    This work proposes a novel strategy to improve the continuous processing of wood slurries in hydrothermal liquefaction systems by coprocessing with algae. Of all algae tested, brown seaweeds and microalgae perform best in preventing slurries dewatering, the main reason for pumpability issues...... with wood slurries. Rheological tests (viscosity–shear rate profile) indicate that the addition of these two algae to the wood slurry causes the highest increase in viscosity, which coincides with improved wood slurries stability and pumpability. Hydrothermal liquefaction of wood-algae slurries at 400 °C...

  15. Reducing capital and operating costs in gas processing, liquefaction, and storage

    Energy Technology Data Exchange (ETDEWEB)

    Krusen, III, L C [Phillips Petroleum Co., Bartlesville, OK (United States). Research Div.

    1997-06-01

    The LNG industry is unanimous that capital costs must be reduced throughout the chain, and especially at the liquefaction facility including associated gas processing and LNG storage. The Ken ai LNG plant provides an example of how both reduced capital and operating costs were attained. This paper will cover cost production strategies that can be applied to liquefaction processes in general, and will than focus on their realization in the Phillips Optimized Cascade LNG process. The paper concludes that reduced LNG plant costs are attainable. (Author).

  16. Reducing capital and operating costs in gas processing, liquefaction, and storage

    International Nuclear Information System (INIS)

    Krusen, L.C. III

    1997-01-01

    The LNG industry is unanimous that capital costs must be reduced throughout the chain, and especially at the liquefaction facility including associated gas processing and LNG storage. The Ken ai LNG plant provides an example of how both reduced capital and operating costs were attained. This paper will cover cost production strategies that can be applied to liquefaction processes in general, and will than focus on their realization in the Phillips Optimized Cascade LNG process. The paper concludes that reduced LNG plant costs are attainable. (Author)

  17. Method of controlling a distillatory coulumn in a liquefaction and distillation device for radioactive rare gases

    International Nuclear Information System (INIS)

    Kimura, Shigeru; Awata, Yoshihisa.

    1975-01-01

    Object: To automatically and securely perform controlling purity of column bottom liquid, which is most difficult in the liquefaction and distillation device. Structure: In a liquefaction and distillation device for liquefying and separating rare gas krypton in fuel reprocessing gases, a difference in temperature between the column bottom liquid (column top) and the distillation portion is detected so as to maintain temperature in the distillation portion of the distilling column constant, and the vaporization amount of column bottom liquid is varied with the difference in temperature to control purity of the column bottom liquid. (Kamimura, M.)

  18. Probabilistic and Scenario Seismic and Liquefaction Hazard Analysis of the Mississippi Embayment Incorporating Nonlinear Site Effects

    Science.gov (United States)

    Cramer, C. H.; Dhar, M. S.

    2017-12-01

    The influence of deep sediment deposits of the Mississippi Embayment (ME) on the propagation of seismic waves is poorly understood and remains a major source of uncertainty for site response analysis. Many researchers have studied the effects of these deposits on seismic hazard of the area using available information at the time. In this study, we have used updated and newly available resources for seismic and liquefaction hazard analyses of the ME. We have developed an improved 3D geological model. Additionally, we used surface geological maps from Cupples and Van Arsdale (2013) to prepare liquefaction hazard maps. Both equivalent linear and nonlinear site response codes were used to develop site amplification distributions for use in generating hazard maps. The site amplification distributions are created using the Monte Carlo approach of Cramer et al. (2004, 2006) on a 0.1-degree grid. The 2014 National Seismic Hazard model and attenuation relations (Petersen et al., 2014) are used to prepare seismic hazard maps. Then liquefaction hazard maps are generated using liquefaction probability curves from Holzer (2011) and Cramer et al. (2015). Equivalent linear response (w/ increased precision, restricted nonlinear behavior with depth) shows similar hazard for the ME compared to nonlinear analysis (w/o pore pressure) results. At short periods nonlinear deamplification dominates the hazard, but at long periods resonance amplification dominates. The liquefaction hazard tends to be high in Holocene and late Pleistocene lowland sediments, even with lowered ground water levels, and low in Pleistocene loess of the uplands. Considering pore pressure effects in nonlinear site response analysis at a test site on the lowlands shows amplification of ground motion at short periods. PGA estimates from ME liquefaction and MMI observations are in the 0.25 to 0.4 g range. Our estimated M7.5 PGA hazard within 10 km of the fault can exceed this. Ground motion observations from

  19. Characteristics of process oils from HTI coal/plastics co-liquefaction runs

    Energy Technology Data Exchange (ETDEWEB)

    Robbins, G.A.; Brandes, S.D.; Winschel, R.A. [and others

    1995-12-31

    The objective of this project is to provide timely analytical support to DOE`s liquefaction development effort. Specific objectives of the work reported here are presented. During a few operating periods of Run POC-2, HTI co-liquefied mixed plastics with coal, and tire rubber with coal. Although steady-state operation was not achieved during these brief tests periods, the results indicated that a liquefaction plant could operate with these waste materials as feedstocks. CONSOL analyzed 65 process stream samples from coal-only and coal/waste portions of the run. Some results obtained from characterization of samples from Run POC-2 coal/plastics operation are presented.

  20. Alternative breeder reactor technologies

    International Nuclear Information System (INIS)

    Spinrad, B.I.

    1978-01-01

    The significance of employing breeder reactors to stretch the world resources of nuclear fuels is briefly discussed, and the various types of breeder concepts are described. General descriptions, advantages, and disadvantages of the liquid metal cooled fast breeder, gas cooled fast breeder, molten salt breeder, thermal breeders, and spectral-shift control reactors are presented. Aspects of safeguarding fissile material connected with breeder operation are examined. 31 references

  1. Kinetics assisted design of catalysts for coal liquefaction. Final report

    Energy Technology Data Exchange (ETDEWEB)

    Klein, M.T.; Foley, H.C.; Calkins, W.H.; Scouten, C.

    1998-02-01

    The thermal and catalytic reactions of 4-(1-naphthylmethyl)bibenzyl (NBBM), a resid and coal model compound, were examined. Catalytic reaction of NBBM was carried out at 400 C under hydrogen with a series of transition metal-based catalytic materials including Fe(CO){sub 4}PPh{sub 3}, Fe(CO){sub 3}(PPh{sub 3}){sub 2}, Fe(CO){sub 2}(PPh{sub 3}){sub 2}CS{sub 2}, Fe(CO){sub 5}, Mo(CO){sub 6}, Mn{sub 2}(CO){sub 10}, Fe{sub 2}O{sub 3} and MoS{sub 2}. Experimental findings and derived mechanistic insights were organized into molecular-level reaction models for NBBM pyrolysis and catalysis. Hydropyrolysis and catalysis reaction families occurring during NBBM hydropyrolysis at 420 C were summarized in the form of reaction matrices which, upon exhaustive application to the components of the reacting system, yielded the mechanistic reaction model. Each reaction family also had an associated linear free energy relationship (LFER) which provided an estimate of the rate constant k{sub i} given a structural property of species i or its reaction. Including the catalytic reaction matrices with those for the pyrolysis model provided a comprehensive NBBM catalytic reaction model and allowed regression of fundamental LFER parameters for the catalytic reaction families. The model also allowed specification of the property of an optimal catalyst. Iron, molybdenum and palladium were predicted to be most effective for model compound consumption. Due to the low costs associated with iron and its disposal, it is a good choice for coal liquefaction catalysis and the challenge remains to synthesize small particles able to access the full surface area of the coal macromolecule.

  2. Cooperative Research Program in Coal-Waste Liquefaction

    Energy Technology Data Exchange (ETDEWEB)

    Gerald Huffman

    2000-03-31

    The results of a feasibility study for a demonstration plant for the liquefaction of waste plastic and tires and the coprocessing of these waste polymers with coal are presented. The study was conducted by a committee that included nine representatives from the CFFS, six from the U.S. Department of Energy - Federal Energy Technology Center (FETC), and four from Burns and Roe, Inc. The study included: (1) An assessment of current recycling practices, particularly feedstock recycling in Germany; (2) A review of pertinent research, and a survey of feedstock availability for various types of waste polymers; and (3) A conceptual design for a demonstration plant was developed and an economic analysis for various feedstock mixes. The base case for feedstock scenarios was chosen to be 200 tons per day of waste plastic and 100 tons per day of waste tires. For this base case with oil priced at $20 per barrel, the return on investment (ROI) was found to range from 9% to 20%, using tipping fees for waste plastic and tires typical of those existing in the U.S. The most profitable feedstock appeared to waste plastic alone, with a plant processing 300 t/d of plastic yielding ROI's from 13 to 27 %, depending on the tipping fees for waste plastic. Feedstock recycling of tires was highly dependent on the price that could be obtained for recovered carbon. Addition of even relatively small amounts (20 t/d) of coal to waste plastic and/or coal feeds lowered the ROI's substantially. It should also be noted that increasing the size of the plant significantly improved all ROI's. For example, increasing plant size from 300 t/d to1200 t/d approximately doubles the estimated ROI's for a waste plastic feedstock.

  3. Advanced Direct Liquefaction Concepts for PETC Generic Units - Phase II

    Energy Technology Data Exchange (ETDEWEB)

    None

    1997-09-01

    Reported here are the results of Laboratory and Bench- Scale experiments and supporting technical and economic assessments conducted under DOE Contract No. DE- AC22- 91PC91040 during the period April 1, 1997 to June 30, 1997. This contract is with the University of Kentucky Research Foundation which supports work with the University of Kentucky Center for Applied Energy Research, CONSOL, Inc., LDP Associates, and Hydrocarbon Technologies, Inc. This work involves the introduction into the basic two stage liquefaction process several novel concepts which includes dispersed lower- cost catalysts, coal cleaning by oil agglomeration, and distillate hydrotreating and dewaxing. This report includes a data analysis of the ALC- 2 run which was the second continuous run in which Wyodak Black Thunder coal was fed to a two kg/ h bench- scale unit. One of the objectives of that run was to determine the relative activity of several Mo- based coal impregnated catalyst precursors. The precursors included ammonium heptamolybdate (100 mg Mo/ kg dry coal), which was used alone as well as in combination with ferrous sulfate (1% Fe/ dry coal) and nickel sulfate (50 mg Ni/ kg dry coal). The fourth precursor that was tested was phosphomolybdic acid which was used at a level of 100 mg Mo/ kg dry coal. Because of difficulties in effectively separating solids from the product stream, considerable variation in the feed stream occurred. Although the coal feed rate was nearly constant, the amount of recycle solvent varied which resulted in wide variations of resid, unconverted coal and mineral matter in the feed stream. Unfortunately, steady state was not achieved in any of the four conditions that were run. Earlier it was reported that Ni- Mo catalyst appeared to give the best results based upon speculative steady- state yields that were developed.

  4. PWR type reactor plant

    International Nuclear Information System (INIS)

    Matsuoka, Tsuyoshi.

    1993-01-01

    A water chamber of a horizontal U-shaped pipe type steam generator is partitioned to an upper high temperature water chamber portion and a lower low temperature water chamber portion. An exit nozzle of a reactor container containing a reactor core therein is connected to a suction port of a coolant pump by way of first high temperature pipelines. The exit port of the coolant pump is connected to the high temperature water chamber portion of the steam generator by way of second high temperature pipelines. The low temperature water chamber portion of the steam generator is connected to an inlet nozzle of the reactor container by way of the low temperature pipelines. The low temperature water chamber portion of the steam generator is positioned lower than the high temperature water chamber portion, but upper than the reactor core. Accordingly, all of the steam generator for a primary coolant system, coolant pumps as well as high temperature pipelines and low temperature pipelines connecting them are disposed above the reactor core. With such a constitution, there is no worry of interrupting core cooling even upon occurrence of an accident, to improve plant safety. (I.N.)

  5. LWR type reactor

    International Nuclear Information System (INIS)

    Kato, Kiyoshi.

    1993-01-01

    A water injection tank in an emergency reactor core cooling system is disposed at a position above a reactor pressure vessel. A liquid phase portion of the water injection tank and an inlet plenum portion in the reactor pressure vessel are connected by a water injection pipe. A gas phase portion of the water injection tank and an upper portion in the reactor pressure vessel are connected by a gas ventilation pipe. Hydraulic operation valves are disposed in the midway of the water injection pipe and the gas ventilation pipe respectively. A pressure conduit is disposed for connecting a discharge port of a main recycling pump and the hydraulic operation valve. In a case where primary coolants are not sent to the main recycling pump by lowering of a liquid level due to loss of coolants or in a case where the main recycling pump is stopped by electric power stoppage or occurrence of troubles, the discharge pressure of the main recycling pump is lowered. Then, the hydraulic operation valve is opened to release the flow channel, then, boric acid water in the water injection tank is sent into the reactor by a falling head, to lead the reactor to a scram state. (I.N.)

  6. Summary of FY 1980 results of Sunshine Project. Development of coal liquefaction techniques; 1980 nendo sekitan ekika gijutsu no kaihatsu seika hokokusho. Sunshine keikaku itaku kenkyu kaihatsu

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1981-03-01

    This report summarizes the results of the 3 R and D themes for coal liquefaction techniques, pursued by the Sunshine Project; (1) development of solvent extraction type liquefaction plant, and brown coal liquefaction technique R and D demonstration surveys, (2) development of solvolysis type liquefaction plant, and (3) development of direct hydrogenation type liquefaction plant. For the theme (1), the 1 T/D test plant, solid/liquid separator and small-size continuous settlement separator are constructed, and partly completed. The elementary studies include solvent extraction type liquefaction process, materials for coal liquefaction plant and solid/liquid separation. Australia's Victoria brown coal and Chinese coal are studied to clarify the possible problems involved in liquefaction of these coal species for commercialization of the liquefaction techniques in the early stage. The elementary techniques studied include dehydration of brown coal, milling at high temperature in oil, de-ashing, and secondary and primary hydrogenation. For the theme (2), the 1 T/D plant is inspected and maintained to clarify the problems involved in the continuous operation, revamped and repaired as necessary, given preventive maintenance, and tested for operability confirmation. The elementary studies include solvolysis type liquefaction process, scale-up, hydrogenation plant for solvolysis pitch. For the item (3), the 2.4 T/D test plant is constructed, and the elementary studies are conducted, for, e.g., liquefaction reactions in the presence of an iron-based catalyst. (NEDO)

  7. Summary of FY 1980 results of Sunshine Project. Development of coal liquefaction techniques; 1980 nendo sekitan ekika gijutsu no kaihatsu seika hokokusho. Sunshine keikaku itaku kenkyu kaihatsu

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1981-03-01

    This report summarizes the results of the 3 R and D themes for coal liquefaction techniques, pursued by the Sunshine Project; (1) development of solvent extraction type liquefaction plant, and brown coal liquefaction technique R and D demonstration surveys, (2) development of solvolysis type liquefaction plant, and (3) development of direct hydrogenation type liquefaction plant. For the theme (1), the 1 T/D test plant, solid/liquid separator and small-size continuous settlement separator are constructed, and partly completed. The elementary studies include solvent extraction type liquefaction process, materials for coal liquefaction plant and solid/liquid separation. Australia's Victoria brown coal and Chinese coal are studied to clarify the possible problems involved in liquefaction of these coal species for commercialization of the liquefaction techniques in the early stage. The elementary techniques studied include dehydration of brown coal, milling at high temperature in oil, de-ashing, and secondary and primary hydrogenation. For the theme (2), the 1 T/D plant is inspected and maintained to clarify the problems involved in the continuous operation, revamped and repaired as necessary, given preventive maintenance, and tested for operability confirmation. The elementary studies include solvolysis type liquefaction process, scale-up, hydrogenation plant for solvolysis pitch. For the item (3), the 2.4 T/D test plant is constructed, and the elementary studies are conducted, for, e.g., liquefaction reactions in the presence of an iron-based catalyst. (NEDO)

  8. Nuclear reactors

    International Nuclear Information System (INIS)

    Barre, Bertrand

    2015-10-01

    After some remarks on the nuclear fuel, on the chain reaction control, on fuel loading and unloading, this article proposes descriptions of the design, principles and operations of different types of nuclear reactors as well as comments on their presence and use in different countries: pressurized water reactors (design of the primary and secondary circuits, volume and chemistry control, backup injection circuits), boiling water reactors, heavy water reactors, graphite and boiling water reactors, graphite-gas reactors, fast breeder reactors, and fourth generation reactors (definition, fast breeding). For these last ones, six concepts are presented: sodium-cooled fast reactor, lead-cooled fast reactor, gas-cooled fast reactor, high temperature gas-cooled reactor, supercritical water-cooled reactor, and molten salt reactor

  9. A case study of liquefaction risk analysis based on the thickness and depth of the liquefaction layer using CPT and electric resistivity data in the Hinode area, Itako City, Ibaraki Prefecture, Japan

    Science.gov (United States)

    Jinguuji, Motoharu; Toprak, Selcuk

    2017-12-01

    The Hinode area of Itako City in Ibaraki Prefecture, Japan, suffered some of the most severe liquefaction damage of any areas in the Great Eastern Japan Earthquake in 2011. This liquefaction damage has been investigated by Itako City, as well as by universities and research institutes in Japan. The National Institute of Advanced Industrial Science and Technology (AIST) has carried out numerous investigations along the Tone River, and in particular, intensive surveys were done in the Hinode area. We have conducted a risk analysis based on the thickness and depth of the liquefaction layer measured using cone penetration testing (CPT) data and electric resistivity data obtained in the Hinode area. The distribution of the risk estimated from CPT at 143 points, and that obtained from analysis of the resistivity survey data, agreed with the distribution of actual damage. We also carried out conventional risk analyses method using the liquefaction resistance factor (FL) and liquefaction potential index (PL) methods with CPT data. The results show high PL values over the entire area, but their distribution did not agree well with actual damage in some parts of the study area. Because the analysis of the thickness and depth of the liquefaction layer, using geophysical prospecting methods, can cover a widespread area, this method will be very useful in investigating liquefaction risk, especially for gas and water pipelines.

  10. Reactor as furnace and reactor as lamp

    International Nuclear Information System (INIS)

    Goldanskii, V.I.

    1992-01-01

    There are presented general characteristics of the following ways of transforming of nuclear energy released in reactors into chemical : ordinary way (i.e. trough the heat, mechanical energy and electricity); chemonuclear synthesis ; use of high-temperature fuel elements (reactor as furnace); use of the mixed nγ-radiation of reactors; use of the radiation loops; radiation - photochemical synthesis (reactor as lamp). Advantage and disadvantages of all above variants are compared. The yield of the primary product of fixation of nitrogen (nitric oxide NO) in reactor with the high-temperature (above ca. 1900degC) fuel elements (reactor-furnace) can exceed W ∼ 200 kg per gram of burned uranium. For the latter variant (reactor-lamp) the yield of chemical products can reach W ∼ 60 kg. per gram of uranium. Such values of W are close to or even strongly exceed the yields of chemical products for other abovementioned variants and - what is particularly important - are not connected to the necessity of archscrupulous removal of radioactive contamination of products. (author)

  11. Reactor feedwater device

    International Nuclear Information System (INIS)

    Igarashi, Noboru.

    1986-01-01

    Purpose: To suppress soluble radioactive corrosion products in a feedwater device. Method: In a light water cooled nuclear reactor, an iron injection system is connected to feedwater pipeways and the iron concentration in the feedwater or reactor coolant is adjusted between twice and ten times of the nickel concentration. When the nickel/iron ratio in the reactor coolant or feedwater goes nearer to 1/2, iron ions are injected together with iron particles to the reactor coolant to suppress the leaching of stainless steels, decrease the nickel in water and increase the iron concentration. As a result, it is possible to suppress the intrusion of nickel as one of parent nuclide of radioactive nuclides. Further, since the iron particles intruded into the reactor constitute nuclei for capturing the radioactive nuclides to reduce the soluble radioactive corrosion products, the radioactive nuclides deposited uniformly to the inside of the pipeways in each of the coolant circuits can be reduced. (Kawakami, Y.)

  12. The current status of coal liquefaction technologies - Panorama 2008; La liquefaction du charbon: ou en est-on aujourd'hui? - Panorama 2008

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    2008-07-01

    In 2008, a first coal liquefaction unit to produce motor fuel (20,000 BPSD) will come on-stream in Shenhua, China (in the Ercos region of Inner Mongolia). Other, more ambitious projects have been announced in China for between now and 2020. Since oil production is expected to peak in the medium term, this technology may develop regionally in the next 20 years to cover ever-increasing demand for motor fuel.

  13. Hydrothermal liquefaction of pinewood (Pinus ponderosa) for H2, biocrude and bio-oil generation

    International Nuclear Information System (INIS)

    Tungal, Richa; Shende, Rajesh V.

    2014-01-01

    Highlights: • Ni(NO 3 ) 2 , Ca(NO 3 ) 2 , Co(NO 3 ) 2 and Fe(NO 3 ) 3 were investigated for HTL of pinewood. • Ni(NO 3 ) 2 showed higher selectivity for H 2 and biocrude generation. • O/C ratio of LBO, HBO and residue recovered was lower than O/C of the pinewood. • HHVs of LBO, HBO and residue were found to be higher than HHV of the pinewood. - Abstract: This study reports hydrothermal liquefaction (HTL) of pinewood at 200–275 °C for H 2 , biocrude and bio-oil production in presence of a nitrate salt catalyst: Ni(NO 3 ) 2 , Ca(NO 3 ) 2 , Co(NO 3 ) 2 and Fe(NO 3 ) 3 . Among these catalysts, Ni(NO 3 ) 2 showed higher selectivity towards H 2 and biocrude generation. To generate H 2 and biocrude, a slurry of pinewood was prepared with different biomass to solvent (B:S) ratios of 1:10, 1:30, and 1:75 and loaded in the SS316 PARR reactor and heated to different temperatures. While the reaction was in progress, gas samples were withdrawn and analyzed using GC equipped with Chrompack capillary column and thermal conductivity detector. The analysis of product gas revealed the presence of H 2 , CO 2 , CO and CH 4 . The liquid samples collected during the reaction were centrifuged to separate residue and analyzed using TOC analyzer, HPLC and GC–MS. Among different homogeneous catalysts used, Ni(NO 3 ) 2 yielded 12.26 mol% H 2 at 275 °C and a maximum biocrude of 55 wt% at 250 °C using 200 psi N 2 partial pressure. The biocrude was found to contain sugars, C 1 -C 3 carboxylic acids such as lactic, propionic, acetic and formic, HMF/furfural and other oxygenated compounds, which were thoroughly analyzed by GC–MS. Among different C 1 -C 3 acids, lactic acid was observed in the major amount of 83.92 wt% using B:S of 1:75 at 250 °C. The biocrude obtained was further processed to recover light bio-oil (LBO), heavy bio-oil (HBO) and residue which were found to have higher heating value (HHV) as compared with original pinewood

  14. Characterization of the aqueous fractions from hydrotreatment and hydrothermal liquefaction of lignocellulosic feedstocks

    International Nuclear Information System (INIS)

    Panisko, Ellen; Wietsma, Thomas; Lemmon, Teresa; Albrecht, Karl; Howe, Daniel

    2015-01-01

    In this study the aqueous phases resulting from the hydrothermal liquefaction (HTL) of biomass and the hydrotreatment (HT) of fast pyrolysis bio-oils were analyzed via TC, COD, GC-MS, GC-FID, HPLC, and ICP-OES to determine the organic and inorganic species present and the quantitative amounts of each. This work is necessary to address a significant knowledge gap in the literature related to the aqueous phases from thermochemical processes. Results showed that water from the hydrotreatment of eight different bio-oils contained less than 1 wt% total carbon, in many cases less than 0.2%. Negligible organic carbon was observed. HTL samples contained between 1 and 2 wt% carbon. Due to the large volume of water added to the HTL feedstock and the dilute samples generated, this accounts for 34–45% of the total carbon sent to the reactor. The majority of this carbon was present as acids, with glycolic acid and acetic acid having the highest concentrations. Alcohols, specifically methanol and ethanol, were also present. Numerous ketones were observed, consisting of mainly acetone and cyclopenta-ones. The amount of the total carbon identified and quantified in the HTL samples ranged from 64 to 82%. Inorganic species present in the HT samples were sodium, silicon, and sulfur. The highest levels of sulfur were observed in the grasses and agricultural residue (corn stover). The HTL samples exhibited much higher inorganic content, with very high levels of sodium and potassium. Alkali and alkali earth metals, as well as sulfur, were also present at levels high enough to raise concerns for the use of catalysts in downstream upgrading or reforming processes. - Highlights: • Hydrotreatment samples are less than 1 wt% total carbon with negligible organic C. • 64–82% of the total carbon in HTL samples was identified and quantified. • Organic species in HTL samples were mainly acids, alcohols, and ketones. • Inorganic species in HT samples were mainly Na, Si, and S.

  15. Influence of the void ratio and the confining on the static liquefaction in slopes in shangi sand

    Directory of Open Access Journals (Sweden)

    Alfonso Mariano Ramos Cañón

    2015-01-01

    Full Text Available A numerical study on the onset of static liquefaction in slopes under undrained conditions of loading was developed based on a general liquefaction flow instability criterion for elastoplastic soils based on the concept of loss of controllability. The criterion is applied to the case of axisymmetric loading to detect the onset of static liquefaction. The criterion is used in conjunction with an elastoplastic model for sands and is tested by means of numerical simulations of element tests. The numerical results are compared with experimental evidence obtaining good agreement. A quantitative study of the influence of the mean pressure, void ratio and the anisotropy of stress on the onset of static liquefaction is presented for the Changi sand. From the analysis of the numerical results, it can be concluded that: a. the mobilized friction angle at the onset of liquefaction is not an intrinsic property of the material, but is a state variable b. Despite of the multiple variables involved in the process of generation of undrained instability, the state of stresses at the onset of static liquefaction can be conveniently represented by a linear relation between Dq/po and no . This graphical representation can be used in the practice of geotechnical engineering to quantify the margin of security against the static liquefaction of a sandy slope.

  16. Thermodynamic Analysis on of Skid-Mounted Coal-bed Methane Liquefaction Device using Cryogenic Turbo-Expander

    Science.gov (United States)

    Chen, Shuangtao; Niu, Lu; Zeng, Qiang; Li, Xiaojiang; Lou, Fang; Chen, Liang; Hou, Yu

    2017-12-01

    Coal-bed methane (CBM) reserves are rich in Sinkiang of China, and liquefaction is a critical step for the CBM exploration and utilization. Different from other CBM gas fields in China, CBM distribution in Sinkiang is widespread but scattered, and the pressure, flow-rate and nitrogen content of CBM feed vary significantly. The skid-mounted liquefaction device is suggested as an efficient and economical way to recover methane. Turbo-expander is one of the most important parts which generates the cooling capacity for the cryogenic liquefaction system. Using turbo-expander, more cooling capacity and higher liquefied fraction can be achieved. In this study, skid-mounted CBM liquefaction processes based on Claude cycle are established. Cryogenic turbo-expander with high expansion ratio is employed to improve the efficiency of CBM liquefaction process. The unit power consumption per liquefaction mole flow-rate for CBM feed gas is used as the object function for process optimization, compressor discharge pressure, flow ratio of feed gas to turbo-expander and nitrogen friction are analyzed, and optimum operation range of the liquefaction processes are obtained.

  17. ORPHEE reactor. Upgrade of the installation

    International Nuclear Information System (INIS)

    Farnoux, B.; Maziere, M.

    1995-01-01

    Designed by the end of the seventies, the ORPHEE Reactor is equipped with two hydrogen cold sources, one hot source and six cold neutron guides. The neutron beams are extracted by nine beam ports and used in two experimental halls, the reactor hall and the neutron guide hall. After fourteen years of use, a modernisation programme is in progress. One step concerns the neutron guides, another one the cold sources with the modification of the cell geometry in order to increase the cold neutron flux. This operation requires the use a new cryogenerator to ensure liquefaction capabilities for the new cells. It is also scheduled to replace the Zircaloy core housing in order to avoid difficulties linked to the expansion under irradiation. (author)

  18. Report on results of R and D of coal liquefaction technology under Sunshine Project in fiscal 1981 (development of motive force recovery system by hydrohoist); 1981 nendo sekitan ekika gijutsu no kenkyu kaihatsu, chokusetsu suiten ekika plant no kaihatsu seika hokokusho. Hydrohoist ni yoru doryoku kaishu system no kaihatsu

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1982-03-01

    This paper explains the results of development of a hydrohoist system in a direct hydro-liquefaction plant under the Sunshine Project in fiscal 1981. Coal liquefaction deals with three phases of gas, liquid and solid at high pressures of 100-300 kg/cm{sup 2}. Slurry consisting of coal, catalyst and solvent is once fed into a supply chamber by a low pressure slurry pump. A high pressure slurry formed in a liquefaction reactor, after the separation of gaseous object, is boosted by a booster pump and force-fitted into the supply chamber from the above, discharging the slurry in the chamber to the high pressure reactor side. Since the high pressure product is used as the driving liquid, a force-feeding motive force can be greatly curtailed. It is a motive force recovery type hydrohoist. The product slurry in the supply chamber is discharged from a valve in the upper part; with the inner pressure going down quickly, the discharge valve wears very little. The basic experimental equipment was manufactured in fiscal 1980, with a test research conducted using the improved main equipment in fiscal 1981, and with the conceptual design of the hydrohoist also implemented on the assumption that it was applied to a pilot plant. (NEDO)

  19. Fiscal 1989 report on the bituminous coal liquefaction section meeting; 1989 nendo rekiseitan ekika bukai hokokusho

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1990-03-01

    At the 1st, 2nd, and 3rd group meetings held for the fiscal year, reports are given and discussions are made about the progress of research and development. Reported and discussed in relation to the progress of the pilot plant support research are studies with the 1t/d PSU (process supporting unit) (Nippon Steel Corporation, Mitsui Coal Liquefaction Co., Ltd., and Japan Coal Oil Co., Ltd.); improvement on distillate distribution (Sumitomo Metal Industries, Ltd.); development of an optimum decalcification technique (Sumitomo Coal Mining Co., Ltd., and Sumitomo Metal Industries, Ltd.); studies of solvent hydrogenation catalysts (Sumitomo Metal Mining Co., Ltd., and Chiyoda Corp.); and studies of coal liquefaction conditions (Mitsui Engineering and Shipbuilding Co., Ltd.). In relation to studies using a bituminous coal liquefaction pilot plant, the progress of the 150t/d PP (pilot plant) effort (Japan Coal Oil, Co., Ltd.) and the outlines of pilot surveys (Japan Coal Oil Co., Ltd.) are reported and discussed, the latter covering liquefaction solvent performance optimization, slurry preheating furnaces, coal slurry properties, and so forth. (NEDO)

  20. Hydrothermal co-liquefaction of microalgae, wood, and sugar beet pulp

    NARCIS (Netherlands)

    Brilman, D. W.F.; Drabik, N.; Wądrzyk, M.

    2017-01-01

    Hydrothermal co-liquefaction of mixed (wet and dry) biomass residue streams would greatly enhance the viability and scale up potential of the technology as platform in bioenergy and biorefinery applications. This study aims to identify possible interaction effects between three different feeds

  1. Comparison of the sand liquefaction estimated based on codes and practical earthquake damage phenomena

    Science.gov (United States)

    Fang, Yi; Huang, Yahong

    2017-12-01

    Conducting sand liquefaction estimated based on codes is the important content of the geotechnical design. However, the result, sometimes, fails to conform to the practical earthquake damages. Based on the damage of Tangshan earthquake and engineering geological conditions, three typical sites are chosen. Moreover, the sand liquefaction probability was evaluated on the three sites by using the method in the Code for Seismic Design of Buildings and the results were compared with the sand liquefaction phenomenon in the earthquake. The result shows that the difference between sand liquefaction estimated based on codes and the practical earthquake damage is mainly attributed to the following two aspects: The primary reasons include disparity between seismic fortification intensity and practical seismic oscillation, changes of groundwater level, thickness of overlying non-liquefied soil layer, local site effect and personal error. Meanwhile, although the judgment methods in the codes exhibit certain universality, they are another reason causing the above difference due to the limitation of basic data and the qualitative anomaly of the judgment formulas.

  2. Influence of saturation degree and role of suction in unsaturated soils behaviour: application to liquefaction

    Directory of Open Access Journals (Sweden)

    Vernay Mathilde

    2016-01-01

    Full Text Available The effect of the pore fluid compressibility on liquefaction has been studied by various authors. But few papers have been published about the role of suction in cyclic behavior of unsaturated soils. Most of these works use Skempton coefficient B as a reference in terms of saturation degree to analyze their results. The use of B in experimental conditions is convenient, but is not accurate when studying liquefaction behavior, since effects of suction are neglected. In this paper, the influence of saturation degree on mechanical behavior of a soil under dynamic loads is studied. Cyclic undrained triaxial tests were performed on sand samples, under various levels of saturation. Soil-water characteristic curve was used, in order to study influence of suction. The first results confirm that when the degree of saturation decreases, the resistance increases. Initial positive suction tends to stiffen the soil. It also appears that the presence of air delays the occurrence of liquefaction, but doesn’t prevent it. Indeed, liquefaction is observed, whether the soil is saturated or not.

  3. Microalgae growth on the aqueous phase from Hydrothermal Liquefaction of the same microalgae

    NARCIS (Netherlands)

    Garcia Alba, Laura; Torri, Cristian; Fabbri, Daniele; Kersten, Sascha R.A.; Brilman, Derk Willem Frederik

    2013-01-01

    Cultivation of Desmodesmus sp. microalgae in the recycled aqueous phase (AP) recovered after Hydrothermal Liquefaction (HTL) of the same microalgae was studied to evaluate the potential of nutrients recycling. AP dilution ratio was systematically varied, using either water or water enriched with

  4. Effect of methanol on the liquefaction reaction of biomass in hot compressed water under microwave energy

    Science.gov (United States)

    Junming Xu; Jianchun Jiang; Chun-Yun Hse; Todd F. Shupe

    2013-01-01

    Liquefaction of sawdust was studied in methanol-water solutions using an acid catalyst under microwave energy. The effect of the methanol concentration on the changes of components in the liquefied products was analyzed by gas chromatography−mass spectrometry (GC−MS). It was found that 5-hydroxymethylfurfural (HMF) and levulinic acid are the...

  5. Liquefaction analysis of alluvial soil deposits in Bedsa south west of Cairo

    Directory of Open Access Journals (Sweden)

    Kamal Mohamed Hafez Ismail Ibrahim

    2014-09-01

    Full Text Available Bedsa is one of the districts in Dahshour that lays south west of Cairo and suffered from liquefaction during October 1992 earthquake, Egypt. The soil profile consists of alluvial river Nile deposits mainly sandy mud with low plasticity; the ground water is shallow. The earthquake hypocenter was 18 km far away with local magnitude 5.8; the fault length was 13.8 km, as recorded by the Egyptian national seismological network (ENSN at Helwan. The analysis used the empirical method introduced by the national center for earthquake engineering research (NCEER based on field standard penetration of soil. It is found that the studied area can liquefy since there are saturated loose sandy silt layers at depth ranges from 7 to 14 m. The settlement is about 26 cm. The probability of liquefaction ranges between 40% and 100%. The presence of impermeable surface from medium cohesive silty clay acts as a plug resisting and trapping the upward flow of water during liquefaction, so fountain and spouts at weak points occurs. It is wise to use point bearing piles with foundation level deeper than 14 m beyond the liquefiable depth away from ground slopes, otherwise liquefaction improving techniques have to be applied in the area.

  6. Catalytic Liquefaction of Humin Substances from Sugar Biorefineries with Pt/C in 2-Propanol

    NARCIS (Netherlands)

    Wang, Y.; Agarwal, S.; Heeres, H. J.

    The catalytic liquefaction of humins, the solid byproduct from the conversion of C6 sugars (glucose, fructose) to S-hydroxymethylfurfural (HMF) and levulinic acid (LA), using a supported Pt/C catalyst in isopropanol (IPA) as the solvent was investigated. At bench mark conditions (400 degrees C, 7 h,

  7. Renewable hydrocarbon fuels from hydrothermal liquefaction: A techno-economic analysis

    DEFF Research Database (Denmark)

    Pedersen, Thomas Helmer; Hansen, Nick Høy; Pérez, Oscar Miralles

    2018-01-01

    This study demonstrates the economic feasibility of producing renewable transportation drop-in fuels from lignocellulosic biomass through hydrothermal liquefaction and upgrading. An Aspen Plus® process model is developed based on extensive experimental data to document a techno-economic assessmen...

  8. To the vibrational over wetting and liquefaction effects in moistured soils

    International Nuclear Information System (INIS)

    Karimov, F.H.; Oripov, G.O.; Saidov, R.M.; Tojibekov, M.

    2003-01-01

    There is a lot of evidence of the dynamical effects in soils when they become wetted or during or after the earthquakes or explosions. There are some quantitative estimates for the vibrational wetting and liquefaction of soils under consideration. For the models in the present research the moistured sands and weak soils like losses are accepted. The first model is focusing on soil fractures sliding down under the action of vibrations, tightening of a hard phase, squeezing water phase out and thus bringing to soil liquefaction. The second is based on soil fractures plunging at the action of vibrations into the aquatic background. This mechanism seems to be more effective for the high degree moistured soils. The third mechanism is based on capillary phenomena in moistured porous medium. When inertia forces are large enough the resultant force, consisting of sliding down gravity component and inertia forces, overcomes friction and fracture becomes unstable. Both vibrations amplitude and frequency are the stability controlling factors, playing an important role in the vibrational wetting and liquefaction effects through porous water phase squeezing out or capillary lifting phenomena leading to the wetting or liquefaction of the medium. (author)

  9. Biocrude production via supercritical hydrothermal co-liquefaction of spent mushroom compost and aspen wood sawdust

    DEFF Research Database (Denmark)

    Jasiunas, Lukas; Pedersen, Thomas Helmer; Toor, Saqib Sohail

    2017-01-01

    The work investigates a new potential feedstock source for hydrothermal liquefaction (HTL) driven biocrude production. Specifically, the focus is set on utilizing spent mushroom compost (SMC), the primary waste by-product from mushroom farming. It is considered as a feedstock for HTL conversion due...

  10. Shear-wave velocity-based probabilistic and deterministic assessment of seismic soil liquefaction potential

    Science.gov (United States)

    Kayen, R.; Moss, R.E.S.; Thompson, E.M.; Seed, R.B.; Cetin, K.O.; Der Kiureghian, A.; Tanaka, Y.; Tokimatsu, K.

    2013-01-01

    Shear-wave velocity (Vs) offers a means to determine the seismic resistance of soil to liquefaction by a fundamental soil property. This paper presents the results of an 11-year international project to gather new Vs site data and develop probabilistic correlations for seismic soil liquefaction occurrence. Toward that objective, shear-wave velocity test sites were identified, and measurements made for 301 new liquefaction field case histories in China, Japan, Taiwan, Greece, and the United States over a decade. The majority of these new case histories reoccupy those previously investigated by penetration testing. These new data are combined with previously published case histories to build a global catalog of 422 case histories of Vs liquefaction performance. Bayesian regression and structural reliability methods facilitate a probabilistic treatment of the Vs catalog for performance-based engineering applications. Where possible, uncertainties of the variables comprising both the seismic demand and the soil capacity were estimated and included in the analysis, resulting in greatly reduced overall model uncertainty relative to previous studies. The presented data set and probabilistic analysis also help resolve the ancillary issues of adjustment for soil fines content and magnitude scaling factors.

  11. Liquefaction of H2 molecules upon exterior surfaces of carbon nanotube bundles

    International Nuclear Information System (INIS)

    Han, Sang Soo; Kang, Jeung Ku; Lee, Hyuck Mo; Duin, Adri C.T. van; Goddard, William A. III

    2005-01-01

    We have used molecular dynamics simulations to investigate interaction of H 2 molecules on the exterior surfaces of carbon nanotubes (CNTs): single and bundle types. At 80 K and 10 MPa, it is found that charge transfer occurs from a low curvature region to a high curvature region of the deformed CNT bundle, which develops charge polarization only on the deformed structure. The long-range electrostatic interactions of polarized charges on the deformed CNT bundle with hydrogen molecules are observed to induce a high local-ordering of H 2 gas that results in hydrogen liquefaction. Our predicted heat of hydrogen liquefaction on the CNT bundle is 97.6 kcal kg -1 . On the other hand, hydrogen liquefaction is not observed in the CNT of a single type. This is because charge polarization is not developed on the single CNT as it is symmetrically deformed under the same pressure. Consequently, the hydrogen storage capacity on the CNT bundle is much higher due to liquefaction than that on the single CNT. Additionally, our results indicate that it would also be possible to liquefy H 2 gas on a more strongly polarized CNT bundle at temperatures higher than 80 K

  12. Fiscal 1990 report on the bituminous coal liquefaction section meeting; 1990 nendo rekiseitan ekika bukai hokokusho

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1991-03-01

    At the 1st, 2nd, and 3rd group meetings held for the fiscal year, reports are delivered and discussions are made concerning the progress of research and development activities. Reported and discussed in relation to the pilot plant support research, etc., are studies with the 1t/d PSU (process supporting unit) (Nippon Steel Corporation, Mitsui Coal Liquefaction Co., Ltd., and Japan Coal Oil Co., Ltd.); development of an optimum coal refining technique (Sumitomo Coal Mining Co., Ltd.); development of an optimum pretreatment technique and improvement on distillate distribution (Sumitomo Metal Industries, Ltd.); studies of coal liquefaction conditions (Mitsui Engineering and Shipbuilding Co., Ltd.); and studies of solvent hydrogenation catalysts (Sumitomo Metal Mining Co., Ltd., and Chiyoda Corp.). Reported and discussed in relation to researches using a bituminous coal liquefaction pilot plant are the progress of the 150t/d PP (pilot plant) effort (Japan Coal Oil Co., Ltd.) and the outlines of pilot surveys (Japan Coal Oil Co., Ltd.), the latter covering liquefaction solvent performance optimization, slurry pre-heating furnaces, coal slurry properties, and so forth. (NEDO)

  13. Fiscal 1993 report. Coal liquefaction committee; 1993 nendo sekitan ekika iinkai hokokusho

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1994-03-01

    The committee in this fiscal year had the 1st meeting in July 1993, the 2nd in December 1993, and the 3rd in March 1994, when fiscal 1993 research and development programs and results were reported and discussed. Reported and discussed at the 2nd meeting were the compilation of brown coal liquefaction technology development project results, evaluation report on the same, hydrorefining of oil from brown coal and the research and development of application technologies for the same, and an environmental safety evaluation test on the same. In selecting a standard coal for the operation of the 150 ton/day pilot plant, PSU (process supporting unit)-aided studies were made on the analytical values presented by coals, yield of the liquid, yield of the liquefaction residue, yield of the generated gas, amount of the hydrogen consumed, coal oil properties, liquefaction residue properties, operationality, etc. On-site investigations were conducted also in Indonesia, and a conclusion was reached that Tanito Harum coal would be the most suitable for the pilot plant. Concerning the liquefaction catalyst for the pilot plant, a report was given on a comparison made between the activity of a synthetic iron sulfide and that of natural pyrite. (NEDO)

  14. Fiscal 1994 report. Liquefaction key technology subcommittee; 1994 nendo ekika kiban gijutsu bukai hokokusho

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1995-03-01

    The subcommittee held the 1st meeting in August 1994 and the 2nd in March 1995, when preceding fiscal year's research results, fiscal 1994 research plans, fiscal 1994 research results, etc., were introduced, and deliberated. In the study of hydrorefining of naphtha, kerosene, and light oil fractions, a nitrogen concentration level of not more than 5 ppm was achieved by refining oils from Indonesian coal. Studies were also made about the two-step hydrorefining system, the relationship between the coal oil refining level and sludge formation, etc. In the research for the development of novel catalysts for upgrading coal oil, the active life of a nickel-supporting catalyst for hydrogenation at the 1st step was somewhat prolonged with an increase in the amount of nickel. In the study of coal liquefaction conditions, an AWIP method was deliberated, wherein liquefaction process waste water was utilized as one of catalytic component adjusting materials. For upgrading liquefaction key technologies, studies were made for catalyst improvement and pretreatment method development, and about the behavior of liquefaction reaction in a high boiling solvent-aided process. (NEDO)

  15. Hydrothermal liquefaction of Spirulina and Nannochloropsis Salina under subcritical and supercritical water conditions

    DEFF Research Database (Denmark)

    Toor, Saqib; Reddy, H.; Deng, S.

    2013-01-01

    residue, and recycling process water for algae cultivation. GC-MS, elemental analyzer, FT-IR, calorimeter and nutrient analysis were used to analyze bio-crude, lipid-extracted algae and water samples produced in the hydrothermal liquefaction process. The highest bio-crude yield of 46% was obtained...

  16. Bio-char derived from sewage sludge by liquefaction: Characterization and application for dye adsorption

    Energy Technology Data Exchange (ETDEWEB)

    Leng, Lijian [College of Environmental Science and Engineering, Hunan University, Changsha 410082 (China); Key Laboratory of Environment Biology and Pollution Control, Hunan University, Ministry of Education, Changsha 410082 (China); Yuan, Xingzhong, E-mail: yxz@hnu.edu.cn [College of Environmental Science and Engineering, Hunan University, Changsha 410082 (China); Key Laboratory of Environment Biology and Pollution Control, Hunan University, Ministry of Education, Changsha 410082 (China); Huang, Huajun [School of Land Resources and Environment, Jiangxi Agricultural University, Nanchang 330045 (China); Shao, Jianguang; Wang, Hou [College of Environmental Science and Engineering, Hunan University, Changsha 410082 (China); Key Laboratory of Environment Biology and Pollution Control, Hunan University, Ministry of Education, Changsha 410082 (China); Chen, Xiaohong [School of Business, Central South University, Changsha 410083 (China); Zeng, Guangming [College of Environmental Science and Engineering, Hunan University, Changsha 410082 (China); Key Laboratory of Environment Biology and Pollution Control, Hunan University, Ministry of Education, Changsha 410082 (China)

    2015-08-15

    Graphical abstract: - Highlights: • SS liquefaction bio-chars were effective on MG and MB removal from aqueous. • MG adsorption capacity depended strongly on carboxylic and phenolic groups. • Metal release accounted for nearly 30% of the total MG adsorbed on bio-chars. • Acetone and low temperature favor effective adsorbent production by liquefaction. - Abstract: Bio-chars produced by liquefaction of sewage sludge with methanol, ethanol, or acetone as the solvent at 260–380 °C were characterized in terms of their elemental composition, thermogravimetric characteristics, surface area and pore size distribution, and oxygen-containing functional groups composition. The surface area and total volume of the bio-chars were low, but the contents of oxygen-containing functional groups were high. The bio-chars were effective on Malachite green (MG) and Methylene blue (MB) removal from aqueous solution. The MG adsorption equilibrium data showed excellent fit to the Langmuir model and the kinetic data fitted well to the Pseudo-second-order model. Thermodynamic investigations indicated that MG adsorption on bio-char was spontaneous and endothermic. The MG adsorption mechanism appears to be associated with cation release and functional group participation. Additionally, liquefaction of SS with acetone as the solvent at low temperature (280 °C) would favor the production of bio-char adsorbent in terms of bio-char yield and MG and MB adsorption capacity.

  17. Quantitative characterization of the aqueous fraction from hydrothermal liquefaction of algae

    Energy Technology Data Exchange (ETDEWEB)

    Maddi, Balakrishna; Panisko, Ellen; Wietsma, Thomas; Lemmon, Teresa; Swita, Marie; Albrecht, Karl; Howe, Daniel

    2016-10-01

    Aqueous streams generated from hydrothermal liquefaction contain approximately 30% of the total carbon present from the algal feed. Hence, this aqueous carbon must be utilized to produce liquid fuels and/or specialty chemicals for economic sustainability of hydrothermal liquefaction on industrial scale. In this study, aqueous fractions produced from the hydrothermal liquefaction of fresh water and saline water algal cultures were analyzed using a wide variety of analytical instruments to determine their compositional characteristics. This study will also inform researchers designing catalysts for down-stream processing such as high-pressure catalytic conversion of organics in aqueous phase, catalytic hydrothermal gasification, and biological conversions. Organic chemical compounds present in all eight aqueous fractions were identified using two-dimensional gas chromatography equipped with time-of-flight mass spectrometry. Identified compounds include organic acids, nitrogen compounds and aldehydes/ketones. Conventional gas chromatography and liquid chromatography methods were utilized to quantify the identified compounds. Inorganic species in the aqueous stream of hydrothermal liquefaction of algae were identified using ion chromatography and inductively coupled plasma optical emission spectrometer. The concentrations of organic chemical compounds and inorganic species are reported. The amount quantified carbon ranged from 45 to 72 % of total carbon in the aqueous fractions.

  18. New fast reactor installation concept

    International Nuclear Information System (INIS)

    Anon.

    1976-01-01

    The large size and complexity of fast reactor installations are emphasised and these difficulties will be increased with the advent of fast reactors of higher power. In this connection a new concept of fast reactor installation is described with a view to reducing the size of the installation and enabling most components, including even the primary vessel, to be constructed within the confines of a workshop. Full constructional details are given. (U.K.)

  19. Advanced Direct Liquefaction Concepts for PETC Generic Units - Phase II

    Energy Technology Data Exchange (ETDEWEB)

    None

    1997-12-01

    The results of Laboratory and Bench-Scale experiments and supporting technical and economic assessments conducted under DOE Contract No. DE-AC22-91PC91040 are reported for the period July 1, 1997 to September 30, 1997. This contract is with the University of Kentucky Research Foundation which supports work with the University of Kentucky Center for Applied Energy Research, CONSOL, Inc., LDP Associates, and Hydrocarbon Technologies, Inc. This work involves the introduction into the basic two stage liquefaction process several novel concepts which include dispersed lower-cost catalysts, coal cleaning by oil agglomeration, and distillate hydrotreating and dewaxing. Results are reported from experiments in which various methods were tested to activate dispersed Mo precursors. Several oxothiomolybdates precursors having S/Mo ratios from two to six were prepared. Another having a S/Mo ratio of eleven was also prepared that contained an excess of sulfur. In the catalyst screening test, none of these precursors exhibited an activity enhancement that might suggest that adding sulfur into the structure of the Mo precursors would be beneficial to the process. In another series of experiments, AHM impregnated coal slurried in the reaction mixture was pretreated withH S/H under pressure and successively heated for 30 min at 120, 250 2 2 and 360 C. THF conversions in the catalyst screening test were not affected while resid conversions o increased such that pretreated coals impregnated with 100 ppm Mo gave conversions equivalent to untreated coals impregnated with 300 ppm fresh Mo. Cobalt, nickel and potassium phosphomolybdates were prepared and tested as bimetallic precursors. The thermal stability of these compounds was evaluated in TG/MS to determine whether the presence of the added metal would stabilize the Keggin structure at reaction temperature. Coals impregnated with these salts showed the Ni and Co salts gave the same THF conversion as PMA while the Ni salt gave higher

  20. Assessment of Susceptibility to Liquefaction of Saturated Road Embankment Subjected to Dynamic Loads

    Science.gov (United States)

    Borowiec, Anna; Maciejewski, Krzysztof

    2014-03-01

    Liquefaction has always been intensely studied in parts of the world where earthquakes occur. However, the seismic activity is not the only possible cause of this phenomenon. It may in fact be triggered by some human activities, such as constructing and mining or by rail and road transport. In the paper a road embankment built across a shallow water reservoir is analyzed in terms of susceptibility to liquefaction. Two types of dynamic loadings are considered: first corresponding to an operation of a vibratory roller and second to an earthquake. In order to evaluate a susceptibility of soil to liquefaction, a factor of safety against triggering of liquefaction is used (FSTriggering). It is defined as a ratio of vertical effective stresses to the shear stresses both varying with time. For the structure considered both stresses are obtained using finite element method program, here Plaxis 2D. The plastic behavior of the cohesionless soils is modeled by means of Hardening Soil (HS) constitutive relationship, implemented in Plaxis software. As the stress tensor varies with time during dynamic excitation, the FSTriggering has to be calculated for some particular moment of time when liquefaction is most likely to occur. For the purposes of this paper it is named a critical time and established for reference point at which the pore pressures were traced in time. As a result a factor of safety distribution throughout embankment is generated. For the modeled structure, cyclic point loads (i.e., vibrating roller) present higher risk than earthquake of magnitude 5.4. Explanation why considered structure is less susceptible to earthquake than typical dam could lay in stabilizing and damping influence of water, acting here on both sides of the slope. Analogical procedure is applied to assess liquefaction susceptibility of the road embankment considered but under earthquake excitation. Only the higher water table is considered as it is the most unfavorable. Additionally the

  1. Liquefaction assessment based on combined use of CPT and shear wave velocity measurements

    Science.gov (United States)

    Bán, Zoltán; Mahler, András; Győri, Erzsébet

    2017-04-01

    Soil liquefaction is one of the most devastating secondary effects of earthquakes and can cause significant damage in built infrastructure. For this reason liquefaction hazard shall be considered in all regions where moderate-to-high seismic activity encounters with saturated, loose, granular soil deposits. Several approaches exist to take into account this hazard, from which the in-situ test based empirical methods are the most commonly used in practice. These methods are generally based on the results of CPT, SPT or shear wave velocity measurements. In more complex or high risk projects CPT and VS measurement are often performed at the same location commonly in the form of seismic CPT. Furthermore, VS profile determined by surface wave methods can also supplement the standard CPT measurement. However, combined use of both in-situ indices in one single empirical method is limited. For this reason, the goal of this research was to develop such an empirical method within the framework of simplified empirical procedures where the results of CPT and VS measurements are used in parallel and can supplement each other. The combination of two in-situ indices, a small strain property measurement with a large strain measurement, can reduce uncertainty of empirical methods. In the first step by careful reviewing of the already existing liquefaction case history databases, sites were selected where the records of both CPT and VS measurement are available. After implementing the necessary corrections on the gathered 98 case histories with respect to fines content, overburden pressure and magnitude, a logistic regression was performed to obtain the probability contours of liquefaction occurrence. Logistic regression is often used to explore the relationship between a binary response and a set of explanatory variables. The occurrence or absence of liquefaction can be considered as binary outcome and the equivalent clean sand value of normalized overburden corrected cone tip

  2. Report on the FY 1998 results of the New Sunshine Project (B version). Development of coal liquefaction technology (Development of base technology of liquefaction (Project on internationalization of coal liquefaction technology)); 1998 nendo sekitan ekika gijutsu kaihatsu seika hokokusho (B ban). Ekika kiban gijutsu no kaihatsu (sekitan ekika gijutsu no kokusaika jigyo)

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1999-03-01

    In 1994, a memorandum on the research cooperation was agreed between NEDO and BPPT (The Agency for the Assessment and Application Technology) in Indonesia, based on the request for the coal liquefaction technology cooperation from BPPT. It includes the following items: conference for professionals to be held, invitation and training of Indonesian engineers, activity for joint field survey and potential survey of location of coal liquefaction commercial plant. Further in 1997, the secondary memorandum was concluded for the potential survey for securing the hydrogen required for coal liquefaction by coal gasification. The survey was summarized as the potential survey for location of coal liquefaction. In the testing study for improving economical efficiency of liquefaction process, it was made clear that the higher the Fe content of Banko coal is, the higher the reaction of liquefaction is, and that Fe compounds in coal show catalysis. In the Soroako area in Sulawesi island, there are the nickel mine run by PT. Inco. Soroako limonite is promising as catalyst material for commercial-scale coal liquefaction. In the gasification method, the plant construction cost increases, but the production amount of coal-derived liquid can be increased. That is more profitable than the production of hydrogen from natural gas. (NEDO)

  3. Dynamic behavior of potentially unstable soils and application of model for seismic risk reduction from liquefaction occurrence

    International Nuclear Information System (INIS)

    Sheshov, Vlatko

    2002-11-01

    Throughout the last decades, liquefaction phenomenon has been one of the most frequently discussed subjects in geotechnical earthquake engineering. Liquefaction has been a problem arousing considerable attention among the world scientists. The consequences from liquefaction occurrence have been present after each stronger earthquake. We have been witnesses of several strong earthquakes (Kobe - Japan, Chi Chi-Taiwan, Bhuj-India) that have occurred in the last decade. In these earthquakes, the liquefaction phenomenon caused severe damage to structures, loss of their functioning and indirect loss of human lives. Liquefaction as a phenomenon should not arouse fear but should call for serious elaboration and attention instead. The destructive nature of liquefaction could be mitigated, i.e., overcome in two ways: avoiding construction at locations characterized by high liquefaction potential which is not always possible and taking of measures for improvement of foundation soil. Finding out suitable measures for improvement of soil and thus mitigating the liquefaction potential has been the main incentive for the elaboration of this dissertation. The dissipation method involving the use of vertical drains as one of the measures for improvement of soils has been elaborated in details in this scientific work. The doctoral dissertation has been realized through experimental and analytical investigations. The experimental investigations done in the first phase represent model seismic shaking table tests of the efficiency of vertical drains (prefabricated and gravel drains). The analytical investigations in this phase have involved mathematical simulation of the effect of vertical drains upon pore pressure state during the experiments. The second phase of the experimental investigations has involved model tests of the behavior of pile foundations in soils susceptible to liquefaction with installed prefabricated drains. In this phase, the 'p - y' relationships have been

  4. Liquefaction of Semen Generates and Later Degrades a Conserved Semenogelin Peptide That Enhances HIV Infection

    Science.gov (United States)

    Liu, Haichuan; Usmani, Shariq M.; Neidleman, Jason; Müller, Janis A.; Avila-Herrera, Aram; Gawanbacht, Ali; Zirafi, Onofrio; Chu, Simon; Dong, Ming; Kumar, Senthil T.; Smith, James F.; Pollard, Katherine S.; Fändrich, Marcus; Kirchhoff, Frank; Münch, Jan; Witkowska, H. Ewa; Greene, Warner C.

    2014-01-01

    ABSTRACT Semen enhances HIV infection in vitro, but how long it retains this activity has not been carefully examined. Immediately postejaculation, semen exists as a semisolid coagulum, which then converts to a more liquid form in a process termed liquefaction. We demonstrate that early during liquefaction, semen exhibits maximal HIV-enhancing activity that gradually declines upon further incubation. The decline in HIV-enhancing activity parallels the degradation of peptide fragments derived from the semenogelins (SEMs), the major components of the coagulum that are cleaved in a site-specific and progressive manner upon initiation of liquefaction. Because amyloid fibrils generated from SEM fragments were recently demonstrated to enhance HIV infection, we set out to determine whether any of the liquefaction-generated SEM fragments associate with the presence of HIV-enhancing activity. We identify SEM1 from amino acids 86 to 107 [SEM1(86-107)] to be a short, cationic, amyloidogenic SEM peptide that is generated early in the process of liquefaction but that, conversely, is lost during prolonged liquefaction due to the activity of serine proteases. Synthetic SEM1(86-107) amyloids directly bind HIV-1 virions and are sufficient to enhance HIV infection of permissive cells. Furthermore, endogenous seminal levels of SEM1(86-107) correlate with donor-dependent variations in viral enhancement activity, and antibodies generated against SEM1(86-107) recognize endogenous amyloids in human semen. The amyloidogenic potential of SEM1(86-107) and its virus-enhancing properties are conserved among great apes, suggesting an evolutionarily conserved function. These studies identify SEM1(86-107) to be a key, HIV-enhancing amyloid species in human semen and underscore the dynamic nature of semen's HIV-enhancing activity. IMPORTANCE Semen, the most common vehicle for HIV transmission, enhances HIV infection in vitro, but how long it retains this activity has not been investigated. Semen

  5. Assessment of thermodynamic models for the design, analysis and optimisation of gas liquefaction systems

    International Nuclear Information System (INIS)

    Nguyen, Tuong-Van; Elmegaard, Brian

    2016-01-01

    Highlights: • Six thermodynamic models used for evaluating gas liquefaction systems are compared. • Three gas liquefaction systems are modelled, assessed and optimised for each equation of state. • The predictions of thermophysical properties and energy flows are significantly different. • The GERG-2008 model is the only consistent one, while cubic, virial and statistical equations are unsatisfying. - Abstract: Natural gas liquefaction systems are based on refrigeration cycles – they consist of the same operations such as heat exchange, compression and expansion, but they have different layouts, components and working fluids. The design of these systems requires a preliminary simulation and evaluation of their performance. However, the thermodynamic models used for this purpose are characterised by different mathematical formulations, ranges of application and levels of accuracy. This may lead to inconsistent results when estimating hydrocarbon properties and assessing the efficiency of a given process. This paper presents a thorough comparison of six equations of state widely used in the academia and industry, including the GERG-2008 model, which has recently been adopted as an ISO standard for natural gases. These models are used to (i) estimate the thermophysical properties of a Danish natural gas, (ii) simulate, and (iii) optimise liquefaction systems. Three case studies are considered: a cascade layout with three pure refrigerants, a single mixed-refrigerant unit, and an expander-based configuration. Significant deviations are found between all property models, and in all case studies. The main discrepancies are related to the prediction of the energy flows (up to 7%) and to the heat exchanger conductances (up to 11%), and they are not systematic errors. The results illustrate the superiority of using the GERG-2008 model for designing gas processes in real applications, with the aim of reducing their energy use. They demonstrate as well that

  6. St. Louis area earthquake hazards mapping project; seismic and liquefaction hazard maps

    Science.gov (United States)

    Cramer, Chris H.; Bauer, Robert A.; Chung, Jae-won; Rogers, David; Pierce, Larry; Voigt, Vicki; Mitchell, Brad; Gaunt, David; Williams, Robert; Hoffman, David; Hempen, Gregory L.; Steckel, Phyllis; Boyd, Oliver; Watkins, Connor M.; Tucker, Kathleen; McCallister, Natasha

    2016-01-01

    We present probabilistic and deterministic seismic and liquefaction hazard maps for the densely populated St. Louis metropolitan area that account for the expected effects of surficial geology on earthquake ground shaking. Hazard calculations were based on a map grid of 0.005°, or about every 500 m, and are thus higher in resolution than any earlier studies. To estimate ground motions at the surface of the model (e.g., site amplification), we used a new detailed near‐surface shear‐wave velocity model in a 1D equivalent‐linear response analysis. When compared with the 2014 U.S. Geological Survey (USGS) National Seismic Hazard Model, which uses a uniform firm‐rock‐site condition, the new probabilistic seismic‐hazard estimates document much more variability. Hazard levels for upland sites (consisting of bedrock and weathered bedrock overlain by loess‐covered till and drift deposits), show up to twice the ground‐motion values for peak ground acceleration (PGA), and similar ground‐motion values for 1.0 s spectral acceleration (SA). Probabilistic ground‐motion levels for lowland alluvial floodplain sites (generally the 20–40‐m‐thick modern Mississippi and Missouri River floodplain deposits overlying bedrock) exhibit up to twice the ground‐motion levels for PGA, and up to three times the ground‐motion levels for 1.0 s SA. Liquefaction probability curves were developed from available standard penetration test data assuming typical lowland and upland water table levels. A simplified liquefaction hazard map was created from the 5%‐in‐50‐year probabilistic ground‐shaking model. The liquefaction hazard ranges from low (60% of area expected to liquefy) in the lowlands. Because many transportation routes, power and gas transmission lines, and population centers exist in or on the highly susceptible lowland alluvium, these areas in the St. Louis region are at significant potential risk from seismically induced liquefaction and associated

  7. Effects of relative density and accumulated shear strain on post-liquefaction residual deformation

    Directory of Open Access Journals (Sweden)

    J. Kim

    2013-10-01

    Full Text Available The damage caused by liquefaction, which occurs following an earthquake, is usually because of settlement and lateral spreading. Generally, the evaluation of liquefaction has been centered on settlement, that is, residual volumetric strain. However, in actual soil, residual shear and residual volumetric deformations occur simultaneously after an earthquake. Therefore, the simultaneous evaluation of the two phenomena and the clarification of their relationship are likely to evaluate post-liquefaction soil behaviors more accurately. Hence, a quantitative evaluation of post-liquefaction damage will also be possible. In this study, the effects of relative density and accumulated shear strain on post-liquefaction residual deformations were reviewed through a series of lateral constrained-control hollow cylindrical torsion tests under undrained conditions. In order to identify the relationship between residual shear and residual volumetric strains, this study proposed a new test method that integrates monotonic loading after cyclic loading, and K0-drain after cyclic loading – in other words, the combination of cyclic loading, monotonic loading, and the K0 drain. In addition, a control that maintained the lateral constrained condition across all the processes of consolidation, cyclic loading, monotonic loading, and drainage was used to reproduce the anisotropy of in situ ground. This lateral constrain control was performed by controlling the axial strain, based on the assumption that under undrained conditions, axial and lateral strains occur simultaneously, and unless axial strain occurs, lateral strain does not occur. The test results confirmed that the recovery of effective stresses, which occur during monotonic loading and drainage after cyclic loading, respectively, result from mutually different structural restoration characteristics. In addition, in the ranges of 40–60% relative density and 50–100% accumulated shear strain, relative

  8. Comparison of oxygen liquefaction methods for use on the Martian surface

    Science.gov (United States)

    Johnson, W. L.; Hauser, D. M.; Plachta, D. W.; Wang, X.-Y. J.; Banker, B. F.; Desai, P. S.; Stephens, J. R.; Swanger, A. M.

    2018-03-01

    In order to use oxygen that is produced on the surface of Mars from In-Situ production processes in a chemical propulsion system, the oxygen must first be converted from vapor phase to liquid phase and then stored within the propellant tanks of the propulsions system. There are multiple ways that this can be accomplished, from simply attaching a liquefaction system onto the propellant tanks to carrying separate tanks for liquefaction and storage of the propellant and loading just prior to launch (the way that traditional rocket launches occur on Earth). A study was done into these various methods by which the oxygen (and methane) could be liquefied and stored on the Martian surface. Five different architectures or cycles were considered: Tube-on-Tank (also known as Broad Area Cooling or Distributed Refrigeration), Tube-in-Tank (also known as Integrated Refrigeration and Storage), a modified Linde open liquefaction/refrigeration cycle, the direct mounting of a pulse tube cryocooler onto the tank, and an in-line liquefier at ambient pressure. Models of each architecture were developed to give insight into the performance and losses of each of the options. The results were then compared across eight categories: Mass, Power (both input and heat rejection), Operability, Cost, Manufacturability, Reliability, Volume-ility, and Scalability. The result was that Tube-on-Tank and Tube-in-Tank architectures were the most attractive solutions, with NASA's engineering management choosing to pursue tube on tank development rather than further differentiate the two. As a result NASA is focusing its Martian surface liquefaction activities and technology development on Tube-on-Tank liquefaction cycles.

  9. Analysis of flammability limits for the liquefaction process of oxygen-bearing coal-bed methane

    International Nuclear Information System (INIS)

    Li, Q.Y.; Wang, L.; Ju, Y.L.

    2011-01-01

    Highlights: → A novel liquefaction and distillation process is designed for oxygen bearing coal-bed methane. → Oxygen contained in coal-bed methane is removed in distillation process. → Flammability limits are analyzed for the whole operation process. → We find explosion hazard may exist in distillation tower. → Effective measures are proposed to ensure the operation safety in distillation tower. - Abstract: A novel liquefaction and distillation process has been proposed and designed for the typical oxygen-bearing coal-bed methane (CBM), in which the impurities of the oxygen and nitrogen components are removed in the distillation column. The flammability limit theory combining with HYSYS simulation results are employed to analyze and calculate the flammability limits and the results indicate that no flammability hazard exists in the stages of compression, liquefaction and throttling. However, flammability hazard exists at the top the distillation column because the methane mole fraction decreases to the value below the upper flammability limit (UFL). The safety measures of initially removing oxygen content from the feed gas combining with the control of the bottom flowrate (flowrate of the liquid product at column bottom) are proposed to ensure the operation safety of the liquefaction process. The results reveal that the operation safety of the whole process can be guaranteed, together with high methane recovery rate and high purity of the liquid product. The applicability of the liquefaction process has also been analyzed in this paper. The simulation results can offer references for the separation of oxygen from CBM, the analysis of flammability limits and the safety measures for the whole process.

  10. Status of health and environmental research relative to direct coal liquefaction: 1976 to the present

    Energy Technology Data Exchange (ETDEWEB)

    Gray, R.H.; Cowser, K.E. (eds.)

    1982-06-01

    This document describes the status of health and environmental research efforts, supported by the US Department of Energy (DOE), to assist in the development of environmentally acceptable coal liquefaction processes. Four major direct coal liquefaction processes are currently in (or have been investigated at) the pilot plant stage of development. Two solvent refined coal processes (SRC-I and -II), H-coal (a catalytic liquefaction process) and Exxon donor solvent (EDS). The Pacific Northwest Laboratory was assigned responsibility for evaluating SRC process materials and prepared comprehensive health and environmental effects research program plans for SRC-I and -II. A similar program plan was prepared for H-coal process materials by the Oak Ridge National Laboratory. A program has been developed for EDS process materials by Exxon Research and Engineering Co. The program includes short-term screening of coal-derived materials for potential health and ecological effects. Longer-term assays are used to evaluate materials considered most representative of potential commercial practice and with greatest potential for human exposure or release to the environment. Effects of process modification, control technologies and changing operational conditions on potential health and ecological effects are also being evaluated. These assessments are being conducted to assist in formulating cost-effective environmental research programs and to estimate health and environmental risks associated with a large-scale coal liquefaction industry. Significant results of DOE's health and environmental research efforts relative to coal liquefaction include the following: chemical characterization, health effects, ecological fate and effects, amelioration and risk assessment.

  11. H Reactor

    Data.gov (United States)

    Federal Laboratory Consortium — The H Reactor was the first reactor to be built at Hanford after World War II.It became operational in October of 1949, and represented the fourth nuclear reactor on...

  12. The 2006 Pingtung Earthquake Doublet Triggered Seafloor Liquefaction: Revisiting the Evidence with Ultra-High-Resolution Seafloor Mapping

    Science.gov (United States)

    Su, C. C.; Chen, T. T.; Paull, C. K.; Gwiazda, R.; Chen, Y. H.; Lundsten, E. M.; Caress, D. W.; Hsu, H. H.; Liu, C. S.

    2017-12-01

    Since Heezen and Ewing's (1952) classic work on the 1929 Grand Banks earthquake, the damage of submarine cables have provided critical information on the nature of seafloor mass movements or sediment density flows. However, the understanding of the local conditions that lead to particular seafloor failures earthquakes trigger is still unclear. The Decemeber 26, 2006 Pingtung earthquake doublet which occurred offshore of Fangliao Township, southwestern Taiwan damaged 14 submarine cables between Gaoping slope to the northern terminus of the Manila Trench. Local fisherman reported disturbed waters at the head of the Fangliao submarine canyon, which lead to conjectures that eruptions of mud volcanoes which are common off the southwestern Taiwan. Geophysical survey were conducted to evaluate this area which revealed a series of faults, liquefied strata, pockmarks and acoustically transparent sediments with doming structures which may relate to the submarine groundwater discharge. Moreover, shipboard multi-beam bathymetric survey which was conducted at the east of Fangliao submarine canyon head shows over 10 km2 area with maximum depth around 40 m of seafloor subsidence after Pingtung earthquake. The north end of the subsidence is connected to the Fangliao submarine canyon where the first cable failed after Pingtung earthquake. The evidences suggests the earthquake triggered widespeard liquefaction and generated debris flows within Fangliao submarine canyon. In May 2017, an IONTU-MBARI Joint Survey Cruise (OR1-1163) was conducted on using MBARI Mapping AUV and miniROV to revisit the area where the cable damaged after Pingtung earthquake. From newly collected ultra-high-resolution (1-m lateral resolution) bathymetry data, the stair-stepped morphology is observed at the edge of canyon. The comet-shaped depressions are located along the main headwall of the seafloor failure. The new detailed bathymetry reveal details which suggest Fangliao submarine canyon head is

  13. Making Connections

    Science.gov (United States)

    Pien, Cheng Lu; Dongsheng, Zhao

    2011-01-01

    Effective teaching includes enabling learners to make connections within mathematics. It is easy to accord with this statement, but how often is it a reality in the mathematics classroom? This article describes an approach in "connecting equivalent" fractions and whole number operations. The authors illustrate how a teacher can combine a common…

  14. Emergency reactor cooling device

    International Nuclear Information System (INIS)

    Arakawa, Ken.

    1993-01-01

    An emergency nuclear reactor cooling device comprises a water reservoir, emergency core cooling water pipelines having one end connected to a water feeding sparger, fire extinguishing facility pipelines, cooling water pressurizing pumps, a diesel driving machine for driving the pumps and a battery. In a water reservoir, cooling water is stored by an amount required for cooling the reactor upon emergency and for fire extinguishing, and fire extinguishing facility pipelines connecting the water reservoir and the fire extinguishing facility are in communication with the emergency core cooling water pipelines connected to the water feeding sparger by system connection pipelines. Pumps are operated by a diesel power generator to introduce cooling water from the reservoir to the emergency core cooling water pipelines. Then, even in a case where AC electric power source is entirely lost and the emergency core cooling system can not be used, the diesel driving machine is operated using an exclusive battery, thereby enabling to inject cooling water from the water reservoir to a reactor pressure vessel and a reactor container by the diesel drive pump. (N.H.)

  15. Reactor control device

    International Nuclear Information System (INIS)

    Kameda, Akiyuki.

    1979-01-01

    Purpose: To enable three types of controls, that is, level control, scram control and excess reactivity control required for a reactor by a same mechanism by feeding neutron absorber liquid and pressure control gas to several blind pipes provided in the reactor core. Constitution: A plurality of blind pipes are disposed spaced apart in a reactor core and connected by way of injection pipes to a neutron absorber liquid tank. A pressure regulator is connected to the blind pipes, to which pressure control gas is supplied. The neutron absorber liquid used herein consists of sodium, potassium or their alloy, or mercury as a basic substance incorporated with one or more selected from boron, tantalum, rhenium, europium or their compounds. The level control, scram control and excess reactivity control can be attained by moderating the pressure changes in the pressure control gas or by regulating the fluctuation in the liquid level. (Horiughi, T.)

  16. Meltdown reactor core cooling facility

    International Nuclear Information System (INIS)

    Matsuoka, Tsuyoshi.

    1992-01-01

    The meltdown reactor core cooling facility comprises a meltdown reactor core cooling tank, a cooling water storage tank situates at a position higher than the meltdown reactor core cooling tank, an upper pipeline connecting the upper portions of the both of the tanks and a lower pipeline connecting the lower portions of them. Upon occurrence of reactor core meltdown, a high temperature meltdown reactor core is dropped on the cooling tank to partially melt the tank and form a hole, from which cooling water is flown out. Since the water source of the cooling water is the cooling water storage tank, a great amount of cooling water is further dropped and supplied and the reactor core is submerged and cooled by natural convection for a long period of time. Further, when the lump of the meltdown reactor core is small and the perforated hole of the meltdown reactor cooling tank is small, cooling water is boiled by the high temperature lump intruding into the meltdown reactor core cooling tank and blown out from the upper pipeline to the cooling water storage tank to supply cooling water from the lower pipeline to the meltdown reactor core cooling tank. Since it is constituted only with simple static facilities, the facility can be simplified to attain improvement of reliability. (N.H.)

  17. Agreement of 10 September 1991 between the International Atomic Energy Agency and the Government of the Islamic Republic of Pakistan for the application of safeguards in connection with the supply of a miniature neutron source reactor from the People's Republic of China

    International Nuclear Information System (INIS)

    1991-10-01

    The document reproduces the text of the Agreement of 10 September 1991, between the Government of the Islamic Republic of Pakistan and the International Atomic Energy Agency for the application of safeguards in connection with the supply of a miniature neutron source reactor from the People's Republic of China. The Agreement was approved by the Agency's Board of Governors on 20 February 1990 and entered into force upon signature on 10 September 1991

  18. Survey on peripheral techniques of brown coal liquefaction techniques; Kattan ekika gijutsu ni kansuru shuhen gijutsu no chosa

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1980-09-01

    Described herein are results of survey on brown coal liquefaction techniques and peripheral techniques, centered by COSTEAM process under development in USA, solubilization by alcohol and liquefaction and cracking with the aid of tetrahydroquinoline as the hydrogen donor under development in Japan, and low-temperature carbonization and new promising techniques. The COSTEAM process shows higher reaction rates, conversions and oil yields for brown coal liquefaction than the one using hydrogen gas. Some of the problems involved in this process high viscosity and oxygenated compound content of the product oil. The product oil is acceptable as fuel for power generating plants and can be produced at a moderate cost, but may be unsuitable as vehicle fuel. Coal liquefaction and solubilization processes are mainly represented by those which use hydrogen. The hydrogen cost, which is high, determines the product price. The processes which use alcohol or tetrahydroquinoline are still in the experimental stage. (NEDO)

  19. About Connections

    Directory of Open Access Journals (Sweden)

    Kathleen S Rockland

    2015-05-01

    Full Text Available Despite the attention attracted by connectomics, one can lose sight of the very real questions concerning What are connections? In the neuroimaging community, structural connectivity is ground truth and underlying constraint on functional or effective connectivity. It is referenced to underlying anatomy; but, as increasingly remarked, there is a large gap between the wealth of human brain mapping and the relatively scant data on actual anatomical connectivity. Moreover, connections have typically been discussed as pairwise, point x projecting to point y (or: to points y and z, or more recently, in graph theoretical terms, as nodes or regions and the interconnecting edges. This is a convenient shorthand, but tends not to capture the richness and nuance of basic anatomical properties as identified in the classic tradition of tracer studies. The present short review accordingly revisits connectional weights, heterogeneity, reciprocity, topography, and hierarchical organization, drawing on concrete examples. The emphasis is on presynaptic long-distance connections, motivated by the intention to probe current assumptions and promote discussions about further progress and synthesis.

  20. Numerical modeling of liquefaction-induced failure of geo-structures subjected to earthquakes

    International Nuclear Information System (INIS)

    Rapti, Ioanna

    2016-01-01

    The increasing importance of performance-based earthquake engineering analysis points out the necessity to assess quantitatively the risk of liquefaction. In this extreme scenario of soil liquefaction, devastating consequences are observed, e.g. excessive settlements, lateral spreading and slope instability. The present PhD thesis discusses the global dynamic response and interaction of an earth structure-foundation system, so as to determine quantitatively the collapse mechanism due to foundation's soil liquefaction. As shear band generation is a potential earthquake-induced failure mode in such structures, the FE mesh dependency of results of dynamic analyses is thoroughly investigated and an existing regularization method is evaluated. The open-source FE software developed by EDF R and D, called Code-Aster, is used for the numerical simulations, while soil behavior is represented by the ECP constitutive model, developed at Centrale-Supelec. Starting from a simplified model of 1D SH wave propagation in a soil column with coupled hydro-mechanical nonlinear behavior, the effect of seismic hazard and soil's permeability on liquefaction is assessed. Input ground motion is a key component for soil liquefaction apparition, as long duration of main shock can lead to important nonlinearity and extended soil liquefaction. Moreover, when a variation of permeability as function of liquefaction state is considered, changes in the dissipation phase of excess pore water pressure and material behavior are observed, which do not follow a single trend. The effect of a regularization method with enhanced kinematics approach, called first gradient of dilation model, on 1D SH wave propagation is studied through an analytical solution. Deficiencies of the use of this regularization method are observed and discussed, e.g. spurious waves apparition in the soil's seismic response. Next, a 2D embankment-type model is simulated and its dynamic response is evaluated in dry, fully drained

  1. Effect of operating conditions on direct liquefaction of low-lipid microalgae in ethanol-water co-solvent for bio-oil production

    International Nuclear Information System (INIS)

    Ji, Changhao; He, Zhixia; Wang, Qian; Xu, Guisheng; Wang, Shuang; Xu, Zhixiang; Ji, Hengsong

    2017-01-01

    Highlights: • Low-lipid microalgae was selected as feedstock for DL in ethanol-water co-solvent. • Operating conditions had great influence on product yields and conversion rate. • Bio-oil could be obtained from all three main components. • Ethanol and water showed obviously synergistic effect during the DL of microalgae. • Bio-oil composition from DL of microalgae was different from lignocellulose biomass. - Abstract: In this work, the direct liquefaction (DL) of low-lipid microalgae Spirulina was investigated in a 50 ml autoclave reactor with ethanol and water as co-solvent. The objective of this research was carried out to examine the effect of operating conditions such as reaction temperature, reaction time, solvent/microalgae (S/M) ratio and ethanol-water co-solvent (EWCS) composition on product distribution and bio-oil characterization. The results revealed that the optimal operating conditions for bio-oil yield and conversion rate were reaction temperature of 300 °C, reaction time of 45 min, ethanol content of 50 vol.% and S/M ratio of 40/4 ml/g, which gave the bio-oil yield of 59.5% and conversion rate of 94.73%. Conversion rate in EWCS was significantly higher than that in pure water or ethanol, suggesting the synergistic effect between ethanol and water during microalgae DL. Distinct difference in composition and relative content of compound among bio-oils in different solvents were observed by GC–MS and FT-IR. Compared with hydrothermal liquefaction, the most abundant compounds in bio-oil from both EWCS and pure ethanol were esters. The presence of ethanol could enhance the bio-oil yield and improve bio-oil quality by promoting the formation of esters.

  2. Gas cooled reactors

    International Nuclear Information System (INIS)

    Kojima, Masayuki.

    1985-01-01

    Purpose: To enable direct cooling of reactor cores thereby improving the cooling efficiency upon accidents. Constitution: A plurality sets of heat exchange pipe groups are disposed around the reactor core, which are connected by way of communication pipes with a feedwater recycling device comprising gas/liquid separation device, recycling pump, feedwater pump and emergency water tank. Upon occurrence of loss of primary coolants accidents, the heat exchange pipe groups directly absorb the heat from the reactor core through radiation and convection. Although the water in the heat exchange pipe groups are boiled to evaporate if the forcive circulation is interrupted by the loss of electric power source, water in the emergency tank is supplied due to the head to the heat exchange pipe groups to continue the cooling. Furthermore, since the heat exchange pipe groups surround the entire circumference of the reactor core, cooling is carried out uniformly without resulting deformation or stresses due to the thermal imbalance. (Sekiya, K.)

  3. Method of reactor fueling

    International Nuclear Information System (INIS)

    Saito, Toshiro.

    1983-01-01

    Purpose: To decrease the cost and shorten the working time by saving fueling neutron detectors and their components. Method: Incore drive tubes for the neutron source range monitor (SRM) and intermediate range monitor (IRM) are disposed respectively within in a reactor core and a SRM detector assembly is inserted to the IRM incore drive tube which is most nearest to the neutron source upon reactor fueling. The reactor core reactivity is monitored by the SRM detector assembly. The SRM detector asesembly inserted into the IRM drive tube is extracted at the time of charging fuels up to the frame connecting the SRM and, thereafter, IRM detection assembly is inserted into the IRM drive tube and the SRM detector assembly is inserted into the SRM drive tube respectively for monitoring the reactor core. (Sekiya, K.)

  4. Internet Connectivity

    Indian Academy of Sciences (India)

    First page Back Continue Last page Overview Graphics. Internet Connectivity. BSNL, SIFY, HCL in Guwahati; only BSNL elsewhere in NE (local player in Shillong). Service poor; All vendors lease BW from BSNL.

  5. Mathematics Connection

    African Journals Online (AJOL)

    MATHEMATICS CONNECTION aims at providing a forum topromote the development of Mathematics Education in Ghana. Articles that seekto enhance the teaching and/or learning of mathematics at all levels of theeducational system are welcome.

  6. HR Connect

    Data.gov (United States)

    US Agency for International Development — HR Connect is the USAID HR personnel system which allows HR professionals to process HR actions related to employee's personal and position information. This system...

  7. Survival of Legionella in earthquake-induced soil disturbance (liquefaction) in residential areas, Christchurch, New Zealand: implications for disease.

    Science.gov (United States)

    Graham, Frances F; Harte, David Jg

    2017-05-12

    To investigate a possible link between liquefaction dust exposure and the noticeable increase in legionellosis cases in response to major earthquakes in 2010 and 2011 that resulted in widespread soil disturbance (liquefaction) in parts of Christchurch, New Zealand. We culture tested liquefaction-affected soil for Legionella spp. in the six months following the first earthquake in 2010. Thirty silt samples were collected randomly from locations within Christchurch's metropolitan area that were affected by liquefaction. The samples were tested to determine the presence of Legionella using qualitative and quantitative methods. Liquefaction-affected soil samples from three sites were further subjected to particle size distribution analysis and determination of major oxides. A controlled field study was established using six silt samples and one control (commercial compost), seeded with a wild-type strain of Legionella bozemanae serogroup (sg) 1 and persistence monitored over a 60-day period by culturing for the presence of Legionella. Dry matter determinations were undertaken so that total Legionella could be calculated on a dry weight basis. Legionella bacteria were undetectable after day one in the silt samples. However, L. bozemanae sg1 was detected in the control sample for the entire study period. This study showed that the liquefaction-affected soil could not contribute directly to the observed increase in legionellosis cases after the earthquakes due to its inability to support growth and survival of the Legionella bacteria.

  8. Evaluation of liquefaction potential of soil based on standard penetration test using multi-gene genetic programming model

    Science.gov (United States)

    Muduli, Pradyut; Das, Sarat

    2014-06-01

    This paper discusses the evaluation of liquefaction potential of soil based on standard penetration test (SPT) dataset using evolutionary artificial intelligence technique, multi-gene genetic programming (MGGP). The liquefaction classification accuracy (94.19%) of the developed liquefaction index (LI) model is found to be better than that of available artificial neural network (ANN) model (88.37%) and at par with the available support vector machine (SVM) model (94.19%) on the basis of the testing data. Further, an empirical equation is presented using MGGP to approximate the unknown limit state function representing the cyclic resistance ratio (CRR) of soil based on developed LI model. Using an independent database of 227 cases, the overall rates of successful prediction of occurrence of liquefaction and non-liquefaction are found to be 87, 86, and 84% by the developed MGGP based model, available ANN and the statistical models, respectively, on the basis of calculated factor of safety (F s) against the liquefaction occurrence.

  9. Liquefaction induced by modern earthquakes as a key to paleoseismicity: A case study of the 1988 Saguenay event

    International Nuclear Information System (INIS)

    Tuttle, M.; Cowie, P.; Wolf, L.

    1992-01-01

    Liquefaction features, including sand dikes, sills, and sand-filled craters, that formed at different distances from the epicenter of the 1988 (Mw 5.9) Saguenay earthquake are compared with one another and with older features. Modern liquefaction features decrease in size with increasing distance from the Saguenay epicenter. This relationship suggests that the size of liquefaction features may be used to determine source zones of past earthquakes and to estimate attenuation of seismic energy. Pre-1988 liquefaction features are cross-cut by the 1988 features. Although similar in morphology to the modern features, the pre-1988 features are more weathered and considerably larger in size. The larger pre-1988 features are located in the Ferland area, whereas the smallest pre-1988 feature occurs more than 37 km to the southwest. This spatial distribution of different size features suggests that an unidentified earthquake source zone (in addition to the one that generated the Saguenay earthquake) may exist in the Laurentide-Saguenay region. Structural relationships of the liquefaction features indicate that one, possibly two, earthquakes induced liquefaction in the region prior to 1988. The age of only one pre-1988 feature is well-constrained at 340 ± 70 radiocarbon years BP. If the 1663 earthquake was responsible for the formation of this feature, this event may have been centered in the Laurentide-Saguenay region rather than in the Charlevoix seismic zone

  10. Geological occurrence response to trace elemental migration in coal liquefaction based on SPSS: take no. 11 coalbed in Antaibao mine for example

    Science.gov (United States)

    Xia, Xiaohong; Qin, Yong; Yang, Weifeng

    2013-03-01

    Coal liquefaction is an adoptable method to transfer the solid fossil energy into liquid oil in large scale, but the dirty material in which will migrate to different step of liquefaction. The migration rule of some trace elements is response to the react activity of macerals in coal and the geological occurrence of the element nature of itself. In this paper, from the SPSS data correlation analysis and hierarchical clustering dendrogram about the trace elements with macerals respond to coal liquefaction yield, it shows the trace elements in No.11 Antaibao coal seam originated from some of lithophile and sulphophle elements. Correlation coefficient between liquefaction yield of three organic macerals and migration of the elements in liquefaction residue indicated that the lithophile are easy to transfer to residue, while sulphophle are apt to in the liquid products. The activated macerals are response to sulphophle trace elements. The conclusion is useful to the coal blending and environmental effects on coal direct liquefaction.

  11. Reactor water sampling device

    International Nuclear Information System (INIS)

    Sakamaki, Kazuo.

    1992-01-01

    The present invention concerns a reactor water sampling device for sampling reactor water in an in-core monitor (neutron measuring tube) housing in a BWR type reactor. The upper end portion of a drain pipe of the reactor water sampling device is attached detachably to an in-core monitor flange. A push-up rod is inserted in the drain pipe vertically movably. A sampling vessel and a vacuum pump are connected to the lower end of the drain pipe. A vacuum pump is operated to depressurize the inside of the device and move the push-up rod upwardly. Reactor water in the in-core monitor housing flows between the drain pipe and the push-up rod and flows into the sampling vessel. With such a constitution, reactor water in the in-core monitor housing can be sampled rapidly with neither opening the lid of the reactor pressure vessel nor being in contact with air. Accordingly, operator's exposure dose can be reduced. (I.N.)

  12. Re-Condensation and Liquefaction of Helium and Hydrogen Using Coolers

    International Nuclear Information System (INIS)

    Green, Michael A.

    2009-01-01

    Coolers are used to cool cryogen free devices at temperatures from 5 to 30 K. Cryogen free cooling involves a temperature drop within the device being cooled and between the device and the cooler cold heads. Liquid cooling with a liquid cryogen distributed over the surface of a device combined with re-condensation can result in a much lower temperature drop between the cooler and the device being cooled. The next logical step beyond simple re-condensation is using a cooler to liquefy the liquid cryogen in the device. A number of tests of helium liquefaction and re-condensation of helium have been run using a pulse tube cooler in the drop-in mode. This report discusses the parameter space over which re-condensation and liquefaction for helium and hydrogen can occur.

  13. Liquefaction of Warukin Formation Coal, Barito Basin, South Kalimantan on Low Pressure and Low Temperature

    Directory of Open Access Journals (Sweden)

    Edy Nursanto

    2013-06-01

    Full Text Available Research focusing on the quality of coal in Warukin Formation has been conducted in coal outcrops located on Tabalong area, particularly in 3 coal seams, namely Wara 120 which consists of low rank coal (lignite. Meanwhile, coals in seam Tutupan 210 and Paringin 712 are medium rank coal (sub-bituminous. Coal liquefaction is conducted in an autoclave on low pressure and temperature. Pressure during the process is 14 psi and temperature is 120oC. Catalyst used are alumina, hydrogen donor NaOH and water solvent. Liquefaction is conducted in three times variables of 30 minutes, 60 minutes and 90 minutes. This process shows following yield : Wara seam 120: 25.37% - 51.27%; Tutupan seam 210: 3.02%-15.45% and seam Paringin 712:1.99%-11.95%. The average result of yield shows that coals in seam Wara has higher yield conversion than coals in seam Tutupan and Paringin.

  14. Fractional Multistage Hydrothermal Liquefaction of Biomass and Catalytic Conversion into Hydrocarbons

    Energy Technology Data Exchange (ETDEWEB)

    Cortright, Randy [Virent, Inc., Madison, WI (United States); Rozmiarek, Robert [Virent, Inc., Madison, WI (United States); Dally, Brice [Virent, Inc., Madison, WI (United States); Holland, Chris [Virent, Inc., Madison, WI (United States)

    2017-08-31

    The objective of this project was to develop an improved multistage process for the hydrothermal liquefaction (HTL) of biomass to serve as a new front-end, deconstruction process ideally suited to feed Virent’s well-proven catalytic technology, which is already being scaled up. This process produced water soluble, partially de-oxygenated intermediates that are ideally suited for catalytic finishing to fungible distillate hydrocarbons. Through this project, Virent, with its partners, demonstrated the conversion of pine wood chips to drop-in hydrocarbon distillate fuels using a multi-stage fractional conversion system that is integrated with Virent’s BioForming® process. The majority of work was in the liquefaction task and included temperature scoping, solvent optimization, and separations.

  15. Determination of soil liquefaction characteristics by large-scale laboratory tests

    International Nuclear Information System (INIS)

    1975-05-01

    The testing program described in this report was carried out to study the liquefaction behavior of a clean, uniform, medium sand. Horizontal beds of this sand, 42 inches by 90 inches by 4 inches were prepared by pluviation with a special sand spreader, saturated, and tested in a shaking table system designed for this program, which applied a horizontal cyclic shear stress to the specimens. Specimen size was selected to reduce boundary effects as much as possible. Values of pore pressures and shear strains developed during the tests are presented for sand specimens at relative densities of 54, 68, 82, and 90 percent, and the results interpreted to determine the values of the stress ratio causing liquefaction at the various relative densities

  16. Catalyst dispersion and activity under conditions of temperature-staged liquefaction

    Energy Technology Data Exchange (ETDEWEB)

    Davis, A.; Schobert, H.H.; Mitchell, G.D.; Artok, L.

    1993-02-01

    This research program involves the investigation of the use of highly dispersed catalyst precursors for the pretreatment of coals by mild hydrogenation. During the course of this effort solvent preswelling of the coal was evaluated as a means of deeply impregnating catalysts into coal, active phases of catalysts under reaction conditions were studied and the impact of these techniques were evaluated during pretreatment and temperature-staged liquefaction. Two coals, a Texas subbituminous and a Utah high volatile A bituminous, were used to examine the effects of solvent swelling pretreatment and catalyst impregnation on conversion behavior at 275[degrees]C, representative of the first, low-temperature stage in a temperature-staged liquefaction reaction. Ferrous sulfate, iron pentacarbonyl, ammonium tetrathiomolybdate, and molybdenum hexacarbonyl were used as catalyst precursors. Without swelling pretreatment, impregnation of both coals increased conversion, mainly through increased yields of preasphaltenes.

  17. Catalyst dispersion and activity under conditions of temperature-staged liquefaction. Final report

    Energy Technology Data Exchange (ETDEWEB)

    Davis, A.; Schobert, H.H.; Mitchell, G.D.; Artok, L.

    1993-02-01

    This research program involves the investigation of the use of highly dispersed catalyst precursors for the pretreatment of coals by mild hydrogenation. During the course of this effort solvent preswelling of the coal was evaluated as a means of deeply impregnating catalysts into coal, active phases of catalysts under reaction conditions were studied and the impact of these techniques were evaluated during pretreatment and temperature-staged liquefaction. Two coals, a Texas subbituminous and a Utah high volatile A bituminous, were used to examine the effects of solvent swelling pretreatment and catalyst impregnation on conversion behavior at 275{degrees}C, representative of the first, low-temperature stage in a temperature-staged liquefaction reaction. Ferrous sulfate, iron pentacarbonyl, ammonium tetrathiomolybdate, and molybdenum hexacarbonyl were used as catalyst precursors. Without swelling pretreatment, impregnation of both coals increased conversion, mainly through increased yields of preasphaltenes.

  18. A preliminary analysis of floating production storage and offloading facilities with gas liquefaction processes

    DEFF Research Database (Denmark)

    Nguyen, Tuong-Van; Carranza-Sánchez, Yamid Alberto; Junior, Silvio de Oliveira

    2016-01-01

    Floating, production, storage and offloading (FPSO) plants are facilities used in upstream petroleum processing. They have gained interest because they are more flexible than conventional plants and can be used for producing oil and gas in deep-water fields. In general, gas export is challenging...... because of the lack of infrastructure in remote locations. The present work investigates the possibility of integrating liquefaction processes on such facilities, considering two mixed-refrigerant and two expansion-based processes suitable for offshore applications. Two FPSO configurations are considered...... in this work, and they were suggested by Brazilian operators for fields processing natural gas with moderate to high content of carbon dioxide. The performance of the combined systems is analysed by conducting energy and exergy analyses. The integration of gas liquefaction results in greater power consumption...

  19. Liquefaction of lignohemicellulosic waste by processing with carbon monoxide and water

    Energy Technology Data Exchange (ETDEWEB)

    El-Saied, H

    1977-09-01

    The liquefaction of lignohemicellulosic waste by processing with carbon monoxide and water for 10 minutes at 250/sup 0/-440/sup 0/C and 40 to 70 atm initial pressure in a rocking autoclave produced benzene-soluble heavy oil in yields up to 80%. High conversion and yields were favored by high thermal stress, short reaction times, and sufficient hydrogen to prevent radical recombination in the critical liquefaction stages. The addition of sodium or calcium hydroxide, sodium carbonate, iron oxide, etc. in small amounts gave good oil yields under less severe conditions. Lignins from rice straw, bagasse, and other grasses gave higher yields than the woody lignin obtained from cotton stalks. In products obtained by liquefying black liquor lignohemicellulose from an Eyptian rice straw pulping plant, the hydrogen-carbon atomic ratio was 1.0 to 1.3:1.

  20. RESEARCH ON THE DEGREE OF SATURATION INVESTIGATION BY THE SAMPLING OF THE SAND FOR LIQUEFACTION

    Science.gov (United States)

    Fujii, Nao; Ohuchi, Masatoshi; Sakai, Katsuo; Nishigaki, Makoto

    The liquefaction countermeasure technical method, whereby the liquefaction strength is enhanced by making sand deposit in the state of unsaturation, is currently under study. The author et al have suggested a simple method of verifying the persistence of residual air using the undisturbed sample under ordinary temperature and sampling underground water; and have actually implemented the method in the adjacent ground with the foundation of viaduct pneumatic caisson where the leaked air during the construction was considered to have been trapped. We demonstrated the method of correcting the influence of the pressure of sampling specimen as well as of the dissolved air, and studied the precision of required degree of saturation. As the result, it has been shown that the residual air entrapped in the sand deposit is sustainable for as long time as about 28 years.

  1. Liquefaction-induced lateral spreading in Oceano, California, during the 2003 San Simeon Earthquake

    Science.gov (United States)

    Holzer, Thomas L.; Noce, Thomas E.; Bennett, Michael J.; Di Alessandro, Carola; Boatwright, John; Tinsley, John C.; Sell, Russell W.; Rosenberg, Lewis I.

    2004-01-01

    The December 22, 2003, San Simeon, California, (M6.5) earthquake caused damage to houses, road surfaces, and underground utilities in Oceano, California. The community of Oceano is approximately 50 miles (80 km) from the earthquake epicenter. Damage at this distance from a M6.5 earthquake is unusual. To understand the causes of this damage, the U.S. Geological Survey conducted extensive subsurface exploration and monitoring of aftershocks in the months after the earthquake. The investigation included 37 seismic cone penetration tests, 5 soil borings, and aftershock monitoring from January 28 to March 7, 2004. The USGS investigation identified two earthquake hazards in Oceano that explain the San Simeon earthquake damage?site amplification and liquefaction. Site amplification is a phenomenon observed in many earthquakes where the strength of the shaking increases abnormally in areas where the seismic-wave velocity of shallow geologic layers is low. As a result, earthquake shaking is felt more strongly than in surrounding areas without similar geologic conditions. Site amplification in Oceano is indicated by the physical properties of the geologic layers beneath Oceano and was confirmed by monitoring aftershocks. Liquefaction, which is also commonly observed during earthquakes, is a phenomenon where saturated sands lose their strength during an earthquake and become fluid-like and mobile. As a result, the ground may undergo large permanent displacements that can damage underground utilities and well-built surface structures. The type of displacement of major concern associated with liquefaction is lateral spreading because it involves displacement of large blocks of ground down gentle slopes or towards stream channels. The USGS investigation indicates that the shallow geologic units beneath Oceano are very susceptible to liquefaction. They include young sand dunes and clean sandy artificial fill that was used to bury and convert marshes into developable lots. Most of

  2. Coupling hydrothermal liquefaction and anaerobic digestion for energy valorization from model biomass feedstocks.

    Science.gov (United States)

    Posmanik, Roy; Labatut, Rodrigo A; Kim, Andrew H; Usack, Joseph G; Tester, Jefferson W; Angenent, Largus T

    2017-06-01

    Hydrothermal liquefaction converts food waste into oil and a carbon-rich hydrothermal aqueous phase. The hydrothermal aqueous phase may be converted to biomethane via anaerobic digestion. Here, the feasibility of coupling hydrothermal liquefaction and anaerobic digestion for the conversion of food waste into energy products was examined. A mixture of polysaccharides, proteins, and lipids, representing food waste, underwent hydrothermal processing at temperatures ranging from 200 to 350°C. The anaerobic biodegradability of the hydrothermal aqueous phase was examined through conducting biochemical methane potential assays. The results demonstrate that the anaerobic biodegradability of the hydrothermal aqueous phase was lower when the temperature of hydrothermal processing increased. The chemical composition of the hydrothermal aqueous phase affected the anaerobic biodegradability. However, no inhibition of biodegradation was observed for most samples. Combining hydrothermal and anaerobic digestion may, therefore, yield a higher energetic return by converting the feedstock into oil and biomethane. Copyright © 2017 Elsevier Ltd. All rights reserved.

  3. Method for controlling boiling point distribution of coal liquefaction oil product

    Science.gov (United States)

    Anderson, Raymond P.; Schmalzer, David K.; Wright, Charles H.

    1982-12-21

    The relative ratio of heavy distillate to light distillate produced in a coal liquefaction process is continuously controlled by automatically and continuously controlling the ratio of heavy distillate to light distillate in a liquid solvent used to form the feed slurry to the coal liquefaction zone, and varying the weight ratio of heavy distillate to light distillate in the liquid solvent inversely with respect to the desired weight ratio of heavy distillate to light distillate in the distillate fuel oil product. The concentration of light distillate and heavy distillate in the liquid solvent is controlled by recycling predetermined amounts of light distillate and heavy distillate for admixture with feed coal to the process in accordance with the foregoing relationships.

  4. Japan`s New Sunshine Project. 1996 Annual Summary of Coal Liquefaction and Gasification; 1996 nendo new sunshine keikaku seika hokokusho gaiyoshu. Sekitan no ekika gasuka

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1997-11-01

    In reference to the results of the research and development under the fiscal 1996 New Sunshine Project, a report was summed up on coal liquefaction and coal gasification. As to the R and D of coal liquefaction technology, researches were conducted on liquefaction characteristics and engineering properties by coal kind, catalysts for coal liquefaction, liquefaction reaction of coal and reformation utilization of the liquefied products, liquefaction reaction mechanism and coking mechanism, solubility of coal in solvent and catalytic reaction mechanism, solvent reaction mechanism by hydrogen donor solvent, etc. Concerning the R and D of coal gasification technology, made were the basic study of eco-technology adaptable gasification technology and the study of coal gasification enhancing technology. Further, as to the development of bituminous coal liquefaction technology, carried out were the study in pilot plants and the support study of pilot plants. Additionally, R and D were done of the basic technology of coal liquefaction such as upgrading technology and environmentally acceptable coal liquefaction technology, and of coal hydrogasification technology. 3 refs., 81 figs., 25 tabs.

  5. Establishing Connectivity

    DEFF Research Database (Denmark)

    Kjær, Poul F.

    Global law settings are characterised by a structural pre-eminence of connectivity norms, a type of norm which differs from coherency or possibility norms. The centrality of connectivity norms emerges from the function of global law, which is to increase the probability of transfers of condensed ...... and human rights can be understood as serving a constitutionalising function aimed at stabilising and facilitating connectivity. This allows for an understanding of colonialism and contemporary global governance as functional, but not as normative, equivalents.......Global law settings are characterised by a structural pre-eminence of connectivity norms, a type of norm which differs from coherency or possibility norms. The centrality of connectivity norms emerges from the function of global law, which is to increase the probability of transfers of condensed...... social components, such as economic capital and products, religious doctrines and scientific knowledge, from one legally structured context to another within world society. This was the case from colonialism and colonial law to contemporary global supply chains and human rights. Both colonial law...

  6. Nuclear reactor apparatus

    International Nuclear Information System (INIS)

    Braun, H.E.; Bonnet, H.P.

    1978-01-01

    The reactor and its containment, instead of being supported on a solid concrete pad, are supported on a truss formed of upper and lower reinforced horizontal plates and vertical walls integrated into a rigid structure. The plates and walls from chambers within which the auxiliary components of the reactor, such as valves, pumping equipment and various tanks, are disposed. Certain of the chambers are also access passages for personnel, pipe chases, valve chambers and the like. In particular the truss includes an annular chamber. This chamber is lined and sealed by a corrosion-resistant liner and contains coolant and serves as a refueling cooling storage tank. This tank is directly below the primary-coolant conductor loops which extend from the reactor above the upper plate. The upper plate includes a sump connected to the tank through which coolant flows into the tank in the event of the occurrence of a loss-of-coolant accident. The truss extends beyond the containment and has chambers in the extending annulus. Pumps for circulating the coolant between the refueling coolant storage tank and the reactor are provided in certain of these chambers. The pumps are connected to the reactor by relatively short coolant conductors. Access to these pumps is readily afforded through hatches in the extending annulus

  7. Reactor containing facility

    International Nuclear Information System (INIS)

    Akagawa, Katsuhiko.

    1992-01-01

    A cooling space having a predetermined capacity is formed between a reactor container and concrete walls. A circulation loop disposed to the outside of the concrete walls is connected to the top and the bottom of the cooling space. The circulation loop has a circulation pump and a heat exchanger, and a cooling water supply pipe is connected to the upstream of the circulation pump for introducing cooling water from the outside. Upon occurrence of loss of coolant accident, cooling water is introduced from the cooling water supply pipe to the cooling space between the reactor container and the concrete walls after shut-down of the reactor operation. Then, cooling water is circulated while being cooled by the heat exchanger, to cool the reactor container by cooling water flown in the cooling space. This can cool the reactor container in a short period of time upon occurrence of the loss of coolant accident. Accordingly, a repairing operation for a ruptured portion can be conducted rapidly. (I.N.)

  8. Predicted Liquefaction in the Greater Oakland and Northern Santa Clara Valley Areas for a Repeat of the 1868 Hayward Earthquake

    Science.gov (United States)

    Holzer, T. L.; Noce, T. E.; Bennett, M. J.

    2008-12-01

    Probabilities of surface manifestations of liquefaction due to a repeat of the 1868 (M6.7-7.0) earthquake on the southern segment of the Hayward Fault were calculated for two areas along the margin of San Francisco Bay, California: greater Oakland and the northern Santa Clara Valley. Liquefaction is predicted to be more common in the greater Oakland area than in the northern Santa Clara Valley owing to the presence of 57 km2 of susceptible sandy artificial fill. Most of the fills were placed into San Francisco Bay during the first half of the 20th century to build military bases, port facilities, and shoreline communities like Alameda and Bay Farm Island. Probabilities of liquefaction in the area underlain by this sandy artificial fill range from 0.2 to ~0.5 for a M7.0 earthquake, and decrease to 0.1 to ~0.4 for a M6.7 earthquake. In the greater Oakland area, liquefaction probabilities generally are less than 0.05 for Holocene alluvial fan deposits, which underlie most of the remaining flat-lying urban area. In the northern Santa Clara Valley for a M7.0 earthquake on the Hayward Fault and an assumed water-table depth of 1.5 m (the historically shallowest water level), liquefaction probabilities range from 0.1 to 0.2 along Coyote and Guadalupe Creeks, but are less than 0.05 elsewhere. For a M6.7 earthquake, probabilities are greater than 0.1 along Coyote Creek but decrease along Guadalupe Creek to less than 0.1. Areas with high probabilities in the Santa Clara Valley are underlain by latest Holocene alluvial fan levee deposits where liquefaction and lateral spreading occurred during large earthquakes in 1868 and 1906. The liquefaction scenario maps were created with ArcGIS ModelBuilder. Peak ground accelerations first were computed with the new Boore and Atkinson NGA attenuation relation (2008, Earthquake Spectra, 24:1, p. 99-138), using VS30 to account for local site response. Spatial liquefaction probabilities were then estimated using the predicted ground motions

  9. Deactivation by carbon of iron catalysts for indirect liquefaction

    Energy Technology Data Exchange (ETDEWEB)

    Bartholomew, C.H.

    1990-10-11

    This report describes recent progress in a fundamental, three-year investigation of carbon formation and its effects on the activity and selectivity of promoted iron catalysts for Fischer-Tropsch (FT) synthesis, the objectives of which are: determine rates and mechanisms of carbon deactivation of unsupported Fe and Fe/K catalysts during CO hydrogenation over a range of CO concentrations, CO:H{sub 2} ratios, and temperatures; model the rates of deactivation of the same catalysts in fixed-bed reactors. During the thirteenth quarter design of software for a computer-automated reactor system to be used in the kinetic and deactivation studies was continued. Further progress was made toward the completion of the control language, control routines, and software for operating this system. Progress was also made on the testing of the system hardware and software. H{sub 2} chemisorption capacities and activity selectivity data were also measured for three iron catalysts promoted with 1% alumina. 47 refs., 8 figs., 1 tab.

  10. Indirect Liquefaction of Biomass to Transportation Fuels Via Mixed Oxygenated Intermediates

    Energy Technology Data Exchange (ETDEWEB)

    Tan, Eric C.D.

    2016-11-14

    This paper presents a comparative techno-economic analysis of four emerging conversion pathways from biomass to gasoline-, jet-, and diesel-range hydrocarbons via indirect liquefaction with specific focus on pathways utilizing oxygenated intermediates. The processing steps include: biomass-to-syngas via indirect gasification, gas cleanup, conversion of syngas to alcohols/oxygenates followed by conversion of alcohols/oxygenates to hydrocarbon blendstocks via dehydration, oligomerization, and hydrogenation.

  11. Conceptual design of an integrated hydrothermal liquefaction and biogas plant for sustainable bioenergy production

    DEFF Research Database (Denmark)

    Hoffmann, Jessica; Rudra, Souman; Toor, Saqib

    2013-01-01

    Initial process studies carried out in Aspen Plus on an integrated thermochemical conversion process are presented herein. In the simulations, a hydrothermal liquefaction (HTL) plant is combined with a biogas plant (BP), such that the digestate from the BP is converted to a biocrude in the HTL...... grid or for CHP. An estimated 62–84% of the biomass energy can be recovered in the biofuels....

  12. Shear wave velocity-based evaluation and design of stone column improved ground for liquefaction mitigation

    Science.gov (United States)

    Zhou, Yanguo; Sun, Zhengbo; Chen, Jie; Chen, Yunmin; Chen, Renpeng

    2017-04-01

    The evaluation and design of stone column improvement ground for liquefaction mitigation is a challenging issue for the state of practice. In this paper, a shear wave velocity-based approach is proposed based on the well-defined correlations of liquefaction resistance (CRR)-shear wave velocity ( V s)-void ratio ( e) of sandy soils, and the values of parameters in this approach are recommended for preliminary design purpose when site specific values are not available. The detailed procedures of pre- and post-improvement liquefaction evaluations and stone column design are given. According to this approach, the required level of ground improvement will be met once the target V s of soil is raised high enough (i.e., no less than the critical velocity) to resist the given earthquake loading according to the CRR- V s relationship, and then this requirement is transferred to the control of target void ratio (i.e., the critical e) according to the V s- e relationship. As this approach relies on the densification of the surrounding soil instead of the whole improved ground and is conservative by nature, specific considerations of the densification mechanism and effect are given, and the effects of drainage and reinforcement of stone columns are also discussed. A case study of a thermal power plant in Indonesia is introduced, where the effectiveness of stone column improved ground was evaluated by the proposed V s-based method and compared with the SPT-based evaluation. This improved ground performed well and experienced no liquefaction during subsequent strong earthquakes.

  13. Hydrothermal Liquefaction of Enzymatic Hydrolysis Lignin: Biomass Pretreatment Severity Affects Lignin Valorization

    DEFF Research Database (Denmark)

    Jensen, Mads M.; Djajadi, Demi T.; Torri, Cristian

    2018-01-01

    Alkalinehydrothermal liquefaction (HTL) of lignin-rich enzymatichydrolysis residues (EnzHR) from wheat straw and Miscanthusx giganteus was performed at 255, 300, and 345 °C to investigate valorization of this side-stream from second-generation bioethanol production. The EnzHR were from biomass...... contributed with additional chemical information as well as confirming trends seen from quantified monomers. This work is relevant for future lignin valorization in biorefineries based on current second-generation bioethanol production....

  14. Combined hydrothermal liquefaction and catalytic hydrothermal gasification system and process for conversion of biomass feedstocks

    Science.gov (United States)

    Elliott, Douglas C.; Neuenschwander, Gary G.; Hart, Todd R.

    2017-09-12

    A combined hydrothermal liquefaction (HTL) and catalytic hydrothermal gasification (CHG) system and process are described that convert various biomass-containing sources into separable bio-oils and aqueous effluents that contain residual organics. Bio-oils may be converted to useful bio-based fuels and other chemical feedstocks. Residual organics in HTL aqueous effluents may be gasified and converted into medium-BTU product gases and directly used for process heating or to provide energy.

  15. Development of 1-D Shake Table Testing Facility for Liquefaction Studies

    Science.gov (United States)

    Unni, Kartha G.; Beena, K. S.; Mahesh, C.

    2018-04-01

    One of the major challenges researchers face in the field of earthquake geotechnical engineering in India is the high cost of laboratory infrastructure. Developing a reliable and low cost experimental set up is attempted in this research. The paper details the design and development of a uniaxial shake table and the data acquisition system with accelerometers and pore water pressure sensors which can be used for liquefaction studies.

  16. NATURAL GAS LIQUEFACTION UNITS ON THE BASE OF EXPANDER NITROGEN CYCLES

    OpenAIRE

    Кузьменко, И. Ф.; Передельский, В. А.; Довбиш, А. Л.

    2014-01-01

    It is necessary to create large-capacity LNG-units for natural gas peaks consumption shaving and also to expand liquefied natural gas (LNG) marketing. It is proposed to create such natural gas liquefaction units with the use of outer nitrogen cryogenic thermodynamic cycles. It is necessary to use turboexpander-compressor sets (TECS) in them for maximizing cycles efficiency. Different technological schemes of LNG-units including nitrogen cryogenic units with TECS from one to four have been exa...

  17. Study on hydrogen transfer in coal liquefaction by tritium and carbon-14 tracers

    International Nuclear Information System (INIS)

    Nitoh, Osamu; Kabe, Toshiaki; Kabe, Yaeko.

    1985-01-01

    For the analysis of mechanism of hydrogenation and cracking of coal, the liquefaction of Taiheiyo coal using tritium labeled gaseous hydrogen and tritium labeled tetralin with small amounts of carbon-14 labeled naphthalene has been studied. Taiheiyo coal(25g) was thermally decomposed in tetralin or naphthalene solvent(75g) at 400--440 0 C under the initial hydrogen pressure of 5.9MPa for 30min with Ni-Mo-Al 2 O 3 catalyst(0--5g). The reaction mixture in an autoclave was separated by filtration, distillation and solvent extraction. Produced gas, oils and the solvent were analyzed by gas chromatography. The tritium and carbon-14 contents of separated reaction products were measured with a liquid scintilation counter to study the hydrogen transfer mechanism. The distribution of reaction products and the amount of hydrogen transfer from gas or solvent to the products were also determined. In hydrogen donor solvent such as tetralin, the coal liquefaction yield was independent from the catalyst, but the catalyst was effective in hydrocracking of preasphaltene and asphaltene. In naphthalene solvent, the coal liquefaction reaction hardly occured in the absence of the catalyst, because hydrogen transfer from both the solvent and gaseous hydrogen was scarce. Tritium distribution in the reaction products showed that complicated hydrogen exchange reactions between gaseous hydrogen, coal liquids and solvent came out by the presence of coal liquids and catalyst. The very small amounts of carbon-14 transferred to the liquefaction products showed that carbon exchange or transfer between solvent and coal did not take place. (author)

  18. Advanced direct liquefaction concepts for PETC generic units. Final report, Phase I

    Energy Technology Data Exchange (ETDEWEB)

    NONE

    1995-03-01

    The Advanced Concepts for Direct Coal Liquefaction program was initiated by the Department of Energy in 1991 to develop technologies that could significantly reduce the cost of producing liquid fuels by the direct liquefaction of coal. The advanced 2-stage liquefaction technology that was developed at Wilsonville over the past 10 years has contributed significantly toward decreasing the cost of producing liquids from coal to about $33/bbl. It remains, however, the objective of DOE to further reduce this cost to a level more competitive with petroleum based products. This project, among others, was initiated to investigate various alternative approaches to develop technologies that might ultimately lead to a 25 % reduction in cost of product. In this project a number of novel concepts were investigated, either individually or in a coupled configuration that had the potential to contribute toward meeting the DOE goal. The concepts included mature technologies or ones closely related to them, such as coal cleaning by oil agglomeration, fluid coking and distillate hydrotreating and dewaxing. Other approaches that were either embryonic or less developed were chemical pretreatment of coal to remove oxygen, and dispersed catalyst development for application in the 2-stage liquefaction process. This report presents the results of this project. It is arranged in four sections which were prepared by participating organizations responsible for that phase of the project. A summary of the overall project and the principal results are given in this section. First, however, an overview of the process economics and the process concepts that were developed during the course of this program is presented.

  19. Reactor Physics

    International Nuclear Information System (INIS)

    Ait Abderrahim, A.

    2002-01-01

    SCK-CEN's Reactor Physics and MYRRHA Department offers expertise in various areas of reactor physics, in particular in neutron and gamma calculations, reactor dosimetry, reactor operation and control, reactor code benchmarking and reactor safety calculations. This expertise is applied in the Department's own research projects in the VENUS critical facility, in the BR1 reactor and in the MYRRHA project (this project aims at designing a prototype Accelerator Driven System). Available expertise is also used in programmes external to the Department such as the reactor pressure steel vessel programme, the BR2 materials testing reactor dosimetry, and the preparation and interpretation of irradiation experiments by means of neutron and gamma calculations. The activities of the Fuzzy Logic and Intelligent Technologies in Nuclear Science programme cover several domains outside the department. Progress and achievements in these topical areas in 2001 are summarised

  20. Reactor Physics

    Energy Technology Data Exchange (ETDEWEB)

    Ait Abderrahim, A

    2001-04-01

    The Reactor Physics and MYRRHA Department of SCK-CEN offers expertise in various areas of reactor physics, in particular in neutronics calculations, reactor dosimetry, reactor operation, reactor safety and control and non-destructive analysis of reactor fuel. This expertise is applied in the Department's own research projects in the VENUS critical facility, in the BR1 reactor and in the MYRRHA project (this project aims at designing a prototype Accelerator Driven System). Available expertise is also used in programmes external to the Department such as the reactor pressure steel vessel programme, the BR2 reactor dosimetry, and the preparation and interpretation of irradiation experiments by means of neutron and gamma calculations. The activities of the Fuzzy Logic and Intelligent Technologies in Nuclear Science programme cover several domains outside the department. Progress and achievements in these topical areas in 2000 are summarised.